ML20197H642

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SALP Repts 50-498/97-99 & 50-499/97-99 for Period 960324-971115
ML20197H642
Person / Time
Site: South Texas  STP Nuclear Operating Company icon.png
Issue date: 12/22/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20197F278 List:
References
50-498-97-99, 50-499-97-99, NUDOCS 9712310340
Download: ML20197H642 (7)


See also: IR 05000498/1997099

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SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

Report 50-498/97 99: 50 499/97 99

1. BACKGROUND

The SALP Board convened on November 19,1997, to assess the nuclear safety

performance of the South Texas Project for the period March 24,1996, through

November 15,1997. The Board was conducted in accordance with Management

Directive 8.6, " Systematic Assessment of Licensee Performance." The board members

included: T. P. Gwynn (Board Chairperson), Director, Division of Reactor Projects:

D. D. Chamberlain, Deputy Director, Division of Reactor Safety; and J. N. Hannon, Director,

Project Directorate ill 1, Office of Nuclear Reactor Regulation. This assessment was

reviewed and approved by the Regional Administrator.

Eunctional Areas and Ratinas .

Current Previous

Plant Operations 1 2

Maintenance 1 1

Engineering 2 2

Plant Support 1 1

11. PLANT OPERATIONS

Overall performance in the operations functional area improved and attained a superior

rating. Management oversight and supervisory presence in the plant were effective,

resulting in conservative decision-making and contributing to the organization functioning

well as a team. An excellent safety focus was maintained throughout the organization.

Routine and nonroutine activities were performed well, although equipment clearance-

orders needed management attention. Operator performance improved with superior

operating practices being the norm. Emergency operating procedures were properly

implemented. The training organization continued to thoroughly train, evaluate and critique

operating crews, contributing to the professional response of the operators to plant events.

Some examples were noted where the training staff lacked an understanding of NRC

requirements. Self-assessments were effective in improving operational performance.

Management involvement and oversight were effective and resulted in conservative

decision-making and excellent safety focus. This was particularly evident in the decision to

take Unit 2 off-line to repair an iso-phase bus duct boot following restart from the fifth

refueling outage. Management support of site activities was evident at alllevels.

Additionally, a strong sense of teamwork permeated the organization. Supervisory

presence in the plant continued to increase the staff's awareness of management

expectations.

Procedural and administrative controls governing plant operations, refueling activities, and

reduced inventory operations were excellent. Reduced inventory operations conducted

- during the latter half of the assessment period showed marked improvement. Containment

closeout inspections performed during the latter half of the assessment period were

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thorough and provided assurance of containment recirculation sump operability. Shift

turnovers and pre-evolution shift briefs were thorough and professional, contributing to the

effective and efficient operation of the units. However, instances of inadequate equipment

clearance orders and improper use of equipment clearance orders to implement de facto

procedure changes were identified, indicating the need for increased management attention

to this performance area.

Operators performed well during routine activities. Operator attentiveness to the plant,

formality of operational practices, and professionalism were notable. Excellent

communications continued to be a strength. Self verification was routinely observed, and

operators properly implemented the requirements of operating and surveillance procedures

with few exceptions. Operator response to plent perturbations and transients resulted in

safe and effective control of the units. This was particularly notable in the response to a

f ailed open moisture separator reheater relief valva. Supervision, communications,

coordination of operational activities across the organization, alarm response, and

implementation of emergency procedures were all strengths.

The material condition of plant equipment wcs excellent. The reliable oper3 tion of

equipment in response to plant events and the small number of restraints to plant restart

after trips were clear evidence of the excellent material condition of the plant. Systems

were routinely found properly aligned and safety equipment availability was high. However,

some examples of problems during the manipulation of controls and components were

noted. This was particularly evident in the inadvertent manipulation of the wrong valves

which resulted in the loss of level control for the volume control tank and, in another

instance, for the spent fuel pool. These remote, manually-operated valves were later found

to have inadequate position indication.

Operator training remained very effective with thorough evaluations and good crew

critiques. Previous training program weaknesses had been corrected. Critiques were

instrumentalin focusing attention on areas for performance improvement. Training

provided strong support to operations and was routinely involved in preparing the operating

staf f for infrequently performed evolutions. This was particularly evident in the

preparations for a major control room modification that was to be perfort ;n-line. The

quality of operator training was reflected in the professional response of tne operators to

plant perturbations and events. Notwithstanding this high level of training performance,

there were three examples of a lack of understanding of NRC requirements by the training

staff during the assessment period. These involved the f ailure to provide requalification

training to a licensed senior reactor operator with an inactive license, the submittal of poor

quality examination materials to the NRC, resulting in a necessary delay in the

administration of initiallicense examinations, and erroneously exempting the staff involved

in developing examination materials from taking requalification examinations.

A strong self-critical assessment process was evident in the operations functional area.

Both the regu%r feedback & the operating organization and the relatively high level of self-

identification and correction of problems demonstrated this. The condition reporting

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process was effectively used with a low threshold for problem identification. Nevertheless,

several events were caused, in part, by incomplete or inadequate corrective actions to

similar events, indicating additional opportunities to improve in this area. Examples

included the repetitive problems with control of spent fuel pool level and the repeat loss of

reactor coolant system level instrumentation during reduced inventory operations.

Overall performance in the Plant Operations functional area was rated Category 1.

Ill. MAINTENANCE

Overall safety performance in the maintenance functional area continued at a superior level

during this assessment period. Effective management oversight was frequently evident

with conduct of maintenance activities. Outage planning and execution was superior.

Maintenance backlogs were effectively controlled, including the emphasis on control room

annunciator and inttrument deficiencies and any conditions requiring special astention by

plant operators. Very few equipment problems caused plant challenges during the

assessment period and, for those challenges or transients that did occur, plant and

equipment response was excellent. Management and staff continued to take an aggressive

approach to resolving equipment deficiencies. The licensee had achieved and was

maintaining an outstanding material condition at the facility.

Senior management support of maintenance activities was outstanding and conservative

safety conscious decision making was routinely demonstrated in addressing plant and

equipment problems. The licensee's approach to addressing the control rod insertion

problems was indicative of the overall safety conscious approach to issues. Maintenance

programs and implementation were strong, with maintenance planning and scheduling

particularly notable and maintenance schedule adherence high. Problems identified by the

licensee demonstrated a continuing emphasis on assuring quality procedures. Program and

procedure problems were addressed promptly when identified. Maintenan::e personnel

routinely demonstrated a thorough understanding of tasks to be performed. Examples of

isolated problems with maintenance implementation included the identification that

maintenance personnelleft three plastic bags containing equipment in containment and the

f ailure to isolate the component cooling water supply to the residual heat removal pump for

disassembly of the pump.

Outage planning and execution was superior. The "one-stop shopping" concept utilized to

f acilitate and coordinate outage activities was particularly noteworthy and effective.

Licensee control of on-line maintenance activities was effective, including outstanding

utilization of risk insights with well developed risk program tools provided to the plant staff.

Licensee use of equipment mockups was particularly noteworthy for complex maintenance

activities as demonstrated by the activities associated with the control room f acility

upgrades.

The surveillance program and procedures were generally of high quality. Sumellance

program implementation was generally strong, with only a few performance problems that

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were usually identified and corrected by the licensee. Program and procedure problems

were addressed promptly when identified. Licensee actions in response to Generic

Letter 96-01, Testing of Safety Related Logic Circuits, were effective in identifying and

correcting procedure problems.

Trainin0 and qualification of . maintenance and surveillance personnel was a strength.

' Utilization of strong on the job training techniques were noted during observation of

maintenance activities. Formal training programs were strong and the licensee effectively

utilized equipment mockups for training and pre-job planning. Personnel performance errors

were few and not indicative of training or qualification deficiencies. Self assessment and

corrective action processes in the Maintenance area were strengths, with the licensee

utilizing both internal and external assessments to identify areas for improvement.

Utilization of the condition report process to self identify and correct problems was a ,

notable strength.

Overall performance in the Maintenance functional area was rated Category 1.

IV. ENGINEERING

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Overall safety performance in engineering was very good. Engineering support to other

organizations was generally strong and particularly noteworthy in systems engineering, The

engineering workload was generally well managed. Engineering programs were generally of

high quality and were being executed effectively. Of particular note was the continued strong

use of probabilistic risk assessment in support of the plant. However, deficiencies related to

corrective actions for set point problems, the proper control of calculations, and condition report

classification s,t the appropriate condition adverse to quality threshold within the design

engineering organization detracted from otherwise strong engineering performance.

System engineering support for operations and maintenance was generally thorough, timely and

conservative. Engineering and safety evaluations were generally of excellent quality. Examples

included review and development of corrective actions related to a bound control rod drive

mechanism and a seal leak of containment Spray Pump 1B, as well as the inspection of an

essential cooling water system annubar flow element to evaluate long-term performance.

System engineers were knowledgeable of their systems, had good communications with other

. plant disciplines, and readily identified plant problems. The_ operability implications of degraded

plant conditions were satisfactorily' addressed, with few exceptions.

The excellent use of probabilistic risk assessment (PRA) insights identified during the last SALP

period continued into this period and matured to a high level. Several industry leading initiatives

took place: PRA insights were used to support an application for extending the allowed outage

times for the standby diesel generators, and PRA insights effectively supported the graded

quality assurance program' application. Both appications were approved by NRC during this

SALP period in addition, PRA insights were being used effectively to monitor plant performance

on a day 4o-day basis and for scheduling and planning purposes

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The training program for engineering personnel continued to be strong. In addition to position

specific and general continuing training, approximately 50 engineers have been Senior Reactor

Operator (SRO) certified.

Management effectiveness and focus on safety were mixed. Management provided the proper

safety focus in dealing with the phenomenon of incomplete control rod insertion. Bumup in

rodded fuel assemblies was iimited, periodic rod drop tests were performed, analyses to support

continued safe operation were performed, and a fuel design change was made. In addition,

support for the condition reporting and corrective action program was evident, and the program

effectiveness continued to improve over the SALP period, in general, condition reports were

thorough and the corrective actions adequate to prevent recurrence. Engineers were

knowledgeable of the corrective action program and confident in its use. Industry operating

experience information was appropriately disseminated and reviewed, and appropriate

corrective action was taken. However, notable exceptions were identified where the corrective

action process was not effectively implemented. One significant exception noted early in the

SALP period involved leakage from the safety injection system outside containment that was not

evaluated until questioned by the NRC. The initial engineering evaluation of this adverse

condition failed to address the design basis aspects of the leakage. Another exception occurred

where timely corrective action was not taken for setpoint problems. Further, engineering

management had not provided sufficient resources for design engineering to have the proper

modeling tools to maintain the design calculations for electrical load studies. NRC involvement

was also needed during this SALP period for design engineering to focus on the design of the

advanced liquid waste processing system. When it was installed in 1992, it replaced portions of

the original processing equipment without clearly meeting the associated Updated Final Safety

Analysis Report commitments and without a documented safety evaluation.

The quality of design engineering was mixed. Design change packages, engineering

evaluations, and 10 CFR 50.59 safety evaluations were generally of excellent quality. Examples

include changes to the qualified display processing system, replacement of a thimble tube fitting,

and the addition of storage racks inside Unit 1 containment. However, there were some

weaknesses in design engineering. For example, the control of calculations for electrical,

mechanical, and instrumentation and control design bases needed improvement. In addition, as

a result of a programmatic weakness, there was not a procedural requirement to evaluate

calculation changes for impact on the Updated Final Safety Analysis Report.

In the area of self assessment and quality verification, performance was good, but selected

areas needed improvement. Effective corrective action was taken for the deficiencies noted in

the previous SALP report. The self-assessment of engineering identified some adverse

conditions; however, there we:e examples where the resulting corrective action was too

narrowly focused. For example, the corrective actions for molded case circuit breaker sizir.g

only assured that the circuit breaker in question was properly s!2ed and did not verify that other

similar circuit breakers were also properly sized. In another instance involving a problem with

essential chiller insulation degradation, the licensee did not assess the adequacy of corrective

r ctions for prev!ous similar condition reports. There were other instances where management

was not effective in assuring that design engineering condition reports were correctly classified

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at the appropriate condition adverse to quality threshold. For example, set point calculation

deficiencies, which were identified by the licensee in 1992 and again in 1995, were not identified

as conditions adverse to quality in tha> condition report system. In ancther instance, a potential

nonconservatism in the auxiliary feedwater storage tank useable volume instrument uncertainty

calculation was not identified as a condition adverse to quality. Consequently, effective

prioritization for corrective action was not always accomplished. Strengths were noted in the

steam generator replacement program and in the quarterly oversight planning and scheduling

process. Corrective actions resulting from the cuality assurance quarterly monitoring reports

were generally appropriate.

Overall performance in the Engineering functional area was rated Category 2.

V. PLANT SUPPORT

Overall performance in the Plant Support area continued at a superior level. Performance in

the radiological controls area was superior, with excellent support provided for plant

activities and only isolated performance problems noted over the assessment period.

Security performance continued to be outstanding, with plant and equipment upgrades

significantly improving capabilities over the assessment period. Emergency Preparedness

performance continued at the superior level attained during the previous assessment period

with a notable commitment to excellence dernonstrated by the entire organization.

Housekeeping was outstanding over the assessment period and the fire protection program

continued to be effectively implemented. Self assessment and corrective action

effectiveness were strong, routinely resulting in early identification of problems and

elimination of recurring problems.

Superior performance in the radiological controls area continued during the assessment

period. Radiation protection personnel provided excellent support for routine plant activities

and outage activities. An excellent ALARA program maintained the 3-year average person-

rem exposure among the top performers in the industry. Control of radioactive materials,

surveys, and personnel monitoring were excellent. Isolated problems were usually

identified by the licensee and timely and etfective corrective actions were implemented.

Superier performance was noted in the chemistry, radiological waste effluents

management, radiological environmental monitoring, solid radioactive waste management,

and transportation of radioactive materials programs. Training and qualification programs

for the staff were excellent and effectively implemented. Qualifications and technical

expertise of the staff remained at a high level.

Superior oerformance was noted in the physical security, access authorization, and fitness-

for duty program areas. Senior management support for the security program continued to

be outstanding. Plant and equipment upgrades in the security area provided notable

improvements in capabilities over the assessment period and significantly enhanced the

ability of the security organization to perform at a superior level. The design and

installation of the vehicle barrier system was excellent. The new video assessment system

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and tiie badge / hand geometry access system significantly enhanced program performance.

, Training and qualification programs were effective, with excellent facilities provided.

- Emergency Preparedness performance continued at the superior level achieved during the ,

previous assessment period, demont,trating a high level of commitment to excellence and

teamwork b/ the entire organization.' Crew performance during simulator walkthroughs

was excellent. The overall performance during the biennial emergency preparedness

exercise was excellent, with only one weakness identified related to recotective measures

for offsite field monitoring teams. Strengths were identiflod related to exercise control and

the critique process. The emergency plan, procedures, and facilities were appropriately

maintained. Training and qualification programs were strong, with personnel demonstrating

a high level of knowledge regarding changes to emergency implementing procedures.

Housekeeping was a notable strength and was considered outstanding over the assessment

period. The fire protection program continued to be effectively implemented. Self.

assessments and corrective action processes in the Plant Support area were strong.

Critical self assessments and audits along with effective problem identification and

correction routinely resulted in early identification of problems and elimination of recurring

problems. ,

Overall performance in the Plant Support functional area was rated Category 1.

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