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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARML23129A2872022-09-14014 September 2022 Fifth Ten-Year Interval ISI Program and Third Ten-Year Interval Containment Inservice Inspection Program, Revision 4 ML21130A0842021-04-21021 April 2021 Fifth Ten-Year Interval Inservice Inspection Program and Third Ten-Year Interval Containment Inservice Inspection Program, Revision 3 ML21130A0852021-04-21021 April 2021 0 to Updated Final Safety Analysis Report, Appendix J, Inservice Inspection Program NLS2021009, Inservice Inspection OAR-1 Owner'S Activity Report2021-01-21021 January 2021 Inservice Inspection OAR-1 Owner'S Activity Report NLS2019005, Inservice Inspection OAR-1 Owner'S Activity Report2019-02-14014 February 2019 Inservice Inspection OAR-1 Owner'S Activity Report NLS2017071, Inservice Inspection Program Fifth Ten-Year Interval 10 CFR 50.55a Relief Requests2017-08-17017 August 2017 Inservice Inspection Program Fifth Ten-Year Interval 10 CFR 50.55a Relief Requests NLS2017006, Inservice Inspection OAR-1 Owner'S Activity Report2017-02-0202 February 2017 Inservice Inspection OAR-1 Owner'S Activity Report NLS2015003, Inservice Inspection OAR-I Owner'S Activity Report2015-01-28028 January 2015 Inservice Inspection OAR-I Owner'S Activity Report NLS2013031, Inservice Inspection OAR-I Owner'S Activity Report2013-02-27027 February 2013 Inservice Inspection OAR-I Owner'S Activity Report NLS2011082, Inservice Inspection Owner'S Activity Report (OAR-1) Owner'S Activity Report2011-08-0505 August 2011 Inservice Inspection Owner'S Activity Report (OAR-1) Owner'S Activity Report NLS2010016, Inservice Inspection OAR-I Owner'S Activity Report for the Fall 2009 Refueling Outage2010-02-0202 February 2010 Inservice Inspection OAR-I Owner'S Activity Report for the Fall 2009 Refueling Outage NLS2009006, 10 CFR 50.55a Request Number RI-21, Revision 0, and Request Number RI-22, Revision 02009-02-16016 February 2009 10 CFR 50.55a Request Number RI-21, Revision 0, and Request Number RI-22, Revision 0 NLS2008065, Inservice Inspection Summary Report for the Spring 2008 Refueling Outage2008-08-14014 August 2008 Inservice Inspection Summary Report for the Spring 2008 Refueling Outage NLS2008007, Correction to Inservice Inspection Summary Report2008-01-17017 January 2008 Correction to Inservice Inspection Summary Report NLS2007013, Inservice Inspection Summary Report2007-02-20020 February 2007 Inservice Inspection Summary Report NLS2006064, Response to NRC Request for Additional Information Regarding Relief Request RI-13 for the Fourth 10-Year Inservice Inspection Interval Cooper Nuclear Station2006-08-0101 August 2006 Response to NRC Request for Additional Information Regarding Relief Request RI-13 for the Fourth 10-Year Inservice Inspection Interval Cooper Nuclear Station NLS2006015, 10 CFR 50.55a Requests for Fourth Ten-Year Inservice Inspection Interval2006-02-23023 February 2006 10 CFR 50.55a Requests for Fourth Ten-Year Inservice Inspection Interval NLS2005074, Fourth Ten-Year Interval Pump and Valve Inservice Testing Program Relief Requests2005-10-19019 October 2005 Fourth Ten-Year Interval Pump and Valve Inservice Testing Program Relief Requests NLS2005086, Inservice Inspection Relief Requests RI-21, Revision 2, and RI-36 and Withdrawal of Relief Request RI-202005-09-28028 September 2005 Inservice Inspection Relief Requests RI-21, Revision 2, and RI-36 and Withdrawal of Relief Request RI-20 NLS2005049, Inservice Inspection Summary Report2005-05-16016 May 2005 Inservice Inspection Summary Report NLS2004125, Inservice Inspection Relief Request RI-35 Cooper Nuclear Station2004-10-25025 October 2004 Inservice Inspection Relief Request RI-35 Cooper Nuclear Station NLS2004009, Inservice Inspection Relief Requests PR-03, RC-06, RC-07, R1-17, R1-31, R1-32, and R1-332004-02-12012 February 2004 Inservice Inspection Relief Requests PR-03, RC-06, RC-07, R1-17, R1-31, R1-32, and R1-33 NLS2003059, Inservice Testing Program Relief Request RP-06, Revision 12003-09-19019 September 2003 Inservice Testing Program Relief Request RP-06, Revision 1 NLS2003080, Inservice Inspection (ISI) Summary Report for the Spring 2003 Refueling Outage at Cooper Nuclear Station2003-07-21021 July 2003 Inservice Inspection (ISI) Summary Report for the Spring 2003 Refueling Outage at Cooper Nuclear Station NLS2002111, Inservice Testing Program Relief Request RP-06, RP-072002-11-14014 November 2002 Inservice Testing Program Relief Request RP-06, RP-07 NLS2002040, Inservice Inspection Summary Report for Cooper Nuclear Station2002-03-28028 March 2002 Inservice Inspection Summary Report for Cooper Nuclear Station 2022-09-14
[Table view] Category:Letter type:NLS
MONTHYEARNLS2024006, Response to Nuclear Regulatory Commission'S Request for Additional Information for Relief Request RC3-022024-01-25025 January 2024 Response to Nuclear Regulatory Commission'S Request for Additional Information for Relief Request RC3-02 NLS2024007, Emergency Plan Implementing Procedure 5.7.1, Revision 732024-01-16016 January 2024 Emergency Plan Implementing Procedure 5.7.1, Revision 73 NLS2024003, 30 Day Report - Unauthorized Disassembly of Liquid Scintillation Detector2024-01-15015 January 2024 30 Day Report - Unauthorized Disassembly of Liquid Scintillation Detector NLS2024004, Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 20232024-01-10010 January 2024 Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 2023 NLS2023053, ISFSI, Supplement to Exemption Request from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-11-30030 November 2023 ISFSI, Supplement to Exemption Request from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation NLS2023050, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-11-22022 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation NLS2023045, Application to Revise Technical Specifications to Adopt TSTF-374, Revision to Diesel Fuel Oil Testing Program2023-11-15015 November 2023 Application to Revise Technical Specifications to Adopt TSTF-374, Revision to Diesel Fuel Oil Testing Program NLS2023051, Response to Nuclear Regulatory Commission Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements2023-10-10010 October 2023 Response to Nuclear Regulatory Commission Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements NLS2023049, 10 CFR Part 21 Report Regarding HGA Relays2023-09-0606 September 2023 10 CFR Part 21 Report Regarding HGA Relays NLS2023029, License Amendment Request to Revise Technical Specifications to Support Inspection of Diesel Fuel Oil Storage Tanks2023-09-0606 September 2023 License Amendment Request to Revise Technical Specifications to Support Inspection of Diesel Fuel Oil Storage Tanks NLS2023047, Licensee Guarantees of Payment of Deferred Premiums2023-07-26026 July 2023 Licensee Guarantees of Payment of Deferred Premiums NLS2023033, 10 CFR 50.55a Relief Request RC3-022023-06-27027 June 2023 10 CFR 50.55a Relief Request RC3-02 NLS2023039, Preparation and Scheduling of Operator Licensing Examinations2023-06-0101 June 2023 Preparation and Scheduling of Operator Licensing Examinations NLS2023038, Nebraska Public Power District 2022 Financial Report2023-05-22022 May 2023 Nebraska Public Power District 2022 Financial Report NLS2023031, Annual Radiological Environmental Report2023-05-11011 May 2023 Annual Radiological Environmental Report NLS2023017, Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements2023-05-0303 May 2023 Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements NLS2023018, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-0303 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling NLS2023030, Annual Radioactive Effluent Release Report2023-04-27027 April 2023 Annual Radioactive Effluent Release Report NLS2023007, Technical Specification Bases Changes2023-04-17017 April 2023 Technical Specification Bases Changes NLS2023027, Annual Report of Individual Exposure Monitoring2023-04-13013 April 2023 Annual Report of Individual Exposure Monitoring NLS2023021, Quality Assurance Program Changes2023-04-10010 April 2023 Quality Assurance Program Changes NLS2023020, Decommissioning Funding2023-03-29029 March 2023 Decommissioning Funding NLS2023019, Property Insurance Coverage2023-03-23023 March 2023 Property Insurance Coverage NLS2023010, Inservice Inspection OAR-1 Owner'S Activity Report for Cooper Nuclear Station2023-02-0909 February 2023 Inservice Inspection OAR-1 Owner'S Activity Report for Cooper Nuclear Station NLS2023005, Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 20222023-01-19019 January 2023 Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 2022 NLS2022054, Preparation and Scheduling of Operator Licensing Examinations2023-01-0505 January 2023 Preparation and Scheduling of Operator Licensing Examinations NLS2022055, Emergency Plan, Revision 812023-01-0404 January 2023 Emergency Plan, Revision 81 NLS2022053, CNS-2022-11 Post Exam Submittal2022-11-22022 November 2022 CNS-2022-11 Post Exam Submittal NLS2022050, Notification of Revision to Cooper Nuclear Station Emergency Response Data System Data Point Library2022-11-0909 November 2022 Notification of Revision to Cooper Nuclear Station Emergency Response Data System Data Point Library NLS2022048, Management Change and Correspondence Update2022-11-0101 November 2022 Management Change and Correspondence Update NLS2022047, Core Operating Limits Report, Cycle 33, Revision 02022-10-14014 October 2022 Core Operating Limits Report, Cycle 33, Revision 0 NLS2022042, 10 CFR 50.59(d)(2) and 10 CFR 72.48(d)(2) Summary Report2022-10-0707 October 2022 10 CFR 50.59(d)(2) and 10 CFR 72.48(d)(2) Summary Report NLS2022037, Emergency Plan, Revision 80, Summary of 50.54(q) Analyses2022-08-18018 August 2022 Emergency Plan, Revision 80, Summary of 50.54(q) Analyses NLS2022035, Evacuation Time Estimate Report for Cooper Nuclear Station2022-08-16016 August 2022 Evacuation Time Estimate Report for Cooper Nuclear Station NLS2022031, Licensee Guarantees of Payment of Deferred Premiums2022-07-19019 July 2022 Licensee Guarantees of Payment of Deferred Premiums NLS2022005, Application to Revise Technical Specifications to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements2022-06-16016 June 2022 Application to Revise Technical Specifications to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements NLS2022025, Nebraska Public Power District Letter (NLS2022010) to U.S. Nuclear Regulatory Commission Dated April 5, 2022, Annual Report of Individual Exposure Monitoring2022-06-0606 June 2022 Nebraska Public Power District Letter (NLS2022010) to U.S. Nuclear Regulatory Commission Dated April 5, 2022, Annual Report of Individual Exposure Monitoring NLS2022016, Annual Radiological Environmental Report2022-05-10010 May 2022 Annual Radiological Environmental Report NLS2022020, Nebraska Public Power District, Cooper Nuclear Station, 2021 Financial Report2022-05-0202 May 2022 Nebraska Public Power District, Cooper Nuclear Station, 2021 Financial Report NLS2022014, Annual Radioactive Effluent Release Report2022-04-27027 April 2022 Annual Radioactive Effluent Release Report NLS2022010, Annual Report of Individual Exposure Monitoring2022-04-0505 April 2022 Annual Report of Individual Exposure Monitoring NLS2022009, Property Insurance Coverage2022-03-23023 March 2022 Property Insurance Coverage NLS2022011, Preparation and Scheduling of Operator Licensing Examinations2022-03-18018 March 2022 Preparation and Scheduling of Operator Licensing Examinations NLS2022004, Response to Nuclear Regulatory Commission'S Request for Additional Information Regarding Relief Request RR5-01, Revision 12022-02-0707 February 2022 Response to Nuclear Regulatory Commission'S Request for Additional Information Regarding Relief Request RR5-01, Revision 1 NLS2022003, Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 20212022-01-20020 January 2022 Annual Report of Changes and Errors in Emergency Core Cooling System Evaluation Models for 2021 NLS2021067, ISFSI - Independent Spent Fuel Storage Installation Decommissioning Funding Plan2021-12-16016 December 2021 ISFSI - Independent Spent Fuel Storage Installation Decommissioning Funding Plan NLS2021069, Withdrawal of Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements2021-12-15015 December 2021 Withdrawal of Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements NLS2021066, Response to Nuclear Regulatory Commission'S Request for Additional Information Regarding Alternative Request RI5-02, Revision 32021-12-10010 December 2021 Response to Nuclear Regulatory Commission'S Request for Additional Information Regarding Alternative Request RI5-02, Revision 3 NLS2021065, Clarification of Response to Nuclear Regulatory Commission'S Request for Additional Information for Alternative Request RS-012021-12-0606 December 2021 Clarification of Response to Nuclear Regulatory Commission'S Request for Additional Information for Alternative Request RS-01 NLS2021056, Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements2021-11-16016 November 2021 Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements 2024-01-25
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H Nebraska Public Power District Always there when you need us NLS2019005 February 14, 2019 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555-0001
Subject:
Inservice Inspection OAR-1 Owner's Activity Report Cooper Nuclear Station, Docket No. 50-298, DPR-46
Dear Sir or Madam:
The purpose of this letter is to provide to the Nuclear Regulatory Commission the Inservice Inspection OAR-I Owner's Activity Report for the Fall 2018 Refueling Outage at Cooper Nuclear Station (CNS). This report is submitted in accordance with the requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code,Section XI, Code Case N-532-5. The enclosure contains the completed OAR-1 Owner's Activity Report form, a table identifying the description of items with flaws or relevant conditions that required evaluation for continued service, and a table providing an abstract of repair/replacement activities required for continued servfoe.
This letter does not contain commitments. Should you have any questions regarding this matter, please contact me at (402) 825-2788.
Sincerely, Licensing Manager
/bk
Enclosure:
OAR-1 Owner's Activity Report cc: Regional Administrator w/enclosure Cooper Project Manager w/enclosure USNRC - Region IV USNRC - NRR Plant Licensing Branch IV Senior Resident Inspector w/enclosure NPG Distribution w/o enclosure USNRC-CNS CNS Records w/enclosure
~OOPER NUCLEAR STATION P.O. Box 98/ Brownville, NE 68321-0098 Telephone: (402) 825-3811 / Fax: (402) 825-5211 www.nppd.com
NLS2019005 Enclosure Page 1 of 6 Enclosure OAR-1 Owner's Activity Report
NLS2019005 Enclosure Page2 of6 FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number _R_E_3_0_-_1_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __
Plant Cooper Nuclear Station, P.O. Box 98, 72676 648A Ave, Brownville, NE 68321 Unit No. Commercial Service Date 7/1/1974 Refueling Outage No. _R_E_3_0_ _ __
(W applicable)
Current Inspection Interval 5th Interval (Class 1, 2, 3); 3rd Interval (Class MC)
(1st. 2nd, 3rd, 4th, other)
Current Inspection Period 1st Period (Class 1, 2, 3, MC)
(1st, 2nd, 3rd)
Edition and Addenda of Section XI applicable to the inspection plans 2007 Edition, 2008 Addenda Date and Revision of inspection plans 1/24/19, Revision 2 (Class 1, 2, 3 combined)
Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans Same Code Cases used for inspection and evaluation: N-513-4 Approved per Relief Request RR5-03, N-532-5 (If applicable, including cases modified by Case N-532 and later revisions)
CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of RE30 conform to the requirements of Section XI. (Refueling Outage Number) 0,µ~ Signed Ste~son-Acting Engineering Programs & Components Manager Date 2/8/2019 Owner or Owne(s Designee, nu.e ----------------
CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by The Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's ActivityReport, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or loss of any kind arising from or connected with this inspection.
Scott Masca NB# 14725, Endorsements C, I, N, R (National BoardNumber and Endorsement)
Date (N-532-5)
NLS2019005 Enclosure Page 3 of 6 COOPER NUCLEAR STATION TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Item Description Category and Evaluation Description Item Number On 9/12/18, a localized area of wall thinning below the The pipe section was evaluated by the application of Code Case N-513-design minimum wall thickness was identified on eighteen 4 as approved per Relief Request RR5-03 to allow continued operation D-B, D2.10 (18) inch diameter Service Water piping section SW-E until it could be repaired in refueling outage RE30.
2851-3. The condition was entered into the station corrective action program per CR-CNS-2018-05403.
On 9/14/18, a localized area of wall thinning below the The pipe section was evaluated by the application of Code Case N-513-design minimum wall thickness was identified on eighteen 4 as approved per Relief Request RR5-03 to allow continued operation D-B, D2.10 (18) inch diameter Service Water piping section SW-E until it could be repaired in refueling outage RE30.
2851-3. The condition was entered into the station corrective action program per CR-CNS-2018-05439.
On 9/17 /18, a localized area of wall thinning below the The pipe section was evaluated by the application of Code Case N-513-design minimum wall thickness was identified on eighteen 4 as approved per Relief Request RR5-03 to allow continued operation D-B, D2.10 (18) inch diameter Service Water piping section SW-E until it could be repaired in refueling outage RE30.
2851-7. The condition was entered into the station corrective action program per CR-CNS-2018-05470.
On 9/27/18, a localized area of wall thinning below the The pipe section was evaluated by the application of Code Case N-513-design minimum wall thickness was ioentified on eighteen 4 as approved per Relief Request RR5-03 to allow continued operation D-B, D2.10 (18) inch diameter Service Water piping section SW-P-8A- until it could be repaired in refueling outage RE30.
2851-3. The condition was entered into the station corrective action program per CR-CNS-2018-05663.
On 9/28/18, localized areas of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness were identified on eighteen could be repaired in refueling outage RE30.
D-B, D2.10 (18) inch diameter Service Water piping section SW-P-4A-2851-3. The condition was entered into the station corrective action program per CR-CNS-2018-05684.
NLS2019005 Enclosure Page4 of6 COOPER NUCLEAR STATION TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Item Description Category and Evaluation Description Item Number On 9/28/18, localized areas of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness were identified on eighteen could be repaired in refueling outage RE30.
D-B, 02.10 (18) inch diameter Service Water piping section SW-P-3A-2851-3. The condition was entered into the station corrective action program per CR-CNS-2018-05691.
On 9/29/18, localized areas of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness were identified on eighteen could be repaired in refueling outage RE30.
D-B, 02.10 (18) inch diameter Service Water piping section SW-ZS-2851-7. The condition was entered into the station corrective action program per CR-CNS-2018-05713.
On 9/29/18, localized areas of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness were identified on eighteen could be repaired in refueling outage RE30.
D-B, 02.10 (18) inch diameter Service Water piping section SW-Z6-2851-7. The condition was entered into the station corrective action program per CR-CNS-2018-05716.
On 10/7/18,* a localized area of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness was identified Jon eighteen could be repaired in refueling outage RE30.
D-B, 02.10 (18) inch diameter Service Water piping section SW-P-3C-2851-3. The condition was entered into-the station corrective action program per CR-CNS-2018-06138.
On 10/7/18, a localized area of wall thinning below the The pipe section was evaluated to allow continued operation until it design minimum wall thickness was identified on eighteen could be repaired in refueling outage RE30.
D-B, 02.10 (18) inch diameter Service Water piping section SW-Z12-285F7. The condition was entered into the station corrective action program per CR-CNS-2018-06140. .
NLS2019005 Enclosure Page 5 of6 COOPER NUCLEAR STATION TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Repair/
Date Code Class Item Description Description of Work Replacement Completed Plan Number Localized wall thinning identified in pipe section Pipe below Min-Wall. Replaced section of 3 SW-E-11-2852-8 was replaced in Cycle 30. This Service Water pipe in Cycle 30 per Work Order 12/18/16 16-045R3 condition was identified in CR-CNS-2016-08783. 5148640.
Localized wall thinning identified in pipe section Pipe was below Min-Wall. Repaired section of SW-E-9-2851-3 downstream of support SW-H-58 Service Water pipe per Work Order 5166222.
3 12/16/16 16-047 was repaired in Cycle 30. Condition identified in CR-CNS-2016-08790.
Service water pump C (SW-P-C) sent to Repaired the pump columns and discharge 3 manufacturer for restoration. Sections of pump head by weld build up per PO# 4500189099 3/30/17 15-052R2 columns and discharge head were thinned. and reinstalled per Work Order 5061142.
Localized wall thinning identified by CR-CNS- Pipe below Min-Wall. Replaced section of
- - -- 3 2018-01415 and CR-CNS-2018-01416 in pipe Service Water pipe per Work Order 5235199.
3/15/18 18-016 section SW-E-4-2851-3 downstream of SW-H-52 was repaired in Cycle 30.
As identified in Table 1, the localized wall Pipe was below Min-Wall. Replaced section of 3 thinning identified in pipe section SW-E thinned pipe per Work Order 5265739. 10/18/18 18-039 2851-3 was replaced in RE-30.
As identified in Table 1, the localized wall Pipe was below Min-Wall. Repaired thin 3 thinning identified in pipe section SW-E-8-2851- section of pipe per Work Order 5266082. 10/18/18 18-040 3 was repaired in RE30.
As identified in Table 1, the localized wall Pipe was below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-E-7-2851- Service Water pipe per Work Order 5266083. 10/18/18 18-041 7 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-P-3A- Service Water pipe per Work Order 5267092. 10/18/18 18-044 2851-3 was repaired in RE30.
NLS2019005 Enclosure Page 6 of6 COOPER NUCLEAR STATION TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Repair/
Code Class Date Item Description Description of Work Replacement Completed Plan Number As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-P-4A- Service Water pipe per Work Order 5267091. 10/18/18 18-045 2851-3 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-P-8A- Service Water pipe per Work Order 5267011. 10/18/18 18-046 2851-3 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-28-2851-7 Service Water pipe per Work Order 5267093. 10/18/18 18-047 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-26-2851-7 Service Water pipe per Work Order 5267094. 10/18/18 18-048 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-212-2851- Service Water pipe per Work Order 5268304. 10/18/18 18-050 7 was repaired in RE30.
As identified in Table 1, the localized wall Pipe below Min-Wall. Repaired section of 3 thinning identified in pipe section SW-P-3C- Service Water pipe per Work Order 5268305. 10/18/18 18-051 2851-3 was repaired in RE30.
Cracked welds found on support RF-H71 were Hanger was welded per work order 5267634.
1 10/28/18 18-057 repaired in RE30.