ML20214G986

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SALP Rept 50-423/85-98 for Sept 1985 - Feb 1987
ML20214G986
Person / Time
Site: Millstone Dominion icon.png
Issue date: 04/16/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20214G943 List:
References
50-423-85-98, NUDOCS 8705270232
Download: ML20214G986 (59)


See also: IR 05000423/1985098

Text

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ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER 50-423/85-98

MILLSTONE NUCLEAR STATION, UNIT 3

ASSESSMENT PERIOD: SEPTEMBER 1, 1985 - FEBRUARY 28, 1987

BOARD MEETING DATE: APRIL 16, 1987

8705270232 870514l

DR ADOCK 050004 3

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TABLE OF CONTENTS

PAGE

I. INTRODUCTION......................................................... 1

II. CRITERIA............................................................. 2

III. SUMMARY OF RESULTS................................................... 3

A. Overall Summary................................................. 3

B. Background...................................................... 4

1. Licensee Activities........................................ 4

2. Inspection Activities...................................... 4

C. Facility Performance Analysis Summary........................... 5

D. Plant Trips and Unplanned Shutdowns............................. 6

IV. PERFORMANCE ANALYSIS................................................. 10

A. Plant Operations................................................ 10

B. Radiological Controls........................................... 14

C. Maintenance..................................................... 18

D. Survei11ance.................................................... 21

E. Emergency Preparedness.......................................... 23

F. Security and Safeguards......................................... 25

G. Outage Management............................................... 28

H. Licensing Activities............................................ 30

I. Engineering Support............................................. 32

J. Training and Qualification Effectiveness........................ 35

K. Assurance of Quality............................................ 37

V. SUPPORTING DATA AND SUMMARIES........................................ 40

A. Investigation and Allegation Review............................. 40

B. Escalated Enforcement Actions................................... 40

C. Management Conferences.......................................... 40

D. Licensee Event Reports.......................................... 40

E. Licensing Activities............................................ 42

TABLES

Table 1 - Inspection Report Activities

Table 2 - Inspection Hours Summary

Table 3 - Enforcement Summary

Table 4 - Licensee Event Reports

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I. INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP).is a periodic, inte-

grated NRC staff effort to collect observations and data and evaluate licensee.  ;

performance. SALP supplements the normal regulatory processes used to ensure

compliance with NRC regulations. SALP is' intended to be sufficiently diagnos-

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tic to provide.a rational basis for allocating NRC resources and to provide ~

meaningful guidance to licensee management to promote quality and safety of ,

plant. operation. .

The NRC SALP Board met on April IC, 1987 to review performance observations

and data in accordance with the guidance in NRC Manual Chapter 0516, " System- '

atic Assessment of Licensee Performance". A summary of the guidance and

evaluation criteria is provided in Section II of this report. ,

This report addresses performance at the Millstone Nuclear Power Station, Unit

3 from September 1, 1985 through February 28, 1987. The_ findings'and data

reflect an 18 month assessment period. Although this includes activities

during construction and initial fuel loading, the evaluation of licensee per-

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formance has emphasized the period of power operation from January 23, 1986

through February 28, 1987.

The SALP Board was composed of the following:

Chairman:

W. F. Kane, Utrector, Division of Reactor Projects (DRP)

Members:

W. V. Johnston, Director, Division of Reactor Safety (DRS)

S. J. Collins, Deputy Director, DRP

E. C. Wenzinger, Chief, Projects Branch No. 3, DRP

R. R. Bellamy, Chief, Emergency Preparedness and Radiological Protection ,

Branch, Division of Radiation Safety and Safeguards (DRSS) (Part-Time) '

E. C. McCabe, Chief, Reactor Projects Section No. 38, DRP  !

E. L. Doolittle, Project Manager, PWR Project Directorate No. 5, Division

of PWR Licensing-A, NRR (Part-Time) L

J. T. Shedlosky, Senior Resident Inspector .

Other Attendees (non-voting):

N. J. Blumberg, Acting Chief, Operational Projects Section, DRS (Part-Time)

E. L.- Conner, Project Engineer, DRP (Part-Time)

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M. C. Kray, Reactor Engineer, DRP 3

W. J. Madden, Physical Security Inspector, DRSS (Part-Time) '

W. J.~Pasciak, Chief, Effluents Radiation Protection Section, DRSS.(Part-Time) i

J. A. Schumacher, Senior Emergency Preparedness Specialist, DRSS (Part-Time)

A. A. Weadock, Radiation Specialist, DRSS (Part-Time) '

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,. II. CRITERIA

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Licensee performance is assessed in selected functional areas. These areas

are significant to nuclear. safety and the environment, and are normal pro-

grammatic areas. The following criteria were used as appropriate to assess

[

l each area.

1. Management involvement and control in assuring quality.

-2. -Approach to resolution of technical issues from a safety standpoint.

!

3. Responsiveness to NRC initiatives.  !

4. Enforcement history.

5. _ Reporting and analysis of reportable events.

6. . Staffing (including management). i

7. Training effectiveness and qualification.

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Based upon the SALP Board assessment, each functional area is classified into

one of three performance categories. These are: i

. Category l'. Reduced NRC attention may be appropriate. Licensee management

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i attention and involvement are aggressive and oriented toward nuclear safety;.

licensee resources are ample and effectively used so that a high level of

.

performance with respect to operational safety is being achieved.

j Category 2. NRC attention should be maintained at normal levels. Licensee

i- management attention and involvement are evident and concerned with nuclear

~ safety; licensee resources are adequate and reasonable effective such that

satisfactory performance with respect to operational safety is being achieved.

, Category 3. Both NRC and licensee attention should be increased. Licensee

management attention or involvement is acceptable and considers nuclear safety,

but weaknesses are evident; licensee resources appear strained'or not effec-

tively used such that minimally satisfactory performance with respect to

'

operational safety is being achieved.

. .

[ The SALP Board has also categorized the performance trend over the course of

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the SALP assessment period. The SALP. trend categories are:

j Improving: Licensee performance was determined to be improving near the close

of the assessment period.

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Declining: Licensee performance was determined to be declining near the close

of the assessment period.

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A trend is assigned only when a definite trend of performance is discernible,

and the SALP Board believes that continuation of the trend may result in a

change of performance level.

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III. SUMMARY OF RESULTS

A. Overall Summary

l~ This assessment found a well-staffed licensee with strong and visibly

involved managers. Strengths were observed in self-identification of.

'. problems, in response to problems, and in searching for root causes.

There was diligent attention to proper performance at all levels, and

performance improved as the SALP period progressed.

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Operations phase programs, procedures, and management controls were in '

place and fundamentally sound. Minor setpoint errors and procedure in-

adequacies in the surveillance area were one of the few weaknesses found.

Program implementation was good in all areas.

There were four reactor scrams before initial criticality and 15 more 1

during the subsequent year. While this is a high number,-it is consist-

l ent with the performance of similar plants during initial operation.

t Also, licensee responsiveness to these events resulted in a scram fre-

) quency decrease of about a factor of two during successive four month

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operating periods. -

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Review of scrams and other operating events points to personnel error,

equipment characteristics, and component failures (in that order) as the

main factors. In many cases, scrams were caused by a combination of

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I personnel error and the high degree of difficulty of steam generator

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level control. In addition to steam generator level control equipment

I performance improvement, this SALP identified a need for reducing the

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number of illuminated control room annunciators and improving the per-

l formance of equipment such as the Power Operated Relief Valves. A strong '

i program to reduce personnel errors and improve' equipment performance is

j needed. Improvements in scram and feedwater transient reduction and in

i the number of lighted annunciators indicate that the licensee's correc-

tive action approach is working.

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i Licensee command and control was notably good. Activities were carefully

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' planned and conducted, with outages being a noteworthy example. Managers

were actively involved and inserted themselves into decision-making and

} activity direction at appropriate levels. Operating supervisors and

plant personnel were knowledgeable and alert, with strong corrective

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action evident when a discrepancy in performance and supervision occurred.

l Overall, this SALP reflects careful and safe performance of initial plant

operation.-

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B. Background

1. Licensee Activities

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Millstone 3 received a low power license (NPF-44) on November 25,

! 1985. Initial criticality was on January 23, 1986. A full power

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license (NPF-49) was issued on January 31, 1986. Power operation

was first attained on February 3. The plant reached 100% power on

April 17, was declared commercial on April 23, and completed the

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100-Hour Warranty run on April 29.

There were four reactor scrams before initial criticality and 15

reactor scrams during the first year of operation. The major factor

i in the scrams was difficulty with steam generator level control,

a ' which contributed to 10 scrams. There were also two unplanned and ,

three planned outages to correct equipment deficiencies and perform

i surveillances. These outages and the reactor scrams are tabulated

in Section IIID (Page 6) of this SALP. The plant achieved an 86%

capacity factor for the commercial operating period beginning on

April 23, 1986 until the end of the SALP period on February 28, 1987.

2. Inspection Activities

l Two NRC resident inspectors were assigned to the site during the

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entire 18-month assessment period. The NRC inspections are summar-

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ized in Table 1 and re

} (4790 hours0.0554 days <br />1.331 hours <br />0.00792 weeks <br />0.00182 months <br /> per year),present an inspection

distributed as shown in effort of 2.

Table 7130 hours0.0825 days <br />1.981 hours <br />0.0118 weeks <br />0.00271 months <br />'  ;

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Special team inspections were made of operational readi. ness (April

14-24,1986); as-built pipe and supports, electrical, and instrument

and controls (September 9-20, 1985); and the site emergency exercise

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(November 19,1986.)

This report also assesses " Training and Qualification Effectiveness"

and " Assurance of Quality" as separate' areas. .These separate areas

! provide a synopsis of these topics, which.are also incorporated in

other functional areas through their use as evaluation criteria.

!. For example, assurance of quality was assessed on a day-to-day basis

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' by the resident inspectors and as an integral part of all specialist

' inspections. Although the management tools for measuring quality

include QA inspections and audits, quality work is the responsibil-

t ity of every employee. Major quality factors such as involvement

of first-line supervision, safety committees, and worker attitudes

are considered in each functional area.

! Fire protection was not addressed as a separate area during this

l SALP because 10 CFR 50,~ Appendix R implementation has not yet been

specifically inspected onsite. Engineering support was added as

i a functional area to provide better focus on support functions which

[ were previously addressed in several functional areas.

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C. Facility Performance Analysis Summary

Last Period This period

(9/1/84- (9/1/85- Recent

Functional Area 8/31/85) 2/28/87) Trend

A. Plant Operations 2 2 Improving

8. Radiological Controls 2 2 Improving

C. Maintenance 2 1 --

, D. Surveillance 3. 2 --

E. Emergency Preparedness 2 1 --

F. Security and Safeguards 1 1 --

G. Outage Management # 1 --

H. Licensing Activities 2 1 --

I. Engineering Support # 2 --

J. Training and Qualification # 2 --

Effectiveness

K. Assurance of Quality # 1 --

L. Preoperational Testing 1 ## ##

M. Fire Protection and 1 ## ##

Housekeeping

, N. Construction 1 ## ##

  1. Not previously assessed as a separate area
    1. Not assessed this period

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l 0. Plant Trips (Scrams) and Unplanned Shutdowns

j- Power Root Functional

j Date Level Description Cause Area

j 12/15/85 Cold Scram when improper.applica- Startup testing Operations

l Shutdown tion of a jumper during Procedure

j. testing resulted in revers- inadequacy.

j ing the steam generator- '

l 1evel logic.

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1 1/16/86 Hot Scram due to rate compensated Operator error Operations

i Standby steam line low pressure due

j. to too quick opening of atmos-

i pheric steam dump valve when

MSIVs were shut.

i 1/18/86 Hot Scram due to source range Construction Operations

Standby monitor spike due to welding personnel error-

cables in proximity to. work control

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nuclear instrumentation

i cables.

1 1/19/86 Hot Scram due to rate compensated Operator error- Operations

l Standby steam line low pressure due high T-avg. com-

! to opening of a steam pounded by misad-

i generator relief valve with justed relief valve

j misadjusted setpoint. setpoint

j [1/23/86 INITIAL CRITICALITY]

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2/4/86 15% Scram due to low steam Operator error Operations

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generator level during manual

j control of feedwater flow.

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) 2/7/86 15% Scram due to low steam Improper settings Engineering.

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generator level auxiliary on auxiliary steam Support ,

{ steam relief stuck open. relief valve and

! gain (high) of-

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feedwater regulat-

ing bypass valve

i 2/10/86 15% Scram due to low steam Faulty design of Surveillance

i generator level. During control card test

surveillance, the level set points, plus I&C

l point input to control card technician failure '

i faulted to ground. (Probe to follow special ,

j contacted two test points.) instructions on '

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probe'use.

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Power Root Functional

Date Level Description Cause Area

2/12/86 29% Scram due to low steam Procedure Operations

generator level - transfer inadequacy

from turbine-driven to motor-

driven feedwater pump with

only one running condensate

resulted in low suction pres-

sure trip of feedwater pump

and then feed instability.

2/13/86 15% Scram due to spurious actu- Equipment: Cause --

ation of RPS inoperability unknown (possible

protection (General warning power supply

annunciator) during problem)

surveillance.

2/21-3/5/86 Shutdown to lower steam Manufacturing or --

generator chemistry to with- construction resi-

in owners group guidelines. due, or resin in-

jection.

3/19/86 10% Scram due to low steam Procedure Operations

generator level caused by inadequacy

failure to shift control to

feedwater regulating bypass

valves following a turbine

trip. Remained shutdown

through 3/20 to clean trans-

former insulators.

4/10/86 15% Scram due to low steam Operator error Operations

generator level - level

oscillation started with

control rods manually moved

to control average RCS tem-

perature during turbine

loading.

4/23/86 7% Scram due to low steam Operator error Operations

generator level following

rapid power reduction from

60% in response to secondary

steam leak from moisture

separator reheater drain tank

manway cover. Steam Generator

level control was in manual

at the time of the scram.

(18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> outage).

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Power Root Functional

-Date Level Description Cause Area

! 5/9/86 80% Scram automatically followed Management error- Operations

manual turbine trip caused poor planning.

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by decreasing condenser Fouling of circu-

i vacuum (92 hour-outage). .lating water intake

i screens while wash

system was out of

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service for main-

tenance }

7/24/86 20% Scram due to low steam Defective valve --

i generator level after feed- positioners caused

i water isolation due to over- bypass valves to be i

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feeding caused by partially partially open ,

j open bypass valves. As one i

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consequence, a planned mid-

! cycle maintenance outage was i

j begun early. The plant re-  !

i mained shutdown through i'

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August 17 (552 hour0.00639 days <br />0.153 hours <br />9.126984e-4 weeks <br />2.10036e-4 months <br /> outage).

8/17/86

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11% Scram due to low steam Operator error com- Operations

generator level - after - pounded by feed

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shifting to automatic control control system

! operators attention was alignment

l diverted from steam genera -

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tor while controlling others

! in manual (13 hour1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> outage).

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i 8/17/86 21% Scram due to low steam -Operator error Operations

! generator level after feed- compounded by feed _,

j water isolation due to high pump control re-

. steam generator level -scram sponse time

j occurred because of inade-

! quate coordination between

two operators who opened a

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feedwater regulating valve

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as feed pump speed was in-

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} creased (10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> outage). t

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9/6/86 80% Scram due to low steam Random equipment --

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generator level following failure

j spurious closure of a feed-

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water isolation valve (25

j houroutage).

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Power Root Functional

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Date Level Description Cause Area

1/13/87 100% Scram followed low vacuum Operator error Operations

turbine trip after circulat- (improper lubicat-

ing water pumps tripped due ing water lineup)

to low lubricating water flow

(31 hour3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br /> outage).

1/14/87 7% Scram due to high source Operator error Operations

range neutron flux when trip (brushed against

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block was accidentally reset panel switch)

(7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> outage).

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The below table summarizes scram performance versus time, and shows the decrease

in scram frequency as the first year of operation progressed.

AT/BELOW 15% POWER ABOVE 15% POWER lTOTAll

1 WHEN EQUIP PERS & PROCED EQUIP PERS & PROCED

Before Criticality 0 4 -- --

4

2/86 - 5/86 2 5 0 2 9

6/86 - 9/86 0 1 2 1 4

10/86 - 1/87 0 1 0 1 2

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NOTE: The root causes in these Tables are the opinion of the SALP Board based

on inspector assessments and may differ from the LERs.

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IV. PERFORMANCE ANALYSIS

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.A. Plant Operations (1365 Hours, 19%)

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1. Analysis

The previous SALP, completed prior to initial fuel loading, rated

i " Operations Support" as Category 2, consistent. Concerns included

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control over jumpers and lifted leads, tagging, log keeping, shift

! turnover adequacy, and root cause addressal. Of these, only equip- -

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ment tagging presented a concern during the current SALP period.  ;

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On March 1, 1986, a reactor coolant system-(RCS) hot leg injection  ;

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valve was. tagged shut.without an effective cross-reference to the

i subsequent plant heatup. The result was accomplishment of a pro-- '

hibited change in operating mode during heatup. The licensee then

i verified proper flow in other systems and' reviewed all tagouts and

i tag clearances. Overlapping management controls were implemented t

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to prevent similar occurrences due to a failure in one management

i system. These corrective actions were comprehensive. No further -

tagout problems were observed during the remaining 12 months of the

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SALP period.

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The transition from construction and testing to power operations l

occurred smoothly, mainly due to the significant nuclear operating '

experience of Northeast Utilities. Adding to this was an early

shift, during construction, in control room activities to that of

an operating plant, to the use of a plant-specific simulator for '

operator training, and to strict adherence to. written procedures.

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Overall, the startup test program was well managed and controlled.

! Initially, there were NRC concerns about the number of persons in

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the control room, about too"many tests being done simultaneously,

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and about the number of last minute procedure changes. When the

licensee was informed, prompt and effective action was taken. Ex-

! cess personnel were not allowed in the control room. More deliber-

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ate test conduct was observed. Test preparations and procedures

became more thorough and timely. Startup testing proceeded rapidly

and in accordance with NRC requirements. Startup personnel were-

knowledgeable and quickly' identified and corrected testing problems.

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A good interface was evident between startup, operations, reactor

engineering, I&C, maintenance, and QA/QC. The entire startup or-

f ganization was' assessed as' extremely capable and professional ~.

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As shown in the Supplementary Table in Section IIID (Page 9) of this

j SALP, there were a high number of scrams, with improvement evident

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by the decreased scram frequency with time. Fifteen of the 19

scrams were due to personnel and procedures. Eleven of the 15 were

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at or below 15% power. System and personnel responses to the scrams '

were proper. The errors were mainly in manual control of steam

generator levels. Quick operator response to changing conditions

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was evident. Operator performance is considered to have lowered

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the scram rate substantially because feedwater transients which

caused many of the early scrams were handled expertly later on, and

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scrams were thereby averted. Proficient operator actions which

prevented challenges to safety systems included res

l petitive losses of fourth point heater drain pumps,ponses to re-

to feedwater-

regulating valve _ failure with a simultaneous motor-driven feed pump

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' minimum flow valve _ failure, and to loss of turbine plant closed

cooling water. Operator excellence was also shown in prompt re-

i sponse to'a major steam leak from the moisture separator drain tank

and to leaks of turbine electro-hydraulic control. system fluid. -

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Overall, operating shift functioning was evaluated as smooth and

professional. Activities were conducted carefully and with suffi-

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cient formality. The operators.themselves were strong proponents

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of control room formality. Operator attitudes were' assessed as

l positive. Alertness was routinely observed in operator performance ,

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during day'and backshift inspections. Distractions such as ex-

traneous reading material were not permitted or observed in the

{ control room. Shift turnovers were observed to be consistently

thorough and effective. Briefings for tests and infrequent evolu-

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tions were detailed and involved free exchanges of questions and

answers. Written procedures were routinely followed. Shift-logs '

j and records were found discrepancy free during frequent. review.

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A high number of main board annunciators were illuminated'during

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operation, with about 100 identified in April 1986. This was

! largely due to annunciation of conditions which did not affect

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operation but presented a potential distraction to operators. The

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licensee has since reduced the lighted annunciators to about 60.

This is acceptable progress, but continued attention to this~ aspect

i is needed. '

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Operator technical knowledge was good. During the NRC license ex-

! aminations given this SALP period, 43,of the 52 license candidates

j passed. No significant generic weaknesses were noted.' This~83%

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pass rate is a substantial improvement over the_ previous pass rate  ;

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of 52% (11 of 21). Also, the operators _have consistently exhibited

detailed and thorough knowledge of the' equipment, its status, and

associated requirements. A recent example was shift supervisor ~(SS) i

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L review of surveillance of charging pump suction valve surveillance.

The SS recognized.that the valves were interlocked such that their

cycle times should be added to determine shift-over time between

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water sources, precipitating licensee reassessment of the associated

. engineered safety feature response times..

} A few minor training weaknesses were observed..- The operators did

not know how to take local manual control of a feedwater regulating '

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valve upon valve positioner failure-(an'in-line valve was used as

an alternate control instead). Also, an incorrect simulation of

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plant configuration contributed to a safety injection when a main

steam isolation (MSI) signal was reset with an atmospheric dump set

below steam line pressure. In these cases, the training response

and initiation of procedure and simulator changes were evaluated

as appropriate and timely, and representative of the licensee's

overall good approach to correcting problems.

Licensee management support of training and rewarding of operator

proficiency has been evident. The facility has a modern plant-

specific simulator with a training staff that has been expanded to

about 20 individuals. Several experienced operators have been pro-

moted to the training staff. There is a six shift rotation during

power operation, with full-time training for one shift being a re-

gular part of the rotation. Station management involvement in

training was evident in their knowledgeable discussions with NRC

personnel and in their obvious interaction with the training staff

and observance of simulator training.

Management attention to operations was evident in frequent plant

superintendent control room tours and detailed weekly plant material

walkdowns by a team of Health Physics, Maintenance, and Operations

supervisory personnel.

Overall, operating procedures were satisfactory. No major procedure

inadequacies were found. Personnel routinely followed procedures

and properly proposed appropriate changes. There were many minor

changes, as is expected during initial operation. In this case,

that is considered reflective of licensee determination to eliminate

procedure inadequacies. However, procedure flaws contributed to

three operational problems. One was a reactor scram on loss of

feedwater flow when an additional condensate pump was not started

before shifting feed pumps. A second was an emergency core cooling

pump inoperability for over three days when a valve was left shut

during surveillance. The third was a feedwater isolation and reac-

tor scram while shutting down without shifting to bypass valve

feedwater control prior to tripping the main. turbine.

Operations Review Committee performance was very good. Meeting inputs

were well prepared and showed a clear understanding of issues. The

approach to problem resolution was technically sound, very thorough,

and routinely conservative. Root causes of problems were actively

pursued. During meetings and in NRC discussions with higher level

managers, there was a licensee willingness to face facts and an

atmosphere of healthy self-criticism.

Housekeeping was poor at the end of construction and into startup

testing. After cleanliness and storage problems were identified

to station management, general plant cleanliness was upgraded and

attention was placed on removing or securing heavy items near safety-

related equipment. Four cubicles in the Engineered Safeguards

Features Building were completely cleaned and painted out. Cleanup

_ _

.- .

13

efforts and correction of packing leakage diminished the number and

size of the radiologically contaminated areas which had begun ex-

panding as the plant progressed into operation. Overall, house-

keeping was satisfactory.

1

Licensee Event Reports were routinely reviewed by the inspection

staff and generally _found to be complete, accurate, timely and to

contain adequate corrective actions. A special NRC Incident Re-

sponse Branch review of ENS reporting and classification as well

as use of event cause codes in LERs found adequate reporting.

Licensee command and control of operations were strong overall.

Managers were aware of operating status and details, and actively

inserted themselves at the appropriate organizational level. Shift

management was knowledgeable and exerted positive control over

activities affecting operation. An exception was the three-day

emergency core cooling pump inoperability. This involved improper

shift supervisor staff assistant (SSSA) performance, inadequate

training of SSSAs in valve operating requirements, and an inadequate

surveillance procedure. Strong corrective actions were taken. The

procedure and training flaws were corrected. Licensee review found

a lack of potential for other similar events. The individual and

cognizant line management were reprimanded. No similar occurrences

were observed.

Licensee management is strong. Corporate and unit goals and poli-

cies are detailed and well communicated, and administrative controls

i are effectively implemented. There is a strong safety first orien-

tation at all levels in the licensee's organization. Licensed

operators were professional, knowledgeable and thorough, and their

performance became excellent as the initial operating period pro-

-

gressed. The operator errors were assessed to be largely due to

inexperience with steam generator level control characteristics and

to the high degree of difficulty of manual control of steam genera-

tor level. Scram frequency decreased in the latter part of the SALP

period. Housekeeping also improved. _ Concerns identified in the

previous SALP were effectively addressed. Overall, operating per-

1

formance was satisfactory and improving.

2. Conclusion

i

.

Category 2, Improving.

3. Board Recommendations

l

Licensee: Reduce unnecessary annunciations and reactor scrams.

j

l

NRC: None. '

i

I

!

)

l

__ _ _. __ . . __ _ - - . _ ._ -_. _ _ _ _ . _ _ - _. __

.. .

14

8. Radiological Controls (845 Hours, 12%)

1. Analysis

The Radiological Controls Program was previously rated Category 2,

consistent. There were no major concerns identified.

1.1 Radiation Protection

An effective, well-defined organizational structure is in place

to control unit radiological work activities. Adequate levels

of supervisory and technician level personnel were available

to support routine radiological activities. NRC inspectors

observed that Radiation Protection (RP) supervision were ac-

cessible to the RP staff and exhibited a strong "in-the-field"

presence. RP and Operations supervision regularly perform

joint tours of the controlled area to identify sources of con-

tamination and potential radiological concerns, and licensee

records and files document actions being initiated as a result.

The RP staff performed aggressively in directing decontamina-

tion efforts and initiating fixes for identified contamination

sources.

The number of audits of radiological operations routinely per-

formed by the RP corporate staff was assessed as good. However,

the audits were noted review to station RP activities as a

whole without always providing an in-depth review of unit ac-

tivities. This weakness was identified by the licensee and

actions have been started to improve the audit system. Over-

all, audits were considered satisfactory and the associated

audit program corrective actions were good.

Clear procedures and policies were in place and effectively

implemented. No procedure deficiencies were found by the NRC.

Radiation Protection personnel were trained and qualified in

accordance with a good program. However, RP technician re-

qualification training in 1986 contained only a limited dis-

,

cussion of plant systems. That NRC identified aspect was found

!

to be the only significant deficiency. The licensee is re-

viewing this matter.

Several noteworthy improvements were initiated in the radio-

logical training program. Detailed mockups of the RCP seals

and of a radwaste shipping cask have been procured to enhance

job-specific radiological training. An elaborate, complete

chemistry laboratory has been constructed in the training

facility for the instruction of chenistry technicians.

3

I

i

. .

15

The program for surveying, posting, and controlling radiological

areas was found to be well implemented. An extensive and

thorough radiation survey program to evaluate shielding effec-

4

tiveness was performed by the licensee during unit startup.

NRC specialist review of the Radiation Work Permit System found

it effective in controlling radiological work activities.

A special inspection was conducted to review post-accident

sampling. The licensee was able to adequately demonstrate this

capability. There were specific concerns with equipment

operability, monitor calibration procedures, and handling and

analysis of high activity samples. These required licensee

response and improvement, but were relatively minor items.

Collective exposure during 1986 was low (approximately 27

, person rem). The monthly exposure average was typically well

below the ALARA goal of 5 person-rem / month of operation. Dur-

ing previous. review of station ALARA activities, it was noted

that sometimes conflicting exposure goals were developed

separately by the unit and corporate staffs. The exposure

goal-setting process for 1987 has been improved in that the

unit ALARA staff provided significant input to the formulation

of corporate goals.

Overall, in plant health physics was a notable licensee strength.

This is attributed to a sound program, a capable staff, and

supervisory excellence.

1. 2 Unit 3 Radioactive Waste Management

Reviews of the liquid waste, gaseous waste and ventilation

systems installation and testing found that the systems were

installed as described on the Piping and Instrumentation Dia-

grams in the FSAR and testing was completed in an orderly and

timely manner to support initial criticality, power ascension

and commercial operation. Design deficiencies in those systems

discovered during preoperational and startup testing were re-

solved with very little impact on plant startup schedules.

There was no operational radwaste management assessment because

of the low level radwaste of processing activity during in-

itial operation. (Unit 1 and 2 radwaste considerations were

not considered in this Unit 3 SALP.)

1. 3 Radiological Effluent Control and Monitoring

Area, effluent and process radiation monitoring capabilities

were demonstrated during preoperational and startup testing.

There were recurring problems with the adequacy of monitor

calibration and licensee performance of Technical Specification

!

% y.- -

. .-- . . . = . - - - . . - - . -- - -.

k

. . ,

.

16

i

i

,' action statements required by monitor inoperability. Procedural

i. inadequacies included the failure of effluent monitor surveil-

lance procedures to adequately test Technical Specification

,.

required auto-isolation and alarm annunciation features and

'

also resulted in the non-conservative calibration of contain-

ment high range area monitors. The above deficiencies resulted

in the generation of several LERs. Additionally, weaknesses

i

in the comparison of monitor and laboratory sample data and

quality control for vendor laboratories were noted, showing

inattention to technical detail in procedural development and

review. Nonetheless, the licensee's analysis of radioactive .

samples was in agreement with the NRC values. The licensee '

provided adequate technical resolution of the weaknesses.and

promptly updated and corrected the procedures.

i

, 1.4 Water Chemistry Controls '

f

The licensee demonstrated a strong commitment to water chemis-

try control.

' Chemistry analysis was. thoroughly reviewed during ,

i

the daily management meetings, and operations were thereupon

modified to optimize chemistry conditions.

i

.

Reviews of the water chemistry control program indicated a

! generally adequate program was developed and implemented. The

j

licensee was using upgraded analytical procedures and state

! of the art instrumentation in the laboratory. The training

!

and qualification program for supervisors and technicians in-

! cluded formal classroom training, written demonstration of

proficiency and,.for technicians, participation in an intra-

,

1

laboratory spiked sample program evaluated by their supervision. i

An elaborate chemistry laboratory has been constructed for the

l

instruction of chemistry technicians. The good training and

i facilities contributed positively to performance. ,

3

' NRC review found five of twenty-two comparisons of analytical a

' results against NRC standard samples were in disagreement. '

!

The differences were due to laboratory control program weak- t

nesses including single point calibrations of instruments, lack

} of measurement control charts, and sampling errors.

t

,

4

The program for controlling water purity in the primary and

secondary coolant loops was adequate. The ifcensee provided

i

a documented management commitment to and support for the pro-

l gram and closely monitored performance. During testing of

!

plant water systems, the licensee noted and corrected condenser

l inleakage, closely monitored unusual sulfate levels in the -

i

steam generators and administrative 1y controlled contaminants

j~ i

at levels generally well below consensus guidance. However,  ;

i

several occurrences were noted suggesting-inadequate design

! review and failure to note lessons from Unit 2's operating ex-

i

4

i

l

l l

l

I

_ . _ . . ,

- - . ..- . - .. . . - - . _ - - -

. ..

17

-perience. As~a probable result of inadequate delay for Nitro-

gen-16 decay, the sampling location of the reactor coolant pro-

vided high radiation levels with no evidence of failed fuel.

Resin retention filters experienced strainer failures due to

.

'

.

) design problems identified initially at and corrected in Unit

j 2. In addition, the licensee failed to monitor the feedwater

system for metallic transport which could result in excessive

, sludge buildup in the steam generators.

The licensee proceeded with caution while steam generator

'

secondary chemistry difficulties were being worked out during ~

the power ascension test program. That involved a shutdown

]

from 30% power to drain and refill the steam generators to

lower sulfate concentrations below the vendor recommended limit

of 20 parts per billion. Also, domineralizer webbing was re-

1

placed to prevent resin pass-through to the steam generators.

3 The seven-day shutdown taken in this' case is considered repre-

sentative of the licensee's normal emphasis on safety and
quality having priority over operation.

r- During this assessment period, the licensee implemented a generally

effective radiological controls program supporting early commercial

operation. Recurring deficiencies were noted, however, with the

adequacy of procedures for and calibration of area radiation and

effluent monitors. Overall, inasmuch as the low levels of radiation

,

and contamination encountered during initial startup and operation

i did not present a strong radiation protection challenge, a high

performance rating was not considered appropriate. Performance was

!

! assessed as satisfactory, and improving as a result of the quality

4

and results of corrective actions.

f 2. Conclusion

[

Category 2, Improving.

.

l 3. Board Recommendation

na

f

Licensee

Improve technical oversight of radiological monitor calibration,

'

j and laboratory quality assurance / quality control activities.

NRC

None. l

l

3

1

..

4

!

!

. .

18

C. Maintenance (359 Hours, 5%)

1. Analysis

The previous SALP rated Maintenance as Category 2, consistent. It

was recommended that the licensee schedule completion and implemen-

tation of maintenance procedures and training programs. This has

since been accomplished.

During this SALP period, maintenance was reviewed during two region-

based inspections and by the resident inspectors. No scrams or

challenges to protective systems were attributed to maintenance.

Safety system readiness and inservice testing (IST) performance

evidenced the effects of good preventive and corrective maintenance.

An example was the rebuilding of two service water pumps late in

the SALP period because of IST results.

Corrective maintenance was generally performed in strict accordance

with policies and work orders. Troubleshooting and significant

supervisory involvement led to accurate problem assessment and

formulation of proper corrective action. Work was thorough and

technically sufficient. Rework was seldom required. Only one in-

stance of poor maintenance was observed. A feedwater regulating

valve stem packing was tightened enough to retard valve motion.

It then failed to close on a Feed Water Isolation signal because

the packing was too tight (the next valve downstream did close).

Later, the same valve stuck in automatic control and then popped

open, causing a feedrate which caused reactor power to exceed 3445

MWth (101% of design). The licensee has since committed to full

stroke testing of such control valves after packing adjustments.

There were three instances of breaching or fouling of fire, control

building, and Secondary Leak Collection and Recovery System (SLCRS)

boundaries by process fluid hoses or staging. Also, there were

numerous instances of broken penetration seals, either by work in

progress or left over from construction. Increased licensee man-

agement attention was applied, and the resident inspectors noted

that such occurrences decreased in frequency.

The maintenance department was fully staffed with well trained, com-

petent and dedicated mechanics, electricians and machinists having

diverse backgrounds. Maintenance assistance was available from the

other three Northeast Utilities plants. Observations and discus-

sions showed maintenance supervisors and managers to be knowledge-

able, and active in on-scene oversight of activities. Effective

planning minimized outage and operational scheduling impacts. Co-

ordination with other departments was excellent. In fact, communi-

cation and cooperation between all departments, both at grass roots

and management levels, has been a key to timely and effective

troubleshooting and corrective maintenance on numerous occasions.

. .

19

A computerized maintenance management system (PMMS) has been in-

strumental in planning, controlling and documenting work. Its

machinery history function has been routinely used to trend equip-

ment performance for establishing corrective actions. PMMS is con-

sidered an excellent tool for managing maintenance.

Control of maintenance and testing was generally very effective.

Outages usually included between 700-900 work activities and tagouts

with minimal interference or failures in the control program. Main-

tenance and modification activities during normal plant operations

were controlled and performed within the bounds of Technical Speci-

fication Limiting Conditions for Operation. This was evident in

the routine daily performance of 6-8 preventive maintenance activi-

ties. Infrequent lack of control was observed, however: work on

main turbine stop valves commenced without a reapproved work order;

staging cross-bracing blocked operation of a Feed Pump turbine trip;

and Linear Variable Differential Transformers (LVDTs) were installed

on the Feedwater Regulating Valves without Operations Department

approval and to installation details modified after PORC approval.

These events affected equipment which is not safety-related, were

detected and corrected by the licensee, and had no operational

consequences.

Removal of a trash conveyor from its foundation created a potential

access route to the protected area. This maintenance error was

licensee-identified and promptly corrected.

Unavailability of improved replacement parts resulted in delaying

troubleshooting for all potential causes of Power Operated Relief

Valve (PORV) leakage, and effective repair of leaking PORVs was not

timely. As a result, although the valves have undergone a major

-

modification as well as two separate repairs, both PORVs were

blocked for a major part of the plant's operation. In addition,

due to either PORV and blocking valve leakage or safety valve leak-

age, the TMI action plan mandated positive indication of safety

valve status indicated open safety valves for most of the operating

period.

A significant maintenance action involved improper blowdown ring

settings on the Main Steam Safety Valves (MSSVs). In response to

an NRC information notice, the licensee spent considerable effort

verifying the ring settings for all 25 site valves, noting and cor-

recting a related problem of short ring lock pins and readjusting

the rings to a common setting. The ring readjustment was based on

documented phone conversations to the vendor. These confirmed the

technical manual setting values. In this case, maintenance

thoroughness significantly improved the assurance of proper MSSV

blowdown.

__________ - __-_ -

. .

20

The procurement program was well organized and allowed material

traceability to work orders. The warehouse was administrative 1y

well controlled and housekeeping was adequate.

In summary, licensee performance in the maintenance area has been

good overall, with the discrepancies noted being isolated and non-

representative. The maintenance program is properly established,

implemented and staffed. Plant equipment has performed with a high

degree of reliability.

2. Conclusion

Category 1.

3. Board Recommendations

Licensee: Assure thorough testing after maintenance.

NRC: Maintain current level of inspection.

.

1

4

1

I

. .

21

D. Surveillance (554 Hours, 8%)

1. Analysis

Surveillance was rated Category 3 during the previous assessment

period. A major factor was the tardy development of procedures.

This analysis is based on frequent NRC inspections by the resident

inspectors and four inspections by regional specialists.

The management program for controlling surveillances was found

especially strong in the Instrumentation and Controls (I&C) and

Maintenance Departments. Both departments used an automated system

to identify up-coming surveillances. Initially, the Operations Oe-

partment used a manual tracking system. Although it was cumbersome,

all required surveillances were completed. Operations is now also

using a computer system for tracking surveillances.

The inspectors have found that the technicians or operators conduct-

ing a test generally have a very good understanding of both system

and procedure requirements. This is particularly significant when

the complex electronic systems included in the Unit 3 design are

considered, and is a notable strength of the program.

The surveillance procedures are very detailed and form a solid basis

from which to build a successful program. Licensee personnel have

demonstrated a strong commitment to these procedures by active use

of the procedure change system. Changes were requested and drafted

by persons working with surveillance tests and processed in accord-

ance with the Technical Specification system for procedure changes.

The surveillance program has been managed conscientiously. Event

reports (LERs) documented seven missed surveillances. All were

licensee-identified. No single type of surveillance or responsible

working group was responsible for the missed tests. LERs also

identified some inadequate shift checks and compensatory actions.

Inasmuch as the lapses represent seven of several thousand surveil-

lances, and no significant safety degradation was involved, the

overall performance of required surveillances was excellent.

Surveillance caused a reactor scram from 15% power when a technician

inserted a test probe too far into a test point, contacting another

test point and grounding the level set point signal. The potential

for such an occurrence had been previously realized, and instruc-

tions had been issued to use short (non-standard) test probes for

such measurements. After this event, the licensee corrected the

basic problem by installing a barrier between the test point rows.

There were also seven instances of incorrect instrument setpoints

as the result of inadequacies in surveillance or calibration pro-

cedures. Four of these affected Reactor Protection System instru-

_ ..._ _. _ _ . _ _ . _ . - . _ _ . . =_ . _ . _ _ . _ . _ _

._.7._._._

.. , v

4

22

l

-

l

t

mentation setpoints. As a result, non-conservative settings were

j. used in over-temperature differential pressure scram setpoints, .

4

intermediate range neutron flux monitor scram setpoints,-reactor.

coolant system flow setpoints and the power range neutron flux.P-8

i interlock setpoint. Although none of these resulted in exceeding 'o

a Limiting Safety System Setting, their existence showed a potential

for such an excess. Because of these problems, the licensee re- 7

evaluated Technical Specification setpoints by comparing NSSS Vendor

,

Safety analysis documents to the Technical Specifications and the

l settings specified in surveillance and calibration procedures.

1

Recalculations were made for each setting; these contained all the.

,' conversions needed to track between plant primary parameters and

instrument electrical values. These licensee corrective actions

were assessed as comprehensive and found no additional inadequacies.

'

Five other occurrences resulted from inadequate surveillance proce-

) dures. These included isolation of service water to safeguards pump

j heat exchangers without the knowledge of shift supervision; incor-

.

rectly set throttle discharge valves in the control room pressuri- '0

,

zation system; an unnecessary safety injection during Engineered ,

j Safeguards Features (ESF) actuation relay testing; application of

I

full Reactor Coolant System (RCS) pressure to low pressure letdown

1 system piping during ESF actuation relay testing; and the failure

i to carry through a construction design change by deleting references

to uninstalled remote shutdown panel transfer switches from the,

.

Technical Specifications and the surveillance procedures.. While 1

1

these items are minor from a safety viewpoint, they point out in- ,

j adequacies in validation of procedures prior to operational use. ..

'

(A procedure validation program is being considered by the licensee.)

'

In summary, although the program is sound overall, surveillance

! procedures have detracted from performance because'of setpoint and

i other problems. This appears to be a carry-over effect from the

tardy development of surveillance procedures. The excellence noted-

in performing prescribed surveillances indicates a potential for

a higher rating once it is demonstrated that procedure inadequacies

j have essentially been eliminated.

I '

j 2. Conclusion c .,

\ . , ,

'

Category 2. c,

,t, -

1 3. Board Recommendations 7

.

l Licensee: Continue to emphasize procedure adequacy, and give evalu-

] ation of procedure validation priority emphasis.

,

,, 1

j NRC: None.

5

4

$

l

1 , ;

)

i

!

!

!

. - - . - , . - . - - . - , _ - , - , - - - - - . - - - - _ , , - . . - _ ~ , - . - , . . - - . - . - -

- .. . . ~. . .- - - . . - - - - - . ~ -

1 j,

'

23

.

t

!

-

s, E. Emergency Preparedness (173 Hours, 2%)

T ,

1. Analysis

.

J

During the previous SALP, this area was rated Category 2. Timely

,

resolution of NRC concerns was identified as needing improvement.

1

Emergency preparedness is a site function with conImon Emergency

' Plans, facilities, and personnel. This assessment covers the Sep-

-

tember 1, 1985 through February 28, 1987 period. It represents an

, ,

evaluation of all three Units but does not repeat applicable parts

j_ ,

of the three unit a uessment in-the Millstone 1/2 SALP for the

period ending May 31, 1986. During the current assessment period,

there were two region-based inspections.

'

" Inspection on July 7-10, 1986 closed fifteen emergency preparedness .

  • items. Two long lead time items remain open. These are a descrip--

s tion of the Offsite Facilities Information System (OFIS) and its

!

' maintenance procedure for inclusion in the Emergency Plan, and com-  ;

pletion of the installation and testing of the Technical Support

Center (TSC) and Operations Support Center (OSC) hardware [0FIS,

4

i

Area Radiation Monitoring System (ARMS), Safety Parameter Display

System (SPDS), and the evacuation alarm]. Initially, a planning-

date for completion of the procedures was set for January 1986.

This is presently projected for completion in June 1987. That

schedule is acceptable to the NRC. '

.

c i

,

r

The annual exercise was observed on November 19-20, 1986 (full par-

ticipation, including ingestion pathway). No significant deficien- j

cies were identified, but several minor weaknesses were noted. Two j

i of these were the direct result of a power failure caused by an ice '

storm. Back-up procedures and ' equipment worked satisfactorily,

is Both the Control Room and TSC staffs were knowledgeable and innova-

4

tive is solving problems presented as part of the exercise scenario.

The Control Room staff response.was prompt and conservative. They

j

quickly recognized changing plant conditions and were able to anti- '

l ' cipate possible corrective actions. The TSC staff demonstrated the

i t

ability to promptly identify and classify scenario events and make l

l protective action recommendations to offsite agencies. Emergency l

i Response Organization personnel were well trained and qualified for

!

their positions, and positive command and control of all emergency

4

response facility operations was demonstrated by the respective ,

'

i

'

facility managers. Overall licensee performance on the exercise-

was good.

Dedicated emergency response facilities are well maintained onsite

i

by the licensee. The Emergency Operations Facility (EOF) and TSC

.

i '

are common facilities for all three units. Both facilities have

adequate space and were designed to meet-the habitability require-

-

! , ments of NUREG-0696. Units 1 and 2 share a common OSC, with a

,t

l

.

J

.<

t

,v=wey-+,e g.9 . -n+.,s = wm,u.- -+-- --w.%-..-m-,--m., # .w .o e, r--o..m c , , , , , , - . , -,,,-r ,-sv, ,.,e,.,, ,=t--n-c. ,-

_

. .

24

separate OSC for Unit 3. All facilities are well equipped to func-

tion under emergency conditions. During the November 1986 exercise,

the emergency response facilities were promptly staffed and acti-

'

vated by the Emergency Response Organization personnel. Augmenta-

tion of the initial response to the emergency facilities was timely.

Contingency planning was evident when a hurricane was carefully an-

ticipated in August 1986. Severe weather preparations were imple-

mented. Shutdown planning was halted when the storm track shifted

substantially.

The Emergency Preparedness Staff at Millstone is ample, consisting

of a Senior Emergency Preparedness Coordinator and an Emergency

Preparedness Coordinator. Both have offices onsite. Additional

assistance is available from the Emergency Preparedness Supervisor

at the Corporate Headquarters in Berlin, Connecticut. Northeast

Utilities continues to maintain an excellent working relationship

with the State of Connecticut and local governmental agencies, as

evidenced by the continuing cooperation demonstrated during exer-

cises.

Overall, the licensee has a sound emergency preparedness program.

,

Management has adequately focused attention on this area as evi-

denced by good exercise performance, well-maintained emergency re-

sponse facilities, and an excellent working relationship with off-

site officials. There are few open NRC items.

2. Conclusion

Category 1.

3. Board Recommendations

None.

_ _

- - - . _ .

..

. .

25

F. Security and Safeguards (409 Hours, 6%)

1. Analysis

During the previous SALP period, no regulatory concerns were iden-

tified and the licensee's performance was assessed as Category 1.

The licensee was primarily involved in training and qualifying new

security force members and installing and testing new systems and

equipment for the integration of the Unit 3 program into the exist-

ing program for Units 1 and 2. During the current period, the lic-

ensee's staff was involved in monitoring the performance of new

security systems and equipment, evaluating the effectiveness of

training and assessing the need for changes as a result of imple-

menting the expanded security program.

In the current assessment period, a total of four preoperational

reviews, one special inspection and five routine inspections were

performed by region-based inspectors. Nine-of these inspections

involved the licensee's physical protection (security) program and

one reviewed the licensee's control of and accounting for special

nuclear material.

Corporate and plant management's involvement in and support for the

security program was very evident, resulting in the relatively

trouble-free integration of Unit 3 into the site security program.

The allocation of a sufficient number of experienced technical and

support personnel resulted in sound designs, good planning, timely

procurement, and quality installations.

An aggressive and comprehensive surveillance program was developed

to monitor the performance of new systems and equipment in their

initial period of use. The program was carried out by a team com-

posed of personnel with expertise in security, engineering, I&C,

and computers. The team approach was highly effective in accomp-

lishing this activity and was continued during the development of

routine surveillance testing and maintenance procedures.

As experience with systems, equipment and facilities was gained,

plans were developed and modifications were initiated for upgrading

existing systems, equipment and facilities. This demonstrated the

licensee's continuing attention to establishing and maintaining a

high quality and effective security program.

Staffing for the expanded security organization involved hiring -

about 150 new personnel. Due to the shortage of qualified candi-

dates in the local area, extensive recruitment efforts were required.

These efforts were successful and the necessary mannW, training,

and qualification were achieved on schedule. These efforts further

demonstrate the licensee's intent to implement a quality program.

!

l

1

. .

26

The training and qualification program was well developed with qual-

ity. lesson plans and instructional aids. It was adminisi;ered by

three full-time and experienced instructors provided by the security

contractor. The training program is effective and of high quality,

as indicated by the relatively small number of identified personnel-

errors. Training is continually upgraded as a result of feedback'

from operational experience and on-the-job performance observations.

Oversight of the training program is provided by a senior licensee

security supervisor and this is. considered by the NRC to be a major

strength of the program.

The licensee developed and implemented a comprehensive records man-

agement system. It included such things as manufacturers' specifi-

cations, acceptance criteria and testing data for the new systems

and equipment, design and construction information for new systems

and facilities, as well as the routine security program records.

The system provided for clear identification, ease of retrievability

and mandatory retention periods, and demonstrated the licensee's '

commitment to quality.

Necessary revisions to the licensee's corporate security audit pro-

gram, to reflect the integration of Unit 3 with the site security

program, were accomplished during the pre-operational phase as the

new systems and equipment were accepted for operation by the licen-

see. In this manner, the licensee was able to ensure that all new

program elements were included. ..The audit plan is comprehensive

and is maintained up-to-date in order to provide quality information

concerning the implementation of the program.

Fourteen Unit-3 related event reports, which required reporting

in accordance with 10 CFR 73.71, occurred during this' assessment

period. Seven of these events were minor problems with new equip-

ment / systems; of those, three concerned a deficiency in the new

intrusion detection system which, when located, was promptly cor-

rected by an engineering modification. Two events involved person-

nel errors by members of the security force. One of these was a

security officer leaving his post early; this individual was re-

trained. The other_was a security officer found asleep on duty;

this individual was fired. Licensee response to these two events

showed their strong insistence upon proper performance of duty.

Four events resulted from poor interface / coordination between vari-

ous plant functional groups and security. Another event resulted

from a contractor employee who-surrendered a' weapon prior to enter-

ing the plant protected area. The remaining event' involved a bomb

threat. Each of the above events was appropriately handled and

compensatory measures were promptly initiated when required. The'

event reports were clear,' concise and promptly submitted to NRC.

The cumulative downtime for the equipment / systems related events

was less than 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, indicating prompt attention to and detection

and correction of the problems. This timely support by I&C and

. _

e

- - -- . - . - . . - - . - - - .. - .

,

.~ .

27

.

Computer Services to the maintenance of the security systems and

equipment demonstrates the-licensee's commitment to a high quality

,

maintenance program.

During the assessment period, the' licensee submitted seven changes

to the Training / Qualification,^ Contingency, and Security Plans under '

the provisions of 10 CFR 50.54(p) and provided its response to the

August 4, 1986 Miscellaneous Amendments to 10 CFR 73.55, codified

by the NRC. The changes were described in' a summary transmitted 1

with each revision and referenced to plan pages that were marked .i

to facilitate review by NRC. Revisions were generally of high

'

, quality. The licensee's safeguards licensing function is adequately

staffed by experienced personnel who are knowledgeable of NRC pro-

.

gram objectives. The quality'of the submittals is further evidence

i of the licensee's commitment to a quality security program. '

2

'

The licensee's program and procedures'to control and account for

special nuclear material at Unit 3 were found to be adequate, as

,

was the licensee's: plan for the protection of new fuel.

In summary, corporate and site management-involvement in the program

1 resulted in the efficient and effective integration of Unit 3 into

,

a consolidated site' security program.- Significant management over-

sight and direction and the application of a well-planned and exe-

i

cuted team approach were largely responsible for the ease with which

i

this. evolution was accomplished. These factors remained strongly i

'

evident throughout the assessment period in monitoring personnel

I

and equipment / systems performance and in customizing the program .

to meet its expanded needs whole conforming to NRC program objec- '

tives. The only NRC concern identified was for a possible adverse

effect from future retirements of highly experienced and capable

individuals, and that does not affect the performance rating for ,

the current SALP period.

2. Conclusion

Category-1.

'

3. Board Recommendations

!

l

' Licensee: Place emphasis on maintaining high performance during the

transitions when senior personnel retire.

'

NRC: None.

.

,

l

!

,

a

. ,r- ..~,, ., - .,-,,_..,.,..,.,y ,, yy _g. . . , . , , , .,7 -4 , ,_4 n,, , e w. -

. . . - .- . -- . .- - - - - . . - -

1 . .

28

i

G. Outage Management (127 Hours, 2%) ,

, 1. Analysis

This is the first_ time that Outage Management has been assessed for

Millstone 3. The plant is in its first operating cycle so there was

, no refueling outage. There were, however, two planned and three

unplanned outages and planning activities for the March -1987 outage.

Outage planning, mobilization, performance, restoration and restart

,

were observed as part of the routine inspection program.

Outages were planned in detail and very closely managed. . As job

needs were identified, requisite plant conditions and materials were

'

, noted with expected durations delineated by exoerienced personnel.

The data was incorporated, with the aid of critical path management

software, into a master outage schedule complete with bar charts,

i sensitivity analysis for each task that might impact the critical

path, and logical ties between tasks. The schedule received senior

'

and supervisory ranagement reviews and modifications prior to outage

' commencement. Twice daily during an outage, an expanded time base

printout of the current _three-day window, including all recent up-

,

_ dates to the master schedule, was provided to-all supervisors during

i a status meeting. These meetings were characterized by accurate

,

assessments of work in progress and resolution of conflicts. Tight

l

controls over the schedule and plant conditions were maintained and

many potential problems were avoided by early addressal. During

these meetings, NRC observers noted a strong spirit of cooperation

,

and a very positive attitude toward nuclear safety and high quality

performance.

One safety impact of good planning has been that sufficient time

was allotted to careful completion of safety related equipment

lineups and surveillance requirements.

Administrative control of maintenance and tagging was for the most'

part effective. A notable exception was a failure to clear an Auto-

mated Work Order and its associated tag during recovery from an

outage, leaving a-Safety Injection Hot. Leg Recirculation manual

isolation valve shut until in Mode 3 (hot shutdown). During that

same outage,' two work orders that resulted in the breach of Control

4

Room and Secondary Leak Collection Recovery System.(SLCRS) pressure

boundaries were approved by Shift Supervisors without realization

that these boundaries were impacted. This was during one of the

earlier outages. Corrective actions for these licensee-identified

4

losses of control appear effective, in that there have been no re- '

peat occurrences.

Management at both the unit and department levels was proficient'

at planning and scheduling, determining contingency _ strategies, and

quickly adapting to changing conditions. An example was the 24-day

1

, , - , - ..,,,,--,v, , , , - - - sm,,- -- . , . . . ,,c - , . , - ,- ,_,~,-. ,.e- -v,- , - ,

, - . . - .. . = - . _ . _ . - - . . ___ .

i .. -.-

1

29

.

outage beginning in July 1986. The licensee had a future three-week

outage in the planning stage when performance of an inaccurate sur-

veillance procedure damaged the letdown. relief valve (this over-

pressurization of letdown piping is incorporated in the Surveillance

functional area), forcing the plant down to cold shutdown for re-

pairs. As the reactor was being cooled down, planning sessions were

called to scope the full work load and determine the critical path

,

for accomplishment of all-' commitments up to February _1987 (the ten-

l tative date for a mid-cycle outage). Many vendor and material ar-

rangements were expedited to meet the new schedule. What started

l_ as an unplanned shutdown grew into a successful 24-day outage during

( which much corrective and preventive maintenance, and major techni- '

s

' cal specification surveillances, were completed. .This effective

utilization of forced plant conditions eliminated the need for an

additional outage during the SALP period.

'

,

In summary, the controi of outage activities was a significant man- '

agement strength, based on the quality evident in the successful

l completion of numerous complex tasks during five observed outages.

1

2. Conclusion

Category 1.

l 3. Board Recommendations

i None.

!

,

i

,

i

T

. - . - .

- . - - - - = - '

. .

30

I. Licensing Activities

1. Analysis

The previous SALP rated this area as Category 2. To assure more

timely resolution of licensing issues, increased licensee management

involvement in the licensing process was recommended.

Licensee management involvement in licensing activities was evident

during the current SALP period. An example was their extensive

comments on the staff's Station Blackout [10 CFR 50.54(f)] letter

and associated discussions with NRC reviewers and management. In

addition, licensee management was active in the NUMARC industry

group addressing this activity, thereby ensuring a high level of

review and decision making on this. issue. The licensee, Northeast

Nuclear Energy Company (NNECO), also consistently demonstrated evi-

dence of prior planning and assignment of priorities, and had well

stated, controlled, and explicit procedures for control of licensing

activities. NNEC0 worked aggressively toward completing license

conditions and commitments to the NRC, and maintained a priority

list corresponding to the NRC Licensing Action Priority list. The

Unit 3 lead licensing engineer's ability to provide schedular and

technical information on past and present licensing activities in-

dicated that licensee records were complete, well maintained, and

available.

The NNEC0 licensing staff was evaluated as well qualified, and NNECO

assigned the necessary technical people to develop complete, high

quality responses to NRC requests. For exaraple, NNECO technical

staff and managers attended four NRC staff meetings to support the

NRC review of a request for approval to operate with N-1 loops.

Requests for information were responded to in meetings, conference

calls, and correspondence. Licensee responses were usually tech-

nically sound, had appropriate management review and approval, and

were submitted on or ahead of schedule.

One expedited Technical Specification change was requested, for

extending the 18-month diesel generator surveillance schedule. The

licensee notified the NRC of the schedule well in advance, and plant

management promptly responded to a request for more information.

NNEC0 was generally responsive to the staff's concerns. They took

the initiative to resolve issues through conference calls and meet-

ings, and promptly followed-up with response submittals. For the

proposed installation of one feedwater venturi inspection port in-

stead of two, the licensee provided a drawing showing the proposed

venturi meter installation which showed the inspection port and the

effect of the inspection port opening on the accuracy of the reading.

The licensee also provided ASME paper 83-JPGC-PTC-3 which described

a similar installation at Calvert Cliffs. NNEC0 was also excep-

.

. .

31

tionally responsive during the NRC staff's review of reactor cool-

ant system flow anomalies at the Callaway and Wolf Creek plants.

When asked to repeat the RCS flow measurements taken at Callaway

and Wolf Creek, the licensee took the data and promptly provided

the results in a meeting with the NRC staff, even though flow

anomalies had not been observed at Millstone 3.

Infrequent lack of responsiveness to NRC concerns was noted. One

example was responses and submittals concerning open items on reac-

tor coolant loop stop valve interlocks in the staff's Safety Evalu-

ation Report (SER) on N-1 loop operation. Some drawing submittals

were not the latest revision available. After a staff visit to the

site to obtain the latest drawings, review indicated that further

revision was needed to eliminate additional errors.

For the eight Technical Specification change requests submitted,

the licensee advised the NRC of the need for the changes and the

submittal schedule well in advance. Seven of the eight requests -

were thorough and technically sound. The eighth was an exception

which would have allowed the Nuclear Review Board (NRB) quorum to

consist of less than a majority of the NRB members. This was found

unacceptable by the NRC. Submittal of this request represented an

apparent lack of understanding of the intent of the Westinghouse

standard technical specifications.

Initially, licensee submittals lacked details on criteria for

reaching a "no significant hazards" determination. Improvement was

shown during the SALP period. A recent submittal related to ESF

response times contained detailed information from the associated

safety analysis, providing a strong basis for the "no significant

hazards" determination.

Overall, the licensee provided effective licensing liaison with NRR

and showed a clear understanding of the issues. There was effective

centralization, with one point of contact with NRC. Timely and

acceptable resolution was thereby facilitated.

2. Conclusion

Category 1.

3. Board Recommendations

Licensee: Assure accuracy of submittals to the NRC.

NRC: None.

l

l

l

.-- -

. .

32

I. Engineering Support (262 Hours, 4%)

1. Analysis

This is a new functional area. It encompasses technical activities

in addition to thos'e provided by the operations, maintenance, and

instrumentation and controls (I&C) departments.

Northeast Utilities maintained an appropriately sized onsite engi-

neering presence in both the operating company (NNEC0) and the sup-

port company (NUSCO). The NNEC0 engineering department is currently

staffed to 28 full time employees and includes reactor, mechanical

and electrical engineering functions as well as in-service inspec-

tion (ISI). The NUSCO onsite engineering group includes mechanical,

electrical, I&C, and civil / structural / stress engineering. Each of

these four groups has a NUSCO engineer as supervisor, with the large

majority of working level engineers being contracted from the Unit

3 architect / engineer. The onsite groups report directly to central

management at the utility headquarters. Additional technical sup-

port is provided by the Production Test Group. These electrical

and electronic technicians and engineers, mainly concerned with

generation and distribution equipment, are used for complex trouble-

shooting and repair problems.

The above groups above were composed of technically knowledgeable

personnel with skillful, seasoned supervision. They exhibited per-

severance and dedication to perform tasks correctly the first time.

Examples included timely and thorough assessments of the effects

of failed snubbers on the systems they restrained and the active

and timely resolution of pipe vibration problems.

The NNEC0 Reactor Engineering and ISI sections effectively.antici-

pated plant conditions and scheduled related surveillances. Reactor

physics and core surveillances were accurate, well controlled and

timely. Numerous NRC observations of inservice pump testing found

skilled and kr.owledgeable technicians performing well-controlled

tests and questioning the results for possible trends. Technique

and measurement accuracy for Local Leak Rate Tests (LLRTs) have

, never come into question. Mechanical and electrical NNECO engineer-

ing sections performed well in supporting evolutions affecting plant

operation. An example was identifying Volume Control Tank tempera-

ture reduction as a temporary means of decreasing reactor coolant

pump seal leakage. This group also did an excellent job of origi-

nating and managing special inservice tests (ISTs) when required.

An example was the special IST of the motor-driven auxiliary feed-

water pumps, identifying the cause of low suction pressure trips ,

as a pressure oscillation. I

'I

l

i

-

. _ _ _ _ _ _ _ . - _ _

. .

33

i

i

Support from NUSCO engineering was essential and well utilized.

Numerous design deficiencies were effectively addressed. Contain-

ment Recirculation System (RSS) heat exchanger service water con-

nections and chemical addition tank seismic supports were both up-

graded prior to full power licensing. The Condensate Storage Tank l

was redesigned by NUSCO with improved overpressure relief protection.

Main Steam Valve Building (MSVB) Heating, Ventilation and Air Con-

ditioning (HVAC) design problems were addressed with interim changes.

(Permanent modifications are planned.) The Main Steam _ low pressure

trip sensing lines froze (rendering 3 of 4 channels inoperative);

alternately, the Environmental Qualification high temperature limits

were routinely exceeded. Both site engineering groups coordinated

effectively to correct such deficiencies.

Engineering and design considerations contributed to several events

during this SALP period. The reactor scrams and feedwater isola-

tions due to steam generator level transients were in part due to

the equipment design, the difficulty of manual control of steam

generator level, the need for extensive system grooming, and impro-

per equipment setpoints. Corrective actions were generally good

and performance improved, but there appears to be considerable room

for further engineering improvement of steam generator level control.

Two errors in the Reactor Protective System (RPS) Overtemperature

Differential Temperature (0 tdt) setpoint calibration procedure led

to incorrect entries into the RPS for calculation of 0 tdt. One was

an incorrect constant for the setpoint calculation, the other was

a setpoint reduction for excessive Axial Flux Difference (AFD).

Both errors were caused by failure to recognize changes in NSSS

vendor setpoint documents. The result was a slight (<1%) non-con-

servative shift in the trip setpoint. In a similar instance, due

to a change between procedure setpoints and the Technical Specifi-

cations, three loop protective interlock P-8 reset at a thermal

power higher than was allowed by Technical Specifications. These

items were discovered by licensee reactor engineers, thoroughly

analyzed, and subjected to timely'and sound corrective actions

(procedure changes and re-review of~all RPS setpoints).

In one case, immediate corrective actions were evaluated as not

conservative enough. During Startup Report review, the NSSS vendor

discovered that the reactor coolant system resistance temperature

detector (RTD) response time interpretation and acceptance criteria

were in error. The error involved late provision of information

by the vendor and licensee failure to retrofit that information~ into

the Startup Manual. When correctly evaluated, loop 2 RTDs exceeded

the acceptance criteria and required a review for impact on the

Final Safety Analysis. Between the time the vendor raised the issue

and the time a Justification of Interim Operation (JIO) was provided,

five accident analy;es were in question. The licensee did not then

trip the loop 2 bistables that provide protection for these acci-

. _ - _ _ . .

. ___ _ _ _ _ .

, ..'

34

dents. Those_three bistables, as well as.two interlock and one

permissive bistables, were tripped about eight hours later when the

vendor-supplied JIO did not satisfactorily address all five accident

analyses. Subsequently, following reallocation of some design mar-

gin and additional JIO, the licensee reset these 6 bistables.

Several engineering issues which adversely affected performance were

being acted upon. Continued licensee attention to resolution of

the following of these .is needed:

- Steam Generator Feedwater Flow oscillations.

- Elimination of illuminated. control board annunciators.

- Power Operated Relief Valve internal leakage.

- Control Building ventilation radiation monitor causing spurious

ventilation isolations.

- Main Steam Valve Building Heating and Cooling.

In summary, engineering support has been satisfactory. There was

a high workload and much competent work. Some design changes were

not carried through to modification of the technical specifications

and procedures. Further, some procedures were not changed to re-

flect technical specification changes in reactor protection set-

points. Performance would have been better if steam generator level

control difficulties had been resolved-early during initial opera-

tion, and if . unnecessary control room annunciations had been signi-

ficantly lower. However, the problems were not unusual for early

operation,-and the licensee response ~was sound.

2. _ Conclusion

, Category 2.

3. Board Recommendations

Licensee: Resolve issues requiring engineering attention.

NRC: None.

f

l

'

<

!

i

- ,-- , - . - - , , - , - . , ,

.--n , - -- ~+ - , - -

- -- - . - . . .. - - - - .

,, .-

l

35

l

l

.

.

J. Training and Qualification Effectiveness

1. Analysis

,

Training and Qualification Effectiveness.is an evaluation ~ criterion  !

for each functional area. During this SALP, it also is being con- I

<

sidered as a separate area (for the first time). This area is a i

synopsis of the assessments in the other. areas. Training effective-

i ness has been measured primarily by the observed performance ofL

!

licensee personnel and, to a lesser degree, through program review.  !

A strong training commitment was. evident in the investment in. staff l

j and facilities. ..The plant specific simulator was a'significant- l

i benefit in training operators and was used to train managers as well.  ;

,

The licensee has built the training staff to'over twenty instructors, t

!

three quarters of whom hold operating licenses. There is a strong '

'

supervisory organization to manage the training staff.

Four reactor scrams-were assessed as having training implications.

These were the 1/16/86 scram due to too quick opening of a steam

, dump valve with the main steam isolation valves shut, the 1/18/86'

scram due to welding cables being near nuclear instrumentation

cables, the 3/19/86 scram caused by failure to' shift to feedwater

regulating bypass valve control,.and the 4/10/86 scram due to low

steam generator level during manual control. - While better training

'

should have reduced such events, the associated training effective-

ness is considered representative of a sound program during its

initial application to actual operation. The licensee's training

organization separately reviewed licensee event reports (LERs) and

, plant information reports-(PIRs) for training aspects, and the on-

i site safety committee (PORC) actively probed training considerations

i during its regular reviews. These feedback' loops represented man-

agement involvement and provided good corrective action inputs.

As noted in the plant operations area, operator performance ~on NRC

license examinations was good. While consistency has not yet been t

shown in that performance, NRC concern about there being too much

of a cookbook approach to accident response and too little indivi- i

-

dual case assessment no longer exists. Also, operator performance

, on shift was excellent, with quick response to changing conditions i

evident in spite of the high number of lighted annunciators.

!

j

~

The licensee is actively pursuing accreditation.by the' Institute 1

of Nuclear Power Operations (INPO). Operator training is based.on

Northeast Utility programs which are INPO accredited.- 1

,

.

'Non-licensed staff training was inspected and found acceptable. l

!

Plant equipment operators, maintenance, production test, and~I&C

i technicians have been observed performing normal and infrequent

1

1  !

l

,

_ _ _ - . _ - . _ _ _ . . . _ . ___ - _ _ _ - . _ _ _ _, _ , _ , _. - - , _ _ , . _ _ ,

. .

36

operations, maintenance activities and surveillances. These indi-

viduals have been found to be knowledgeable and to perform their

assigned tasks safely and competently.

The maintenance and I&C technician training program was actively

pursued. Training commitments were scheduled and strictly followed.

Senior department personnel actively assured that their juniors had

the knowledge for performing assigned tasks. NRC questioning of

in-service inspection technicians revealed excellent knowledge of

equipment, procedures, and applications.

A significant weakness in Shift Supervisor Staff Assistant (SSSA)

training was identified by the licensee. Use of the marginally

trained SSSAs for a task in excess of their training contributed

to isolation of an emergency core cooling subsystem without the

knowledge of shift supervision. This isolated incident was an ex-

ception to the generally excellent non-licensed personnel perform-

ance.

General Employee Training (GET) is common to the three Millstone

units. The program adequately addresses orientation, radiation

protection, security, emergency planning, safety, and assurance of

quality. Program content is directed by a steering committee made

up of the Unit Superintendents and other managers who determine the

emphasis of GET based on station performance goals.

In summary, the licensee's commitment to training was evident in

enhanced training staffing with a high percentage of experienced

licensed operators and expenditure of considerable resources for

training. The operators were assessed as becoming excellent per-

formers early in the initial operating period. Also, a high level

of operator and support personnel knowledge was consistently demon-

strated. Performance on NRC exams was good. Notwithstanding the

large number of reactor scrams, training was generally effective

in providing well qualified personnel who contributed positively

to safe operation.

2. Conclusion

Category 2.

3. Board Recommendations

Licensee: Continue training development to achieve accredited

training and assure consistently good operator examina-

tion results.

NRC: None.

..

. - -_ . _ . - . - . . . . - _ . - . . - - -- -. . . . - .

, , .

37

j

'

K. Assurance of Quality (424 Hours, 6%)

! 1. ' Analysis

Management involvement in assuring quality is an evaluation cri- '

] terion in each functional area. Quality assurance (QA) is an in-

4- tegral part of each functional area and the respective QA-inspection

'

hours are included in each one. This area is a synopsis of the

assessments of the assurance of quality. in other areas. During

1

the current SALP period, there were three QA inspections, inspec-

! tions by the' resident inspectors, and a readiness for operation's

j team inspection.

The related area of quality assurance was not rated during the pre-

vious SALP. Strengths were, however, noted in management's strong-

commitment to assure quality throughout the design, procurement;

construction and preoperational test phases. . No breakdowns in-

j quality programs or serious-individual quality problems were noted.

.

,

During the current SALP period, daily observations found Millstone

3 personnel to.have a standard of completing assigned work correctly

i on the first attempt. This positive attitude was repeatedly dis-

played. Shoddy workmanship or lack of attention to detail were

,

typically not tolerated by peers or supervisors. Department Heads

! were very knowledgeable of the status of work. -Plant personnel

'

exhibited a good attitude towards QA and adherence to procedures.

i The individuals closest to the work (operators, technicians,-me-

chanics, electricians, engineers, etc.) exhibited high personal

'

1

' performance standards and detailed knowledge of equipment and pro-

cedures.

'

QA/QC personnel were found knowledgeable of the tests they were

raonitoring. QC inspectors were found to be trained,' qualified and

i certified to the level of their responsibilities. Site staffing

!

levels were found adequate to support the startup test program and

i

normal operations, with headquarters and contractor personnel

available as needed. Questionable trends were investigated to de-

l termine their. root cause.

. First line supervisors provided close oversight of work activities.

Maintenance, I&C, and Production Test supervisors were generally

' knowledgeable of the plant design and station administrative re-

quirements. They were often observed'to be providing technical

, guidance and oversight to workers at'the work site. Further, Shift

Supervisors repeatedly demonstrated that they were knowledgeable

,

of plant activities and that they were effectively managing activi-

,

ties and shift personnel.

j

)

!

i

i

.

w- y =%-9,y-w-, y -,m,~w,-,,-, , v w e , e m m y--. ,---r.. --%m_., -,t t -- - w e t- -*T..r w. - , _ . . m ,

.

-. .

38

Department supervisors were also frequently observed in the plant

conducting personal inspections. NRC inspectors found them to be

knowledgeable of specific problems and active participants in prob-

lem resolution. These individuals were members of the onsite safety

committee, the Plant Operations Review Committee (PORC), and their

sound safety perspective extended into PORC activities. NRC obser-

vers continually witnessed frank, open, and knowledgeable PORC dis-

cussions of issues. PORC members clearly demonstrated sound safety

and facility knowledge, and their contribution to safety was a not-

able licensee strength. The many related examples of thorough

problem resolution include the licensee reviews upon discovery that

a reactor coolant loop hot leg injection valve, tagged shut for

maintenance while the plant was in cold shutdown, remained shut

while the plant was taken to hot shutdown. The basic operator error

was addressed. There also were two days of intensive PORC review

of operating procedures, tagout control, work activity control, work

activity control, and retest and training requirements. Procedure

improvements resulted. A design change to annunciate main steam

isolation was initiated as a side effect.

Senior plant staff were assigned as Duty Officers to act for licen-

see management on a weekly basis during operations and outages.

Management Representatives were assigned on eight-hour shifts round

the clock on site for coverage of outages. Daily staff meetings

were used to discuss plant conditions and each department was re-

quired to present the status of its work items. Issues were dis-

cussed and tracked in detailed reports which were updated and dis-

tributed daily. These controls provided excellent management of

ongoing activities.

Plant management attention was rapidly focused on problem areas by

the Plant Incident Report (PIR) system. This system has a very low

threshold for PIR origination and mandates unit superintendent re-

view as well as assignment of follow-up activity. Four hundred PIRs

were written during 1986. NRC inspectors found the PIRs to be an

excellent tool for keeping senior licensee managers informed, and '

senior managers did pay significant attention to root cause assess-

ment and corrective actions. This was routinely observed to occur

during daily management and PORC meetings.

The plant superintendent was observed making frequent control room

tours. Weekly plant walkdowns by operations, maintenance, and

health physics supervisors resulted in improved housekeeping, in

diminished size of contaminated areas, and in enhanced correction

of packing leakage and other lesser maintenance items.

Nuclear Safety Engineering (NSE), the independent safety engineering

group which is part of the corporate staff, was active in its cover-

age of Unit 3. This on-site group had ready access to the plant

staff, equipment and records. NSE assessed plant safety programs

i

!

l

__

- . . - . . -

.. -.

~i

39

and evaluated plant operating experiences.through reviews-of proce- '

dures and data including independent reviews of the resolution of

Licensee Event Reports (LERs) and PIRs. NSE made a significant

effort to participate in the Institute of Nuclear Power Operations ,

(INP0) sponsored Human Performance Evaluation Study Program (HPES).

Recommendations for corrective actions were provided from evalu-

ations of incidents or "near misses" reported to the HPES coordina-

tor. In addition to site specific corrective action, .the licensee

provided information to the INP0-HPES data base. Although no meas-

ured improvement in plant performance resulted, the fact that de-

tailed evaluations on human performance were performed is assessed

as contributing positively to root cause identification.

The Millstone Unit 3 Nuclear Review Board (NRB) was thorough in its

reviews. Its meeting agendas were extensive, the board discussions

were probing, and open issues were conscientiously tracked.

Plant. management losses have included the station superintendent,

the station services superintendent, and the unit superintendent.

The fact that no notable drop in performance resulted indicates

depth in management expertise and careful management of the transi- ,

,

tion periods involved.

The licensee's audit program was well planned. Audits were found

to be in depth and conclusive. Audit checklists were well organized

and comprehensive. Some audit findings, however, were left unre-

solved for as long as three years. Although no significant indi-

.

vidual concerns were involved, the three year delay in resolving

i findings indicates an audit response system inadequacy.

In summary, there was excellent regard for assurance of quality in

all aspects of plant operation. Management expended significant

effort to ensure that processes were controlled, that problems were

'

discovered, communicated and corrected, and that process controls

were modified to prevent problem recurrence.

2. Conclusion

Category 1.

3. Board Recommendations

i

None.

<

i

i

. . . _ _ - _ . . . . , _ ,

. _ . _ _ __ . _ . . . _ . , . _ _ , _ , , . _ . . _

. . _ .

.. . _. . _ . . .

. .

40

l

V. SUPPORTING DATA AND SUMMARIES

A. Investigation and Allegation-Review

None.

B. Escalated Enforcement Actions

1. Civil Penalties-

None.

2. Orders

, None.

3. Confirmatory Action Letters

None.

C. Management Conferences

11/5/85 Management Meeting onsite to discuss completion status for

construction, testing, and procedure development.

1/9/86 Enforcement Conference - failure to report a construction de-

ficiency in accordance with 10 CFR 50.55(e) when an error was

detected ir, the load path for a reactor. coolant pump snubber

support. A Level III violation was ultimately issued.

3/13/86 Management Meeting to ' discuss operating experience, plant in-

cidents, and reportable events occurring during the startup~

test program.

3/27/87 Enforcement Conference to discuss the events affecting the

operability of the "B" high pressure safety injection pump '

during 11/26-30/86. A Level IV_ violation was ultimately issued.

"

D. Licensee Event Reports

. A tabulation of Licensee Event Reports (LERs)-by functional area,-and

i. an LER synopsis, is attached as. Table 4.

1. Licensee Event Reports Reviewed

LER Nos.85-001'through 85-003,86-001 through 86-059,87-001

through 87-007, and fourteen security-related event reports.

,

-

y e y, - - - , - , - _ - - - -..m- , , - , - , - , - - . ,, , ,, .---m, y -

---r-- - ,-

w -,13- +

. .. .

. .

41

2. Causal Analysis

a. Tabulation by Common Cause Factors-

Causes:

C - Communications Inadequate

Cn - Construction

D - Design Inadequacy

E - Equipment Failure

K - Lack of Knowledge (possible training inadequacy)

M - Management Planning or Control Error

Pe - Personnel Error

Pf - Procedure Not Followed

Pr - Procedure Inadequacy

l l NUMBER l l

CAUSES OF LERs LER NUMBERS

Pe & Pr 13 85-02, 86-07, 86-15, 86-19, 86-20, 86-21,

I l 186-28, 86-30, 86-56, 86-58, 87-05, 86-06,1

Security 86-13

Pe & K 10 86-01, 86-02, 86-19, 86-21, 86-26, 86-28

l l l86-30, 86-56, Security 85-32, Security- l

86-30

Pe 6 85-03, 86-04, 86-08, 86-10, 86-33, 86-44

Pe & E 5 86-13, 86-32, 86-41, 86-48, 86-49

Pe & D 5 86-03, 86-12, 86-14, 86-26, 87-02

Pe & Cn 5 86-02, 86-06, 86-36, 86-38, 86-59

Pe & M 3 86-35, 86-52, 86-56

Pe & C 1 87-01 ,

Pe & Pf 1 86-33

Note: The causes in this table are not mutually exclusive.

For example, LER 86-21 was evaluated as having personnel

error, procedure, and training causes, and was listed

under both "Pe & Pr" and "Pe & K."

b. Tabulation By Common Event Description

Failure of Safeguards Channel due to instrument line freezing:  !

86-05 and 86-22.

Missed Surveillance: 86-07, 86-26, 86-33, 86-34, 87-06, and

87-07.

Safety Injection System Actuation: 86-01, 86-03, 86-19, and

86-21.

l

_

l

. . .

42

Steam General Level Transients: 86-10, 86-14, 86-15, 86-30,

86-32, and 86-48.

Supplementary Leak Collection System Boundary Problems: 86-06,

86-38, and 86-59.

High Temperatures in EEQ Monitored Areas: 86-29 and 86-50.

Security-Related Equipment Problems: 50-245/86-01, 86-02,

4

86-03, 86-04, 86-20, 86-21, and 86-31.

E. Licensing Activities

1. NRR/ Licensee Meetings

4

a. NRC Headquarters

1/8/86 Meeting to discuss status of licensing issues in

preparation for issuing full power operating-license.

1/23/86 Meeting to discuss Millstone 3 Station Blackout.

2/19/86 Meeting to discuss NU response to NRC's 50.54(f)

letter of December 18, 1985 on Station Blackout.

7/15/86 Meeting to discuss status of licensing activities.

7/28/86 Meeting to discuss staff concerns related to 3 loop

operation.

b. Site Visits

5/12/86 Meeting to discuss status of licensing activi-

ties.

11/14/86 Meeting to review drawings of solid state pro-

tection system for 3 loop operation.

12/23-24/86 Site visit to review Plant Design change request

files.

~

2/25/87 Site visit to simulator and control room in

support of 3 loop operation.

2. Commission Briefings

1/29/86 Vote on Full Power-License Issuance for Millstone 3.

i

i

I

I

I

l

,

, y

e -+ - -- ,

.

. . .

43

3. Schedule Extensions Granted

None.

4. Reliefs Granted

None.

5. Exemptions Granted

None.

6. License Amendments Issued

1/22/86 Low Power License (NPF-44) Amendment 1 - Remote Shutdown

Instrumentation

9/9/86 Full Power License (NPF-49) Amendment 1 - Fire Protection

Audits

7. Emergency Technical Specifications Issued

None.

8. Orders Issued

None.

9. NRR/ Licensee Management Conferences

None.

i

i

i

2

- -

-

- , - -

-

- ,

. .

TABLE 1

INSPECTION REPORT ACTIVITIES

REPORT / DATES INSPECTOR HOURS AREAS INSPECTED

423/85-54 SPECIALIST 375 AS-BUILT INSPECTION OF PIPING, DUCTING,

9/9-20/85 TEAM SUPPORTS, ELECTRICAL POWER, INSTRUMENTATION

INSPECTION AND CONTROL OF SELECTED SAFETY-RELATED

SYSTEMS

423/85-55 SPECIALIST 176 OPERATING PROCEDURES, EMERGENCY PROCEDURES,

9/16-23/85 AND REVIEW 0F LICENSEE ACTIONS ON PREVIOUS

FINDINGS

423/85-56 SPECIALIST 74 REVIEW STATUS OF PREVIOUSLY IDENTIFIED

9/30-10/4/85 ITEMS, PRE 0P STATUS OF SOLID RADWASTE

SYSTEM AND TASK ITEMS IDENTIFIED IN NUREG

0737

423/85-57 SPECIALIST 205 SURVEILLANCE, CALIBRATION CONTROL, MAIN-

11/12-27/85 TENANCE PROCEDURES, EMERGENCY PROCEDURES,

OPERATING PROCEDURES, INITIAL FUEL LOAD

PROCEDURES REVIEW, PRECRITICAL TEST PRO-

CEDURES REVIEW, STARTUP TEST PROGRAM

423/85-58 SFECIALIST 32 SITE PHYSICAL SECURITY PROGRAM

9/30-10/4/85

423/85-59 SPECIALIST 131 OPERATIONAL STAFFING, OPERATIONAL STAFF

9/30-10/4/85 TRAINING, MAINTENANCE PROCEDURES

423/85-60 IE TEAM N/A ENGINEERING ASSURANCE TECHNICAL AUDIT

8/26/85-9/19/85

423/85-61 SPECIALIST 454 PREOPERATIONAL TEST PROGRAM

9/30-11/1/85

423/85-62 RESIDENT 594 REVIEW 0F PREVIOUS FINDINGS, REVIEW 0F

9/24-11/18/85 NUREG 0737 ACTION ITEMS, OBSERVATION AND

WITNESSING OF H0T FUNCTIONAL TESTING AND

RETESTING

423/85-63 SPECIALIST 31 PHYSICAL SECURITY PROGRAM

10/21-25/85

423/85-64 SPECIALIST 68 REV 0 PHYSICAL SECURITY PLAN, SAFEGUARDS

11/4-11/8/85 CONTINGENCY PLAN, TRAINING AND QUALIFICA-

TION PLAN, AND IMPLEMENTING PROCEDURES

T1-1

_

_ -

.. - _ _. .. . _ _ _ ___ __ __

. .

4

REPORT / DATES INSPECTOR HOURS AREAS INSPECTED

'

423/85-65 SPECIALIST 100 CHEMISTRY AND RADI0 ACTIVE EFFLUENT CONTROL

_ -10/21-25/85 PROGRAMS

i

'

423/85-66 . SPECIALIST 27 EMERGENCY PLAN IMPLEMENTATION APPRAISAL

10/21-11/8/85

4

423/85-67 SPECIAL N/A INITIAL OPERATING LICENSE REVIEW REPORT

REPORT

423/85-68 SPECIALIST 24 FIRE PROTECTION / PREVENTION PROGRAM

11/4-6/85

423/85-69 SPECIALIST 326 PRE 0PERATIONAL TEST PROGRAM

11/12-27/85

423/85-70 SPECIALIST 10 NUCLEAR MATERIAL CONTROL AND ACCOUNTING

11/12-15/85

-423/85-71 SPECIALIST 216 SURVEILLANCE PROCEDURES

11/11-22/85

i'

423/85-72 SPECIALIST 18 PHYSICAL SECURITY INCLUDING: PHYSICAL BAR-

12/16-19/85 RIERS, COMPENSATORY MEASURES, ASSESSMENT

i

AIDS, ACCESS CONTROL, DETECTION AIDS, ALARM

STATIONS, COMMUNICATIONS, PERSONNEL TRNG

'

423/85-73 SPECIALIST N/A MANAGEMENT MEETING - COMPLETION STATUS FOR

11/5/85 CONSTRUCTION, TESTING, AND PROCEDURES

423/85-74 RESIDENT 417 NUREG 0737, WITNESSING OF SYSTEM AND COM-

11/19/85- PONENT TESTING,~0BSERVATION OF CORE LOAD, '

1/6/86 SURVEILLANCE, MAINTENANCE, AND PHYSICAL

PROTECTION

423/85-75 SPECIALIST 69 PRE 0P TESTING

,

12/9-13/85

423/85-76 SPECIALIST 130 PRE 0P TESTING

12/12-20/85

423/86-01 SPECIALIST 181 STARTUP PROGRAM REVIEW, POST CORE HOT

1/6-17/86 FUNCTIONAL TESTING PROC. REV. , SURVEILLANCE

!

t TEST REVIEW AND WITNESSING

,

'

423/86-02 RESIDENT 470 PLANT EVENTS AND NON ROUTINE REPORTS, NUREG

1/7-2/24/86_ 0737 ITEMS, POST CORE HOT FUNCTIONAL TEST-

ING, APPROACH TO CRITICALITY, LOW POWER

PHYSICS TEST

?

!

T1-2

.

-. . . - .-.- .-. . ,-- _

-.- -- - . . - .

_ _ _ _ _ _ - -

. .

REPORT / DATES INSPECTOR HOURS AREAS INSPECTED

423/86-03 SPECIALIST 36 SITE SECURITY PROGRAM

3/24-27/86

423/86-04 SPECIALIST 68 REVIEW OF PREVIOUSLY IDENTIFIED SIGNIFICANT

1/6-10/86 DEFICIENCIES

423/86-05 MEETING N/A MEETING REPORT: DISCUSSI0fl 0F PLANT EVENTS

3/13/86 REPORT

423/86-06 SPECIALIST 37 CHEMISTRY AND RADI0 ACTIVE EFFLUENT CONTROL

1/27-31/86 PROGRAMS

423/86-07 SPECIALIST 225 STARTUP PROGRAM REVIEW, POST CORE HOT FUNC-

1/19-2/14/86 TIONAL TEST WITNESSING AND TEST RESULTS

REVIEW, INITIAL CRITICALITY AND LOW POWER

PHYSICS TESTS, POWER ASCENSION PROGRAM

423/86-08 RESIDENT 300 PLANT EVENTS, NON-ROUTINE REPORTS AND OB-

2/25-4/14/86 SERVATION OF POWER ASCENSION TESTING,

VERIFICATION OF COMPLETION OF NUREG 0737

ITEMS

423/86-09 SPECIALIST 121 STARTUP PROGRAM REVIEW, POWER ASCENSION

2/18-3/14/86 TEST PROCEDURES REVIEW, TEST RESULTS REVIEW,

TEST WITNESSING

423/86-10 OPERATOR N/A OPERATOR LICENSING EXAMINATION

3/31/-4/4/86 LICENSING

423/86-11 SPECIALIST 90 STARTUP PROGRAM REVIEW, POWER ASCENSION

3/15-4/3/86 TEST WITNESSING AND TEST RESULTS REVIEW,

PRE 0P TEST PROGRAM FINAL REVIEW

423/86-12 SPECIALIST 145 OPERATIONAL TEAM INSPECTION, INCLUDING

4/14-18/86 SURVEILLANCE, MAINTENANCE, QUALITY ASSUR-

ANCE, AND FIRE PROTECTION ACTIVITIES

423/86-13 SPECIALIST 67 NONRADI0 LOGICAL CHEMISTRY PROGRAM, LABORA-

4/7-11/86 TORY ORGANIZATION, TRAINING MEASUREMENT

CONTROL AND ANALYTICAL PROCEDURE EVALUATIONS

423/86-14 SPECIALIST 71 STARTUP TEST RESULTS REVIEW AND STARTUP

4/14-24/86 TEST WITNESSING

423/86-15 RESIDENT 167 PLANT OPERATIONS, RADIATION PROTECTION,

4/15-5/19/86 SURVEILLANCE AND MAINTENANCE

T1-3

_ _

_ _ _

. .

REPORT / DATES INSPECTOR HOURS AREAS INSPECTED

423/86-16 SPECIALIST 32 WATER CHEMISTRY CONTROL PROGRAM

5/5-9/86

423/86-17 SPECIALIST 43 STARTUP TESTING RADIATION SURVEY PROGRAM

6/2-6/86

423/86-18 RESIDENT 153 PLANT OPERATIONS, RADIATION PROTECTION,

5/20-6/23/86 PHYSICAL SECURITY, FIRE PROTECTION, IE

BULLETINS, SURVEILLANCE AND MAINTENANCE

423/86-19 SPECIALIST 16 RADI0 CHEMICAL MEASUREMENTS USING THE NRC

6/2-6/86 REGION I MOBILE LABORATORY

423/86-20 SPECIALIST 31 STARTUP TEST RESULTS REVIEW

6/16-19/86

423/86-21 RESIDENT 115 SHUTDOWN PLANNING, PLANT OPERATIONS, RADI-

6/24-8/11/86 ATION PROTECTION, SECURITY, FIRE PROTECTION,

SURVEILLANCE AND MAINTENANCE

423/86-22 SPECIALIST 18

7/7-10/86 NOTIFICATION AND COMMUNICATION EQUIPMENT

AND PROCEDUP15, OPEN EMERGENCY PREPARED-

NESS ITEMS

423/86-23 SPECIALIST 12 REVIEW 0F RADIATION PROTECTION PROGRAM-

7/7-11/86 TRAINING, EXPOSURE CONTROL, SURVEYS, AUDITS

ALARA

423/86-24 SPECIALIST 26 SITE SECURITY PROGRAM'

7/14-18/86

423/86-25 SPECIALIST 36 MAINTENANCE PROGRAM PROCEDURES, CALIBRATION

7/21-25/86 CONTROL, AND QUALITY ASSURANCE INTERFACE

423/86-26 SPECIALIST 43 QUALITY ASSURANCE PROGRAMS FOR AUDITS

7/21-8/8/86

423/86-27 SPECIALIST 142 LICENSEE'S IMPLEMENTATION AND STATUS OF

8/18-22/86 TASK ACTIONS IDENTIFIED IN NUREG 0737

423/86-28 RESIDENT 203 SHUTDOWN PLANNING, PLANT OPERATIONS, RADI-

8/12-10/6/86 ATION PROTECTION, SECURITY, FIRE PROTECTION,

SURVEILLANCE AND MAINTENANCE

423/86-29 SPECIALIST 36 PROBLEM AREAS ASSOCIATED WITH SNUBBERS,

8/18-22/06 PORVS AND MAIN STEAM SAFETY VALVES

T1-4

.-

. .

REPORT / DATES INSPECTOR HOURS AREAS INSPECTED

423/86-30 SPECIALIST 35 SURVEILLANCE TESTING AND CALIBRATION CON-

9/8-12/86 TROL PROGRAM FOR I&C, PRODUCTION TEST,

OPERATIONS DEPARTMENT

423/86-31 OPERATOR N/A OPERATOR LICENSING EXAMINATION REPORT

12/15-19/86 LICENSING

423/86-32 SPECIALIST 34 QUALITY ASSURANCE AUDIT PROGRAM

9/15-19/86

423/86-33 RESIDENT 132 PLANT OPERATIONS, RADIATION PROTECTION,

10/7-11/17/86 PHYSICAL SECURITY, FIRE PROTECTION, SUR-

VEILLANCE AND MAINTENANCE

423/86-34 SPECIALIST 13 NON-LICENSED STAFF TRAINING

11/17-20/86

423/85-35 RESIDENT 154 OPERATIONAL SAFETY, MAINTENANCE, SURVEIL-

11/18/86- LANCE, LER REVIEW

1/05/87

423/86-36 SPECIALIST 40 EMERGENCY PREPAREDNESS INSPECTION AND OB-

11/19-20/86 SERVATION OF THE ANNUAL EMERGENCY EXERCISE

423/86-37 SPECIALIST 10 0FFSITE REVIEW COMMITTEE ACTIVITIES

12/1-5/86

4

423/86-38 SPECIALIST 16 DEGRADED PROTECTED AREA BARRIER AND COR-

12/11-12/86 RECTIVE ACTIONS

423/86-39 RESIDENT 44 OPERATIONS AND ENGINEERED SAFETY FEATURES

12/29/86-

01/07/87

423/87-01 SPECIALIST 45 ALARA, RADIATION SURVEYS, EXPOSURES, TRAIN-

1/5-9/87 ING

423/87-02 RESIDENT 229 MAINTENANCE, SURVEILLANCE, OPERATIONS,

1/6-2/17/87 RADIATION PROTECTION, RADCON, OUTAGE

TRAINING,QA, SECURITY

423/87-03 SPECIALIST 5 PHYSICAL SECURITY PROGRAM

1/27-29/87

423/87-04 SPECIALIST 12 PHYSICAL SECURITY PROGRAM

2/23-27/87

T1-5

.

. .

,

I

TABLE 2

INSPECTION HOUR SUMMARY

NORMALIZED

FUNCTIONAL AREA HOURS  % OF TIME ANNUAL HOURS

PLANT OPERATIONS 1365 19.1 910

RADIOLOGICAL CONTROLS 845 11.9 560

MAINTENANCE 359 5.0 240

SURVEILLANCE 554 7.8 370

EMERGENCY PREP. 173 2.4 115

SECURITY AND SAFEGUARDS 409 5.7 270

OUTAGE MANAGEMENT 127 1.8 130

LICENSING N/A N/A N/A

ENGINEERING SUPPORT 262 3.7 175

4 TRAINING N/A N/A N/A

.'

ASSURANCE OF QUALITY 424 6.0 280

OTHER* 2612 36.6 1740

1

TOTAL 7130 100.0 4790

  • Includes: construction inspections, the followup of previously identified con-

struction issues, as-built inspection of piping and supports, electrical and in-

strument and controls, preoperational test program implementation, test witnessing

and review and startup test programs, its implementation and test review.

T2-1

_

_ _

__

__ ____

. .

TABLE 3

ENFORCEMENT SUMMARY

SEVERITY LEVEL

FUNCTIONAL AREA 1 2 3 5 TOTAL

4_

,

OPERATIONS 2 1

'

3

RADIOLOGICAL CONTROLS

MAINTENANCE '

SURVEILLANCE ,

l EMERGENCY PREP.

SECURITY AND SAFEGUARDS 3 1 4

OUTAGES

LICENSING I

( TRAINING

ASSURANCE OF QUALITY

OTHER 1 1

_ _ _

2

TOTAL 0 0 1 6 2 9

INSPECTION REQUIREMENT SEVERITY AREA DESCRIPTION

! 423/85-74 ANSI N45.2.2-73 IV CONSTRUCTION EDG CRANKCASE OPENED WITHOUT

! 11/19/85- HOUSEKEEPING MAINTENANCE MATERIAL CONTROLS

1/6/86

10 CFR 50, IV OPERATIONS FAILURE TO FOLLOW EDG FUEL

APP. B.V OIL TRANSFER PROCEDURES

l

SECURITY PLAN V SECURITY FAILURE TO LOCK A VEHICLE f

, SECURITY PLAN IV SECURITY FAILURE TO ESCORT VISITORS

10 CFR III CONSTRUCTION NOT REPORTING A REACTOR

50.55(e) COOLANT PUMP SNUBBER SUPPORT

DEFICIENCY

l

423/86-09 10 CFR 50 V OPERATIONS INDOCTRINATION AND TRAINING

2/18-3/14/86 APP B, CRI 2 0F PERSONNEL {

423/86-38 SECURITY PLAN IV SECURITY FAILURE TO MAINTAIN PRO-

12/11-12/86 TECTED AREA BARRIER

423/86-39 TS 3.5.2 IV OPERATIONS SERVICE WATER T0 "B" HPSI

12/29/86- PUMP ISOLATED

1/6/87

423/87-03 10 CFR 75.21 IV SECURITY FAILURE TO LOCK SAFEGUARDS <

1/27-29/87 INFORMATION REPOSITORY

T3-1

_ - - _ _ _ _ .

__ _ . _ _ . . . __ _ _ _ _ - . . . - - _ . _ ___ _ _-_ _ _ . . . _ _ _ .

-. .- ,,

'

_ .,

/- -(.

>

TABLE 4 i

!

,

LICENSEE EVENT REPORTS

.

~

A. LISTING OF LERs BY FUNCTIONAL AREA.

,

4

CAUSE CODES

FUNCTIONAL-AREA A B C D E X TOTAL

J

OPERATIONS 12 6 3 3 24

l RADIOLOGICAL CONTROLS 3 1 4

l MAINTENANCE 3 1

~

4 '

.

SURVEILLANCE 6 2 6 2 16

1

EMERGENCY PREP. 0 0

SECURITY AND SAFEGUARDS 5 2 7 14

J

'

OUTAGE MANAGEMENT 0

TRAINING -0

LICENSING 0

ASSURANCE OF QUALITY 0

ENGINEERING SUPPORT- 2 17 2 21

TOTAL 31 25 2 10 15 0 83

f

'

Cause Codes

,

.A - Personnel Error

B - Design / Manufacturing / Construction / Installation

C - External Caus'e .

D - Defective Procedure

E - Component Failure

X - Other

l

,'

T4-1

l

. _ - -

_. .. _ _ - .- . . . . _ - - _ , . _ . .. _ _ . ._

_ _ _ _ . _. __

l

. .

l

l

l

B. LER SYNOPSIS

i

CAUSE

LER NUMBER EVENT DATE CODE DESCRIPTION

85-001-00 12/09/85 B EMERGENCY DIESEL GENERATOR "A" FUEL OIL

HEADER LEAK - PERFORATION IN THE RETURN

LINE TUBING

85-002-00 12/15/85 A REACTOR TRIP SIGNAL - TWO LOW-LOW LEVEL

BISTABLES ON STEAM GENERATOR "C" WHEN LEVEL

INCREASED AB0VE SETPOINT - CAUSED BY IN-

STALLED JUMPER

85-003-00 12/14/85- A 480 VOLT AC EMERGENCY-BUS, REQUIRED TO BE

OPERABLE PER TS, TAGGED OUT OF SERVICE TO

PERFORM MAINTENANCE

86-001-00 01/16/86 A REACTOR TRIP WITH SI DUE TO LOW STEAM LINE

PRESSURE

86-002-00 01/18/86 B SOURCE RANGE CHANNEL A REACTOR TRIP

86-003-00 01/19/86 B REACTOR TRIP WITH SI DUE TO LOW STEAM LINE

PRESSURE

86-004-00 01/23/86 A PLANT WENT FROM HOT STANDBY MODE TO STARTUP

MODE WITH TS ACTIONS STMT IN EFFECT WHICH

DID NOT PERMIT THIS CHANGE

86-005-00 01/25/86 B TWO CHANNELS OF STEAM GEN A STEAM LINE

PRESSURE WERE FOUND TO BE FAILED HIGH DUE

TO SENSING LINES ON PRESSURE TRANSMITTERS

BEING FR0 ZEN

86-006-00 01/25/86 B VIOLATION OF SLCRS BOUNDARY PENETRATIONS

86-007-00 02/02/86 A PLANT IN MODE 2 WITH LC0 ACTION STATMT FOR

TS 3.8.4.1 NOT MET FOR VERIFICATION OF

CONTAINMENT ELECTRICAL PENETRATION ISOLA-

TION BREAKER POSITION

86-008-00 02/02/86 A

12 HOUR GRAB SAMPLES REQUIRED BY TS 3.3.3.10 WERE NOT BEING TAKEN WITH PLANT

AT 3% POWER

86-009-00 02/04/86 E FWI OCCURRED DUE TO HIGH LEVELS IN STEAM

GEN. 1 AND 4 '

I

i

!

T4-2

- . -

- - . . . .. .

. -

. .

CAUSE

LER NUMBER EVENT DATE CODE DESCRIPTION

86-010-00 02/04/86 A REACTOR TRIP AT 15% POWER DUE TO LEVEL

DEVIATION IN STEAM GENERATOR 2

86-011-00 02/05/86 B CBI SIGNAL GENERATED DUE TO NOISE SPIKE

IN ONE OF THE INSTRUMENT LOOPS

86-012-00 02/06/86 B FWI SIGNAL FROM HIGH-HIGH WATER LEVEL IN

STEAM GENERATOR "C"

86-013-00 02/07/86 B FEEDWATER ISOLATION WITH REACTOR TRIP DUE

TO STEAM GENERATOR WATER LEVEL TRANSIENT

86-014-00 02/10/86 B REACTOR TRIP DUE TO STEAM GENERATOR WATER

LEVEL TRANSIENT-IMPROPERLY DESIGNED LEAD

BEING USED

86-015-00 02/12/86 D REACTOR TRIP DUE TO LOW STEAM GENERATOR

LEVEL-ERROR IN PROCEDURE COVERING OPERATION

OF MAIN FEEDWATER PUMPS

86-016-01 02/08/86 B PRESSURIZER CUBICLE REACHED A TEMPERATURE

OF 121.2 DEGREES FAHRENHEIT AND PLANT

ENTERED ACTION STATEMENT

86-017-00 02/13/86 E REACTOR TRIP DUE TO SSPS GENERAL WARNING

86-018-00 02/14/86 D FWI ON OPENING THE "A" MAIN STEAM ISOLATION

VALVE

86-019-00 02/28/86 A SAFETY INJECTION DUE TO LOW STEAM LINE

PRESSURE

86-020-00 03/01/86 A WITH PLANT IN MODE 3, THE RCS LOOP 2 HOT

LEG INJECTION VALVE WAS FOUND TO BE DANGER

TAGGED SHUT INSTEAD OF LOCKED OPEN AS

REQ. BY MODE

86-021-00 03/01/86 A SI DUE TO LOW STEAM LINE PRESSURE

86-022-00 03/08/86 B FAILURE OF SAFEGUARDS CHANNEL DUE TO

FREEZING

86-023-00 03/11/86 0 DEFECTIVE PROCEDURE FOR MIS-CALIBRATION

OF AREA RADIATION MONITORS IN CONTAINMENT

BUILDING

T4-3

-. . _

.

. . - - . .- .-

. .

,

.

CAUSE

'

LER NUMBER EVENT DATE CODE DESCRIPTION

,

86-024-00 03/15/86 D P-8 PROTECTIVE INTERLOCK SETPOINT HIGH

86-025-00 03/15/86 B CONTROL BUILDING INLET VENTILATION RADI--

ATION MONITOR-INOPERABILITY

'86-026-00 03/01/86 A FAILURE TO MONITOR AFD

86-027-00 03/19/86 B TRAIN "A" EMERGENCY GENERATOR LOAD

SEQUENCER SAFETY INJECTION SIGNAL-

I

86-028-00 03/19/86 D FEEDWATER ISOLATION AND REACTOR TRIP DUE

TO STEAM GENERATOR WATER LEVEL TRANSIENT

,

'

86-029-00 03/29/86 B AREA ES-07 REACHED A HIGH TEMPERATURE OF

121.2 DEGREES FAHRENHEIT

86-030-00 04/10/86 A REACTOR TRIP DUE TO LEVEL DEVIATION IN

STEAM GENERATOR C-

86-031-00 04/19/86 8 CBI' SIGNAL DUE'TO CHLORINE DETECTOR FAILURE

'

86-032-00 04/23/86 A REACTOR TRIP ON LOW STEAM GENERATOR WATER

LEVEL

4

86-033-00 04/29/86 A DISCHARGE OF THE LOW LEVEL WASTE DRAIN TANK

WAS PERFORMED WITH THE RADIATION MONITOR

SAMPLE PUMP DE-ENERGIZED

86-034-00 05/07/86 D SURVEILLANCE OF ESF BUILDING VENTILATION

4

RADIATION MONITOR SAMPLER FLOW' RATE MONITOR

WAS NOT INCLUDED IN MONITOR SURVEILLANCE

l PROCEDURES

i

86-035-00 05/09/86 A REACTOR TRIP RES8JLTANT FROM TURBINE TRIP

' DUE TO LOW CONDENSER VACUUM SCREEN WASH

REMOVED FOR MAINTENANCE-

'

86-036-00 05/19/86 A PLANT OPERATING IN ACTION' STATEMENT IN THAT

BATTERY BANK 301A-2 WAS NOT OPERABLE DUE'  :

TO AN UNPERFORMED MODIFICATION TO CHARGER l

301A-2

86-037-00 05/10/86 B CBI SIGNAL DUE TO CHLORINE DETECTOR

FAILURE

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CAUSE

LER NUMBER EVENT DATE CODE DESCRIPTION

86-038-00 06/05/86 B PRESSURE BOUNDARY VIOLATION WITHOUT PROPER

NOTIFICATION

86-039-00 06/25/86 8 CBI SIGNAL DUE TO CHLORINE DETECTOR

FAILURE

86-040-00 07/21/86 B CBI SIGNAL DUE TO CHLORINE DETECTOR FAILURE

86-041-00 07/24/86 E RX TRIP CAUSED BY LOW LOW STEAM GENERATOR

LEVEL DUE TO HIGH LEVEL FEEDWATER ISOLATION

86-042-00 07/25/86 B SAFETY INJECTION ACTUATION CAUSED BY IN-

TERMITTENT RESETTING OF PRESSURIZER LOW

PRESSURE SI BLOCK

86-043-00 07/29/86 B INCORRECT MAIN STEAM SAFETY RELIEF VALVE

BLOWDOWN RING SETTINGS

86-044-00 07/31/86 A BYPASSED LIQUID DISCHARGE VALVE WITHOUT

DOUBLE VALVE LINEUP VERIFICATION

86-045-00 07/31/86 E CONTAINMENT LOCAL LEAK RATES EXCEEDED

86-046-00 08/01/86 E FAILURE OF B TRAIN EMERGENCY DIESEL

GENERATOR DUE TO UNKNOWN CAUSES

86-047-00 08/15/86 D OVERTEMPERATURE DELTA T SETPOINT HIGH DUE

TO ADMINISTRATIVE ERROR

86-048-00 08/17/86 A REACTOR TRIP DUE TO STEAM GENERATOR WATER

LEVEL TRANSIENT CAUSED BY OPERATOR ERROR

86-049-00 08/17/86 A FEEDWATER ISOLATION AND REACTOR TRIP DUE

TO STEAM GENERATOR WATER LEVEL TRANSIENT

CAUSED BY OPERATOR ERROR

86-050-01 09/02/86 B AREA TEMPERATURE MONITORING MS-01 -

86-051-00 09/06/86 E REACTOR TRIP DUE TO LOW STEAM GENERATOR

LEVEL CAUSED BY FAILED FEEDWATER ISOLATION

VALVE

86-052-00 09/18/86 A MISSED FIRE PROTECTION SURVEILLANCE

T4-5

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CAUSE

LER NUMBER EVENT DATE CODE DESCRIPTION

86-053-00 10/15/86 D INCORRECT INTERMEDIATE RANGE DETECTOR

SETPOINTS

86-054-00 10/30/86 B FIRE WATCH NOT ESTABLISHED IN REACTOR CON-

TAINMENT WITHIN ALLOTTED TIME

86-055-00 11/06/86 E FAILURE OF B EMERGENCY DIESEL GENERATOR

TO START IN LESS THAN 10 SECONDS

86-056-00 11/30/86 A INOPERABILITY OF "B" TRAIN SAFETY INJECTION

PUMP COOLER

86-057-00 12/16/86 D INCORRECT REACTOR COOLANT SYSTEM FLOW

SETPOINTS DUE TO ADMINISTRATIVE ERROR

86-058-00 12/17/86 A INADEQUATE RAD MONITOR SURVEILLANCES DUE

TO INADEQUATE TS REVIEW

86-059-00 12/27/86 B UNSEALED SLCRS PRESSURE BOUNDARY

87-001-00 01/13/87 A REACTOR TRIP AS A RESULT OF CIRCULATING

WATER PUMP DUE TO PERSONNEL ERROR

87-002-00 01/14/87 A REACTOR TRIP DUE TO ACCIDENTAL RESET OF

SOURCE RANGE CHANNEL BLOCK

87-003-00 01/14/87 E FAILURE OF "B" EMERGENCY DIESEL GENERATOR

TO START IN LESS THAN 10 SECONDS

87-004-00 01/29/87 B MOTOR DRIVEN AUXILIARY FEEDWATER PUMP TRIPS

DUE TO LOW SUCTION PRESSURE TRIPS

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87-005-00 02/01/87 D CONTROL ROOM PRESSURIZATION SURVEILLANCE

FAILURE CAUSED BY MISPOSITIONED THROTTLE

VALVE.

87-006-00 02/01/87 A MISSED AREA TEMPERATURE MONITORING SUR-

VEILLANCE DUE TO PERSONNEL ERROR AND PRO-

CEDURE INADEQUACY

87-007-00 02/11/87 A MISSED TECHNICAL SPECIFICATION ON CONTAIN-

MENT DRAIN SUMP INVENTORY DUE TO OPERATOR

ERROR

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SECURITY RELATED LERs:

CAUSE

LER NUMBER EVENT DATE CODE DESCRIPTION

50-245/85-32 12/28/85 A SECURITY OFFICER LEFT POST PREMATURELY-

50-245/86-01 1/5/86 E INTELLIGENT 000R CONTROLLER FAILURE

50-245/86-02 1/18/86 E INTELLIGENT DOOR CONTROLLER FAILURE

50-245/86-03 1/25/86 E INTELLIGENT 000R CONTROLLER FAILURE

'

50-245/86-04 2/4/86 E INTELLIGENT DOOR CONTROLLER FAILURE

50-245/86-12 4/12/86 A BREACH OF PROTECTED AREA BARRIER

50-245/86-13 4/14/86 A VITAL AREA D0OR DISARMED DURING A

SURVEILLANCE

50-245/86-14 4/21/86 C B0MB THREAT H0AX

50-245/86-16 5/1/86 A SECURITY OFFICER ASLEEP ON DUTY

50-245/86-20 8/12/86 E LOSS OF POWER TO SECURITY SYSTEM

50-245/86-21 9/11/86 E . INTELLIGENT DOOR CONTROLLER FAILURE

50-245/86-24 11/14/86 C CONTRACTOR VIOLATES SITE FIREARMS

RESTRICTION (FIREARM DID NOT ENTER

THE PROTECTED AREA). ,

50-245/86-30 12/11/86 A BREACH OF PROTECTED AREA BARRIER

50-245/86-31 12/23/86 E LOSS OF POWER TO SECURITY SYSTEM

>

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General Offices e Selden Street, Berlin, Connecticut

v,e co cicur uo ' e oma co--

msvm. ss.c mnsasevaccow- P.O. box 270

xvt* waaao"*"" "

HARTFORD, CONNECTICUT 06141-0270

L L J [,* ,,",' ['C,c"o*,,," (203) 665-5000

February 18,1987

Docket No. 50-423

B12186

U. S. Nuclear Regulatory Commission

Attn: Document Control Desk

Washington, D.C. 20555

References: (1) T. E. Murley letter to 3. F. Opeka, Systematic Assessment

of Licensee Performance (SALP) Report No. 50-423/85-99,

dated December 27,1985.

(2) 3. F. Opeka letter to T. E. Murley, Response to SALP

Report 50-423/85-99, dated February 11,1986.

(3) T. E. Murley letter to 3. F. Opeka, Systematic Assessment

of Licensee Performance (SALP) Report No. 50-423/85-99,

dated March 21,1986.

Gentlemen:

Millstone Nuclear Power Station, Unit No. 3

Systematic Assessment of Licensee Performance (SALP)

The purpose of this letter is to inform you of the status of corrective actions

taken as a result of the SALP Board's recommendations that were provided to us

in the last SALP review period. In addition to providing you with the status of

corrective actions, we would also like to take this opportunity to provide some

information concerning our performance over the past year which we believe will

be useful to the SALP board in their next assessment of Millstone Unit 3. In

Reference (1), the NRC issued the Millstone Unit 3 SALP report for the

twelve month period ending August 31, 1985. In Reference (2), Northeast

Nuclear Energy Company (NNECO) provided its responses and comments on

SALP Report No. 50-423/85-99. In Reference (3), the NRC provided its l

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comments on NNECO's Reference (2) submittal. '

At the time of our last submittal (Reference 2), a number of corrective actions

had been completed and they were addressed in that letter. This submittal will

provide information, which is contained in Attachment 1, on the additional

corrective actions taken since then.

Additionally, Attachment 2 provides a summary of some of the key

accomplishments on Millstone Unit 3 over the past year as well as some

examples of Northeast Utilities (NU) productive participation in industry

activities and positive involvement in the regulatory process.

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We believe that you will find the-actions outlined herein that address the Board's '-

recommendations satisfactory and that you may find the additional.information

on our positive involvement in the regulatory process to be of 'v'alue in your next-

~SALP assessment- of Millstone Unit 3. .Please feel freeito contact us if you

- require any additional information.

Very truly yours,

NORTHEAST NUCLEAR ENERGY COMPANY

'

E.JTfoczka - () .

SeniorVice President-

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cc: Dr. Thomas E. Murley, Regional Administrator, Region 1 -

E. L. Doolittle, Licensing Project Manager, NRR ..

3. T. Shediosky, Senior Resident Inspector, Millstone Unit No. 3

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Docket No. 50-423-

B12136

Attachment 1

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Northeast Nuclear Energy Company

Millstone Unit No. 3

Update to SALP Report 50-423/85-99 Recommendations

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February,1987

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Functional Areat OPERATIONS SUPPORT

Board Recommendation:

Review control of ' and training ' for jumpers - and lif ted leads, . tagging, log

keeping, and shift turnover requirements to assure controls are adequate for

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power operation.

Status: -

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. NNECO has implemented Millstone. Station Administrative Control Procedures

ACP-QA-2.06.A, B & C, which cover control of bypass jumpers, lifted leads,_

i- and tagging; ACP 6.12, shif t turnover; and ACP 10.05, log keeping requirements

for- all plants at -the Millstone Station. The controls delineated in these

. procedures were initially implemented at Millstone' Units 1 and 2 and have

4

proven to.be very effective. In or' der to. assure these controls were appropriate

for power operation .and to familiarize Millstone . Unit 3 operating -personnel

with these procedural requirements prior to power operation, these procedures

were instituted during startup testing, far in advance of power operation.

In April,1986, the NRC conducted an operations _ audit . on Millstone Unit 3

- (Audit No. 8612). No weaknesses in the area of bypass jumper and lif ted lead

, - control were identified.

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Functional Area: RADIATION CONTROL

Board Recommendation:

Assure the FSAR accurately describes the solid radwaste system.

Status:

At the present time, the FSAR reflects the as built configuration of the solid

radwaste system. The FSAR will be updated in accordance with 10CFR50.71 to

reflect any modifications made to the system in the future.

We would also like to provide some information concerning our performance

over the past year in the area of radiological controls at Millstone Unit 3. As

noted in the Millstone Unit 3 SALP report (Reference (2)), the radiological

controls implemented at Millstone Unit 3 are identical to those which have been

used at Millstone Units 1 and 2. As a result of SALP Board recommendations on -

Millstone Units 1 and 2, NNECO has strengthened radiological controls in

several areas, namely radiation worker training, radiation exposure reduction,

and radwaste handling and shipping.

Radiation Exposure Reduction

With regard to radiation exposure, the cumulative exposures at Millstone Unit 3

have been extremely low. The 1986 total was about 27 person rem.

Corpora tely, NU has recently undertaken a program to lower collective

exposures for all of our plants to meet INPO goals. The program is

investigating methods of reducing dose rates and work scope in high radiation

areas, and improving worker efficiency at all plants.

Radwaste

Several changes have occurred during the past year which are expected to yield

significant improvements in the implementation of the Millstone Station

radwaste management program. Examples of these are:

o The Millstone radwaste handling group has been expanded in size and

reorganized under a separate supervisor who is responsible solely for

implementation of the radwaste management program.

o increased training is being given to radwaste handling and quality

control personnel to expand their knowledge of radwaste manifest

preparation, shipping, and burial regulations,

o Nuclear Engineering and Operations Procedure 6.07 " Quality

Assurance and Quality Control in Station Radioactive Material

Processing, Classification, Packaging, and Transportation" was issued

which defines the quality related aspects of the radwaste shipping

process.

o A NU corporate radwaste engineering group has been approved for

implementation in 1987. Staffing for this group, which will provide

engineering expertise in all areas of radwaste processing, is currently

underway.

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Radiation Worker Training -

Radiation worker training is administered as part of our. General Employee

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Training Program and is updated annually,to include lessons learned from the -

. previous year, as .well .as . NRC, INPO and NU .significant . findings from the

previous year. ,

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Additionally, supervisors have been reminded of their responsibilities in assuring .

worker radiation protection. This includes providing all .the equipment, training

and controls' necessary to ensure :that their workers: perform their. jobs both .

safely and efficiently.

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in summary, we believe that the above actions illustrate NU's commitment to

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maintaining proper radiological controls at Millstone Station.

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Functional Areat MAINTENANCE

Board Recommendation:

Establish ~a schedule for the completion and implementation of maintenance

related procedures and training programs.

Status:

All maintenance procedures necessary to support operation of the unit have

been approved and implemented.

Please refer to the TRAINING 'AND QUALIFICATION. EFFECTIVENESS

functional area for a discussion of the training programs related to

maintenance.

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Functional Area: SURVEILLANCE

Board Recommendation:

Assure surveillance procedures support future planned testing and operations.

Particular emphasis should be placed on orderly development and review of

procedures.

Status:

All surveillance procedures have been developed, reviewed and implemented to

meet the requirements of the lechnical Specifications.

Beginning in early 1985, a significant effort was expended in the development

of the surveillance testing program. Many of the tests were incorporated into

the startup test program which eliminated duplicate testing and permitted

operational experience to be gained and factored into the surveillance test

procedures.

A number of procedures for tests which are conducted during refueling outages

or less frequently are still under development. These procedures are being

developed on a schedule which will permit adequate review and training prior to

conduct of the tests.

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Functional Area: TRAINING AND QUALIFICATION EFFECTIVENESS

This functional area was not evaluated during the previous Millstone 3 SALP.

However, we feel it is important to inform you of our progress in the areas of

training programs.

Technical Training

On October 1,1986, NU submitted the Millstone Unit 3 technical training

program to INPO for accreditation (approximately 1 1/2 years ahead of

schedule). The decision to expedite the implementation of the accreditation

process was based on NU's continued commitment to excellence. In addition,

the Nuclear Training Department has commenced development of training

programs in the Radioactive Waste Worker and Quality Assurance / Quality

Centrol disciplines to the same accreditation standards. This decision was

predicated on the belief that even though the latter two programs are not part

of the INPO accreditation effort, the critical nature of these job functions in

the day-to-day operation of the unit dictate no less a quality commitment.

The Technical Training Branch is presently staffed with nine full-time technical

instructors who are exclusively committed to supporting the technical training

requirements of Millstone Unit 3. In addition, recognizing the invaluable

benefits of practical hands-on training, NU has established a fully equipped

laboratory for each journeyman discipline. During 1986, 20 % of the entire

training program was presented to approximately 20 % of the student

population. Our 1987 plans call for each mechanic, electrician, and technician

to participate in approximately five weeks of technical training. The

curriculum chosen for the 1987 schedule was guided by the plant supervisory

staff of Millstone Unit 3 based upon their operational requirements.

In a continuing effort to estab!!sh a lead position in the industry through

innovative training techniques, NU is in the process of piloting programs in the

fields of team training, diagnostic training, and such practical hands-on courses

as Reactor Coolant Pump Seal Overhaul. In the case of the latter, the RCP

Seal course is being presented six times prior to the Millstone 3 March,1987

mid-cycle outage. This course incorporates the use of a full scale mockup of

the seat assembly mounted in a bell housing. The team training process involves

Mechanics, Quality Control Engineers, Reliability Engineers, Safety Engineers,

Health Physics Technicians and ALARA Engineers all simultaneously attending

these courses, each offering their expertise to the training process. As a result

of this multi-discipline approach, several modifications to the existing

maintenance procedures have been incorporated that should reduce radiation

exposure and radwaste production, while at the same time improving the overall

human safety aspects of conducting the job.

Operator Training

Many significant improvements have been made in the area of Operator

Training.

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The organization and staffing'of this branch has been strengthened to provide

one supervisor for each nuclear unit with (2) assistant supervisors reporting to

him. The authorized staffing level has been increased to fourteen (14)

instructors per nuclear unit.

To ensure that the Operator Training Branch can attract the talented personnel

necessary to perform this critical function, position grade levels have been

upgraded such that many experienced plant operating personnel have been

attracted to a career in the Nuclear Training Department. It is noteworthy

that this action received corporate and station support, thus illustrating _the

recognition of the importance of the training functions.

During the past year, the Millstone Unit 3 operator training programs

completed cold license training, with 42 of 45 candidates receiving NRC

operator licenses. The Licensed Operator Requalification Training program was

successfully completed by all licensed personnel, and the first training program

for replacement operators was completed with 12 of 12 candidates receiving

NRC operator licenses.

The training program for the Millstone Unit 3 Operations Shif t Advisors was

successfully completed in February,1986.

The Millstone Unit 3 plant specific simulator had an availability of greater than

98% for 1986 bringing the capability for training nuclear plant operators to the

highest possible level.

A job and task analysis has been completed for all operator job positions in

preparation for INPO accreditation. Formal learning objectives are being

developed to support operator training programs, and are being incorporated

into all on-going programs as the development activity proceeds. INPO

accreditation activities are firmly on track, and the Accreditation Self

Evaluation Report will be submitted to INPO by November 1,1987.

General Nuclear Training

In October,1986 a new organization was announced for_ the General Nuclear

Training Branch. The changes primarily affected the personnel that are

supporting general training activities at the nuclear stations and should result in

.

improved efficiency in training station engineering personnel, emergency

response training, radiation worker, fire brigade, production maintenance

management and medic first-aid safety training.

The Branch now consists of three sections, two of which are located at the

Millstone Training Center, and one at the NU corporate office. The Millstone-

based staff supports the training discussed above at both the Millstone and

Haddam Neck sites and the corporate section provides corporate nuclear

training for offsite engineering personnel. The corporate staff is also

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responsible for - managing the Shif t Technical Advisor college program at

Thames Valley State Technical College.

The General' Nuclear Training Branch's priority goal at the present time is to

achieve INPO accreditation of the Haddam Neck and Millstone Technical Staff

and Manager (TSM) Training program, 'a goal that we feel confident about

meeting. The TSM Accreditation Self Evaluation Report (ASER) was submitted -

to INPO 'on October 1,1986 and course work refinements and teaching the -

approximately fifty new courses to plant engineering personnel has begun. We

are hopeful that the INPO Accreditation Team will visit in the latter part of

1987 and ultimately grant NU this important certification.

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Functional Areat LICENSING ACTIVITIES

Board Recommendations:

Increase management involvement in the licensing review process in order to

assure more timely resolution of licensing issues.

Status:

Senior NU management is routinely and actively involved in the management of

licensing issues. This is acknowledged and documented by the NRC in recent

SALP reports issued on our other Millstone plants as well as Millstone Unit

3.(1)(2) NU hss in the past and will continue to utilize all of the experience

gained from its other nuclear plants to develop consistent and technically sound

resolutions to safety issues. A high level of management review and approval

of all correspondence with the NRC is procedurally required at NU to ensure a

consistently clear licensee understanding and responsiveness to NRC initiatives.

Additionally, we have undertaken severalinitiatives to ensure that management

remains fully cognizant and involved in unresolved licensing issues. Examples

of these are discussed below,

o We have designated a Millstone Unit 3 lead licensing engineer to

facilitate communications with the NRC Project Manager.

o Our lead licensing engineer has worked closely with the NRC

Project Manager to establish a prioritization system containing all

key outstanding licensing items. This information is updated

frequently and assures appropriate priority focus and timely

resolution.

o Periodic meetings have been held between NU management and

NRC project management to assess the status of outstanding items

and thus assure that adequate resources are committed to achieve

timely resolution.

o High levels of NU management have been extensively involved in

industry groups that support NRC initiatives. NUMARC, AIF, INPO

and EEI are representative examples.

We believe that the above actions have contributed to maintaining clear

communications between the NRC and NU on outstanding information requests

and other licensing actions thereby allowing timely decisions to be made to

resolve outstanding issues.

(1) T. E. Murley letter to J. F. Opeka, "SALP Report Nos. 50-2t 5/85-98 (Pg.

32 and 33) and 50-336/85-98 (Pg. 31)," dated August 29,1986.

(2) T. E. Murley letter to J. F. Opeka, "SALP Report No. 50 /1 23/85-99" (Pg.

28), dated December 27,1985.

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1-10

During the past year NU has continued to be very responsive to NRC staff

requests for information. NU has provided information required to satisfy the

following 8 of 11 license conditions requiring submittal of additional

information.

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2.C.4 - 3 Loop Operation (July 1,1986)

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2.C.5 - Inservice Inspection Program (May 22, 1986)

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2.C.6 - Instrumentation for Monitoring Post Accident Conditions R.G.

1.97 Revision 2 Requirements (December 9,1985)

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2.C.9 - Operating Staff Experience Requirements (July 3,1986)

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2.C.10 - Changes to Initial Test Program (February 12, February 20,

March 12, March 24, May 2, May 6, May 19, and July 18, 1986)

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2.C.ll - Revised Small Break LOCA Methods to Show Compliance

with 10 CFR 50.46, TMI Stem II.K.3.31 (June 9,1986)

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2.C.13 - Detailed Control Room Design Review (May 20, 1986)

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2.C.14 - Salem ATWS Events Generic Letter 83-28 (May 13,1986)

We have continually strived to provide comprehensive, thorough, and

technically sound submittals. In cases where the NRC staff has required

additional information, we have been quick to respond to the request with

follow up telephone conference calls, meetings or additional written submittals.

We believe a prime example of this has been our pursuit of NRC approval for 3

loop operation. NU is unique in the nuclear industry in its request for approval

to operate Millstone Unit 3 with one reactor coolant loop isolated. We have

expended substantial resources to ensure that our request was founded on a firm

technical base. We have consistently demonstrated diligence in our follow-up

of NRC staff questions and concerns by providing additional information in

meetings, telephone conference calls and written correspondence. In each case,

NU was able to provide the NRC with the necessary information "on-the-spot"

or was able to obtain a clear understanding of what was required to resolve the

concern in a timely manner. It is our understanding that we have provided all

of the information necessary for the NRC to complete its review of this issue

and we are awaiting the staff's final safety evaluation and approval. We have

had a very cooperative working relationship with the NRC on this unique

licensing application.

Another area which we feel exemplifies our responsiveness to the NRC is

updating the Millstone Unit 3 FSAR. Three FSAR updates were submitted

within the first year following license issuance whereas 10CFR50.71 does not

require submittal of the first update until two years. NU has committed

substantial resources to enable us to exceed regulatory requirements in this

regard.

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1-11

We continue to maintain a knowledgable and highly motivated licensing staff.

Millstone Unit 3 licensing personnel have received training both in-house and

outside in areas such as:

- Quality Assurance

- The Nuclear Safety Ethic

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Nuclear Engineering and Operations procedures affecting licensing

(technical specification changes, license amendments, safety evaluations,

FSAR updates)

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Millstone Unit 3 Systems

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NRC Unresolved Safety issues

Additionally, Millstone Unit 3 licensing personnel are participating on various

subcommittees of the Westinghouse Owners Group.

In summary, we feel that the licensing activities associated with Millstone Unit

3 continue to demonstrate that NU management is firmly committed to

providing the proper resources and direction necessary to effectively resolve all

issues which have the potential to affect the safety of the plant.

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Docket No. 50-423

D14156

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Attachment 2

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Northeast Nuclear Energy Company __

Millstone Unit No. 3

Examples of NU Performance During Current SALP Period

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The following is a summary of various meetings, letters, or other activities that

occurred during the period January 1,1986 to January 31,1987 which we feel are

relevant to the Millstone Unit 3 SALP evaluation.

o The following plant startup milestones were achieved:

- January 23,1986 - Initial criticality.

- January 31, 1986 - Issuance of Millstone Unit 3 operating .

license NPF-49 authorizing full power operation.

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April 21,1986 - Completion of the startup test program.

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April 23,1986 - Start of commercial operation.

o January 8,1986 - A meeting was held between NU management and .

-NRC/NRR to discuss the status of remaining licensing issues prior to

issuance of the full power operating Ilcense.

o January 9,1986 - A meeting was held between NU management and

NRC Region 1 to discuss the status of remaining licensing issues prior

to issuance of the full power operating license.

o January 23, 1986 and February 19, 1986 - Meetings were held

between representatives of NU and the NRC to discuss the issue of

station blackout with respect to Millstone Unit 3.

o March 18, 1986 -

NU submitted a letter providing additional

information on station blackout for Millstone Unit 3.

o May 12,1986 - A meeting was held between representatives of NU

and the NRC Licensing Project Manager at the Millstone Station to

discuss the status of licensing activities.

o June 18, 1986 - NU provided comments on the proposed station

blackout rule. NU has been an active member of the industry effort

to resolve the USI-A-44, Station Blackout issue. In this regard, the

industry, via the Nuclear Utility Management and Resource

Committee (NUMARC) and the Nuclear Utility Group on Station

Blackout, has been working with the Staff towards a mutually

agreeable resolution to this issue. NU personnel have lead roles in

these committee initiatives.

o June 18,1986 - NU submitted a letter proposing to extend the use of

Integrated Safety Assessment Program methodology to Millstone

Units 2 and 3.

o June 25,1986 - NU submitted Revision I to the Millstone Unit 3

Inservice Test Program for pumps and valves.

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o July- 3,1986 - NU submitted a letter providing information regarding

actions taken by NU in response to IE Information Notice = 86-47,

Erratic Behavior of Static "0" Ring Differential Pressure Switches.

Although a response to this Information Notice was not required,' NU

felt it was appropriate to inform the NRC of our followup on this'

issue because Millstone was specifically mentioned in the Information

Notice as having received the subject switches.

o July 13,' 1986 - A meeting was held between representatives of NU

and NRC- project management to discuss the status of licensing

activities.

o July 22,1986 - NU submitted the Millstone Unit 3 startup report.

o July 28,1986 - A meeting was held between representatives of NU

and the NRC to discuss NRC staff concerns related to 3-loop

operation of Millstone Unit 3.

o On September 17 and 18,1986, NU hosted a Region I Fire Protection

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Organization seminar. The seminar was attended by NRC-

representatives from NRR and Region I as well as numerous utility

representatives. The seminar was well received by all in attendance

with recommendations that similar seminars be held in the future.

o In September,1986, NU Implemented an emergency preparedness

surveillance tracking system at the Millstone Station to ensure that

facilities and equipment are maintained operational. -

o On October 1,1986, NU provided comments on a draft report written

by Brookhaven National Laboratory entitled " Evaluation of

Reliability Technology Applicable to' LWR Operational Safety."- NU

has undertaken numerous initiatives aimed at maintaining high safety

system availability, such as development and use of living PRAs and

implementation of a Safety System Unavailability -Monitoring

Program.

o On November 19, 1986, a full participation emergency exercise was

successfully conducted at the Millstone Station. The exercise, which

involved Connecticut, Rhode Island, and local Emergency Planning

Zone communities, was evaluated by both FEMA and the NRC. No

major findings of deficiencies were identified.

o On January 13, 1987, Millstone Unit 3 completed 128 days of

continuous operation and estabilshed a plant record for continuous

service.

o in an effort to improve the timeliness of providing site access to

NRC inspectors, NU developed and implemented a " Read and Sign"

training program. On October 10, 1986, NU transmitted a letter to

the NRC Region I describing the program and our plans for

implementing it.

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Noteworthy

the NU QA /QC programs include the following: changes which have occurr

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The Operations QA staff has been relocated from the corporate

offices to the Millstone site. This action -is expected to

increase the effectiveness of the quality organization by

maintaining a full-time presence on site. This will allow

improved communication between the plant operating staff and

QA staff and will expand the QA department's knowledge and

evaluation of plant problems by allowing increased observation

of on-going plant activities.

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A standardized corporate QC manual has been issued which will

result in the Haddam Neck, Millstone, and Betterment

Construction QC organizations working to the same set of

procedures. This will assure consistent application of all QC

activities and will allow better utilization of personnel because

allinspectors will be trained and qualified to the same program.

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