ML20129F931
ML20129F931 | |
Person / Time | |
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Site: | South Texas ![]() |
Issue date: | 10/02/1996 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20129F897 | List: |
References | |
50-498-96-06, 50-498-96-6, 50-499-96-06, 50-499-96-6, NUDOCS 9610070071 | |
Download: ML20129F931 (22) | |
See also: IR 05000498/1996006
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U.S. NUCLEAR REGULATORY COMMISSION
REGION IV !
Docket Nos: 50-498,50-499
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Report No: 50-498/96-06,50-499/96-06 i
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Licensee: Houstua Lighting & Power (HL&P)
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, Facility: South Texas Project Electric Generating Station, Units 1 1
and 2
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Location: 8 Miles West of Wadsworth on FM 521 l
Wadsworth, Texas 77483 '
Dates: July 28 through September 7,1996 l
Inspectors: D. P. Loveless, Senior Resident inspector
J. M. Keeton, Resident inspector
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W. C. Sifre, Resident inspector
Approved by: J. l. Tapia, Chief, Project Branch A
Division of Reactor Projects
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9610070071 961002
PDR ADOCK 05000498
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EXECUTIVE SUMMARY !
South Texas Project, Units 1 & 2
NRC Inspection Report 50-498/96-06,50-499/95-06 ;
This resident inspection included aspects of licensee operations, engineering, maintenance,
and plant support. The report covers a 6-week period of resident inspection.
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Operations
e Operations continued in a safety-conscious and professional manner (Section 01).
Control room operations reflected operator attention to detail, positive shift turnover
activities, quality supervision, and formal communications (Section 01.1).
- Operators demonstrated a detailed knowledge of consequences and proper level of
caution during the performance of infrequently performed procedures and during
operation with automatic equipment out of service (Section 01.1). .
e Equipment material condition, plant cleanliness, and equipment availability were
excellent (Section 02). Equipment clearance orders were properly implemented.
Management was actively involved in overseeing the material condition of the plant
(Section O2.1).
Maintenance
e Maintenance and surveillance activities were professionally performed by
knowledgeable technicians with appropriate levels of field supervision. Activities
observed were well conducted and included good self-verification and independent
verification techniques (Sections M1.1 and M1.2).
. e A noncited violaNon was identified for the f ailure of contractor personnel to install a
set screw in a valve actuator spring pack assembly. This event-revealed and l
licensee-corrected violation is being treated as a noncited violation, consistent with -
Section Vll.B.1 of the NRC Enforcement Policy. Licensee management .!
demonstrated an aggressive approach to determining if the missing set screw was ;
an isolated event (Section M1.5). -
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e Coordination among operations, maintenance, and engineering personnel during the !
replacement of a solid state protection system relay and during the implementation ;
of a plan of action to determine the source of leakage into a Safety injection j
Accumulator were exceptional (Sections M1.6 and M1.7). j
e A violation was identified for the f ailure to establish procedures to verify the '
accuracy of plant process computer constants that were required by the computer
to perform the axial flux difference monitor alarm device function. This violation
was similar to a previous violation and should have been prevented by licensee
corrective action. (Section M1.8). l
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- The design change package for the modification of molde'd case circuit breaker
setpoints was comprehensive and of good quality. The package was properly
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reviewed and the safety evaluation met the requirements of 10 CFR 50.59 (E2.1). -)
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- e The downgrading of a condition report without a documented basis and the
, resultant failure to assess operability and reportability were considered a weakness
in the implementation of the corrective action program (Section M1.3).
, Plant Suocort
l e- The radiological controls, chemistry, physical security, ard fire protection activities
- which were observed and reviewed were appropriately conducted (Sections R1 and
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Report Details
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- Summary of Plant Status
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Unit 1 operated at essentially 100 percent reactor power throughout this inspection period,
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Unit 2 operated at essentially 100 percent reactor power throughout this inspection period.
1. Operations
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01 Conduct of Operations -
- 01.1 Control Room Objervations (Units 1 and 2)
a. Insoection Scoce (71707)
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I. Using inspection Procedure 71707,the inspectors routinely observed conduct of
operations in the Units 1 and 2 control rooms. Daily control board walkdowns,
attendance at shift turnover meetings, observations of operator performance, and 1
- reviews of control room logs and documentation, were performed.
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1 b. Observations and Findinas
On July 29, the inspector observed the unit supervisors in Unit 1 during a control
i board walkdown for shift turnover. The information exchange was very detailed
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j and effective.
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! On August 2, the inspector observed the placement of a fresh cation bed in service ;
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in the chemical and volume control systern in Unit 2. Since this evolution was
l seldom performed at full power and had the potential to affLct reactivity, the
! inspector reviewed the licensee's preparations prior to the evolution. Appropriate
precautions had been taken to prevent or accommodate any reactor coolant system
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boron dilution caused by the activity. Reactor power had been reduced to 99.5
percent. The activity proceeded smoothly with no noticeable power change and in
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' accordance with Plant Operating Procedure OPOPO2-CV-0004, Revision 10,
" Chemical and Volume Control System Subsystem." Good attention to detail was
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- On August 13, the inspectors observed Unit 2 control room operators respond to an
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alarm for Accumulator 2C. The operators referred to the alarm response procedure
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and verified that the alarm was of no immediate concern. Communications related
I- to the alarm investigation were formal and closed loop.
i On August 16, the inspector noted that the Unit 2 main generator voltage regulator
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observed on the output of the automatic voltage regulator. The control room
- supervisor had directed the operators to place the voltage regulator in manual. In
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discussions with the inspector, the operators demonstrated a detailed knowledge of
the consequences of running with the main generator voltage regulator in manual.
c. Conclusions
Operators continued to perform in a safety-conscious and professional manner. Unit
supervisors were observed performing detailed control board walkdowns. Opt ators
were very cautious when performing seldom used procedures. Formal
communications techniques within the control rooms and with reactor plant
operators were good. The response to annunciators by reactor operators was
excellent.
O2 Operational Status of Facilities and Equipment
02.1 Plant Tours (Units 1 and 2)
a. Infnection Scooe (71707)
The inspectors toured portions of the accessible plant areas in Units 1 and 2 on a
daily basis. Areas of special attention during this inspection period included:
- Protected area yard
- Containment penetration rooms in Units 1 and 2
- Emergency electrical switchgear and battery rooms in Unit 2
- Fuel handling buildings for Units 1 and 2
- Turbine generator buildings for Units 1 and 2
- Essential Cooling Water Pump Rooms in Unit 1
The inspectors found that equipment inside the buildings was properly stored. All
areas toured were clean and free of debris.
On August 19, the inspector verified portions of equipment clearance order tagouts
for a Unit 1, Train B, work week. The equipment clearance orders were properly
signed and the equipment tags were properly hung and verified,
c. Conclusions
The inspectors concluded that equipment material condition, plant cleanliness, and
equipment availability were excellent. Equipment clearance orders reviewed were
properly developed and implemented. Licensee management was actively
monitoring work areas for material condition.
08 Miscellaneous Operations issues (92701)
08.1 (Closed) Violation 50-499/96001-01: two main feedwater isolation valves were
made inoperable in violation of Technical Specification 3.0.3.
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The licensee found that the root cause of the occurrence was a misapplication of a f
Technical Specification interpretation. In addition, poor shift turnover practices !
contributed to increasing the duration of the violation. t
The lessons learned from this event resulted in discussions with licensed operators f
regarding management expectations. The discussions focused on communications ,
and control of entries into Technical Specification action statements in addition, - i
guidance was issued regarding work coordination and communications between the .;
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control room staff and the outage work start authority. 6
The licensee also revised Plant Operating Procedure OPOP01-ZO-0022, Revision 8,
" Plant Operations Shift Routines," to include main feedwater isolation valve ;
operability as an item to be reviewed during shift turnover on the Mode 3 safety [
function checklist. The inspectors concluded that the licensee's corrective actions !
had been appropriate. ;
08.2 (Closed) Licensee Event Reoort 50-499/96-001: two main feedwater isolation
valves were made inoperable in violation of Technical Specification 3.0.3.
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Tnis licensee event report documented the event cited in Violation 50-499/96001-
01. This matter was closed in Section 08.1 of this inspection report. No new
issues were revealed in the licensee event report.
08.3 1Cipped) Vio(@n 50-499/95027-01: inadequate controls governing the ,
configuration of luct handling equ;pment.
On October 18,1995, a contract technician improperly attached a safety sling on
the fuel handling machino during fuel movement in Unit 2. . This resulted in
insufficient clearance between the fuel assembly being moved and the fuel racks in
the spent fuel pool. This violation was a repeat violation caused by inappropriate
contractor controls.
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The licensee identified the root cause of this violation as less than adequate
supervisory oversight of the task and concluded that contractor control was
adequate and effectively implemented.
In order to preclude repetition of this event, the licensee enhanced the fuel handling
machine procedure to clarify the proper configuration of the fuel handling machine
hoist and to include independent verification of proper rigging. In addition, the
lessons learned from this event were included as a case study in contract technical
coordinator training.
The inspector concluded that the licensee's corrective actions had been appropriate.
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11. Maintenance
M1 Conduct of Maintenance
M 1.1 General Comments on Field Maintenance Activities
a. Insoection Scone (62707)
The inspectors observed all or portions of the following work activities, identified by
their work authorization numbers:
Unit 1:
- 96077861: Replace Breaker for the Outside Containment isolation Valve in
Auxiliary Feed Water System Train C
- 95003578: Spent Fuel Pool Gate Seal Replacement '
Unit 2:
- 95003280: Lubrication, inspection, and Testing of Fuel Handling Building
Ventilation Backdraft Damper for Exhaust Booster Fan 11C
- 95003297: Lubrication, inspection, and Testing of Fuel Handling Building
Ventilation Backdraft Damper for Exhaust Fan 11C
- 90002276: Steam Generator Header Pressure Loop Calibration
b. Observations and Findinos
The inspectors found the work performed under these activities to be professional
and thorough. The mechanics and technicians demonstrated a detailed knowledge
of the associated procedures and equipment. Self- verification and independent
verification techniques were performed in accordance with management
expectations. Supervisors and managers were observed as having an active role in
providing oversight of the maintenance activities,
c. Conclusions
The inspectors cencluded that the routine maintenance activities observed were
professionally performed by very knowledgeable mechanics and technicians.
Maintenance supervisors were found to be providing an appropriate level of field
supervision and oversight.
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M1.2 General Comments on Surveillance Testina
a. Insoection Scooe (61707)
The inspectors observed all or portions of the following surveillances:
Unit 1:
o Plant Surveillance Procedure OPSP03-DG-0002, Revision 6: Standby
Diesel 12(22) Operability Test
Unit 2:
- Plant Surveillance Procedure OPSPO3-CV-0009, Revision 3: Monthly
Boration Flow Path Verification
b. Observations and Findinas
The inspectors found that the testing activities performed under these activities
were professional and thorough. All observed tests were performed in accordance
with the approved surveillance procedure. Technicians and operators were
experienced and knowledgeable of their assigned tasks. Pretest briefings were !
detailed and included discussions of plant and personnel safety and equipment
integrity issues. Surveillance tests were satisf actorily completed within the
Technical Specification required frequency, and the associated procedures properly
implemented the surveillance requirements. Test instruments were within their
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current calibration cycle. Dual verification was observed when required by
procedures, and the technicians informed the control room operators of expected
alarms.
c. Conclusions
The inspectors concluded that the observed surveillance tests were professional,
thorough, and fully implemented the associated Technical Specification surveillance
requirements.
M1.3 Visual Insoections of Fuel Handlina Buildina Main Exhaust Booster Fan Backdraft
Damners
a. Insoection Scope (62707)
On July 29,1996, during the observation of the lubrication, inspection and testing
of the Fuel Handling Building Main Exhaust Booster Fan 11C backdraft damper, the
inspector noted that a field change had been made to the preventive maintenance
work instructions that was characterized as a one-time change. The change
instructed the mechanics to perform boroscopic inspections of the dampers. Prior
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to the change, the work instruction had directed the mechanics to enter the' plenum, 'l
common to all three trains, between the main exhaust f ans and the main exhaust j
booster fans and visually inspect the damper. The inspector reviewed the basis for {
the work instruction change and the effect of previous preventive maintenance 1
activities on system operability. l
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b. Observations and Findinas ;
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The inspector interviewed craft personnel, the system engineer, and a shift l
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supervisor concerning the work instruction change. On April 9,1996, the shift
supervisor had raised an operability concern prior to work-start of a previcus
occurrence of this maintenance activity. Condition Report 96-4187 had been
written to document that the preventive maintenance task had not been performed
and that the shift supervisor questioned whether the evolution had caused all three
trains to be inoperable in the past. The specific concern raised by the shift.
supervisor was that opening of the plenum access door would render all three trains
of the fuel handling building exhaust filtration system inoperable by providing a
bypass flowpath. The plenum between the main exhaust fans and the booster fans
- was common to all three trains of the fuel handling building main exhaust
subsystems. With the plenum door open, unfiltered air would be drawn from the
fuel handling building, through the main exhaust fans, and out the main plant stack.
During previous performances of this preventive maintenance activity, one
technician had entered the plenum and closed the door. Constant radio contact had
tnen been maintained with a second technician outside the plenum.
While reviewing the condition report, the inspector noted that the condition had
originally been characterized as a station-wide level condition adverse to quality.
On April 11, the Condition Review Group downgraded the condition report to a ;
condition not adverse to quality and, therefore, not a condition requiring i
management level coordination. As a result of this action, an engineering
evaluation for operability or reportability of the past practice of breaching the
system had not been performed. The inspector brought this matter to the attention
of the shift supervisor. The shif t supervisor agreed with the inspector's concern
and requested an engineering evaluation of past system operability. The evaluation I
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l indicated that the momentary opening and closing of the plenum door would not
result in exceeding the offsite dose release limits described in the Updated Final
Safety Analysis Report, did not affect system operability and was not reportable. j
The inspector found the results of the engineering evaluation to be thorough and !
reasonabfe.
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c. Conclusions !
' The past practice of entering the plenum common to all three trains of the fuel
handling building main exhaust systems indicated a previous work process
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weakness. The licensee had adequately addressed this specific practice, however,
questions concerning past system operability were not well addressed. The l
downgrading of the condition report without a documented basis and the resultant i
failure to assess operability or reportability were considered a weakness in the
implementation of the corrective action program. The quality and thoroughness of ;
the engineering evaluation were considered adequate. *
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M 1. 4 Steam Generator 2D Pressure Looo P-0546 (Unit 2)
a. Inspection Scoce (62707)
On August 27, during the performance of a quarterly analog channel actuation test
on Steam Generator 2D Pressure Loop P-0546, the instrumentation and controls
technicians discovered a mispositioned jumper on a lead / lag circuit card. The !
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inspectors reviewed the implications of the mispositioned jumper and the efforts of
the licensee in determining the root cause.
b. Observations and Findinas
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Condition Report 95-10591 was developed to assess the mispositioned jumper. j
The jumper consisted of a lead with two pin positions. The lead was found i
terminated to the " fixed" position pin as opposed to the required " variable" position. j
The inspectors reviewed the control room logs and found that the operators had
entered the appropriate Technical Specification action statements upon discovery of
the failed channel. The analog channel actuation test was correctly reperformed
after proper positioning of the jumper. The pressure loop was declared operable and -
the channel was returned to service.
To ascertain the extent of the problem, the technicians promptly verified the
configuration of the circuits for the other 11 main steam line pressure channels. - All
jumpers were found in the required position. Licensee management established an
event review team to perfnrm the investigation. The team determined that, with the
jumper in the fixed position, all dynamic output response of the circuit was l
removed. Therefore, although the channel would have tripped at a less
conservative fixed setpoint, the rate function would not have caused the channel to
trip prior to reaching the fixed setpoint following a main steam line break. The
impact of this delay in the main steam line isolation trip circuitry was still being
reviewed at the end of this inspection period.
A licensee event report will be issued in accordance with 10 CFR 50.73. The
inspectors will further review this event in conjunction with the closure of this
30-day report.
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c. Conclusion
The immediate response to the event was good. Plant personnel adequately
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addressed the potential for generic implications as well as the return to service of
the specific channel. The issue will remain open and will be addressed after
issuance of the licensee event report.
M1.5 Dearadation of Safety Iniection Motor-Ocerated Valve 1-SI-MOV-0016C Actuator
a. Insoection Scooe (62707)
On August 27, while closing Valve 1-SI-MOV-0016C after pe:formance of a local
leak rate test, a breaker thermal overload indication we= received. Condition
Report 96-10562 was written to investigate the cause. The inspectors followed the
investigation process and reviewed the licensee's findings.
, b. Qbservations and Findinas
The valve actuator was disassembled to determine the cause of the overload
indication. The maintenance technicians found severalindications of damage in the
valve actuator:
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e The motor shaft was cracked along the edges of the key way.
- The grease in the actuator contained bits of shinny brass.
e The brass worm gear had damage on the teeth.
- The bearing cap had damage where it had interfered with the worm gear.
The investigation revealed that a set screw was missing from the bearing cap. The
missing set screw allowed the bearing cap to travel along the threads on the worm
shaft untilit contacted the worm gear. The additional torque had apparently
created enough heat to cause the motor overload indication switch to actuate.
The potential for cracks to occur in the motor shaft key way was a condition that j
had been previously discussed during an owner's group meeting. Engineering l
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management had developed a plan to inspect the susceptible motor shafts prior to
the overload indication occurring. The failure to install a set screw and the
resultant contact of the bearing cap with the worm gear was independent of the
shaft cracking.
During the investigation, engineering personnel determined that the bearing cap set
i screw should have been installed in 1993 during a modification to the actuator
which was performed by a motor-operated valve maintenance contractor. The
same modification had been installed in other valves during that time frame. A plan
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of action was developed that outlined the following steps in investigating the
condition of other valves that could have the same problem:
e inspections were conducted on three additional motor-operated valve
actuators during the week of September 1,1996, with no deficiencies
identified,
o Documentation from the 1993 actuator modifications was reviewed.
e A schedule was developed to inspect valve actuators for the installation of
set screws as motor-operated valves were removed from service for routine ,
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e Valves with potential drive motor shaft cracking were scheduled to be
inspected by November 1996.
Failure to install the set screw during the modification of the actuator in 1993
constituted a noncompliance with the contractor's Maintenance / Operation
Procedure 3.0, Revision 1, "Limitorque Operator Overhaul, Models SMB-0 through
SMB-4." This was in violation of Technical Specification 6.8.1 which required that
maintenance of safety-related equipment be performed in accordance with written ,
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procedures. Based on the licensee response, the missing set screw was determined
to be an isolated instance This event-revealed and licensee-corrected violation is
being treated as a noncited violation, consistent with Section Vll.B.1 of the NRC
Enforcement Policy (Noncited Violation 498/96006-01).
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c. Conclusions l
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A violation was identified for the failure to modify a safety-related valve actuator in
accordance with written procedures which required the installation of a set screw
in the actuator spring pack. This event-revealed and licensee-corrected violation is !
being treated as a noncited violation, consistent with Section Vll.B.1 of the NRC
Enforcement Policy. Licensee management demonstrated an aggressive approach
to determining if the missing set screw was an isolated event. Valve actuators
inspected for similar problems were found to have the bearing cap set screws in
place.
M1.6 Steam Generator 2D Level Looo L-0547 Relav Failure (Unit 2)
a. Insoection Scope (62707)
On August 24, the inspector was informed that Steam Generator 2D Water Level
Loop L-0547 had f ailed and had been placed in a tripped condition in accordance
with appropriate Technical Specifications. The inspector observed and reviewed the
activities involved in the repair of the failed channel.
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b. Observation and Findinas )
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On August 24, Unit 2 operators responded to alarms related to Steam
l Generator 2D. The operators determined that an instrument f ailure had occurred on
Loop L-0547 and took the appropriate actions in accordance with Technical ,
Specification 3.3.2.6.d Action 20 by placing the affected channelin trip condition !
within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. During subsequent troubleshooting, instrumentation and controls.
technicians discovered a f aulty field input relay to the solid state protection system l
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Logic Train R cabinet.
Work planners prepared a work package that contained guidance on replacing the l
field input relay. The package indicated that the solid state protection system i
Protective Channel IV would remain inoperable throughout the evolution. Prior to l
field work, a prejob briefing was conducted with ensuing discussions related to the l
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relay replacement. The shift supervisors elicited discussion on areas of concern
from the control room operators and technicians. The discussions were detailed ;
and exhaustive. A reactor operator identified that the remcici of the relay would I
remove the trip signal provided by Channel IV to the solid state protection system l
Logic Train R. This would have nonconservatively changed the required two-out-of-
four logic. With the field input relay removed, the resulting Train R iogic would i
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have been two out of three channels to trip. In addition, none of the remaining
channels would have been in the tripped condition. Operators determined that, with
the logic train inoperable, Technical Specification 3.3.1.21, Action 9, would be
applicable. Action 9 required a unit shutdown to hot standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> with
no prior allowed outage time.
Notwithstanding the problems encountered with the planning of the package, the
shift supervisor concluded that the replacement of the field input relay should
proceed in an expeditious manner. This decision was based on the increReed risk of
a second channelinadvertently tripping as a result of severe weather that wasin
the area. Several telephone calls were made to offsite duty managers to brief them
on details of the work to be performed. In addition, the work authorization package
received a quality assurance signoff via telecommunication.
The inspector observed the replacement of the f ailed relay in accordance with Work
Authorization 91267. Continuous communications were provided between the field
personnel and control room operators. Precise communications techniques were
observed. Plant Operating Procedure OPOP03-ZG-0006, Revision 6, " Plant
Shutdown From 100% to Hot Standby," was entered when the first wire to the
relay was cut. The work was performed in accordance with approved procedures
and the technicians performed the relay replacement in a very efficient manner.
( Each step of the activity was independently verified. The new relay was soldered in
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place in 16 minutes, the channel trip was reestablished, and the shutdown
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procedure was exited. The new field input relay was tested, Plant Surveillance
Procedure OPOP02-FW-0517, Revision 2, " Steam Generator Narrow Range Level
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ACOT," was performed, and Level Loop L-0547 was returned to service. The shift !
supervisor was observed routinely reviewing and providing oversight at each step of i
the work process. ;
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During a followup review, the inspectors posed the following questions: t
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( * Was it appropriate to enter a Technical Specification action statement that ;
had no allowed outage time in order to make the repair? . ;
I * Was it appropriate to perform a quality assurance review by telephone for a
b system this critical to safety or should quality assurance and control i
l representatives have been present to inspect the work package and repairs? *
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are answered (Unresolved item 498:499/96006-02).
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c. Conclusions
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The replacement of the field input relay and associated activities were conducted in
a carefully controlled manner Supervisory oversight was considered excellent.
Communications among operations, maintenance, and engineering personnel during
the prejob briefing and throughout the evolution had a positive impact on the control
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M 1.7 Accumulator 1C Inleakaae in Unit 1
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a. Insoection Scoce (62707)
l On August 30, Unit 1 control room operators identified that water was leaking into
Safety injection Accumulator 1C. The inspector reviewed the plan of action
developed by the operators and observed portions of the activities associated with
finding the source of the leak,
b. Observations and Findinas
After noting that the water levelin Accumulator 1C had a gradualincrease, the
operators calculated that the level had been increasing at a rate of 3 gallons per
hour. A written plan of action was developed by the unit supervisor and the shift
supervisor to address this inleakage. The plan called for opening and closing certain
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valves in the system to determine where the leak was occurring and for pressurizing
sections of the piping to help seat check valves in the system. The plan was
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i comprehensive and carefully thought out by control room supervision. The shift
j supervisor, unit supervisor, and system angineer provided oversight for each step of
i the plan. A calculation was performed to determine how long it would take to
j dilute the accumulator to below the Technical Specification limit for boron
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concentration if corrective action was not taken. It was determined that it would
take greater than 372 hours0.00431 days <br />0.103 hours <br />6.150794e-4 weeks <br />1.41546e-4 months <br /> at the identified leak rate.
The troubleshooting plan was implemented and the leak was identified as coming I
through one of the test line valves. Pressurizing sections of the piping during the
troubleshooting resulted in reducing the leakage by reseating the check valves.
Similar problems had been previously identified in Unit 2. Condition
Report 96-1443 had been written to address the problem in Unit 2, and Condition
Report 96-10775 was written to specifically address the problem in Unit 1. The
licensee planned further review of the problem and was investigating a proposed
system modification that was designed to eliminate the leakage problems.
c. Conclu_sions
The operators demonstrated "y good attention to detail and a questioning attitude
during the activities. Supervisory oversight was noteworthy. Engineering personnel I
provided good support to the operations staff. l
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M1.8 Obsolete Plant Process Computer Constants Dearade Alarm Function
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a. Insoection Scope (62707)
On August 24,1996, operators determined that the constants in the plant process
computer, utilized for the calculation of axial flux difference, were incorrect. This
calculation was utilized by the plant process computer to provide annunciation in
the main control room should axial flux difference be outside the Technical
Specification required band. Operators determined that, following computer
maintenance on August 23, technicians had input obsolete constants into the
computer's memory instead of the recently revised data contained in the Accessible
Constants Log. The inspectors reviewed this event and the plant process computer
functions related to the axial flux difference monitor alarm,
b. Observations and Fjndinas
The plant process computer provided continuous monitoring of axial flux difference
and compared the instantaneous value with the Technical Specification required
target band. If the axial flux difference was out of tolerance, the clant computer
would generate an alarm on the axial flux difference monitor annunciator in the main
control room. The Technical Specification bases document ndicated that this
function was designed to be automatic as opposed to requiring operators to
routinely log the values of axial flux difference and compare them to the target.
Conversely, Technical Specification 4.2.1.1.b required that manual data logging of
the reactor axial flux difference be performed every hour whenever the alarm
function was inoperable.
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Because the target band changed over the life of the reactor core, new constants
were routinely developed by plant engineers and input into the computer's data
memory. The constants were lost from active memory when the computer was
inadvertently deenergized or required a reboot. Engineers had maintained an
Accessible Constants Log to provide the current design values of system constants.
Through interviews, the inspectors determined that, following a maintenance
activity on August 23,1996, control room operators had not updated the constants
following a computer reboot using the Accessible Constants Log. The
instrumentation and controls technicians had utilized a setpoint checklist which was-
incorrect.
Technical Specification 6.8.1.a required, in part, that written procedures be
established, implemented, and maintained concerning the applicable procedures
recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.
Regulatory Guide 1.33, Appendix A, recommended,in part, that procedures should
be written covering surveillance tests and calibrations of alarm devices.
The failure to establish written procedures covering the control of the constants
necessary for an accurate calibration of the axial flux difference monitor alarm
device following system maintenance was a violation of these requirements
(Violation 50-499/96006-03).
Although this violation was identified and corrected by the licensee, it was not
considered for enforcement discretion because of the similarities of this violation to
a noncited violation documented in NRC Inspection Report 50-498/96-001;
50-499/96-001. The inspectors found that the corrective actions to the noncited
violation should have prevented the August 23,1996, violation.
The inspectors also noted that the data sheets from previous performances of plant
process computer rebooting were not being maintained as quality documents. The
majority of these data sheets were being disposed of after the reboot. In addition,
the Accessible Constants Log was a hand-written log with no apparent independent
verification. The failure to properly implement and maintain the procedural data
sheets as quality records and the informal Accessible Constants Log appeared to be
contributors to the violation.
c. Conclusions
The f ailure to properly verify the accuracy of plant process computer constants
following maintenance of the system resulted in a degradation of the axial flux
dif ference monitor alarm device function. This resulted because an adequate
procedure to address the surveillance and calibration of this alarm device following
maintenance activities was not established. This violation was similar to a previous
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violation and should have been prevented by licensee corrective actions. In
addition, the control and maintenance of quality records appeared to be
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inappropriate.
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111. Enoineerina
E2 Engineering Support of Facilities and Equipment
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E2.1 Evaluation of Desian Chanae Packaae for Molded Case Circuit Breakers
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- a. insoection Scoce (37551)
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i Design Change Package 95-1920-4 was developed to change molded case circuit
j breaker setpoints and, in some cases, replace the circuit breakers for certain
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safety-related motor-operated valves. The inspector reviewed the design change
package for adequacy.
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b. Observations and Findinas
Various molded case circuit breakers used in safety applications at South Texas
,
Project did not meet the revised industry standards contained in IEEE
Standard 741-1990 and NRC Information Notice 92-51. These standards called for
motor-operated valve circuit breakers to have an instantaneous trip value of not less
than 200 percent of nominallocked rotor current.- The replacement molded case
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circuit breakers were designed to handle the high starting currents without
j experiencing spurious trips.
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The inspector determined that the design change package appropriately addressed -
, the concerns in the Information Notice and the Standard.
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The package was developed to support a global change to existing molded case
circuit breakers in safety applications at the South Texas Project. A comprehensive
i screening was conducted in accordance with 10 CFR 50.59. No unreviewed safety
[ question was found to exist. The modification did not require a revision to the
safety analysis report nor did it impact the Technical Specifications.
f c. Conclusions
The inspector concluded that the design change package was comprehensive and of
good quality. ' The safety implications were adequately addressed in the safety
evaluation.
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E8 Miscellaneous Engineering issues
E8.1 Soent Fuel Pool Gate Seal Replacement and Seal Desion Review (Unit 1) l
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a. Insoection Scoce (62707) )
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The inspector observed portions of the performance of a preventive maintenance
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activity to replace the leaking outer gate seal on the cask connecting channel end of I
the spent fuel pool. Discussions were held with control room operators, the system
engineer, the system engineering manager, and the mechanical maintenance
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manager regarding the work activities and technical considerations. 1
The inspectors reviewed the historical problems associated with spent fuel pool gate i
seals documented in NRC Inspection Reports 50-498/95-020: 50-499/95-020. r.; I
50-498/95-021:50-499/95-021.
b. Observations and Findinos
On August 8, the inspector observed the placement of the outer gate into the spent
fuel pool for temporary storage. The outer gate had been replaced with a gate
containing a newly installed seal. After installation, operators did not fill the area
between the gates with water to test that the outer gate would not leak. The spent
fuel pool was designed with a set of gates separating the spent fuel pool from the
spent fuel cask handling area. Each gate had one sealinflated by air from the
instrument air system via a pressure regulator and a check valve. The seals were
not designated as safety related nor seismically qualified.
Engineers stated that the gate seal had previously been tested while installed on the
transfer canal side of the spent fuel pool. The inspectors noted that the licensee
had developed Plant Operating Procedure OPOP07-FH-0001, Revision 0, " Spent Fuel
Pool Gate Seal Operability Check," to ensure the integrity of the gate seals.
Engineers stated that a decision had been made not to perform
Procedure OPOP07-FH-0001 because of concerns that the test would cause the
inner seal to begin leaking.
In a letter dated December 19,1995, the licensee had discussed providing an
additional barrier at the south end of the cask connecting channelin order to
minimize the risk associated with performing maintenance on one of the gates.
Because this maintenance evolution was being performed without an additional
barrier in place, the inspectors inquired about the projected date for installation of
the additional barrier, it was determined that the licensee's 5-year plan scheduled
the installation of a spent fuel pool cask conneuing channel gate for Unit 1 on
July 31,1997, and on October 1,1997, for Unit 2. As of this inspection, no
design work had been conducted.
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During a walkdown of the cask handling area drain system, the inspectors noted
that the drain valves were closed. The valves were not danger tagged closed nor in
the locked valve program. An equipment clearance order had been written to
danger tag the drain valves closed in July 1995. This was documented in NRC
Inspection Report 50-498/95-020:50-499/95-020. During a management meeting
conducted in the Region IV office on July 25,1995, senior licenseo management
had stated that, given the incomplete status of the cask handling areas, the
associated drain valves would be closed and placed in the locked valve program.
However, since that time, engineering personnel determined that the controls were
not necessary and the danger tags were removed and the equipment clearance
order was closed.
Since the additional barrier at the south end of the cask connecting channel had not
been designed and the controls governing the testing of the spent fuel pool gate
seals and the position of cask area drain system valves had been relaxed, the
concerns with not having safety-related seals on the spent fuel pool gates remain.
This matter will be further reviewed and will be tracked as Unresolved
item 498:499/96006-04. The following concerns will be inspected and verified as
a part of this review:
- What design criteria was utilized for the seals during the originallicensing
review?
- What would be the final water level in the spent fuel pool should both
nonsafety-related seals fail?
- Was the cask connecting channel gate considered a critical part of the
originally accepted design?
- Has long-term exposure of the unfinished cask handling area surf aces to
spent fuel pool boric acid affected the integrity of the reinforcing steel?
- Has the licensee performed a flooding analysis considering the potential for
loss of the spent fuel pool gate seals?
c. Conclusions
The inspectors concluded that the seal replacement was a well coordinated and
l planned operation, demonstrating effective communications between interf acing
j plant organizations. However, because maintenance was performed on the spent
I fuel pool gate seals prior to installation of an additional barrier at the south end of
the cask connecting channel, further reviews of the implications of having
nonsafety-related gate seals will be conducted.
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IV. Plant Support
R1 Radiological Protection and Chemistry Controls
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R1.1 Tours of Radioloaically Controlled Areas (RCAs) 1
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a. insoection Scope (71750)
.The inspectors routinely toured the RCAs in Units 1 and 2. These tours included l
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sampling of locked doors, observation of work and verification of proper radiological
work permits, and observations of entrance and egress from the RCAs. l
b. Observations and Findinos
Radiological housekeeping in the areas toured in both units was good. Observed
work was performed in accordance with proper radiological work permits and
approved procedures. Nc discrepancies were identified with sampled locked doors.
Entrances and egresses from the RCAs were observed to be in accordance with
radiological protection procedures. Items carried out of the RCA were properly
frisked prior to leaving the RCAs.
c. Conclusion _g
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implementation of radiological controls and control of RCA entrance and egress was
! good.
S1 Conduct of Security and Safeguards Activities (71750)
The inspector routinely observed security officers performing screening for
l personnelingress and egress, including searches of personnel and packages.
Protected area illumination was spot checked and no deficiencies were noted.
Officers were alert and appropriately attentive. No discrepancies were observed.
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ATTACHMENT
PARTIAL LIST OF PERSONS CONTACTED
Licensee
T. Cloninger, Vice President, Nuclear Engineering 1
K. Coates, Manager, Maintenance 2
D. Daniels, Manager, Operating Experience
B. Dowdy, Assistant to Group Vice President
J. Groth, Vice President, Nuclear Generation
E. Halpin, Manager, Design Engineering Department i
W. Harrison, Supervising Licensing Engineer
S. Head, Licensing Supervisor
T. Jordan, Manager, Systems Engineering
M. Kanavos, Manager, Mechanical Fluid Systems
D. Leazar, Director, Nuclear Fuels and Analysis
F. Mangan, General Manager, Plant Services
l B. Masse, Plant Manager, Unit 2
l G. Parkey, Plant Manager, Unit 1
D. Schulker, Compliance Engineer
W. Waddell, Manager, Maintenance 1
F. Wagar, General Manager, Human Resources
INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
IP 61726: Surveillance Observations
IP 62707: Maintenance Observations
IP 71707: Plant Operations
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IP 71750: Plant Support Activities
IP 92901: Followup - Plant Operations
IP 92903: Followup - Engineering
IP 93702: Prompt Onsite Response to Events at Operating Power Reactors
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ITEMS OPENED, CLOSED, AND DISCUSSED
l Ooened
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498/96006-01 NCV* failure to install a required set screw in a motor-
operated valve actuator spring pack
498;499/96006-02 URI review the adequacy of entering an action statement
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with no allowed outage time for corrective maintenance
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498:499/96006-03 VIO inadequate controls
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498;499/96006-04 URI review the implications of not providing safety-related
seals on the spent fuel pool gates
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Closed
498/96006-01 NCV* failure to install a required set screw in a motor-
, operated valve' actuator spring pack
499/96001-01 VIO two feedwater isolation valves out of service in
violation of Technical Specification 3.0.3
499/96-001 LER two feedwater isolation valves out of service in
violation of Technical Specification 3.0.3
498/95027-01 VIO inadequate controls governing the configuration of fuel
handling equipment
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The noncited violations identified in this report require no further NRC review and
are considered both opened and closed in this inspection report.
LIST OF ACRONYMS USED
lEEE Institute of Electrical and Electronic Engineers
NCV noncited violation
NRC Nuclear Regulatory Commission
PDR Public Document Room
RCA radiological controlled area
URI unresolved item
VIO violation
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