ML20203D571
| ML20203D571 | |
| Person / Time | |
|---|---|
| Site: | South Texas |
| Issue date: | 02/10/1999 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML20203D490 | List: |
| References | |
| 50-498-98-15, 50-499-98-15, NUDOCS 9902160246 | |
| Download: ML20203D571 (23) | |
See also: IR 05000498/1998015
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ENCLOSURE 2
U.S. NUCLEAR REGULATORY COMMISSION
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REGION IV
Docket Nos.:
50-498
50-499
License Nos.:
NPF-80
Report No.:
50-498/98-15
50-499/98-15
Licensee:
STP Nuclear Operating Company
Facility:
South Texas Project Electric Generating Station, Units 1 and 2
Location:
FM 521 - 8 miles west of Wadsworth
Wadsworth, Texas 77483
Dates:
June 14 through November 23,1998
Inspectors:
D. P. Loveless, Senior Resident inspector
C. F. O'Keefe, Senior Resident inspector, STPEGS
G. L. Guerra, Resident inspector, STPEGS
Approved By:
J. l. Tapia, Chief
Project Branch A
Division of Reactor Projects
ATTACHMENT:
SupplementalInformation
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9902160246 990210
ADOCK 05000498
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EXECUTIVE SUMMARY
South Texas Project Electric Generating Station, Units 1 and 2
NRC Inspection Report 50-498/98-15; 50-499/98-15
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This special inspection was conducted to review the circumstances surrounding the June 14 fire
in a potential transformer and the subsequent deenergization of Switchgear E18. The review -
focused on operator performance during the event and circumstances surrounding the retum to
operability of the Gwitchgear E1B vital de subsystem while Battery Bank E1811 was in a
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discharged state. Calculations indicated that the battery was capable of performing its intended
functum throughout the event. However, operator performance during the event was
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considered weak. Licensed operator knowledge and procedure usage were inconsistent and
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resulted in violations of Technical Specifications and plant operating procedures.
Operations
Fire in the Train B switchgear caused operators to deenergize the' train. Vital Battery
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Bank E1811 was discharged for 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, and was, subsequently, considered to be
operable prior to its being fully recharged. The safety significance of not recognizing
that the battery was not operable was considered to be low because calculations
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demonstrated that the battery was still capable of performing its safety function
throughout the event. Although the battery and the associated train's ability to respond
to a station blackout were degraded, the remaining electrical systems continued to be
- able to respond to a station blackout event and to achieve and maintain a safe
shutdown condition (Section 01.1).
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- A number of the procedures used during the event were unclear or not sufficiently.
specific. This resulted in delayed response actions, misdirection of limited operator
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- resources to unnecessary tasks, and delayed questkening of the operability of Battery
Bank E1B11. Annunciator response procedures did not drive resolution of the problem
and did not provide operators with a list of Technical Speification required equipment
rendered inoperable when engineered safety features buses were deenergized, further
slowing operator response. The inspectors concluded that oparators had low
' expectations for the quality of the operating procedures and did not initially take action
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to improve them following this event (Sections 03.1 and O3.2).
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Licensed operators were unable to reenergize a vital bus undo, ixalized station
- blackout conditions because they did not recognize and override an antipumping
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breaker interlock. This prevented establishing standby diesel generator cooling and
delayed the retum of power to vital equipment for an additional 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 20 minutes. The
inability to establish cooling to the standby diesel generator due to a lack of procedural
- guidance and operator knowledge was considered a significant weakness
(Section 03.1).- ' '
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During the initial response to the deenergization of Switchgear E18, licensed operators
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failed to place the Train B equipment hand switches in the pull-to-lock position. This
' failure to follow the requirements of Procedure OPOPO4-AE-0001 was in violation of.
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Technical Specification 6.8.1. However, this nonrepetitive, licensee-identified and
corrected violation is being treated as a noncited violation, consistent with
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Section Vll.B.1 of the NRC Enforcement Policy (Section O3.2).
Licensed operators failed to understand the physical condition of Battery Bank E1B11
because they were unfamiliar with battery theory and the bases for battery-related
- Technical Specifications and surveillance requirements. As a result, the operability of a
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substantially discharged battery was not questioned until challenged by inspectors.' This
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resulted in a violation of the electrical de system operability Technical Specification. In
addition,'the shift supervisor, unit supervisor, duty operations manager, and duty
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engineer misunderstood the basis for Technical Specification 4.8.2.1.b and improperly
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concluded that the battery was operable. This was the result of inadequate reviews and
relying on the preliminary interpretation of each other (Sections 04.1 and 04.2).
Operators failed to place the pressurizer power-operated relief valve hand switch in the
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closed position while the associated block valve was inoperable. Although Technical
Specifications were not violated, the failure to identify that the block valve position.
indicator was not illuminated during shift tumover was not in compliance with operating
procedures. This nonrepetitive, licensee-identified and corrected violation is being -
treated as a noncited violation, consistent with Section Vll.B.1 of the NRC Enforcement
Policy (Section 04.2)
Although the minimum requirements of Technical Specifications were met, the operators
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were slow to identify that an engineered safety features power availability verification
surveillance test was required (Section O4.2).
Maintenance
During the bench testing and installation of a replacement potential transformer,
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procedures and the work order were prcperly implemented. Communication between
electrical maintenance and operations' personnel was observed to be good. First-line
supervision was in the field and providing appropriate oversight (Section M1.1).
Licensee technicians improperly performed a surveillance test to determine the state of
charge of safety-related Battery Bank E1B11. The surveillance test was conducted
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while recharging was in progress, contrary to a prerequisite in the procedure. An
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unfamiliarity with battery theory and the bases for battery-related Technical
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Specifications was the common cause between this and the failure to meet the
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requirements of the Technical Specifications and the corresponding violation
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(Secton M1.2).
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Enaineerina
Engineering calculations and analyses were well documented with reasonable
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assumptions supported by industry standards and vendor information. These efforts
fully supported the conclusion that the battery was capabic of performing its safety
function throughout the event, and thus the safety significance of the event was low.
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However, the licensee's conclusion that Battery Bank E1B11 had been maintained in a
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condition consistent with the Technical Specification requirements focused too narrowly
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on specific gravity as the sole parameter for battery operability and did not recognize the
inaccuracy of the measurements (Section E1.1).
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The inspectors concluded that the inefficient application of engineering staff resources
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may have exacerbated the problems with evaluating the problems with Switchgear E1B.
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However, licensee management was taking broad corrective actions to ensure better
support staff utilization in the future (Section E4.1).
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.' Report Details -
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Summary of Plant Status
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At 5:08 p.m. on June 14, licensod operators deenergized Vital Switchgear E1B in response to
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indications of an electrical fire. Unit 1 had been operating at 100 percent power. At 7:31 p.m. a
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- plant shutdown was commenced in accordance with Technical Specification 3.8.2.1. At -
approximately 10:45 p.m., the unit shutdown was suspended with reactor power at 12 percent,
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- pending completion of repairs to Vital Switchgear E18. At 1:32 a.m. on June 15, licensed '
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operators commenced power escalation, following retum to service and realignment of Train B
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safety-related equipment. At 9:50 p.m., on June 15, Unit 1 reactor power was stabilized at '
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100 percent.
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Unit 2 operated at essentially 100 percent reactor power throughout this event.
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I, Operations
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Conduct of Operations
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01.1
Review of Circurnstances Surroundina a June 14 Fire / Smoke in Switchaear E1B
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Inspection Scope (93702)
A specialinspection was conducted to review the circumstances surrounding the
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. June 14 fire in a potential transformer and the subsequent deenergization of
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Switchgear E18. The review focused on operator performance during the event and
circumstances surrounding the retum to operability of the Switchgear E1B vital dc
subsystem while Battery Bank E1B11 was in a discharged state. On June 14, the
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inspectors responded to the main control room to observe recovery activities.
Corrective maintenance and postmaintenance testing of the switchgear and surveillance
testing of the battery were observed in the field. Following the event, interviews with
licensed cperators and additional personnel involved in the event activities were
conducted. The inspectors reviewed plant computer data and control room logs and
completed procedure data sheets to verify statements of fact developed during the
interviews. The inspectors principally utilized inspection Procedure 93702 to assess the
following areas:
the implications of the event with respect to Technical Specification operability
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and compliance;
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the safety and risk significance of the event; and
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the significance of personnel performance errors while responding to the event.
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Inspection activities documented in this section of the inspection report focus primarily
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on the safety significance of the inoperability of vital Battery Bank E1811. The other
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b.
System Overview
- The Class 1E 125 vde battery system consists of four independent, physically separated
busses, each energized by one of two available battery chargers and one battery. The
battery chargers are powered through transformers from the three 4.16 kv engineered
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safety features buses. Class 1E electrical distribution equipment is located in the
Seismic Category I classification mechanical-electrical auxiliaries building and arranged
so that each train of the three-train system is located on a different floor elevation. This
provides for independent and redundant power source and distribution equipment such
. that no single failure will prevent a system from performing its safety function.
Solid state protection system Channel lil 125 vdc Battery Bank E1811 consists of 59
lead-calcium cells assembled in shock-absorbing, clear-plastic, sealed containers. The
batteries are kept at a continuous float voltage of 2.20 volts per cell and are maintained
in a nominally fully charged state by the battery chargers. Emergency power required
for plant protection and control is supplied by the batteries. The batteries nre sized to
carry their connected loads for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> without power flow from the +.argers in the
event of loss of ac. The four Class 1E 125 vdc channels have sufficient capacity for a
postulated 4-hour station blackout event, and Channel ll can be ac-independent for an
8-hour duration. Upon loss of power from the ac system to the battery chargers, the
batteries automatically assume the load without switching.
c.
Event Descriotion
At 5:05 p.m. on June 14,1998, the Unit 1 control room received alarms for load
sequencer trouble and grounds on the Train B 4160 volt bus, Switchgear E1B. The shift
supervisor left the control room to investigate the sequencer, while another operator
. went across the hall from the control room to investigate the bus. The operator
communicated via radio that there was_ smoke in the Train B switchgear room. The unit
supervisor paged the shift supervisor requesting that he return to the control room, and
the two discussed the situation. The unit supervisor urged the shift supervisor to assess
the condition of Switchgear E1B in person before considering deenergizing the bus.
The shift supervisor again left the control room and returned within a minute to order the
bus deenergized. The fire brigade was then activated. Plant Operating
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Procedure OPOPO4-AE-0001, Revision 11, " Loss of Any 13.8 KV or 4.16 KV Bus" was
entered.
. The fire brigade arrived to find that the smoke had dissipated. No fire alarm was
activated in the room, despite the fact that a fire detector was located directly above the
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affected switchboard. Except for a small hole in the top of the potential transformer, no
damage was observed inside the affected switchboard. Initial assessments concluded
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< that the transformer required replacement and that no parts were believed to be
available on site.
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Shift supervision, with the concurrence of the duty operations manager, concluded that
preparations should be made to shut the unit down. Initial power reduction was
scheduled to start after the 7 p.m. shift turnover. The operators spent the remainder of
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the shift determining which equipment lost power and what Technical Specification
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actions were required. The oncoming shift similarly spent a considerable amount of
time evaluating the status of equipment and determining the applicable Technical
Specification actions required. At approximately 8:30 p.m., operators recognized that a
safety function checklist had not been pedormed since the onset of the event. While
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performing this checklist, operators recognized that the pressurizer power-operated
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relief valve hand switch had not been placed in the closed position as required by
Technical Specifications when the associated block valve lost power.
When the ac bus was deenergized, both battery chargers lost their power supplies. The
operators appropriately declared the Train B de system inoperable. The operability of
the associated battery was not questioned. Operators were concemed that Battery
Bank E1B11 was discharging while its associated chargers were deenergized. A
licensed operator was assigned to report battery voltage periodically and to ensure it did
not go below 110 volts. Licensed operators assessed options for providing temporary
power to the chargers. Reenergizing Switchgear E1B with the potential transformer
isolated was determined to be the best alternative.
At 9:38 p.m., licensed operators started Standby Diesel Generator 12 and closed the
supply breaker, energizing Switchgear E18. However, attempts to close the feeder
breakers to Motor Control Centers E181 and E182 were unsuccessful. Engineers later
determined that the problem had resulted from the expected actuation of an
antipumping breaker interlock. Operators were unaware that, by design, loads on the
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sequencer had to be shed before the load center breakers could be shut as a result of
breaker antipumping circuitry. Standby Diesel Generator 12 was placed in the
emergency stop condition because cooling water to the diesel heat exchangers required
ac power from Motor Control Center E1B2.
During a search of the main warehouse, maintenance personnel were able to locate a -
spare potential transformer. A work package was planned and work commenced to
replace the transformer. Power reduction was halted at approximately 12 percent
reactor power when operators were within an hour of taking the main generator off line
and entering Mode 3. Work was then completed shortly before the self-imposed
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deadline for continuing the entry into Mode 3. Power was restored to all affected
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switchgear at approximately 12:08 a.m. on June 15. Operators pedormed a safety
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function checklist to verify that all equipment was operable, then exited all Technical
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Specification actions associated with the event at 12:36 a.m. At 12:45 a.m., inspectors
questioned battery operability because it was observed to be charging at a high rate.
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Although the shift supervisor considered it operable, he consulted with the duty engineer
who recommended performing the battery quarterly surveillance to confirm this
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conclusion. Power ascension was commenced at 1:32 a.m.
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Electrical maintenance personnel commenced performing the quarterly battery
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operability surveillance test at 1:35 a.m. After measuring the specific gravity in eight
random cells, the duty engineer concluded that the battery was not going to meet the
test procedure's acceptance criteria. None of these measurements were recorded.
This was reported to the shift supervisor at 2:15 a.m. along with a recommendation to
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perform stratification measurements. The shift supervisor concurred and, after some
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delay in locating the required test equipment, measurements were resumed at 3 a.m.
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By this time, specific gravity of the battery cells had increased as a result of the chargeng
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current.: Based on the data taken at that time, the duty engineer determined that'
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stratification measurements were no longer required and a routine midcell measurement
of cell-specific gravity was conducted. However, this action was not discussed with the
shift supervisor. The surveillance test was completed at approximately 4:30 a.m. and
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reviewed at 5:13 a.m. by the shift supervisor. Average specific gravity was noted on the
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test record sheet as not meeting the acceptance criteria, but being within Technical '
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Specification allowable values.
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9bservations and Findinas
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The inspectors reviewed the licensee's assessment of the safety significance of the
- event.~ Engineers performed sizing calculations as documented in Section E1.1. The
engineering study showed that the batteries could have supplied the channel's 2-hour
design-basis loads following the observed 7-hour discharge. This study did not include
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a customary assumption for age-related degradation because the batteries had recently
been replaced. ' Based on a review of this engineering study, the inspectors concluded
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that the safety significance, as it related to the original design basis of the battery, was
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low.
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With regard to the station blackout functions of the battery, South Texas Project relies
on any one of the three standby diesel generators as the alternate ac source. Battery
Bank E1811 was required to provide a 4-hour coping duration. The degraded condition
of the battery following the June 14 discharge left the battery unable to respond to a
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station blackout 4-hour profile. The battery could only have provided station blackout
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loads for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Consequently, the station blackout design for the
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altemate ac capability was degraded. The additional three batteries would have
provided the required capability and would have supported the recovery of either :
Standby Diesel Generator A or C as the alternate ac source. The licensee concluded
that the Station 1 E batteries retained the capability to respond to a station blackout.
Therefore, although Vital Battery Bank E1811 was degraded following a 7-hour
discharge, this did not eliminate the station's ability to respond to a station blackout
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event and achieve and maintain a safe shutdown condition.
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Conclusions
The safety significance of discharging Vital Battery Bank E1B11 for 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and
declaring it operable prior to fully charging the battery was considered low. The battery
continued to meet its design basis requirements throughout the event. Although the
battery and the associated train's ability to respond to a station blackout were degraded,
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the remaining electrical systems continued to be able to respond to a station blackout
event and achieve and maintain a safe shutdown condition.
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03~ , Operations Procedures and Documentation
03.1 ' Quality of Procedures to Combat the Event
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Inspection Scooe (71707)
The inspectors reviewed the procedures utilized in responding to the' June 14 event.'
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Control room logs were reviewed and licensed operator interviews were conducted to .
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ascertain the scope and usage of procedures. The following procedures were evaluated
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in detail to determine their accuracy and adequacy for responding to the event.
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Licensed operator implementation of the procedures was also assessed:
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OPOP09 AN-03M3, Revision 3, " Annunciator Lampbox 3M03 Response
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instructions"
OPOPO4-ZO-0008, Revision 3," Fire / Explosion"
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OPOPO4-AE-0001, Revision 11. " Loss of Any 13.8 KV or 4.16 KV Bus"
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OPSP03-EA-0002, Revision 3, " Engineered Safety Features (ESF) Power
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Availability"
OPSP03-XC-0002A, Revision 4, " Partial Containment inspection (CWainment
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Integrity Established)"
OPOP03-ZG-0006, Revision 8," Plant Shutdown from 100% to Hot Standby"
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OPOP03-ZG-0005, Revision 19, " Plant Startup to 100%"
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OPSP06-DJ-0002, Revision 3,"125 Volt Class 1E Battery Quarterly Surveillance -
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Test"
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Observations and Findinas
Through interviews with conttol room operators, the inspectors determined that a
number of procedures utilized during this event presented problems to the users.
Examples included:
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The annunciator response procedure for the initial alarms received as a result of
the failed transformer, Procedure OPOP09-AN-03M3, did not direct the operators
to a resolution of the problem. ' When operators realized that the affected bus
needed to be deenergized, the annunciator response procedures for the alarms
generated from deenergizing the bus did not provide sufficient information, such
as which Technical Specification equipment was rendered inoperable.
Operators did not have a list of loads supplied by the buses deenergized in
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response to the failure. Procedure OPOPO4-AE-0001 did not io:lude the
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Technical Specification impact statements and was generic in nature. Rather
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than having a separate section for each bus, the procedure applied to all similar
buses.. This caused the Unit Supervisor to send operators to check unaffected
equipment in order to comply with the procedure. Similarly, this procedure did
not direct performance of the safety function checklist, which would have
resulted in a more timely identification that one of the pressurizer
. power-operated relief valve block valves was inoperable.
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Procedure OPOPO4-ZO-0008 presumed that a fire would be initially discovered
by a fire alarm. In this case, a fire alarm was not received in the affected
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- switchgear room. This may have delayed response to the fire because the Shift
- Supervisor decided to personally confirm the situation before deenergizing the
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bus and activating the fire brigade after an operator reported heavy smoke.
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Procedure OPOPO4-AE-0001 did not provide adequate procedural guidance to
reenergize the motor control centers following a blackout condition on
Switchgear E18. Once the sequencer stripped the motor control centers and
locked out, attempts to close the breaker were precluded by an antipumping
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breaker interlock. As documented in Section 01.1, when operators attempted to
reenergize Switchgear E1B with Standby Diesel Generator 12, the load center
breakers were prevented from closing and cooling could not be provided to the
diesel generator. Insufficient operator knowledge of the interlocks precluded
restoring the bus. The inability of operators to reenergize a vital bus under
station blackout conditions was considered a significant weakness. This inability
delayed the return of power to vital equipment for an additional 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />
20 minutec.
Procedure OPSP06-DJ-0002 was not explicit in some regards. For instance, the
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procedure listed acceptance criteria; however, if these acceptance criteria were
not met, then stratification measurements were to be taken. Maintenance
personnel interpreted this to mean that, if stratification measurements averaged
to the required specific gravity, the acceptance criteria would be satisfied, even .
though it did not meet the procedural acceptance criteria.1 This misinterpretation
resulted in a continued belief that the battery.was operable when measurements
indicated the contrary.
The Procedure OPSP06-DJ-0002 steps for taking stratification measurements of
electrolyte-specific gravity could not be performed as written. The procedure
required sampling the electrolyte approximately an inch from the top and bottom .
of the cell and in the middle. ' Inspectors observed that the sample tube extended
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from the cell top to approximately 5 inches below the surface, preventing
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technicians from obtaining a representative sample. A top sample would have
required removing the flame arrester, However, this was procedurally prohibited.
The inspectors found through interviews that operators had low expectations for the
quality of procedures. The operators expressed frustrations about some of the
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procedures and had not submitted procedure improvement requests.
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c.
Conclusions
A number of the procedures used during this event were unclear or not sufficiently.
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specific. This resulted in delayed response actions, misdirection of limited operator
resources to unnecessary tasks, and delayed realization that Battery Bank E1811 was
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inoperable.: Annunciator response procedures did not drive resolution of the problem
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. and did not' provide operators with a list of Technical Specification required equipment
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rendered inoperable when engineered safety features buses were deenergized, further '
slowing operator response. The inspectors concluded that operators had low -
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expectations for the quality of the operating procedures and did not initially take action
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to improve them following this event.
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' Licensed operators were unable to reenergize a vital bus under localized station -
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. blackout conditions because of an antipumping breaker interlock. The inability to
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establish cooling to the standby diesel generator due to lack of procedural guidance and
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operator knowledge was considered a significant weakness. This inability delayed the
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retum of power to vital equipment for an additional 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 20 rninutes.
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03.2 Operations Compliance with Procedur_qg (71707)
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After deenergizing Switchgear E1B, operators performed Plant Operating
Procedure OPOPO4-AE-0001, Revision 11," Loss of Any 13.8 KV or 4.16 KV Bus."
Step 1 in the procedure required operators to verify that all ac engineered safety
features buses were energized.' With Switchgear E1B deenergized, the response was
not obtained. Therefore, the procedure directed operators to place Train B equipment
hand switches in the pull-to-lock position. This action was not performed while
implementing this procedure. Procedure OPOPO4-AE-0001 was completed at 5:36 p.m.
on June 14. However, the Train B equipment hand switches were not placed in the
pull-to-lock position until approximately 9 p.m. The failure to follow the requirements of
Procedure OPOPO4-AE-0001 was in violation of Technical Specification 6.8.1. This is a
nonrepetitive, licensee-identified and corrected violation and is being treated as a
noncited violation, consistent with Section Vll.BM si the NRC Enforcement Policy
(498/98015-01).
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.The; unit supervisor had performed this evolution and stated during an interview that the
failure to place the hand switches in the pull-to-lock position was an oversight. The
event review team documented this occurrence and management took appropriate
action. The inspectors reviewed Condition Report 98-9069. Action 7 described
corrective actions and proposed revisions for the weaknesses in
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Procedure OPOPO4-AE-0001.
During interviews with the unit supervisor and reviews of procedural controls, the
inspectors noted that Procedure OPOP04-AE-0001 was a generic procedure that
covered a!! safety-related and nonsafety-related switchgear in the plant. The lack of
specific direction caused operators to perform unnecessary verifications clearly
unrelated to the deenergization of Switchgear E1B. A review of this procedure's quality
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is covered in Section 03.1 of this inspection report.
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04
Operations Knowledge and Performance
04.1 Operator Knowledae of Batterv Function and Theory -
a.
Inspection Scope (71707)
The inspectors conducted interviews with senior reactor operators, reactor operators,
and reactor plant operators to evaluate the general knowledge of battery theory,
function, and the associated Technical Specification bases. The licensee's event review
team report and the sequence of events were evaluated and were included as part of
~ his assessment.
t
b.
Observations and Findinas
The inspectors observed that the operators involved in this event were not familiar with -
the battery Technical Specifications bases and only had a general knowledge of battery
theory' The inspectors found that this lack of knowledge contributed significantly to the
.
operators' conclusions about batten operability.
During this event, a licensed operator was assigned to monitor battery voltage during
the time it was discharging, as discussed in Section 04.2 of this inspection report. This
was based on a mistaken belief that Technical Specification 4.8.2.1.b implied that the
battery was operable if its output remained above 110 volts. The inspectors determined
that each of the operators involved incorrectly believed that battery voltage was an
indication of the state of charge.
- The inspectors reviewed IEEE Standard 450-1980, "lEEE Recommended Practice for
- Maintenance Testing, and Replacement of Large Lead Storage Batteries for
Generating Stations and Substations." This document stated that the state of charge
was determined by measuring specific gravity of the electrolyte. Howaver, the standard
further stated that specific gravity was not accurate during charging. Thus, the state of -
charge of the battery could not be determined after the discharge was begun until it was
fully recharged. This conclusion was supported by Technical Specification
requirements, but was not understood by operators.
Similarly, the quarterly battery surveillance was performed despite not meeting a
prerequisite that the battery be fully charged and at float voltage. Operators and
electricians mistook this to mean that the charger was set for a float charge. As a
result, operators requested the performance of a surveillance intended to trend the
condition of a fully charged battery over its lifetime with the intent of determining the
state of charge of a substantially discharged battery. When the initial results were not
the desired results, stratification measurements were ordered. After a delay during
which charging continued, measurements were obtained that appeared to support the
initial conclusion that the battery was operable. However, the questionable validity of
these measurements was not recognized. Consequently, the state of charge could not
be accurately determined at that time, and the battery was inoperable.
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.g.
The inspectors noted that the licensee's response plan for this event conservatively
- assumed that repairs would not be made in time and that the plant would require entry
. into Mode 3. When repairs were successful, licensed operators did not fully evaluate
what actions and equipment conditions would be required to retum to full power.
Operability of the battery was never considered until raised by the inspectors. Since the
de electrical supply system was inoperable while the chargers were deenergized,
operators had not been forced to consider battery operability, only the functional status
of the battery.L Once the charger was reenergized, the associated battery condition
became important for operability of the system, but the inoperable condition was not
recognized.-
c.
Conclusions
Operators were unfamiliar with battery theory and the bases for battery-related
Technical Specifications. As a result, the operability of a substantially discharged
battery was not questioned until challenged by inspectors. An inappropriate surveillance
!?st was performed in an attempt to confirm that the battery was operable without
_
- recognizing that the results would be inaccurate and that a prerequisite could not be '
met. The test results were then accepted as assuring that the battery was operable
without recognizing that the wrong standard was being used to determine operability.
O4.2 Operator Knowladae and Usaae of Technical Soecifications
a.
Insoection Scope (71707)
The inspectors evaluated Technical Specification actions required by the events of
June 14 and 15. The licensee's event review team report and the Technical
Specifications were reviewed. Interviews were conducted with control room senior
reactor operators regarding implementation of applicable requirements. Licensed -
operator knowledge and usage of Technical Specification requirements were evaluated.'
' Compliance with the following specific requirements was assessed:
Technical Specification 3.8.2.1, "D. C. Electrical Sources"
.
~
Technical Specification 3.4.4," Power-Operated Relief Valves"
-.
Technical Specification 3.8.1.1.a. " Demonstration of Operability for Independent
.
Offsite A. C. Circuits"
Technical Specification 4.8.2.1.b, " Operability Verification of 125-volt Battery
.
Bank Following Discharge"
>
b.
Observations and Findinos
On June 14 at 5:08 p.m., licensed operators deenergized Switchgear E1B. This
removed the Channel 111 battery chargers from service and placed 125-volt Battery
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Bank E lB11 in' service. - At this time, battery terminal voltage dropped to 117.7 volts,
which equated to an average output of 2.0 volts / cell for the 59 connected cells.
Technical Specification 3.8.2.1 states that:
As a minimum, the foilowing D. C. electrical sources shAll be
OPERABLE . . . Chanteel lli 125-volt Battery Bank E1811.
Table 4.8-2, " Battery Surveillance Requirements," provides, in part, that the allowable
float voltage value for each connected battery cell for Category B parameters
. be >2.07 volts. Table Notation 3 states: "Any Category 8 parameter not within its
allowable value indicates an inoperable battery."
The allowable value for specific gravity, as stated in Technical Specification Table 4.8-2,
is that the " Average of all connected cells > or equal to 1.195 or battery charging current
is less than 2 amps when on charge." As documented in Section 01.1.c of this
inspection report, performance of Procedure OPSP06-DJ-0002 indicated that average
. cell specific gravity was less than Txhnical Specification defined allowable values at
2:15 a.m. on June 15. Similar testing documented that average cell specific gravity was
. greater than 1.195 at approximately 3:30 a.m. Licensed operators had determined that
the batteries were operable at that time. However, subsequent calculations by the
licensee showed that specific gravity was less than 1.195 at 8:02 p.m. Therefore, it can
be concluded that the battery was inoperable by at least 8:02 p.m.
The inspectors noted that data from the emergency response facility data acquisition
and display system indicated that battery charging current was greater than 2 amps until
approximately 10:37 a.m. This value of 2 amps related to an instrument reading of
'
approximately 6 amps with a normal steady-state system loading of approximately
4 amps. Technical Specification 4.8.2.1, Table 4.8-2, stated that battery charging
current must be less than 2 amps when on charge for operability. Given that IEEE
-
Standard 450-1980 stated that specific gravity measurements were not accurate while
charging, charging rate was the goveming Technica! Specification parameter.
Therefore, the battery had been inoperable for at least 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> 35 minutes Technical Specification 3.8.2.1.c, Action a., states:
With one of the required battery banks inoperable, restore the inoperable
i
battery bank to OPERABLE status within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or be in at least HOT
.. STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the
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following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />,
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The failure of the licensed operators to place the Unit 1 reactor in a hot standby
' condition within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of Battery Bank E1B11 becoming inoperable was in violation of
- Technical Specification 3.8.2.1.c (498/98015-02).
On June 14 at approximately 8 p.m., a reactor operator performed Form 10,." Safety
Function Checklist," of Plant Operating Procedure OPOP01-ZQ-0022, Revision 15,
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" Plant Operations Shift Routines." At approximately 8:30 p.m., licensed operators
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identified that Pressurizer Power-Operated Relief Block Valve 1-RC-MOV-0001B had
been deenergized when Switchgear E1B had been isolated at 5:08 p.m. Technical
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Specification 3.4.4.d states:
)
With one block valve inoperable,'within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> restore the block valve to
operable status or place the associated power-operated relief -
)
valve (PORV) in closed position; restore at least one block valve to
OPERABLE status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />; otherwise, be in at least HOT '
~
STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in HOT SHUTDOWN within the
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following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
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The inspectors determined that, although the operators had not placed the power-
operated relief valve in the closed position, the shutdown requirements of the
specification were being met for other reasons. Therefore, it was considered fortuitous
that a Technical Specification violation had not occurred. However, licensed operators
on the day shift had been relieved at approximately 7:20 p.m. and failed to recognize the
loss of power to the block valve and the subsequent failure to place the power-operated
relief valve in the closed position during the shift tumover process. Procedure OPOP01-
20-0022, Section 3.3, required that, during shift tuihover, watchstanders walkdown the
control boards. Specifically, step 3.3.5 required that:
During the control board walkdown, on-coming Control Room
Watchstanders SHALL scan the panels to ensure normally lit
indications are illuminated.
The failure of the oncoming licensed operators to determine that the Block
- Valve 1-RC-MOV-0001 B position, a normally lit indication, was not illuminated was in
violation of Procedure OPOP01-ZQ-0022 requirements. This failure is not considered
minor because it represents a potential for missing entry into required Technical
Specification action statements. This nonrepetitive, licensee-identified and corrected -
,
violation is being treated as a noncited violation, consistent with Section Vll.B.1 of the
!
NRC Enforcement Polig'I%/98015-03).
As discussed in Section 01.1.c of this inspection report, licensed operators performed
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Plant Surveillance Procedure OPSP03-EA-0002 approximately 50 minutes after
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Switchgear E1 B was deenergized. This action was fully in compliance with the
Technical Specification 3.8.1.1.a requirement to demonstrat6 the operability of the
remaining engineered safety features power sources within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of identifying an
iinoperable circuit. However, during interviews with the unit supervisor and the reactor
operator performing the procedure, the requirement to perform the verifications was not
identified until 45 minutes after Switchgear E1B was deenergized. Although the
~ minimum requirements were met, the failure to identify the requirement in a timely
manner was of concern. The adequacy of procedures as a tool to assist the operators
in identifying Technical Specification requirements was reviewed as documented in
Section O3.1 of this inspection report.
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During interviews with the shift supervisor, unit supervisor, duty operations manager,
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and on-call system engineer, the inspectors determined that these individuals
!
misunderstood the basis for Technical Specification.4.8.2.1.b. This specification
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requires demonstration of battery operability:
i
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At least once per 92 days and within 7 days after a' battery discharge with
. j
battery terminal voltage below 110 volts, or battery overcharge with
battery terminal voltage above 135 volts, by verifying that . . . The
!
parameters in Table 4.8-2 meet the Category B limits.
)
Licensed operators had informed the inspectors that Battery Bank E1811 had remained
operable during and following the 7-hour discharge because the battery terminal voltage
had not fallen below 110 volts. The basis document for Technical Specification 4.8.2
states that the surveillance requirements for demonstrating operability of the station
batteries are based, in part, on IEEE Standard 450-1980, "lEEE Recommended Practice
for Maintenance, Testing, and Replacement of Large Lead Storage Batteries for
Generating Stations and Substations." Section 4.3.4,"Special Inspections," of
IEEE 450-1980, states:
If the battery has experienced an abnormal condition (such as a
severe discharge or overcharge), an inspection should be made
to assure that the battery has not been damaged.
Therefore, this specification was intended to specify actions to be taken when the
potential for battery damage exists. It does not imply that a battery with a terminal
voltage of 110 volts under load has sufficient charge to perform its design function.-
Licensee management concurred with this interpretation.
The inspectors found that the operator's erroneous interpretation had been presented to
other control room personnel and had not been reviewed further nor challenged. This
interpretation was supported by the duty engineer. Weaknesses in the operators' ~
knowledge of battery theory and function were reviewed and are discussed further in
Section O4.1 of this inspection report.
c. -
Conclusions
Licensed operators failed to understand the physical condition of Battery Bank E1811
and the basis for battery surveillance requirements. This resulted in a violation of the
electrical de system operability Technical Specification. in addition, the shift supervisor,
unit supervisor, duty operations manager, and duty engineer misunderstood the basis
1
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for the 110 volt limit discussed in Technical Specification 4.8.2.1.b. This resulted from
inadequate reviews and reliance on preliminary interpretations of requirements.
While Technical Specifications were not violated when the operators failed to place the
pressurizer power-operated relief valve hand switch in the closed position while the
associated block valve was inoperable, the failure to identify that the block valve position
,
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indicator was not illuminated during shift tumover was not in compliance with operating
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procedures. Additionally, although the minimum requirements of Technical
Specifications were met, the operators were slow to identify that an engineered safety
- features power availability verification surveillance test was required.
.
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11. Maintenance
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M1'
Conduct of Maintenance -
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~ M1.1 Observation of Field Maintenance Activities (62707)
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a.
Inspection Scope
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The inspectors observed the testing of two spare replacement potential transformers
and the removal and replacement of the degraded potential transformer in the 4.16 kv
]
switchgear.
b.
Qhggrvation and Findinos
After searching for spare potential transformers, maintenance personnel identified two in
the main warehouse. The inspectors observed the technicians bench testing the spare
potential transformers in accordance with Plant Maintenance
Procedure OPMP05-ZE-0206, Revision 1, " Potential Transformer Test." This test
verified that the transformer reduction ratio was consistent with nameplate data. The -
potential transformer specification ratio of 35:1 was verified on both spare transformers.
The_ inspectors observed the removal of the failed potential transformer and the
installation of a bench tested potential transformer in the Train B Class 1E switchgear.-
This was performed in accordance with Work Authorization Number 139620,"4160 VAC
Switchgear E1 Train B 4.16 KV Potential Transformer Appears to Have Failed.'" The -
work was performed as outlined in the work package.
During the replacement, two electricians performed the work while the first-line electrical
supervisor observed and assisted when the electricians requested his opinion. The
licensee maintained sufficient support personnel to assist in the potential transformer
'
. replacement. Engineering personnel also observed the maintenance activity.
Operations and electrical maintenance personnel interfaced well, which resulted in a
- change-out before the end of the Technical Specification action statement for the
battery charger required a unit shutdown. The electricians were careful to align the
- potential transformer so that the stabs would make proper contact with the electrical
- contacts. The potential transformer was energized and the associated equipment
clearance order removed.
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c.
Conclusions
The bench testing and installation of a replacement potential transformer were properly
t
implemented in accordance with procedures and the work order. Communication was
good between electrical maintenance and operations' personnel. First-line supervision
was in the field and providing appropriate oversight.
M1.2 Batterv Surveillance Testina
,
a.
Inspection Scope (61726)
On June 15, the inspectors observed testing performed in accordance with Plant
Surveillance Procedure OPSP06-DJ-0002, Revision 3. "125 Volt Class 1E Battery
Quarterly Surveillance Test." In addition, documentation of testing related to Battery
Bank E1811 was reviewed.
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b.
Observations and Findinas:
In response to the inspectors' questions regarding the operability of Battery
Bank E1811, the duty engineer recommended performing Surveillance
Procedure OPSP06-DJ-0002 to measure battery parameters as documented in
Sections 01.1 and O3.1 of this inspection report. The duty engineer had previously
been the system engineer for the system and was famiiiar with the test.
Inspectors observed technicians measure cell voltage for each cell, then measure the
specific gravity in a number of cells at different locations. All measurements were below
,
the acceptance criteria for average specific gravity, with values of approximately 1.190.
!
The inspectors observed that this was expected by the technicians because the battery
had been substantially discharged and had not been charging very long. Without
completing the specific gravity measurements or recording the as-found data, the duty
engineer went to the control room and reported that the measurements "were not going
to pass." The duty engineer recommended taking stratification measurements and
stated that he expected this testing to meet the acceptance criteria because charging
was known to cause stratification. The Shift Supervisor confirmed that the procedure
allowed this action and concurred. Some delay occurred while the proper test-
equipment was located.
When specific gravity measurements were resumed approximately 45 m,nutes later, the
midcell measurements had risen sufficiently to meet the surveillance procedure
,
acceptance criteria. Consequently, the duty engineer informed the technicians that only
'
midcell measurements needed to be performed. Stratification measurements were
therefore never taken at the direction of the duty engineer. When the completed
surveillance document was returned to the control room for review, the S5ift Supervisor
failed to note that the stratification data was not taken. Measuring the specific gravities
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at midcell did not satisfy the surveillance procedure acceptance criteria; nevertheless,
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the Shift Supervisor noted on the surveillance cover sheet that thb specific gravities
,
were sufficient to satisfy the Technical Specification surveillance criteria. The battery
,
was therefore considered operable based on the surveillance results.
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The inspectors reviewed the completed surveillance document and identified the
following discrepancies:
The work was authorized by the Duty Operations Manager, rather than the Shift
Supervisor, as specified by the procedure.
Prerequisite 4.3 required the battery to be on float charge. This was
misinterpreted by technicians to mean the charger was in the float charge mode,
rather than the intended battery condition of fully charged and at float voltage.
Technicians stopped following the procedure when it was recognized that the
specific gravity was not going to meet the acceptance criteria. Data for the cells
sampled was not recorded. The duty engineer directed the workers to perform a
stratification test from a subsequent part of the procedure without completing the
intervening steps. After a delay while obtaining the required test equipment,
normal midcell measurements resumed when it was recognized that specific
gravity measurements had increased. The stratification test was not performed
despite failure of the midcell measurements to meet the acceptance criteria.
Specific gravity measurements were manually corrected for cell electrolyte level.
e
The surveillance procedure stated that gas bubbles were created as a result of
charging. However, the nonconservative error was not recognized by any
licensee personnel because portions of the surveillance procedure were not
performed.
IEEE Standard 450-1980 stated that, because of the gas bubbles generated by
j
charging, electrolyte level readings should be made only after the battery has been at
i
float voltage for at least 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The inspectors noted that this was not clearly stated
in the surveillance procedure.
Failure to fully comply with all the provisions of Surveillance Procedure OPSP06-DJ-
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0002 contributed to the failure to meet the requirements of Technical Specification 3.8.2.1 and the corresponding violation further described in Section 04.2.
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c.
Conclusions
Licensee technicians did not satisfy a prerequisite and performed a surveillance test to
determine the state of charge of safety-related Battery Bank E1B11. This surveillance
1
test was conducted while recharging was in progress. This resulted in inaccurate
measurements of specific gravity that were then nonconservatively compensated for by
electrolyte level without accounting for gas bubbles created by charging. The inaccurate
results were used as the basis to consider the battery operable. Failure to fully comply
with all the provisions of a surveillance procedure shared a common cause with the
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failure to meet the requirements of Technical Specification 3.8.2.1 and the
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correspondir,g violation.
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111. Enaineerina
-E1
Conduct of Engineering
E1.1
Evaluation of Licensee Batterv Bank E1811 Calculations
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a.
Inspection Scope (37551)
The inspectors reviewed calculations performed by licensee engineers to determine the
capability of Battery Bank E1B11 to meet design basis requirements. The review also
included the applicable Technical Specifications for battery operability to determine if
any Technical Specification limits were exceeded. The following licensee documents
were reviewed:
Study Calculation, " Class 1 E Channel lli Battery Sizing Verification - June 14,
.
1998 Event"
)
Design Change Package 96-3056-35, Calculation EC-5008, Revision 10, "DC
.
' Channel 111 Loading Computation and Battery Size Verification"
Condition Report Engineering Evaluation 98-9069, Supplement 1
. b.
Observation and Findinas
The calculations performed by licensee engineers determined that Battery Bank E1811
was capable of performing its design-basis function throughout the time that the
chargers were not powered. The study calculation showed that the battery had
sufficient margin to carry its design-basis load even after the 7-hour discharge. The
parameters used in the calculation were in agreement with the design-basis calculations
and vendor supplied battery data. The licensee also had its calculations reviewed by the
battery vendor. As discussed in Section 01.1.d of this inspection report, the
calculations supported the licensee's findings that the safety significance of the
discharged battery condition was low.
The calculations were well documented and had been properly reviewed. The
assumptions used were reasonable and supported by industry standards. In addition to
the design-basis analysis, the study calculation used computer logs of battery output in
amperes to determine the estimated specific gravity throughout the event. The
engineers predicted when the specific gravity of Battery Bank E1B11 would have
decreased below the Technical Specification allowable values. The time to recharge the
battery to Technical Specification limits was also calculated.
The inspectors noted that the licensee's battery operability determination and
reportability review for this event relied solely on the calculated specific gravity. While
this approach accounted for instantaneous battery capacity, it did not address the other
parameters required to demonstrate that the battery was operable as specified in
Technical Specifications. These requirements specify that the battery have a terminal
voltage of at least 129 volts, must be supplied by at least one operable battery charger
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(at a higher voltage than the battery is capable of generating), and must have less than
2 amps charging current. To satisfy these requirements, the battery must be essentially
fully charged. Thus, the operability of a battery cannot be determined by calculating the
!
remaining capacity. The inspectors determined that Battery Bank E1B11 was -
inoperable from the time the charger lost power until the battery was essentially fully
>
charged,
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c.
Conclusions
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Engineering calculations and analyses were well documented with reasonable .
!
assumptions supported by industry standards and vendor information. These efforts
,
fully supported the conclusion that the safety significance of the June 14 event was low.
However, the licensee's conclusion that Battery Bank E1811 had been maintained in a
condition consistent with the Technical Specification limiting conditions for operability
l
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focused too narrowly on specific gravity as the sole parameter for battery operability and
did not recognize the inaccuracy of the measurement.
)
E4
Engineering Support of Facilities and Equipment
E4.1
Enoineerina Support to and Utilization by Operations durina the Event (37551)
i
The inspectors interviewed the duty engineer. During the event, he was requested to:
Determine how Switchgear E1B could be reenergized with the failed potential
transformer
T Oversee the potential transformer replacement
e
Evaluate the adequacy of the planned postmaintenance testing
e
L
Estimate how long Battery Bank E1B11 would continue to provide sufficient
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voltage to the de circuits .
,
Review the Technical Specifications for battery operability requirements
e
The duty engineer stated that he typically was not given sufficient time to properly
evaluate or support an item before being directed to start the next. For example, he
stated that he did not have sufficient time to evaluate system design and logic before
the first attempt to energize Switchgear E1B was made at approximately 8:45 p.m.
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The duty engineer stated that he had next reviewed the Technical Specifications and
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noted the 110 volts identified in Technical Specification 4.8.2.1.b. The applicability of
this Technical Specification to evaluating current battery operability was discussed in
i
Section O4.2 of this inspection report. The engineer stated that he had discussed this
specification with one of the licensed operators and erroneously informed him that
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Battery Bank E1B11 would remain operable if voltage remained above 110 volts.
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The inspectors noted that the event review team had identified a number of additional
engineers on site throughout most of this event. Questions regarding the adequacy of
support staff utilization during the event were assessed. Condition Report 98-9069,
Action 17, was written to develop expectations for an "off-normal event support team" to
be used during priority maintenance activities that affect reactor safety. The inspectors
concluded that the inefficient application of engineering staff resources may have
exacerbated the problems. However, licensee management was taking broad corrective
actions to ensure better support staff utilization in the future.
IV. Manaaement Meetinas
X1
Exit Meeting Summary
The inspector presented initial inspection findings to members of licensee management
'
by telephone at the conclusion of the inspection on November 23,1998. After additional
in-office inspection and review, final results were communicated on February 4,1999.
Management personnel acknowledged the findings presented. The inspector asked
whether any materials examined during the inspection should be considered proprietary.
No proprietary information was identified.
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ATTACHMEN~i
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
H. Allgeyer, Operations Shift Supervisor
C. Bowman, Duty Operations Manager
S. Clark, System Engineer
T. Cloninger, Vice President, Nuclear Engineering
W. Cottle, President and Chief Executive Officer
M. Coughlin, Operations Unit Supervisor
G. Danielski, Reactor Operator
E. Dare, Work Control Programs Coordinator
J. Groth, Vice President, Nuclear Generation
G. Janak, Operations Shift Supervisor
G. Parkey, Plant Manager, Unit 1
J. Phelps, Manager, Operations, Unit 1
M. Ruvalcaba, System Engineer
S. Sieben, Operations Unit Supervisor
R. Travino, Reactor Plant Operator
T. Waddell, Manager, Maintenance, Unit 1
INSPECDON PROCEDURES USED
IP 37551: Onsite Engineering
IP 61726: Surveillance Observations
IP 62707: Maintenance Observation
IP 71707: Plant Operations
IP 93702: Prompt Onsite Response to Events
ITEMS OPENED. CLOSED. AND DISCUSSED
CJened
498/98015-01
NCV Failure to place handswitches in pull to lock (Section O3.2).
+
498/98015-02
Vital Battery E1B11 was inoperable for at least 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />
'
35 minutes in violation of the Technical Specification 3.8.2.1.c
requirements (Section O4.2)
498/98015-03
NCV improper control board walkdown during turnover (Section 04.2).
Closed
498/98015-01
NCV Failure to place handswitches in pull to lock (Section 03.2).
498/98015-03
NCV improper control board walkdown during turnover (Section O4.2).
<C