|
---|
Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292A3921996-06-30030 June 1996 WNP-2 Ten Mile EPZ Evacuation Time Estimate Study. ML17291B2931995-12-31031 December 1995 Adjustable-Speed Drive Retrofit for Ormond Beach Fd Fans. ML17291B1401995-07-0606 July 1995 Technical Evaluation Rept,Wppss Plant No 2,Pump & Valve Ist,Rev 0,Second Ten-Yr Interval. ML17291A9421995-06-30030 June 1995 Rev 0 to IPE of External Events WNP2. ML17291A5691994-12-0707 December 1994 Simulator Facility Certification. ML17291A4481994-10-13013 October 1994 WNP-2 Response to Request for Addl Info on Emergency Classification. ML17290A9181993-12-27027 December 1993 Justification for Revised Tornado Design Criteria,Rev 1. ML17290A6901993-10-0808 October 1993 Revised Significant Hazards Consideration Assessment for WNP-2 Power Uprate W/Elll. ML17290A6861993-09-27027 September 1993 Rev 1 to Evaluation of Sources of Radioactive Matl Found in Cooling Tower Sediments at Washington Nuclear Plant 2. ML17290A3831993-05-18018 May 1993 Rept R-R8-111 Re Flaw in Reactor Recirculation Piping ML17289B0751992-11-23023 November 1992 Rev 0 to Technical Memorandum Tm 2025, Secondary Containment/Standby Gas Treatment Design Basis. ML17289A9881992-10-0707 October 1992 Containment Atmosphere Control Sys (CAC) Summary Issues. ML17289A7251992-06-30030 June 1992 Institutional Custody Fiduciary Svcs. ML17289A7231992-06-30030 June 1992 Institutional Custody Fiduciary Svcs. ML17289A9281992-06-24024 June 1992 WNP-2 Simulator Certification NRC Form 474 Supporting Documentation. ML17289A5351992-05-11011 May 1992 App B, 8X8 Extended Burnup, of EMF-92-040, WNP-2 Cycle 8 Reload Analysis. ML17286B0211991-08-20020 August 1991 Root Cause Analysis Summary, Unsatisfactory Licensed Operator Requalification Program, Reflecting Causes of Operators Continued Inability to Respond to Severe Accident Conditions ML17286A9151991-06-30030 June 1991 Asset Summary 910630. ML17286A9141991-06-30030 June 1991 Summary of Transactions for 900630-910630. ML17285A9631989-12-27027 December 1989 Feedwater Nozzle Insp Rept for Refueling Outage RF89A Spring 1989. ML17285A8871989-08-14014 August 1989 Rev 0 to Commercial Grade Dedication Project for Wppss Contract C-30298. ML17285A6411989-07-31031 July 1989 Instrument Air Sys Review Response to Generic Ltr 88-14. W/Six Oversize Figures ML17285A1971988-12-14014 December 1988 Feedwater Nozzle Insp Rept for Refueling Outage RF88A, Spring,1988. ML20237D3121987-11-30030 November 1987 Final Feedwater Temp Reduction Summary Rept ML17279A6251987-04-30030 April 1987 Rev 2A to Wnp 1,2 10-Mile EPZ Evacuation Time Assessment Study. ML17279A1911987-04-0707 April 1987 Comparision of Electrical Design of Wye Pattern Globe Valve Actuator W/Ball Valve,Hanford 2 & River Bend Design. Five Oversize Drawings Encl ML17279A2341987-03-31031 March 1987 Washington Nuclear Plant 2 Performance Indicator Rept. ML20207N2661986-12-31031 December 1986 Assessment of Fire Protection Program Responsibilities & Administration ML20215B7271986-11-25025 November 1986 Feedwater Nozzle Insp Rept for Refueling Outage RF86A, Spring 1986 ML17278B0001986-08-22022 August 1986 Results of Insp of WPPSS-2 Cycle 1 Discharge Fuel. ML17279A6481986-05-0101 May 1986 Draft Lead Test Assembly Program,Wpps 2. ML17278A8051986-03-31031 March 1986 Safety Review of Wppss Nuclear Project 2 at Core Flow Conditions Above Rated Flow Throughout Cycle 1 & Final Feedwater Temp Reduction. ML17278A4721985-09-30030 September 1985 Crdr & Emergency Procedure Functional Task Analysis Summary Rept. ML17278A4281985-07-31031 July 1985 Washington Nuclear Plant Unit 2 Spray Pond Drift Loss Rept. ML17277B6191985-01-31031 January 1985 Rev 2 to Description of Early Warning Sys for Wppss Nuclear Plants 1 & 2. ML17277B5241984-10-0808 October 1984 Feedwater Piping Thermal Deflection Events, Final Design Engineering Rept ML17277B2451983-12-30030 December 1983 RHR Addendum to Design Verification Program. ML17277B2201983-12-11011 December 1983 Qualification of Purge & Vent Valves at WPPSS-2, Vols 1 & 2 ML20080N1941983-12-0707 December 1983 Excerpt from Qvp Overview Rept,Vol I,Book 1 of 1.Related Info Encl ML17277B2961983-11-30030 November 1983 Rept to Governor J Spellman of State of Wa & Governor V Atiyeh of State of Or. ML17277B2231983-11-0808 November 1983 Qualification of Purge & Vent Valves at WPPSS-2, Vol 4: Rev 4 to Equipment Seismic & Hydrodynamic Requalification of 24-Inch Cylinder Operated Butterfly Valves for CSP-V-3, 4,5,6 & 9 & CEP-V-3A & 4A. ML17277B2221983-11-0404 November 1983 Qualification of Purge & Vent Valves at WPPSS-2, Vol 3: Rev 2 to Equipment Seismic & Hydrodynamic Requalification of 30-Inch Cylinder Operated Butterfly Valves CSP-V-1 & 2 & CEP-V-1A & 2A. ML17277A9431983-10-0707 October 1983 Response to NRC Human Factors Engineering Preliminary Design Assessment Audit Rept of 830826. ML17277A8701983-09-30030 September 1983 Design Reverification Program, Vols 1 & 2,final Assessment Rept ML20078M2661983-09-30030 September 1983 Independent Evaluation of Plant Verification Program at WPPSS-2:Vol I Quality Verification ML20080T2071983-09-22022 September 1983 Engineering Insp & Evaluation of Quality Class Ii/Seismic Category I Pipe Supports ML17277A8541983-09-21021 September 1983 Quality Verification Program,Vol 1:Overview Rept,Jul-Sept 1983. ML17292A8091983-09-20020 September 1983 Sheet 1 to Reactor Protection Sys. ML17277A9961983-09-0909 September 1983 Hanford 2 Power Generation Control Complex (Pgcc) Floor Plate Design. 1998-03-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
O WASHINGTON PUBLIC POWER SUPPLY SYSTEM NUCLEAR PLANT NO. 2 FEEDWATER N0ZZLE INSPECTION REPORT FOR REFUELING OUTAGE RF86A l SPRING 1986 l
'O PREPARED BY: N% 11 / 2 s / 8 6 ISI ENGINEE10 DATE g REVIEWED BY: 4 6N U'-' _//[?v/%'
MANAGER, ENGINEERING SYSTEMS SUPPORT DATE 8MANAGER,
- k. NWNP-2 M GENERATION Lsf N uENGINEERING / //d2Tl${#
DATE R LL MANAGER, PLANT TECHNICAL "A &
DATE APPROVED BY: b/YI wu>> ///2r/94 iO PLANT MANAGER DATE
!O lO l
l
!O l
l
,0 8612120296 861204 PDR ADOCK 05000397 G PDR l
l l
EEDWATER N0ZRE INSPECTION REPORT PAGE 1 of 7 O
'O SUMARY
- g This report addresses feedwater nozzle thermal cycling and inspection for WNP-2 for the period of initial start-up ( April 1984) through the first refueling outage (April 1986).
During the spring 1986 refueling outage (RF86A) ultrasonic examination of one
!O reactor feedwater nozzle was perfomed at WNP-2. No recordable indications were found. The plant had experienced 45 startup/ shutdown cycles during this initial inspection period.
'O On/off operation of the feedwater startup level control valve during low flow /startup conditions resulted in themal cycling of the feedwater nozzles.
To minimize this themal cycling, changes were made in the low flow /startup sequence. The reactor feedwater drive turbine low speed stops were reduced to allow the turbine speed level control to operate at lower flow rates. This reduced the time the startup level control valve was required to operate.
Because the thermal cycling of the feedwater nozzles could not be completely prevented, the Supply System perfomed an analysis to determine the effects of O this mode of operation during the initial inspection period. The analysis concluded that no detrimental effects were caused by this cycling.
The Supply System plans to continue its augmented feedwater nozzle inspection 0 at the next refueling outage as committed in the WNP-2 ISI Program Plan. That is one feedwater now . bure, inner radius and safe end will be ultrasonically examined from the reactor outside diameter (00) at the next refueling outage -
currently scheduled for April 1987.
- O
'O 10 FEEDWATER N0ZZLE INSPECTION REPORT PAGE 2 of 7 O
.O NDE INSPECTION O During tne first refueling outage, RF86A, at WNP-2, the Supply System per-fonned ultrasonic examination of one reactor feedwater nozzle safe end, bore and inner radius from the vessel 00. This examination is part of WNP-2's com-mitznent described in FSAR section 5.2.4.10 and Inservice Inspection Program Plan Section 5.3.2 to ultrasonically examine one feedwater nozzle from the OD O
each refueling outage for the first six refueling outages.
The Supply System has developed an angle beam shear wave technique that is unique to the WNP-2 feedwater nozzle design. The procedure was qualified on O
the WNP-2 feedwater nozzle mock-up which is a feedwater nozzle from the scrapped Douglas Point Unit 1 reactor vessel. The inner radius, zone 1, of the nozzle is scanned using a 72 degree angle transducer. The inner radius, zone 2, and bore region, zone 3, are scanned using a 25 degree angle trans-O ducer. The procedures used, QCI 6-4 rev. 3 and QCI 6-13, rev. 3, are con-tained in Appendix I to this report.
Calibration data for reactor feedwater nozzle inner radius exams have been O
predetermined using the WNP-2 feedwater nozzle mock-up. This allows the examiner to use the reactor vessel calibration block representing the shell course containing the feedwater nozzle for calibration. The transfer data is contained in Table I of procedure QCI 6-4. Indications that exceed 25% full O screen height (FSH) are recorded and indications that exceed 50% FSH are evaluated.
The examinations were performed by two teams of Supply System examiners certi-O fled to either Level II or Level III UT per the Supply System Q. A. program.
During the examination they were under the direct supervision of the Supply System Level III responsible for the technique and procedure development.
lO Na recordable indications were found.
Total examiner radiation dose was less than 0.5 Man Rem.
O FEE 0 WATER N0ZZLE INSPECTION REPORT PAGE 3 of 7 O
10 SYSTEM AND PROCEDURE CHANGES THAT AFFECT FEEDWATER FLOW Reactor vessel water inventory is maintained by a control system which O
receives input signals from main steam mass flow rate, feedwater mass flow rate and either of two vessel level transmitters. A switch allows selection of either a single-element mode, utilizing only the vessel level signal, or a three-element mode, in which steam and feedwater flow rates are compared and
- O the resultant error signal modifying the level signal to provide an antict-patory feature. During nonnal power operation the feedwater control signal is used to control the speed of steam turbine-driven feefwater pumps. During startup, shutdown and low plant load conditions the steam turbine-driven feedwater pumps are run at a constant speed and the feedwater control signal is used to modulate an air operated, startup feedwater control valve (startup valve) to maintain proper reactor water level and avoid feedwater nozzle thennal cycling. However, the valve design does not allow effective control
",O of feed flow at these low flow conditions. Therefore cyclic operation of the valve is the only alternative. It has been detennined that the installed valve is not suited for its current application and plans for its replacement are underway.
To reduce the thermal cycling to the feedwater nozzles induced by the cyclic operation of the startup level control valve, changes to the system and its operating procedures have been completed. The low speed stop of the reactor O feed drive turbines has been lowered. This allows turbine speed level control at lower flow rates. The startup flow control valve is closed earlier result-ing in less time that the valve is utilized for low flow level control and fewer thermal cycles are experienced. This mode of operation will continue O until replacement of the startup flow control valve with one of appropriate design and application. Replacement is currently scheduled for the upcoming refueling outage in Spring 1987.
- O In light of the on/off operation of the startup level control valve, the Supply System has perfonned an analysis of the cyclic thermal load on the feedwater nozzle fatigue integrity. The analysis was based on the total number of startups since fuel load and estimated cycling during each startup.
- O l
l FEE 0 WATER N0ZZLE INSPECTION REPORT PAGE 4 of 7 g ,
O The analysis compared the present WNP-2 feedwater system thermal transients with General Electric's generic transients described in " Boiling Water Reactor o Feedwater Nozzle /Sparger", Final Report, NEDE-21821-A, Class III, February 1980 Based on this comparison the estimated feedwater nozzle life exceeds forty years with the present WNP-2 feedwater system design.
g STARTUP/ SHUTDOWN CYCLES WNP-2 has experienced 45 startup/ shutdown cycles between initial heatup
( April 1984) and shutdown for refueling outage RF86A ( April 1986). The data 1 g was compiled from the Final Startup Report and Monthly Core Energy Output Worksheets.
NEXT SCHEDULED EXAMINATION O
The Supply System will perform an ultrasonic examination from the OD of the reactor vessel on one reactor feedwater nozzle inner radius, bore and safe end per the committment in FSAR section 5.2.4.10 and the Inservice Inspection Pro-gram Plan section 5.3.2 during the refueling outage scheduled for Spring 1987.
.O
!O O
O FEEDWATER N0ZZLE INSPECTION REPORT PAGE 5 of 7 O
E)
APPENDIX I
- g. Procedure QCI '6-4, revision 3 Procedure QCI 6-13, revision 3 O
f g-h O
O 3
i 1
o O
O g 'FEEDWATER N0ZZLE INSPECTION REPORT PAGE 6 of 7