IR 05000390/2021003
ML21314A547 | |
Person / Time | |
---|---|
Site: | Watts Bar |
Issue date: | 11/10/2021 |
From: | Tom Stephen Division Reactor Projects II |
To: | Jim Barstow Tennessee Valley Authority |
References | |
IR 2021003 | |
Download: ML21314A547 (24) | |
Text
November 10, 2021
SUBJECT:
WATTS BAR NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000390/2021003 AND 05000391/2021003
Dear Mr. Barstow:
On September 30, 2021, the U.S. Nuclear Regulatory Commission ( NRC) completed an inspection at Watts Bar. On October 28, 2021, the NRC inspecto rs discussed the results of this inspection with Mr. Anthony Williams and other members of your staff. The results of this inspection are documented in the enclosed report.
Two findings of very low safety s ignificance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of th e Enforcement Policy.
If you contest the violations or the significance or severity o f the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Reg ulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies t o the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Watts Bar.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administ rator, Region II; and the NRC Resident Inspector at Watts Bar.
The Regional Administrator has authorized to IP 92722, Follow U p Inspection For Any Severity Level (SL) I or II Traditional Enforcement Violation Or For Two or More Severity Level III Traditional Enforcement Violations in A Twelve Month, to review the licensees response to the Notice of Violation (NOV) dated December 7, 2020 (ML21027A394) because the NOV dated November 6, 2020 (ML20310A341) issued by the NRCs Office of En forcement (OE) contained one SL II and four SL III. Therefore, the inspection of the li censees response and their corrective actions were not appropriately sampled using the bas eline inspection or inspected using supplemental inspection resources. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Thomas A. Stephen, Chief Reactor Projects Branch 5 Division of Reactor Projects
Docket Nos. 05000390 and 05000391 License Nos. NPF-90 and NPF-96
Enclosure:
As stated
Inspection Report
Docket Numbers: 05000390 and 05000391
License Numbers: NPF-90 and NPF-96
Report Numbers: 05000390/2021003 and 05000391/2021003
Enterprise Identifier: I-2021-003-0014
Licensee: Tennessee Valley Authority
Facility: Watts Bar Nuclear Plant
Location: Spring City, TN 37381
Inspection Dates: July 01, 2021 to September 30, 2021
Inspectors: A. Butcavage, Reactor Inspector W. Deschaine, Senior Resident Inspector K. Miller, Resident Inspector D. Simpkins, Senior Tech Training Program Specialist
Approved By: Thomas A. Stephen, Chief Reactor Projects Branch 5 Division of Reactor Projects
Enclosure SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitori ng the licensees performance by conducting an integrated inspection at Watts Bar Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Proc ess is the NRCs program for overseeing the safe operation of commercial nuclear power react ors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Inadequate Design of Component Cooling System Pump Seal Mountin g Bolts Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71152 Systems NCV 05000390,05000391/2021003-01 Open/Closed An NRC identified Green finding and associated non-cited violat ion (NCV) of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified for the licensees failure to adequately design a plant modification of safety related pumps. Specifically, the licensee failed to properly design threaded fasteners retaining the mech anical seal housings on all five of Unit 1 and 2's safety relat ed component cooling system (CCS) pumps. This finding closes URI 05000391/2021012-01.
2A-A Component Cooling System Pump American Society of Mechanical Engineers (ASME)
XI Repair Resulted in Use of Non-Code Pressure Retaining Bolt M aterial Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [H.8] - 71152 Systems NCV 05000391/2021003-02 Procedure Open/Closed Adherence An NRC identified Green finding and associated NCV of 10 CFR Pa rt 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was iden tified for the licensees failure to ensure that a repair of the 2A-A Component Cooling System (C CS) Pump was performed in accordance with Section XI of the ASME Boiler and Pressure V essel Code. Specifically, the licensee failed to comply with licensee procedure NPG-SPP-09.1. 3, ASME Section XI Repair
/ Replacement Activities Program, for replacement of threaded fasteners retaining the mechanical seal housing on the safety related 2A-A CCS pump. T his finding closes URI 05000391/2021012-01.
Additional Tracking Items
Type Issue Number Title Report Section Status URI 05000391/2021012-01 2A-A CCS Pump Seal 71152 Closed Bolting Failure LER 05000391/2020-004-00 LER 2020-004-00 for Watts 71153 Closed Bar Nuclear Plant, Unit 2, Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking
LER 05000390/2021-001-00 LER 2021-001-00 for Watts 71153 Closed Bar Nuclear Plant, Unit 1, Control Room Emergency Ventilation System Inoperable due to Main Control Room Door Being Left Open LER 05000391/2019-002-00 LER 2019-002-00 for Watts 71153 Closed Bar Nuclear Plant, Unit 2, Breach Due to Penetration Boot Seal Separation Results in Shield Building Inoperability NOV 05000390/2020013-01 Violation E (AV 2 of the 92722 Closed NRCs letter of March 9, 2020) Failure to follow TVA Procedure NPG-SPP-01.2.1 during a procedure change NOV 05000390/2020013-04 Violation B (AV 6 of the 92722 Closed NRCs letter of March 9, 2020) Failure to follow TVA Procedure 1-SOI-74.01 while operating the RHR system during a Unit 1 Reactor Start-up
PLANT STATUS
Unit 1 operated at or near 100 percent rated thermal power for the entire inspection period.
Unit 2 began the inspection period at 90 percent rated thermal power. On September 10, 2021, the unit was shutdown for a mid-cycle outage where it remained for the rest of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of th e inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise note d. Currently approved IPs with their attached revision histories are located on the public web site at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspe ction activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Wa ter Reactor Inspection Program - Operations Phase. The inspectors reviewed selected p rocedures and records, observed activities, and interviewed personnel to assess licens ee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergen cy declared by the President of the United States on the public health risks of the coronavi rus (COVID-19), resident and regional inspectors were directed to begin telework and to remo tely access licensee information using available technology. During this time, the resident insp ectors performed periodic site visits each week, increasing the amount of time on site as loca l COVID-19 conditions permitted.
As part of their onsite activities, resident inspectors conduct ed plant status activities as described in IMC 2515, Appendix D; observed risk significant ac tivities; and completed on site portions of IPs. In addition, resident and regional baseline in spections were evaluated to determine if all or a portion of the objectives and requirement s stated in the IP could be performed remotely. If the inspections could be performed remot ely, they were conducted per the applicable IP. In some cases, portions of an IP were comple ted remotely and on site. The inspections documented below met the objectives and requirement s for completion of the IP.
REACTOR SAFETY
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial w alkdowns of the following systems/trains:
(1) Unit 1 B train Motor Driven Auxiliary Feedwater (MDAFW)syst em on August 31, 2021 (2) Unit 2 Residual Heat Removal System during the mid-cycle outage on September 15, 2021 (3) Unit 2 A train Safety Injection system on September 29, 202 1
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protect ion program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
(1) Diesel Generator Rooms and Diesel Generator Building Cable Chases (1st floor) on August 30, 2021 (2) High combustible load areas in the control building (i.e., Auxiliary Instrument Rooms, Computer Room, Shift Managers Offi ce, Conference Room) on September 1, 2021 (3) Aux Building Corridor Elev. 692 on September 2, 2021 (4) Unit 2 Lower Containment on September 11, 2021 (5) Unit 2 Annulus (Shield Building) El. 702.78 to the top of the Containment Dome on September 18, 2021
71111.11Q - Licensed Operator Requalification Program and Licen sed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
(1) The inspectors observed and evaluated licensed operator per formance in the Control Room during the Unit 2 mid-cycle shutdown on September 10th and the Reactor Coolant System (RCS) drain down to hot mid-loop on September 17 th.
Licensed Operator Requalification Training/Examinations (IP Sec tion 03.02) (1 Sample)
(1) The inspectors observed and evaluated a licensed operator r equalification simulator scenario for crew 5 group 5B on August 4, 2021. Additionally, t he inspectors observed and evaluated a licensed operator requalification simu lator scenario for crew 3 group 3A on August 10, 2021 and group 3B on August 11, 2 021. Together these observations make up one sample.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to en sure the following structures, systems, and components (SSCs) remain capable of pe rforming their intended function:
(1) System 68C - U2 Pressurizer Pressure Operated Relief Valve (PORV) (2-FCV-68-334-B)
71111.13 - Maintenance Risk Assessments and Emergent Work Contr ol
Risk Assessment and Management Sample (IP Section 03.01) (5 Sam ples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure config uration changes and appropriate work controls were addressed:
(1) Risk assessment for (week of) July 12, 2021, with the 1B 48 0V Electric Board Room chiller out of service for component outage.
(2) Risk assessment for (week of) August 23, 2021, with the B-B 480V Electric Board Room chiller out of service along with B spent fuel pool heat e xchanger outlet valve due to maintenance.
(3) Risk assessment for (week of) September 7, 2021, with a num ber of safety related chillers out of service for maintenance earlier in the week and a planned Unit 2 shutdown later in the week.
(4) Unit 2 risk assessment for performance of RCS drain down to mid-loop to support removal of steam generator nozzle dams and installation of stea m generator primary manway covers. RCS level was restored above elevation 722 feet on September 18, 2021 at 1455, reducing Overall Station Risk from an Orange to a Yellow Risk Condition.
(5) Unit 2 risk assessment for performance of RCS drain down to mid-loop to support removal of steam generator nozzle dams and installation of stea m generator primary manway covers. RCS level was restored above elevation 722 feet on September 26, 2021 at 1745, reducing Overall Station Risk from an Orange to a Yellow Risk Condition.
71111.15 - Operability Determinations and Functionality Assessm ents
Operability Determination or Functionality Assessment (IP Secti on 03.01) (5 Samples)
The inspectors evaluated the licensee's justifications and acti ons associated with the following operability determinations and functionality assessme nts:
(1) Relief valve found leaking by during 1A Safety Injection Pu mp run; condition report (CR) 1721022 (2) U2 auxiliary feedwater system control air pressure regulato r for steam generator #3 level control valve 2-LCV-3-148 was found out of tolerance; CR 1722737 (3) Auxiliary Building Gas Treatment System (ABGTS) potentially inoperable with Auxiliary Building door A057 having an air lock seal not operat ing correctly allowing both doors to air lock to be opened at the same time; CR 172255 7 (4) Breaker (WBN-2-BKR-030-0448) for the 2A-A Diesel Generator room exhaust fan 1A is not working correctly; CR 1715994 (5) 1A Motor Driven Auxiliary Feedwater (MDAFW) Pump Outboard Bearing Horizontal vibration reading in the Alert Range; CR 1718138
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the following post-maintenance test ac tivities to verify system operability and functionality:
(1) Work Order 120660138, Essential Raw Cooling Water Strainer 1B-B Inspection and Packing Replacement on 6/29 & 7/6/2021.
(2) Work Order 122325520, Replace 30RX Relay for Containment Sp ray (CS) Pump 1B-B due to a faulty electrical contact on 8/11/2021 (3) Work Order 122328570, Motor Driven AFW Pump 2B-B SG 4 Level, Replace the Actuator Diaphragm and Diaphragm Washer for WBN-2-LCV-003-0171-B, was field complete on September 17, 2021.
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
(1) The inspectors evaluated Unit 2 mid-cycle forced outage act ivities from September 10 to October 1, 2021.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (2 Samples)
(1) WO 122202176, 1-SI-0-24, Measurement of the At-Power Modera tor Temperature Coefficient, on August 3, 2021.
(2) WO 121744229, 1-SI-68-35, Pressurizer Heater Capacity, on A ugust 5, 2021
Inservice Testing (IP Section 03.01) (1 Sample)
(1) WO 121838980, 2-SI-74-901-A, Residual Heat Removal Pump 2A-A Quarterly Performance Test, on August 17, 2021.
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
(1) WO 122335062, 2-SI-68-32, Reactor Coolant System Water Inve ntory Balance, on August 14, 2021
FLEX Testing (IP Section 03.02) (1 Sample)
(1) WO 121699475, 0-SOI-360.003, 6900V FLEX Diesel Generator Sy stem, revision 24, for the operation of the 6900V Diesel Generator (DG) 3A on Sept ember 2, 2021.
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (2 Samp les)
The inspectors evaluated:
(1) The residents observed the site emergency response to a tra ining evolution that involved a Loss of Offsite Power, a RCS Cold Leg Loop 3 break, and then a Loss of all Power which led to a general emergency declaration on July 14, 2021.
(2) The residents observed the site emergency response to a tra ining evolution that involved a small RCS leak on Loop 3 that grows into a large bre ak LOCA which after losing multiple safety pumps leads to a general emergency decla ration on September 1, 2021.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submitt als listed below:
MS05: Safety System Functional Failures (SSFFs) Sample (IP Sect ion 02.04) (2 Samples)
(1) Unit 1 July 2020 - June 2021 (2) Unit 2 July 2020 - June 2021
MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)
(1) Unit 1 July 2020 - June 2021 (2) Unit 2 July 2020 - June 2021
MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Sampl es)
(1) Unit 1 July 2020 - June 2021 (2) Unit 2 July 2020 - June 2021
MS10: Cooling Water Support Systems (IP Section 02.09) (2 Sampl es)
(1) Unit 1 July 2020 - June 2021 (2) Unit 2 July 2020 - June 2021
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sampl e)
The inspectors reviewed the licensees implementation of its co rrective action program related to the following issues:
(1) Corrective actions resulting from CR 1651444, and closeout of Licensee Event Report 391/2020-004-00, Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking (ADAMS Accession No. ML21007A022).
On November 11, 2020, it was determined, after evaluation of th e Watts Bar Nuclear Plant (WBN) Unit 2 Steam Generator (SG) tube eddy current test data collected during the 2020 outage, that the WBN Unit 2 Reactor Coolant Sys tem pressure boundary did not meet the performance criteria for SG tube stru ctural integrity.
Specifically, SG number 3 failed the condition monitoring asses sment for conditional burst probability.
The cause of the degradation in the SGs, and particularly SG nu mber 3, was determined to be axial, outside diameter stress corrosion crack ing (ODSCC) of the Alloy 600 mill annealed (MA) SG tubing coincident with the carb on steel tube support plate intersections.
Corrective actions taken included plugging and stabilizing degr aded SG tubes as required by the SG Program. Corrective actions to prevent recur rence also included a reduction in operating temperature and power level, a planned m id-cycle SG inspection and steam generator replacement to occur sooner than anticipated. An LAR was also submitted and approved to support a change to prob ability of detection parameters used in evaluations of SG tubing inspection results.
As typically done in Steam Generat or Programs, WB -2 based their expected life cycle predictions for the Alloy 600 material in the WB-2 SG's, on what appeared to be a reasonable assumption. That is, that the WB-2 SG tubing deg radation would be similar to their previous experience with the WB Unit 1 which u tilized the same type material in its original SGs. WB-2 also considered existing in dustry operating experience data for mill annealed Alloy 600 tubing as required by the Industry Steam Generator Program.
However following the fall 2020 inspections, those assumptions proved to be not conservative when ODSCC at tube support plate locations exceede d expected degradation levels beyond those of WBN Unit-1 and Industry expe rience. While no SG primary to secondary leakage or other SG tubing issues were reported during the run prior to the 2020 inspections, condition monitoring establi shed criteria for the SG Program contained in Generic Letter 95-05 was exceeded as descr ibed in the LER.
It was noted by the inspectors that the licensee followed the t ypical approach applying industry and plant specific experience data when predi cting SG Tubing life cycles based on anticipated degradation mechanisms, therefore n o violation was identified specific to the condition monitoring aspect of this LER.
However, per existing 10CFR50.59 procedures in place at the tim e of the event, a violation was issued for the failure of the licensee to adequat ely perform a detailed evaluation of the licensees use of specific GL 95-05 method of evaluation concerning use of a different Probability of Detection values outside of t hose prescribed for use in GL-95-05. NCV 05000391/2020004-01, "Failure to perform a 50.59 evaluation for a change in calculational methodology", is included in NRC ROP report number 2020-004 (Adams Accession No.(ML21042B877). The violation was addres sed by USNRC Report, Watts Bar Nuclear Plant, Unit 2 - Issuance of Amendmen t No. 48 Regarding Use of Alternate Probability of Detection Values for Beginning of Cycle in Support of Operational Assessment (EPID L-2020-LLA-0273), February 2021. (ADAMS Accession No. ML21027A167).
Based on the Fall 2020 WB-2 SG inspection results, the predicte d allowable in service time based on established SG Program criteria did not s upport a full cycle of operation on the WB-2 unit. Additional evaluations, power and temperature reductions were implemented in order to provide reasonable assu rance that the WB-2 SG's could adequately perform their intended function within th e SG program criteria which provided reasonable assurance that the plant could operat e to a predicted point in time at which, a midcycle inspection would be performe d. The midcycle inspection was completed on 9/29/21.
The IP inspection Procedure 71111.08 (Steam Generator Inspectio n Section) 03.01, Inservice Inspection Activities Samples, Section "d", Steam Gen erator Tube Inspection Activities, was used as a guideline to monitor and r eview the WB-2 mid-cycle inspection activities and inspection results.
Based on the evaluation of the mid-cycle eddy current inspectio n data evaluation as documented in LTR-CDMP-21-48, all four Watts Bar Unit 2 SGs ope rated within the GL 95-05 conditional probability of burst and leak rate require ments during the recently completed Cycle 4a. leading up to the mid-cycle inspec tion. The mid cycle inspection results have been evaluated and reviewed by the OEM. The OEM
provided a justification for start up and a 90 day cycle run wi thin the SG program requirements. The 90 day report provides additional time for a dditional detailed data review and final report completion followed with submittal to t he NRC, NRR group. The final report is expected to provide a basis for rea sonable assurance for a cycle run time to allow plant operation until the accelerated S G replacement project implementation point. The licensee has moved the steam genera tor replacement outage forward as a proactive measure as a result of the accele rated degradation discovered during the 2020 SG Inspections documented in TVA CR 1651444, and is currently scheduled for the spring 2022 refuel outage.
The sample documents reviewed that support that an adequate app roach has been taken by the Licensee to provide reasonable assurance that adequate corrective action have been taken to address the Steam Generato r degradation issue are included in the documents review section.
71153 - Follow Up of Events and Notices of Enforcement Discreti on
Event Report (IP Section 03.02) (3 Samples)
The inspectors evaluated the following licensee event reports ( LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx :
(1) LER 390/2021-001-00, Control Room Emergency Ventilation Sys tem (CREVS)
Inoperable due to Main Control Room Door Being Left Open (ADAMS accession:
ML21130A027). The inspectors reviewed the LER and determined th at the licensee complied with applicable regulatory requirements, Technical Spe cifications, and 50.73 reporting criteria. No violations of NRC requirements occ urred. The inspectors determined that Technical Specification (TS) Limiting Condition of Operation (LCO)
3.7.10 contained a note allowing the control room envelope (CRE ) boundary to be opened intermittently under administrative controls. This note only applies to openings in the CRE boundary that can be rapidly restored to th e design condition, such as doors, hatches, floor plugs, and access panels. For ent ry and exit through doors, the administrative control of the opening is performed b y the person(s)
entering or exiting the area. For other openings, these control s are proceduralized and consist of stationing a dedicated individual at the opening who is in continuous communication with the operators in the CRE. This individual wi ll have a method to rapidly close the opening and to restore the CRE boundary to a condition equivalent to the design condition when a need for CRE isolation is indica ted. The inspectors noted that several signs posted on the CRE boundary door state that Failure to Properly Close this Door Causes th e Loss of Nuclear Safety System Function and CRE Boundary Door - Ensure this Door is CLOSED BY HAND. These signs alert plant personnel to close the CRE boundary door when they enter or exit the area. However, there were approximately eight instances in the past 5 years where plant personnel entered and exited the CRE boundary doors and f ailed to ensure the doors were fully closed, causing a control room alarm after 90 seconds. This resulted in CREVS being declared inoperable and a loss of safet y function for several minutes until the CRE boundary door was closed by control room operators, thus meeting the requirements for an LER submittal. The licensee has initiated a CR level 2 Apparent Cause to review the past occurrences and determine i f any additional
actions are needed to effectively address any human performance error issues.
(2) LER 391/2019-002-00, Breach Due to Penetration Boot Seal Se paration Results in Shield Building lnoperability. The inspectors reviewed the LER and determined that a Green NCV was issued and documented in the quarterly resident i ntegrated inspection report NCV 05000391/2019002-06, Failure to Follow Sy stem Status Control Procedure Results in a Gap in a Bellows Seal and Inoper ability of the Unit 2 Shield Building, dated August 12, 2019 (ML19225B957). No addit ional performance issues or violations of NRC requirements were identified.
(3) LER 391/2020-004-00, Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking (ADAMS Accession No. ML21007A022.) The inspection conclusions associated with this LER are documented in this report under Inspection Results Section IP Section 02.03, Annual Follow-up o f Selected Issues.
OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNOR MAL
92722 - Follow-Up Inspection for Any Severity Level I or II Tra ditional Enforcement Violation or for Two or More Severity Level III Traditional Enforcement Viol ations in a 12-Month Period
Inspection Procedure (IP) 92722 - Follow Up Inspection For Any Severity Level I or II Traditional Enforcement Violation or For Two or More Severity L evel III Traditional Enforcement Violation in A 12 month period.
On November 6, 2020, the NRC issued a Notice of Violation and P roposed Imposition of Civil Penalty (NOV) to TVAs Watts Bar Nuclear Plant (WBN) (ML20310A341). The NOV contained five separate violations (A - E) and related civil penalties, p ertaining to events occurring at WBN Unit 1 in late 2015 to early 2016. In response to the NOV, TVA provided its written reply by letter dated December 7, 2020 (ML21027A394). Based on careful consideration of TVAs written reply, the NRC subsequently issued a revised NOV by let ter dated July 23, 2021 (ML21200A134). The revision concluded that although five viola tions occurred as stated in the November 6, 2020, Notice, revisions were necessary to Violations B, C, and E as discussed below. Note that Violations A and D of the original November 6, 2020 NOV remained unchanged as discussed in the NRCs letter dated July 23, 2021.
Additionally, the NRC concluded that the information regarding the reason for the violations and steps taken to prevent recurrence, and the date when full compl iance was achieved, was adequately addressed in TVAs December 7, 2020 written response.
(Closed) VIO 05000390/2020013-04, Failure to follow TVA Procedu re 1-SOI-74.01 while operating the RHR system during a Unit 1 Reactor Start-up.
The NRCs original Notice of November 6, 2020 documented a Seve rity Level III problem involving 10 CFR Part 50, Appendix B, Criterion V, Instruction s, Procedures, and Drawings, (Violation B, failure to follow TVA Procedure 1-SOI-74.01) and 10 CFR Part 50, Appendix B, Criterion XVII, Quality Assurance Records, (Violation C, fail ure to maintain operator logs). A civil penalty of $300,000 was also proposed.
After reevaluation, the NRC determined that to enhance clarity and understanding of the NRCs safety significance evaluati on and civil penalty assessment pro cess, the two violations (B and C) combined in the original problem would be reevaluated and do cumented separately.
As documented in the NRCs revised NOV dated July 23, 2021, bot h violations occurred as stated in the November 6, 2020 Notice. However, the staff conc luded that there was not sufficient evidence to support the original conclusion that the operators engaged in deliberate misconduct for Violation B in the NRCs original Notice of Nove mber 6, 2020. Therefore, absent willfulness, the significance of the violation was assessed in accordance with Reactor Oversight Program (ROP). In accordance with ROP, the significance of violation B involving the failure to follow plant procedures was evaluated under the NRCs Significa nce Determination Process (SDP) and was determined to be of very low safety significance (Green). Additionally, violation B was appropriately characterized as NCV consistent with Sectio n 2.3.2 of the Enforcement Policy. In accordance with the Enforcement Policy, the Green fi nding and associated violation are not assessed a civil penalty (CP). Therefore, this VIO 050 00390/2020013-04 was closed and it was being treated as NCV 05000390/2020013-04.
Violation C of the NRCs original Notice of November 6, 2020, r egarding failure to maintain operator logs, is discussed below.
(Discussed) VIO 05000390/2020013-03, Failure to Maintain Operat ing Logs.
Regarding Violation C of the NRCs original Notice of November 6, 2020, the NRCs reevaluation concluded that shift managements failure to revie w logs occurred as stated in the November 6, 2020, Notice (violation C). However, as documented in the NRCs revised NOV dated July 23, 2021, the NRC concluded that this violation did not involve willfulness.
Accordingly, Violation C was appropriately characterized as an SL III, with no civil penalty.
(Closed) VIO 05000390/2020013-01 Failure to follow TVA Procedur e NPG-SPP-01.2.1 during a procedure change.
The NRCs original Notice of November 6, 2020 documented a Seve rity Level III violation (Violation E) involving a willful failure to follow procedures as required by 10 CFR 50, Appendix B, Criterion V. Additionally, a civil penalty of $300,000 was proposed for Violation E.
After reevaluation, the NRC concluded that Violation E occurred as stated in the NRCs original Notice of November 6, 2020. However, the staff concluded that there was not sufficient evidence to support the original conclusion of deliberate misco nduct. Therefore, absent willfulness, the significance of the violation was assessed in accordance with ROP. In accordance with ROP, the significance of the failure to follow plant procedures was evaluated under the NRCs SDP and was determined to be of very low safety significance (Green). Additionally, the violation was appropriately charact erized as NCV consistent with Section 2.3.2 of the Enforcement Policy. In accordance with th e Enforcement Policy, the Green finding and associated violation are not assessed a civil penal ty. Therefore, this VIO 05000390/2020013-01 was closed and it was being treated as NCV 05000390/2020013-01.
INSPECTION RESULTS
Inadequate Design of Component Cooling System Pump Seal Mountin g Bolts Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71152 Systems NCV 05000390,05000391/2021003-01 Open/Closed An NRC identified Green finding and associated non-cited violat ion (NCV) of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified for the licensees failure to adequately design a plant modification of safety related pumps. Specifically, the licensee
failed to properly design threaded fasteners retaining the mech anical seal housings on all five of Unit 1 and 2's safety relat ed component cooling system (CCS) pumps. This finding closes URI 05000391/2021012-01.
Description: During the May 2021 PI&R Inspection, the inspecto rs reviewed design documents associated with modifi cation DCN 26968-A, following the inspectors discovery of a broken eyebolt on the 2A-A CCS pump inboard mechanical seal. This modification changed the CCS pump seals from a gland packing design to a Chesterton 221 split mechanical seal design. The inspectors identified that the licensee reused the Manganese Bronze gland eyebolts from the original design to fasten the seal housings t o the pump casings. According to calculation EPMDWP070594, the split mechanical seal housing is an ASME III, Class 3, pressure boundary part for the CCS Pump. This calculation docum ented the adequacy of the fabricated split seal housing to maintain the pressure/temperat ure of the Component Cooling System. The gland eyebolt material is not an approved bolting m aterial for ASME pressure retaining bolting. ASME III, Division 1, Subsection ND, paragr aph ND-2127, Bolting Material, states: (a) Materials for bolts and studs shall conform to the requirements of those specifications listed in Tables I-7.3 and I-8.3. Tables I-7.3 and I-8.3, which are found in ASME III, Division 1, Subsection NA, General Requirements, Appe ndix I, do not include the Manganese Bronze gland eyebolt material (ASTM B 147 - 72, AL 8C ) as an approved bolting material.
Corrective Actions: The licensee is tracking this as a degrade d / nonconforming condition and has corrective actions in place to replace all of the eye b olts in the CCS pumps with approved pressure retaining bolting.
Corrective Action References: CRs 1701046, 1692049, 1695509, 1 710406, 1731647 Performance Assessment:
Performance Deficiency: The failure to adequately design a pla nt modification of the safety related CCS pumps was a perform ance deficiency. Specifically, the licensee failed to properly design threaded fasteners retaining the mechanical sea l housings on all five of the safety related CCS pumps.
Screening: The inspectors determined the performance deficienc y was more than minor because it was associated with the Equipment Performance attrib ute of the Mitigating Systems cornerstone and adversely affected the cornerstone obje ctive to ensure the availability, reliability, and capability of systems that respo nd to initiating events to prevent undesirable consequences. With the threaded fasteners not desig ned to ASME pressure retaining standards the bolts can fail prematurely and adversel y affected the cornerstone objective of ensuring the availability, reliability, and capabi lity of all five of the CCS pumps to transfer heat from various potentially or normally radioactive heat loads to the Essential Raw Cooling Water System (ERCW). The CCS is designed to mitigate t he consequences of Design Basis Events (DBE). A broken eyebolt on the 2A-A CCS pu mp inboard mechanical seal was discovered in May 2021. The licensee declared the pum p inoperable and replaced with a new bolt.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The finding was determined to be very low safety significance (Green) because i t (1) was a design deficiency that did not affect the operability of the CCS pumps, (2) did n ot represent a loss of the PRA function of a single train Technical Specification (TS) system for greater than its TS allowed outage time, (3) did not represent a loss of the PRA function o f one train of a multi-train TS
system for greater than its TS allowed outage time, (4) did not represent a loss of the PRA function of two separate TS systems for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, (5) did not represent a loss of PRA system and/or function as defined in the PRIB or licensee P RA for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and (6) did not represent a loss of the PRA function of one or more non-TS trains of equipment designated as risk-significant in accordance with the licensees maintenance rule program for greater than 3 days.
Cross-Cutting Aspect: Not Present Performance. No cross-cuttin g aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance. Specifically, the performance deficiency occurred in 1994 during development of Calculation EPMDWP070594.
Enforcement:
Violation: 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that measures shall be established to assure that applicable regulat ory requirements and the design basis, as defined in 10 CFR 50.2 and as specified in the licensee application, for those structures, systems, and components to which this appendix appl ies are correctly translated into specifications, drawings, procedures, and instructions. M easures shall also be established for the selection and review for suitability of app lication of materials, parts, equipment, and processes that are essential to the safety-relat ed functions of the structures, systems, and components.
Contrary to the above, since 1994, the licensee failed to estab lished measures to assure that applicable regulatory requirements and the design basis, as def ined in 10 CFR 50.2 and as specified in the licensee application, for those structures, sy stems, and components to which this appendix applies are correctly translated into specificati ons, drawings, procedures, and instructions. Specifically, the licensee failed to properly de sign threaded fasteners retaining the mechanical seal housings on all five of Unit 1 and 2's safe ty related CCS pumps.
Enforcement Action: This violation is being treated as a non-c ited violation, consistent with Section 2.3.2 of the Enforcement Policy.
The disposition of this finding and associated violation closes URI: 05000391/2021012-01.
2A-A Component Cooling System Pump American Society of Mechanical Engineers (ASME)
XI Repair Resulted in Use of Non-Code Pressure Retaining Bolt M aterial Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [H.8] - 71152 Systems NCV 05000391/2021003-02 Procedure Open/Closed Adherence An NRC identified Green finding and associated non-cited violat ion (NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawing s, was identified for the licensees failure to ensure that a repair of the 2A-A Componen t Cooling System (CCS) Pump was performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code.
Specifically, the licensee failed to comply with licensee proce dure NPG-SPP-09.1.3, ASME Section XI Repair / Replacement A ctivities Program, for replac ement of threaded fasteners retaining the mechanical seal housing on the safety related 2A-A CCS pump. This finding closes URI 05000391/2021012-01.
Description: On May 5, 2021, during a CCS walkdown with the sy stem engineer for the problem identification and resolution (PI&R) inspection, the in spectors identified abnormal leakage coming from the 2A-A CCS pump inboard mechanical seal. Upon further investigation, the licensee identified that one of two inboard seal housing fasteners (gland eyebolts) was sheared/missing from the seal housing. The thread ed end of the bolt and hex nut was observed lying in bottom of the seal leak-off catch bas in. As a result of this observation, the licensee declared the 2A-A CCS pump inoperable at 5:10 p.m. on May 5, 2021 and entered technical specification (TS) limiting conditio n for operation (LCO) 3.7.7 which requires restoration of the pump within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. At the time of discovery, the pump was not in operation and was last operated on March 16, 2021 du ring surveillance testing. Work Orders (WOs)122102466 and 122102469 replaced the broken eyebolt and the pump was returned to service on May 6, 2021.
Further review of the WOs by the inspectors noted that licensee did not follow their ASME Section XI Repair/Replacement Activities Program procedure (NPG -SPP-09.1.3) and the Technical Instruction for ASME Section XI Repairs and Replaceme nts (0-TI-100.014). Specifically, the licensee did not treat the broken M anganese Bronze eyebolt replacement as an ASME Section XI Code repair, which required a pproval of a repair plan by the Authorized Nuclear Inspector (ANII) using Form NPG-SPP-09.1.3-4, ANII Review Form, TVA Form 41383. WO 122102466, which replaced the broken eyebolt, contained Step 4, "Ensure Section XI Forms are completed and routed for review in accordance with NPG-SPP-09.1.3 and 0-TI-100.014. N/A if not required. was marked N /A, when in fact the forms were required for replacement of pressure retaining bolting. Th ere was no such form (Form 41383) in the WO. In addition, the Manganese Bronze eyebolt mat erial was not approved by the ASME Code. The current eyebolt installation is a nonconform ing condition. This nonconforming condition actually applies to all five of Unit 1 and 2's CCS pumps, since all the pumps have the same Manganese Bronze eyebolt material that was not an approved bolting material for ASME pressure retaining bolting.
Corrective Actions: The licensee is tracking this as a degrade d / nonconforming condition and has corrective actions in place to replace all of the eye b olts in the CCS pumps with approved pressure retaining bolting.
Corrective Action References: CRs 1701046, 1692049, 1695509, 1 710406, 1731647 Performance Assessment:
Performance Deficiency: The failure to ensure that a repair of the 2A-A CCS pump was performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code was a performance deficiency. Specifically, the licensee failed to comply with licensee procedure NPG-SPP-09.1.3, ASME Section XI Repair / Replacement Activitie s Program, for replacement of threaded fasteners retaining the mechanical seal housing on the safety related 2A-A CCS pump.
Screening: The inspectors determined the performance deficienc y was more than minor because it was associated with the Equipment Performance attrib ute of the Mitigating Systems cornerstone and adversely affected the cornerstone obje ctive to ensure the availability, reliability, and capability of systems that respo nd to initiating events to prevent undesirable consequences. With the threaded fasteners not repai red in accordance with Section XI of the ASME Boiler and Pressure Vessel Code the bolt s can fail prematurely and adversely affected the cornerstone objective of ensuring the av ailability, reliability, and capability of all five of the CCS pumps to transfer heat from v arious potentially or normally
radioactive heat loads to the Essential Raw Cooling Water Syste m (ERCW). The CCS is designed to mitigate the consequences of Design Basis Events (D BE).
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The finding was determined to be very low safety significance (Green) because i t (1) was a design deficiency that did not affect the operability of the CCS pumps, (2) did n ot represent a loss of the PRA function of a single train TS system for greater than its TS al lowed outage time, (3) did not represent a loss of the PRA function of one train of a multi-tr ain TS system for greater than its TS allowed outage time, (4) did not represent a loss of the PRA function of two separate TS systems for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, (5) did not represent a loss of PRA system and/or function as defined in the PRIB or licensee PRA for greater than 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> s, and (6) did not represent a loss of the PRA function of one or more non-TS trains of equipm ent designated as risk-significant in accordance with the licensees maintenance rule program for greater than 3 days.
Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals f ollow processes, procedures, and work instructions. The licensee did not follow their ASME S ection XI Repair /
Replacement Activities Program p rocedure (NPG-SPP-09.1.3) and their Technical Instruction for ASME Section XI Repairs and Replacements (0-TI-100.014). As a result, the replacement of the broken eye bolt resulted in a nonconforming condition.
Enforcement:
Violation: 10 CFR Part 50, Appendix B, Criterion V, Instructi ons, Procedures, and Drawings, states, in part, activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
Contrary to the above, on May 6, 2021, for an activity affectin g quality the licensee failed to accomplish a procedure in accordance with the documented instru ctions. Specifically, the licensee failed to comply with procedure NPG-SPP-09.1.3, ASME Section XI Repair /
Replacement Activities Program, for replacement of threaded fa steners retaining the mechanical seal housing on the safety related 2A-A CCS pump.
Enforcement Action: This violation is being treated as a non-c ited violation, consistent with Section 2.3.2 of the Enforcement Policy.
The disposition of this finding and associated violation closes URI: 05000391/2021012-01.
URI 2A-A CCS Pump Seal Bolting Failure 71152 URI 05000391/2021012-01 Description: On May 5, 2021, during the CCS walkdown with the system engineer for the PI&R inspection, the inspector identified abnormal leakage comi ng from the 2A-A CCS pump inboard mechanical seal. Upon further investigation, the licens ee identified that one of two inboard seal bolts was sheared/missing from the seal housing. T he bolt was observed to be lying in the seal leak off catch basin. As a result of this ob servation, the licensee declared the 2A-A CCS pump inoperable at 5:10 p.m. on May 5, 2021 and entere d technical specification (TS) limiting condition for operation (LCO) 3.7.7 which require s restoration of the pump within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Work Orders (WOs)122102466 and 122102469 replaced th e broken eyebolt and the pump was returned to service on May 6, 2021. An unresolved item (URI) was opened for additional review to determine if appropriate regulatory requir ements or self-imposed
standards were followed for the maintenance of the 2A-A CCS pum p. The inspectors identified two Green findings associated with this URI, that ar e documented under the inspection results section of this report.
Corrective Action Reference(s): CRs 1692049, 1692589, 1695509, 1701046
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 28, 2021, the inspectors presented the integrated i nspection results to Mr.
Anthony Williams and other members of the licensee staff.
17