ML20140C538
ML20140C538 | |
Person / Time | |
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Site: | Davis Besse |
Issue date: | 04/07/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20140C531 | List: |
References | |
50-346-97-03, 50-346-97-3, NUDOCS 9704170091 | |
Download: ML20140C538 (22) | |
See also: IR 05000346/1997003
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U. S. NUCLEAR REGULATORY COMMISSION - ,
REGION 111
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Docket Nos.: 50 346 '
License No.: NPF-3
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Report No: 50-346/97003 .
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Licensee: Toledo Edison Company
Facility: Davis-Besse Nuclear Power Station
Location: 5503 N. State Route 2
Oak Harbor, OH 43449
Dates: January 18, through March 3,1997 and
March 7,1997 I
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inspectors: S. Stasek, Senior Resident inspector
K. Zellers, Resident inspector
Approved by: John M. Jacobson, Chief,
Reactor Projects Branch 4
9704170091 970407 "'
PDR ADOCK 05000346
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EXECUTIVE SUMMARY '
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Davis-Besse Nuclear Power Station
NRC inspection Report 50-346/97003
This inspection included aspects of licensee operations, maintenancs, engineering, and
plant support. The report covers a six-week period of resident inspection.
Operations l
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A February 12, reactor downpower was conducted in a controlled, well managed ]
manner (Sections 01, M1.5). )
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Engineered safety feature systems walked down this inspection period were i
determined to be functional and appropriately lined up in conformance with the
updated safety analysis report (Section 02.1).
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The NRC identified that in one case, operations personnel failed to enter all required
Technical Specificatiun action statements upon determination that an amplifier
associated with nuclear instrument Ni-6 was inoperabis. This was considered one
example of a violation 10 CFR 50, Appendix B, Criterion V (Section 04.1).
Maintenance
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Overall, maintenance and surveillance activities reviewed this inspection period
adequately tested and maintained the associated equipment. However, some
weaknesses were noted related to the administrative control of some maintenance
and testing activities (Section M1.1).
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Two cases were noted where the control of equipment restoration following
maintenance was weak. The fact that associated sections of piping were slightly
drained during both work activities was not well communicated to operations for
consideration during the return to service process. In addition, the NRC identified
that work was performed outside the scope of the maintenance work order in one
of the two cases and is considered a second example of a violation of 10 CFR 50,
Appendix B, Criterion V (Sections M1.2, M1.3).
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The NRC identified that operators had performed procedural steps out of sequence
while surveillance testing the #3 service water pump. This is considered a third
example of a violation of 10 CFR 50, Appendix B, Criterion V (Section M1.4).
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When the licensee identified that a technical specification regtdied leakage rate test
of the decay heat removal watertight enclosure had not beer, performed following
the last opening of the enclosure on May 24,1997, appropriate followup actions
were taken including initiation of a plant shut down. The hRC subsequently issued
a notice of enforcement discretion which allowed the licensee to terminate the
shutdown and retum the unit to power operations. Howev6r, the failure to perform
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j , the leak rate test was considered a violation of the plant technical specifications
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The licensee identified that a requirement to perform an independent verification
that the fitting used to secure an inspection port on the decay heat removal
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watertight enclosure was properly installed following its use was not included in all
necessary procedures / documents. This matter met the criteria for enforcement
discretion specified in Section Vil of the NRC's enforcement policy, and therefore
- this matter was considered a non-cited violation (Section M1.5).
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During a routine plant walkdown, the NRC identified that a service water strainer
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blowdown valve was not closed as expected. Licensee personnel had previously
! noted similar cases as well. At the end of the inspection period, troubleshooting of
! the affected control circuitry was in process (Section M2.1).
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Administrative controls associated with the plant spray shield program appeared
incomplete. Informal guidance only was used to ensure that plant personnel would
j properly secure a spray shield following completion of activities that breached the
spray shield (Section M3.1).
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Plant personnel response to a component cooling water temperature controller
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failure was good (Section M4.1).
Enaineerina
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The licensee identified severalinstances where the design of the reactor coolant
pumps was not in conformance with 10 CFR 50, Appendix R requirements.
Specifically, small sections of oil lines were determined to be located such that
postulated oil leakage from those lines may not have been captured by the installed
oil collection system. It was subsequently determined that no significant safety
consequences would result from the identified configurations. This matter is
currently under NRC review (Section E1.1).
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The NRC identified that a service water pump performance curve included in the
plant " pump curve" book did not accurately reflect the currently installed pump
(Section E3.1).
Plant Suonort
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Appropriate ALARA and contamination controls were noted during the performance
of maintenance activities (Section R1).
- Radiological surveys accurately reflected current area conditions (Section R1)
. The Technical Support Center and Emergency Control Center appeared properly
maintained in a standby condition (Section P2).
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Socurity monitoring equipment was observed to be functional and in a good state of
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repair (Section S2).
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Fire response equipment was appropriately staged and available. Fire brigade
- members staged their protective clothing and other equipment prior to assuming
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their shift duties (Section F2).
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, , Report Details
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. Summary of Plant Status
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The plant operated at nominally full power during the inspection period with the exception
- of one significant downpower. On February 12, a shutdown por Techrucal Specification .
- (TS) 3.0.3 was commenced when the licensee identified that a TS required surveillance j
had not been performed. During the shutdown evolution, the NRC issued a notice of
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onforcement discretion (NOED), allowing termination of the shutdown. Lowest reactor ,
power reached was 10 percent with the main turbine having been tripped. The unit was
! subsequently returned to full power.
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) 1. Operations !
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l 01 Conduct of Operations i
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Plant operations appeared to be effectively controlled overall. Operations shift t
personnel were appropriately aware of and controlled surveillance and maintenance ,
activities that could affect safety significant equipment. Shift turnovers and shift '
briefings effectively disseminated important operational information to operating
crews. Information tags were hung on control room controllers / indications as
needed to communicate needed operational information. In general, operators '
adequately maintained the unit log so that significant shift activities and the status
of important equipment were appropriately documented. One reption was noted -
and is further discussed in Section 04.f below. The February h., reactor ]
downpower was conducted in a controlled, well managed mannei. 1
02 Operational Status of Facilities and Equipment
02.1 Engineered Safety Features System Watkdowns (71707)
The inspectors walked down the accessible portions of the following engineered
safety features (ESF) and important-to-safety systems during the inspection period:
- emergency diesel generators #1 and #2 '
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station blackout diesel generator
- auxiliary feedwater - trains 1 and 2
. high pressure injection system - trains 1 and 2
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decay heat removal system - trains 1 and 2 l
+ containment spray system - trains 1 and 2 !
. motor driven feed pump
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instrument air dryers ;
- service water system - trains 1 and 2, and installed spare i
. containment hydrogen dilution system
Equipment material condition was found to be excellent in all cases. Pump / motor l
fluid levels were within their specified bands. Local and remote controllers were I
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[, correctly positioned and required instrumentation appeared functional. Auxiliary
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' equipment necessary for system operability was also functioning properly. In
general, housekeeping was found to be acceptable. Few oil and fluid leaks were
i noted during the walkdowns. System lineups and major flowpaths were verified to
i be consistent with the updated safety analysis report (USAR). The inspectors
j identified no substantive concerns as a result of the walkdowns.
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04 Operator K.-df-g and Performance
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04.1 Technical Snacification Action Statement Not Anoropriatalv Entsted ;
s. Insoection Scone (71707)
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l The inspector reviewed operator followup actions to a failure of nuclear
j instrumentation NI-6 lower core detector amplifier on January 31,1997.
b. Dhastyations and Findings
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Operations personnel declared Ni-6 inoperable when a step change in its output
, was observed. Subsequently, the assistant shift supervisor, a senior reactor
4 operator (SRO), reviewed TS 3.3.1.1, . Reactor Protection System instrumentation,"
- and identified that the subject failure adversely impacted one channel of both high
j flux and fluxNe/ta flux #/ow reactor trips specified in associated TS Table 3.3-1.
l Both table entries referenced an action' statement 2 which required the channel be
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tripped or bypassed within one hour and the quadrant power tilt be monitored at
i least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Those actions were then initiated as required. !
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l The inspector noted however that an additional TS Table 3.3-1 entry addressing the ;
- high flux / number-of-reactor-coolant-pump-on reactor trip feature was also i
!' applicable. Accordingly, companion action statement 3 should have been invoked )
{ in addition to action statement 2. Action statement 3 also specified that the i
4 affected channel be tripped or bypassed within one hour- . !
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Although operations personnel had met the requirements of action statement 3 by
implementing action 2, they had failed to recognize and log all TS limiting
conditions for operation that were affected by the Ni 6 failure. l
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j Plant administrative procedure DB-OP-OOOO5 (Revision 05), " Operator Logs and
! Rounds," specified in Section 6.2.2.d that, "The following are entries which shall
- be recorded in the Unit Log: . . . Entering / Exiting a Technical Specification Action
{ Statement." Since operations personnel did not recognize that TS 3.3.1 action ;
j statement 3 was applicable, and therefore failed to make the necessary unit log l
} entry, this constituted an example of a violation of 10 CFR Part 50, Appendix B,
j Criterion V, " Instructions, Procedures, and Drawings" (50-346/97003-01s(DRP)). j
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j, c. Conclusions
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- Operations personnel displayed a lack of attention to detail when determining
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appropriate TS actions to take. Some applicable action statements were not
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ll. Maintenance i
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M1 !
l Conduct of Maintenance
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l M1.1 Maintenance and Surveillance Testina Activities
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The following maintenance and testing activities were observed / reviewed during the ;
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MWO 3 97-4602-01 Containment isolation Valve MU-6419 VOTES l
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MWO 1-96-0708-00 Replace DH-100, Leak Test Valve for Pressurizer
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Auxiliary Spray Line
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MWO-3-97-2047-01 Containment Sump Pump Outside Containment 1
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Discharge Isolation Valve VOTES Testing I
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DB-PF-03030 Service Water Pump 3 Quarterly Test
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DB-MI-03201 Channel Functional Test and Calibration of
SFRCS Channel 1 Pressure inputs
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DB-OP-03006 Miscellaneous Instrument Shift Check
j Overall, maintenance and surveillance testing activities reviewed this inspection
period were in accordance with applicable FSAR requirements and adequately
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tested and maintained the associated equipment. However, as discussed below,
some weaknesses were noted related to the administrative control of several
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M1.2 Weak Control of Makeuo Line Restoration Activities
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j a. Insoection Scone (62707) 1
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l The inspector observed the performance of portions of maintenance work order !
- (MWO) 3-97-4602-01, " Containment isolation Velve MU 6419 VOTES Testing," on
February 4,1997,
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F- b. OWations and Findinas
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i The inspector noted that depressurization of associated piping to support MU-6419
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testing was achieved by opening a drain valve. Fluid leakage from the drain valve
was collected with a contaminated water collection rig that was attached to the
i drain valve with transparent tubing. The inspector observed that air bubbles were
gurgling up the transparent tubing, indicating that air was potentially displacing
, water in the high points of the piping. About a half gallon of water was
{' subsequently determined to have been drained from the piping.
- After maintenance activities were completed, the inspector determined that
I operations personnel had not planned to fill ard vont the piping. The assistant shift
supervisor indicated that a fill and vont of the piping was not necessary because
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the line had only been depressurized and not actually drained, however, he
proceeded with plans to vent the line in response to the inspector's concerns.
When the line was filled and vented, no air was noted at the high point vent
connection, indicating the line had not been substantially drained. However,
followup discussion with the assistant shift supervisor revealed that he was
unaware that the line had been depressurized using the drain valve instead of the
vent valve and that a half gallon of water was lost from the line.
M1.3 Maintenance Activities Performed Outside Scone of Work Order
a. Insoection Scone (62707)
The inspector observed the performance of portions of MWO 1-96-0708-00,
" Replace DH-100, Leak Test Valve for Pressurizer Auxiliary Spray Line," on
February 19,1997.
b. Observations and Findinas
The function of the auxiliary spray line was to provide for pressurizer pressure and
temperature control using the decay heat removal (DHR) system during times when
the DHR system was in service. DH-100 was a leak test valve replaced as part of
the MWO; its replacement required that part of the auxiliary spray line be drained.
The inspector noted that a minimum of about six feet of a 1.5-inch line was drained
of water to accommodate the replacement of DH-100. However, the drained line
was not filled and vented following completion of DH-100 replacement activities.
When the inspector questioned the assistant shift supervisor during the restoration
process, the assistant shift supervisor indicated that he felt there was just a small
amount of air in the line following the maintenance; he also added that it would
have proven difficult to completely fill and vent the line due to a lack of a high point
vent in the affected piping. However, he subsequently requested engineering to
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review the matter to assure that the as-left condition was acceptable. In addition,
1* actions were undertaken to attempt to fill the line.
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Engineering thereafter responded that with that portion of line completely drained,
no operational or structural concerns would result. No damage to the system from
- a waterhammer event would be expected because of the low process fluid
i pressures and temperatures, coupled with a robust piping system mechanical !
design. The inspector agreed with the engineering conclusions. ,
) A review of the MWO package revealed that work had been performed outside the ,
j scope of the MWO. Specifically, two MWO steps were not completed as written,
i nor was the package updated to reflect the actual work accomplished. Step 3 of !
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i the MWO stated " Refill, pressurize, inspect and verify no leaks." However, as
i stated above, the piping was not refilled following completion of maintenance.
y Step 1 of the MWO stated "Tagout and drain piping using isolation valves DH-178
, to isolate the LPl/ decay heat removal system and DH-2736 along with DH-2735 to
l isolate the RCS." However, the isolation boundary for the work had been changed
j earlier to eliminate tbs need to tagout and isolate DH-2735 without the MWO being
i appropriately revised to reflect that change. Additionally, an action plan that was
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originally intended to be used as part of the original scope of the maintenance
! activity, had provisions for signature approval authority, but those had not been
! signed-off.
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! The performance of work outside the scope of MWO 1-96-0708-00 is considered a
t second example of a violation of 10 CFR Part 50, Appendix B, Criterion V,
j. " Instructions, Procedures, and Drawings" (50 346/97003-01b(DRP)).
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! c. Maintenance Related Conclusions l
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j Equipment restoration control and communications weaknesses were identified in
i two cases. In one instance, personnel performed work outside the scope of the
i MWO, including a tailure to perform a fill of an auxiliary spray line following
i completion of maintenance, in the second instance, operations shift management
was not aware that a section of makeup system piping had been drained of a half
j gallon of water through a drain line.
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M1.4 Imoroner Seouencina of Test Procedure Steos
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l a. Insoection Scone (62707)
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i The inspector observed operations personnel perform portions of DB-PF-03030
l (Revision 00), " Service Water Pump 3 Quarterly Test," on February 24,1997.
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! b. Observations and Findinas
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- .The inspector determined that part of the test had not been accomplished according
to administrative procedure DB-DP-00013 (Revision 04), " Surveillance and Periodic
- Test Program." DB DP-00013 Section 6.3.7.h stated in part that, " Test
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, prerequisites and procedure steps shall be performed in numerical sequence . . .
unless optional sequencing is allowed by the procedure . . ."
- Contrary to that requirement, DB-PF-03030 steps 4.7.2 through 4.7.5 were
completed before step 4.7.1, with no optional sequencing provided in the
procedure. This is considered a third example of a violation of 10 CFR 50,
Appendix B, Criterion V, " Instructions, Procedures, and Drawings" (50-346/97003-
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l The initial performance of the test failed the pump acceptance criteria due to a
- service water strainer blowdown valve being inappropriately open. The blowdown
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valve was then shut, the test was reperformed, and acceptable test results were
obtained. (Reference report Section M2.1 for additional discussion related to
l troubleshooting of the service water strainer blowdown valve control logic)
} Additionally, the inspector identified that the service water pump performance
, curve used in the test procedure did not match the pump curve provided in the
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pump curve book. (Reference report Section E3.1 for details)
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! Operations personnel failed to follow the stat.on test control procedure that required
! steps be completed in sequence. However, although certain steps were performed
} out of order, results of the test appeared to be valid,
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j M1.5 Decav Heat Pit Water Tiaht Enclosure Leakaan Test Not Performed As Reauired
a. Insoection Scone (71707)
l On February 12,1997, the licensee initiated a unit shutdown per Technical
Specification (TS) 3.0.3 following identification that a TS required surveillance ,
associated with the decay heat removal system had not been performed as j
required. While conducting the shutdown, the licensee concurrently requested a :
notice of enforcement discretion (NOED) from the NRC to allow termination of the j
shutdown. At approximately 8:00 p.m. EST, NRR issued the NOED (No. 97-6- 1
003), and the unit was returned to full power operation. The inspectors reviewed
licensee actions following discovery of the missed surveillance, monitored portions
of the unit shutdown, and subsequently assessed the causes and contributing
factors leading up to the need for the NOED.
b. Observations and Findinas
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-The shutdewn had been initiated in response to plant identification that TS
surveillance 4.5.2.f to perform a vacuum leakage rate test on the decay heat
removal watertight enclosure had not been conducted when last required. The
enclosure, located in containment, houses valves DH-11 and DH-12 in the decay
heat removal / low pressure injection system that are credited for functioning up to
seven days following a loss of coolant accident (LOCA). The vacuum leakage rate
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~, test verified that water intrusion into the enclosure due to post-LOCA flooding
would be limited to an acceptable amount. The TS specified that the test be
performed periodically as well as after each opening of the enclosure. On May 24,
1996, during startup from the last refuel outage, an inspection port on the top of l
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the enc!osure was opened to allow a visual inspection of the enclosure's interior per
ASME Section XI and NRC requirements, and a leakage rate test was not
subsequently performed.
The licensee then determined that the leakage rate test could not be conducted
with the unit at power and a shutdown was then commenced per TS 3.0.3 to place
the unit in a condition where the test could be done. The inspectors reviewed the i
licensee's preparatory activities for the shutdown as well as observed portions of
the actual shutdown evolution itself with no substantive concerns noted. The
shutdown appeared to be conducted in a controlled, well managed manner.
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The licensee requested the NOED based upon, in part, the design of the Kamlock
type fitting utilized to secure the inspection port and its inherent leaktightness.
Regional as well as NRR management were involved with the discussions with the
licensee.
At the time the NOED was issued, the unit was at 10% power and the main turbine
had been tripped. The turbine was thereafter relatched and the unit retumed to
power. 1
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The inspection port ut!Uzing the Kamlock fitting was installed in 1986 as part of i
facility change request (FCR)85-303. The inspectors reviewed the safety i
evaluation (SE) associated with installation of the inspection port and noted that the )
SE indicated that since the Kamlock fitting was specifically designed for the J
purpose of sealing, the TS surveillance would not have to be performed after
opening / closing of the port. However, no followup action was taken to request a ;
TS change to allow this exclusion. l
Alternatively, although not an optimum situation, the licensee could have continued
to ' implement the TS surveillance requirement without requesting a TS change. The
periodic leakage rate test could have been performed during each refueling outage
as before. Heatup of the unit could have then commenced and once in mode 3, the i
required interior inspection of the watertight enclosure could also have been
performed as before via use of the inspection port. However, since opening of the
inspection port constituted opening of the watertight enclosure as specified by the
TS, a shutdown /cooldown of the unit would have had to be performed to support
re-performance of the leakage rate test. Once the test was reperformed, the unit
could have been restarted without having to reopen the inspection port again. I
At the time of discovery, TS 4.5.2.f required that the decay heat removal system 1
be demonstrated operable "by performing e ;scuum leakage test of the watertight
enclosure for valves DH-11 and DH-12 that asures the motor operators on valves
DH-11 and DH-12 will not be flooded fet at least seven days following a
LOCA: . . 2. After each opening of tta watertikht enclosure." Since the
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, inspection port was opened on May 24,1997, and a leakage rate test had not been
subsequently performed, the licensee was considered in violation of TS 4.5.2.f.
Although the required surveillance had not been conducted, the decay heat
remonitiow pressure injection system was not declared inoperable
(50-346/9700342(DRP)).
In addition, the SE also specified that " Confirmation of proper installation (of the
Kamlock fitting) shall be accomplished by independent verification." However, with
the exception of operating procedure DB-OP-06900, " Plant Heatup," this
requirement was not properly translated to all necessary documents. For instance,
no requirements for performing independent verification of the Kamlock fitting
installation following its opening with the plant at power were delineated.
Consequentially, on February 12, plant personnel made a containment entry to
verify the Kamlock fitting's proper installation, and during that evolution, the fitting
was opened /reciosed without formally performing an independent verification.
10 CFR 50, Appendix B, Criterion ill, " Design Control," specifies in part that
measures shall be established to assure that applicable regulatory requirements and
the design basis (including design changes) are correctly translated into
specifications, drawings, procedures, and instructions. Because the independent
verification requirements specified in SE 85-303 were not properly translated to all
appropriate plant documents, this is considered a violation of 10 CFR 50,.
Appendix B, Criterion Ill. However, because the licensee identified the violation
during the initial review of the TS surveillance issue, and as of the end of the
inspection period an evaluation was inprocess to determine the appropriate
procedures / documents within which the independent verification requirement
should be included, this matter is considered a non cited violation (50-346/97003-
03(DRP)), and a Notice of Violation will not be issued consistent with Section Vil of
c. Conclusions
Upon implementation of FCR 85-303, the plant failed to request a TS change to
eliminate having to do a leakage rate test on the watertight enclosure when the
inspection port was opened, nor was the current TS surveillance performed as
required. In addition, the SE requirement to perform independent verifications of
proper Kamlock fitting installation each time the inspection port was opened and
raciosed was not addressed in all appropriate instructions and procedures.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Service Water Strainer Blowdown Valve Failures
a. Insnection Scone (37551)
The inspector conducted a routine walkdown of the service water pump room on
February 10,1997.
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j J, b. Ohwations and Findinas
The inspector noted during the walkdown that the #2' service water strainer
blowdown valve, SW-1380, was open without the necessary conditions present for
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it to be open. SW-1380 was designed to open on a high service water pump
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discharge pressure or a high strainer differential pressure. Neither of these
conditions were present at the time.
Subsequently, the valve apparently reclosed prior to the plant engineer for the
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service water system being ablo to investigate. Because another similar situation
{ had recently occurred, the plant engineer initiated a work request to troubleshoot
j the valve's control circuit.
I- Additionally, on February 24,1997, the #3 service water strainer blowdown valve,
l SW-1381, was found partially open during performance of the #3 service water
- pump quarterly surveillance test. This was the third time that a service water
i blowdown valve was unexpectedly found open. The licensee then initiated
- potential condition adverse to quality report (PCAOR) 97-0235.
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! Subsequent troubleshooting efforts by pont personnel determined that an age- .
j related relay degradation in the control cirNitry was adversely affecting the logic's l
j response timing. Consequently, the station planned to replace the potentially i
degraded relay in the control circuits for all three service water blowdown valve
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! An engineering evaluation to address a worst case scenario irwolving a full open
blowdown valve, determined that, with an ultimate heat sink temperature less that
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50*F, up to 4000 gallons per minute (GPM) of service water flow diversion could
j be accommodated without adversely impacting system response to a LOCA. Since
1 maximum flow from a blowdown valve was estimated at less that 2000 GPM, and
! since the ultimate heat sink temperature was currently about 42'F, the inspector
j had no concems that the situation was an imminent safety concern.
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! However, inspector review of this matter was incomplete at the end of the
, inspection period. The relay degradation noted above could cause a blowdown
3 valve to remain in a full open position as noted in at least two previous cases, but
! did not appear to account for the one valve found in a mid-position. This matter is
I considered an unresolved item (50 346/97003-04(DRP)) pending completion of
I
inspector review,
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, M3 Maintenance Procedures and Documentation
! M3.1 Lack of Sorav Shield Proaram Administrative Controls i
- l
a. Insoaction Scone (62707)
f The inspector observed portions of the performance of MWO-3-97-2047 01
'
" Containment Sump Pump Outside Containment Discharge isolation Valve VOTES
Testing," on February 3,1997.
.
b. Observations and Findinas
The inspector noted that disconnect cabinet CDF11C, located in #4 mechanical
penetration room, had its door open so that test equipment could be powered from
the cabinet's internal electrical outlet. However, the cabinet was marked with a
} " Spray Shield Required" placard that implied that the door was subject to water
i intrusion administrative controls. When station personnel became aware of the
l inspector's observation, potential condition adverse to quality report (PCAOR) 97-
- 0144 w9s initiated.
l 1
, 1
J
The maintenance craft had been using this outlet for several years. Apparently, 1
. they had received verbal guidance to have a person available to shut the door if l
l necessary, and to secure the door once the activity requiring use of the outlet was
completed. i
- Subsequently it was determined that the cabinet was not required to be in the 1
i spray shield program and the spray shield placard was removed. Other plant l
- equipment was found to have spray shield signs that did not require them as well.
} The inspector conducted a search of the plant procedures database to determine if
l any drawings or procedures related to the spray shield program. Drawing M-269
- - documented the requirements for spray shield protection, however no guidance was
!
'
found that provided information as to how personnel should control the breaching
of spray shield enclosures.
I
c. Conclusions
i
- Administrative controls governing the spray shield program appeared incomplete.
j informal verbal guidance was used to ensure that maintenance personnel would not
leave an open spray shield door unattended. Maintenance personnel failed to
question whether the breaching of a cabinet labelled as a spray shield was
appropriate.
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!* M4 Maintenance Staff Knowledge and Performance
,
!
- M4.1 Personnel Resoonse to a Comoonent Coolina Water Temnerature Controller Failure !
i
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i s. Inanection Scone (71707)
!
l The inspector observed a component cooling water (CCW) heat excf. anger being
placed into service.
{
! b. Observations ad Findinas
1
l Operations shift personnel were investigating a CCW heat exchanger temperature
- control valve problem that resulted in minor tempere'
- s ucreases of components
i cooled by CCW. '
. ;
i- Within minutes, operations dispatched an instrumentation and controls (l&C)
technician to investigate. The technician immediately determined that a linkage arm
had fallen off the temperature controller and then took actions to reattached it. The
j . temperature control circuit then started to function properly.
{
,
No temperature alarms were received when the CCW temperature excursion
j temperature control valve would have opened as designed during design basis :
- accident conditions, which was consistent with its updated safety analysis report
(USAR) description.
l
I c. Conclusions:
!
- I&C personnel conducted timely diagnostic and corrective action activities
{ for a failed CCW heat exchanger temperature controller.
, ,
MS Miscellaneous Maintenance issues (92700) (92902) ;
M8.1 (Closed) LER 50-346/96-005-01, inadeouate Control of Heavy Loads in the
Containment Buildina: The event involved the inappropriate traversing of the
reactor vessel head lifting tripod over the open reactor vessel during the tenth ;
refueling outage. The mattor was the sub}ect of previous NRC review which ,
'
concluded with the issuance of a violation (reference NRC Inspection Report
50-346/96005). ;
M8.2 (Closed) LER 50-346/94-001-00, inoperable Emeroency Core Coolina System: This
LER documented a situation where containment radiation monitor RE2OO7 mode 6 ,
'
trip setpoint had been calibrated to a value greater than the allowable limit.
RE2OO7 provided one of four channels of containment radiation monitoring input to !
the safety features actuation system (SFAS). The monitors were set to trip at !
certain values during power operations and to trip at lower values when the plant [
was shut down (i.e., mode 6). ,
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l ~, The setpoints were established via facility change request (FCR) 82-0034. !
l Technical Specifications required at least three of four containment radiation
'
monitors to be operable during core alterations. The licensee determined that core
!- alterations were conducted October 1 through October 7,1g84 with both RE2OO7 i
- and RE2OO5 inoperable.
l
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l- The licensee determined having two containment radiation monitors inoperable did l
'
not adversely impact previous accident analyses. The slightly higher trip setpoint '
4
remained conservative to limits required to meet 10 CFR 100 offsite dose
j guidelines. The previously analyzed fuel handling accident took no credit for
3 automatic containment isolation, a function provided by SFAS. The setpoint was
- subsequently adjusted to the appropriate value prior to personnel performing further
i core alterations.
f lil. Enaineerina
$ E1 Conduct of Engineering
!
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E1.1 Annandix R lasues Associated with Reactor Coolant Pumos
i
. a. Insoection Scone (71707)
i ,
! The licensee recently identified several configuration problems associated with the
reactor coolant pumps (RCPs) involving a failure to meet Appendix R requirements.
The inspectors reviewed the licensee's followup actions.
b. Observations and Findinos
The licensee discovered that the RCP lubrication system piping was routed in such
a manner as to not have all potential leakage paths contained within the RCP's oil
collection system. Specifically the licensee determined that in one case oil pressure j
sensing lines associated with the lift oil system was located above the oil collection
trap. It was concluded that if a sensing line should leak while the lift oil system
was operating, a potential spray condition rould occur and result in the oil to not be
adequately collected.
l
The second case involved installation of a oil fill line whereby personnel could add !
oil to the RCP reservoir from outside of a high radiation area. However,if the fill
line were to break while oil was being added, the leak could be directed outside of
the oil collection system. ;
The third case involved a small length of drain line underneath of the lower oil .
reservoir that was located outside of the oil collection system. If the drain line I
were to leak or rupture, up to 25 gallons of oil could drain from the reservoir to
creas outside of the collection system.
These conditions were documented in licensee event report 50-346/97-004-00. It I
was subsequently determined that no significant safety consequences would result ;
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[ from the identified configurations. Further inspector followup of these issues will i
j be conducted during review of the subject LER.
l
4
E3 Engineering Procedures and Documentation
E3.1 Service Water Pumn Performance Curve Out-of-bate
i ;
- a. inanection Scone (37551)
'
The inspector observed portions of the performance of DB-PF-03030 (Revision 00),
" Service Water Pump 3 Quarterly Test," by operations personnel on February 24, '
- 1997.
l b. Observations and Findinas
.
l
- The inspector discovered that the #3 service water pump curve in Attachment 5 of
- l
DB-PF-03030 did not match the #3 service water pump curve that was in DB-PF-
l 06704 (revision 01), " Pump Curves," Drawing CC14.73.
I
The curve included in DB PF-03030 reflected data collected after the #3 service
i water pump shaft and casing were replaced in 1995 and appeared to represent the
l baseline parameters for the #3 service water pump currently installed. However,
]
- the curve in the pump curve book was dated June 4,1991, and reflected a pump )
that was not currently installed.
. :
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The inspector was concerned that the outdated curve in DB-PF-06704 could be
used by plant personnel to justify engineering and safety evaluations, and flowrate
4
determinations for radioactive affluent calculations. Pending further inspector
,
review of this matter to determine the extent to which the outdated curve was, or
could be used by plant personnel, this is considered an unresolved issue
(50-346/97003-05(DRP)).
E8 Miscellaneous Engineering lasues (92700) (92903)
E8.1 (Closed) Inspection Followuo item (50-346/95007-05(DRP)): Containment air
cooler (CAC) 1-3 electrical alignment not fully evident. By design, CAC 1-3 was
capable of being aligned to either train 1 or train 2 electrical supply. When aligned
to either train, the CAC AC electrical supply was directly monitorable via control
room indication. However, the associated DC electrical alignment was not evident.
1he AC electrical supply was swapped via manipulation of breaker switches. The
DC electrical supply was swapped at the same time the AC supply was swapped ,
via pickup / dropout of relay auxiliary contacts. l
Following discussions with engineering personnel and review of associated Institute I
of Electrical and Electronics Eogineers (IEEE) Standards 279,338 and 352, the i
inspectors determined that the electrical design for CAC 1-3 was in conformance
with standard industry design specifications and the subject relays and contacts
were appropriately tested periodically.
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E8.2 (Closed) Insoection Followun item (50-346/94004-03(DRP11: Nuclear
instrumentation divergence events. The licensee was unsuccessful in determining i
,
specific root cause for the subject divergence events. However, the number of
l
- divergence events, their magnitude, and duration, continued to decline over the last
,
two operating cycles possibly due to current core design, loading, and operating
l . strategies. No significant adverse effects as a result of the current trend is .
i
foreseen. This matter therefore is considered closed.
( ?
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l E8.3 (Closed) Insoection Followun item (50-346/93017-02(DRP)): Testing problems
2
associated with component cooling water isolation valve CC1495. The testing
!. inadequacies associated with the subject valve were subsequently corrected.
- During inspector and licensee review of this matter, a question was raised
l. concerning the setup of air operated valves in general. No additional failures
i
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associated with the setup of AOVs were identified. This specific matter is ,
considered closed, however, the inspectors will continue to assess the proper i
functioning of AOVs during future inspection activities.
'
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'
E8.4 (Closed) LER 50-346/96-002-01. Potential Loss of Remote Shutdown canability
- Due to MOV Fire Induced Damaae: This event report documented that a licensee
.,
review determined that several valves were susceptible to failure similar to that
i
described in NRC Information Notice 92-18. NRC review of this matter was
i previously completed with issuance cf escalated enforcement (reference NRC '
j inspection Report 50-346/96008).
J
$ E8.5 (Closed) LER 50-346/96-004-00. Inadeouste Compensatorv Actions for Thermo-Lao
! for Radiant Enerav Shields: This event report discussed a condition where Thermo- 1
3 Lag was used as radiant energy shields in containment and containment annulus.
l Although the use of Thermo-Lag in applications requiring non-combustible material
i
was subsequently determined to be unacceptable, appropriate compensatory
} measures were not initiated. NRC review of this matter was previously completed
.
with issuance of a Notice of Violation (reference NRC Inspection Report '
- 50-346/96008).
,
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IV. Plant Sunoort
R1 Radiological Protection and Chemistry (RP&C) Controls
The inspectors noted that good ALARA and contamination control practices were
utilized during maintenance activities observed during the period. Maintenance
personnel were cognizant of area dose rates and attempted to utiliza existing
structure for additional shielding when necessary. Radiation protection personnel
were observed to provide appropriate contamination control support.
The inspectors independently verified on a sampling basis that area radiation levels
were consistent with current surveys, radiation areas and high radiation areas were
properly posted and controlled, and contaminated areas were adequately roped off
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, and marked to prohibit station personnel from inadvertently crossing control
! boundaries. I
- P2 Status of EP Facilities, Equipment, and Resources
- I
l- The inspectors walked down the Technical Support Center and Emergency Control l
'
Center during the inspection period. Both emergency response facilities appeared i
j. well maintained in an appropriate standby condition with associated equipment
functional. Personnel access to the facilities was controlled per the licensee's !
program.
- j )
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. 82 Status of Security Facilities and Equipment
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i Protected area ingress and egress monitoring equipment was observed to be i
j functional and in a good state of repair. Protected area lighting and intrusion !
4
detection equipment were also noted to be properly functioning. Guard force ;
- members were observed to conduct normal rounds and security alarm response ;
j activities in a controlled and timely manner. ;
I (
F F2 Status of Fire Protection Facilities and Equipment ;
!,
! Required fire protection equipment appeared to be appro,4iately staged and
! available in their designated plant locations. Fire brigsde members adequately
j staged their protective clothing and other necessary iPe fighting equipment before
i assuming their shift duties. Fire brigade team minimum manning requirements were
j routinely satisfied throughout the inspection period. !
$
[ V. Manaaement Meetings !
l-
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X1 Exit Meeting Summary
The inspectors presented the preliminary inspection results to members of licensee
management at the conclusion of the inspection on March 3,1997. A followup meeting
was held on March 7,1997, where the final inspection results were discussed with
licensee management representatives. The licensee acknowledged the findings presented.
The inspectors asked the licenses whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
,
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$ PARTIAL LIST OF PERSONS CONTACTED
i
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licenses
- J. K. Wood, Vice President, Nuclear
J. H. Lash, Plant Manager
R. E. Donnellon, Director, Engineering & Services
. T. J. Myers, Director, Nuclear Assurance
I L. M. Dohrmann, Manager, Quality Services
R. C. Zyduck, Manager, Design Basis Engineering
,
J. L. Michaelis, Manager, Meintenance
J. L. Freels, Manager, Regulatory Affairs
i M. C. Beier, Manager, Quality Assessment
i W. J. Molpus, Manager, Nuclear Training
- L. D. Hughes, Manager, Supply
'
D. L. Esholman, Manager, Operations
i R. J. Scott, Manager, Radiation Protection
i G. A. Skeel, Manager, Security
H. W. Stevens, Manager, Nuclear Safety & Inspection
l J. W. Rogers, Manager, Plant Engineering
! D. M. Imley, Superinte.. dent, Operations
! D. H. Lockwood, Supervisor, Regulatory Affairs
j G. R. McIntyre, Supervisor, SYME
D. R. Wuokko, Supervisor, Licensing
M. J. Roder, Supervisor, OWCU
- J. E. Reddington, Superintendent, Maintenance
! R. B. Coad, Superintendent, Radiation Protection
] T. J. Chambers, Shift Manager, Operations
4 R. B. Ewing, D. B. Supply
l D. Converse, D. B. Business Services Manager
l M. K. Leisure, Senior Engineer, Licensing
J. W. Marley, Senior Engineer
'
i C. Kraemer, Engineering, Regulatory Affairs
l G. M. Wolf, Engineer, Licensing
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INSPECTION PROCEDURES USED
'
IP 37551: Onsite Engineering
IP 61726: Surveillance
$ IP 62707: Maintenance
IP 71707: Plant Operations
IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power Reactor
- Facilities
IP 92901: Followup - Operations
1
IP 92902: Followup - Maintenance
, IP 92903: Followup - Engineering
l lP 93702: Prompt Onsite Response to Events at Operating Power Reactors
i
<
) ITEMS OPENED, CLOSED, AND DISCUSSED
Opened '
'
50-346/97003-01 VIO Three Examples of Failure to Follow Procedure
50-346/97003-02 VIO Leakage Rate Test Not Performed
} 50-346/97003-03 NCV Independent Verification Requirements Not Translated to All
j Appropriate Plant Documents
>
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50-346/97003-04 URI Service Water Blowdown Valves Found Open
50-346/97003-05 URI Outdated Curve Found in Pump Curve Book
- Closed
[
i 50-346/95007-05 IFl Containment Air Cooler (CAC) 1-3 Electrical Alignment Not
.
Fully Evident <
i 50-346/94004-03 IFl Nuclear Instrumentation Divergence Events
50-346/93017-02 IFl Testing Problems Associated With Component Cooling Water
Isolation Valve CC1495
i 50-346/96-002-01 LER Potential Loss of Remote Shutdown Capability Due to MOV
l Fire Induced Damage
i 50-346/96-004-00 LER inadequate Compensatory Actions for Thermo-Lag for Radiant
Energy Shields
50-346/96-005-01 LER Inadequate Control of Heavy Loads in the Containment
1
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Building
50-346/94-001-00 LER inoperable Emergency Core Cooling System
l
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LIST OF ACRONYMS USED
w
AOV Air Operated Valve
ASME American Society of Mechanical Engineers
CAC Containment Air Cooler j
CFR Code of Federal Regulations '
CNRB Company Nuclear Review Board
l
dpm disintegrations per minute
ECCS Emergem:y Core Cooling System 4
EDG Emergency Diesel Generator
ESF Engineered Safety Feature
EVS Emergency Ventilation System
FCR Facility Change Request
GPM Gallons per Minute
HPl High Pressure injection
I&C Instrumentation and Controls
IFl inspection Followup Item
IR inspection Report
LAR Licensee Amendment Request
LER Licensee Event Report
LPl Low Pressure injection
MCC Motor Control Conter
MOV Motor Operated Valve
MWO Maintenance Work Order
NCV Non-Cited Violation l
NOED Notice of Enforcement Discretion
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation !
OSC Operations Support Center
PCAOR Potential Condition Adverse to Quality Report i
QA Quality Assurance i
OC Ouality Control
i
RCP Reactor Coolant Pump !
RO Reactor Operator l
RP Radiation Protection
SFRCS Steam / Feed Rupture Control System
SRB Station Review Board
TS Technical Specification
VIO Violation
22