ML20107A444

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Insp Rept 50-219/73-10 on 730511.No Violations Noted.Major Areas Inspected:Routine Review of Refueling Operations
ML20107A444
Person / Time
Site: Oyster Creek
Issue date: 06/07/1973
From: Cantrell F, Caphton D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18039A986 List: ... further results
References
FOIA-95-258 50-219-73-10, NUDOCS 9604120297
Download: ML20107A444 (5)


See also: IR 05000219/1973010

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U. S. ATO?lIC ENERGY CO>DlISSION

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DIRECTORATE OF REGULATORY OPGATIONS

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REGION I

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RO Inspection Report No.:

50-219/73-10

Docket No.: 50-219

Licensce: Jersey Central Power & Light Co.

License No.: DPR-16

Oyster Creek

Priority:

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Category: C

Location : Forked River , N.J .

Type of Licensce:

1930 MWt. BWR

Type of Inspection:

Special, announced

Dates of Inspection:

May 11, 1973

Dates of Previous Inspection:Jgagini May 2. 1973.

Reporting Inspector:

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F.S. Cantrell, Reactor Inspector

Date

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Accompanying Inspectors:

None

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Date

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Other Accompanying Personnel:

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Reviewed by:

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D.L. Caphton, Senior Reactor Inspector

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9604120297 960213

PDR

FOIA

DEKOK95-258

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SUMMARY OF FINDINGS

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Enforcement Action

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None

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Licensee Action on Previously Identified Enforcement Items

Not. inspected

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Design Changes

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None

. Unusual Occurrences

The condensate drain valve on the B-isolation condenser failed to

open during a surveillance test on April 14, 1973.

(Details, Para. 4)

Other Significant Findings

A.

Current Findings

Seventy-seven fu&l assemblies were identified as containing leaking

fuel pins as a result of water samples taken from each fuel assembly.

The failed assemblies are scheduled to be replaced during the current

U4N

. regular refueling operations. 146 assemblies are scheduled to .be re-

placed.

(Refueling was reported by phone to be completed May 16, 1973).

B.

Status of Previously Reported Unresolved Items

Nc" inspected

Management Interview

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The exit interview was conducted with Mr. Carroll.

The inspector stated that the prime purpose of the inspection was a routine

review of refueling operations, and that the only deficiency identified was

that the key.for the reactor mode switch was left in the switch when the

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switch was in the " refueling" position. With the key in the switch..the

switch may be technically locked as required'by Technical Specifications,.

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but practically,-the switch is unlocked. Mr. Carroll stated that the key

would be removed and placed under the control of the shift foreman.

(De-

tails, Para. 2k)

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DETAILS

1.

1.

Persons Contacted

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Mr. J.T. Carroll, Station Superintendent

Mr. D.L. Reeves, Operations Supervisor

Mr. 1

!. Riggle, Maintenance Supervisor

Mr. L J. Cooper, Shift Foreman

Mr. F. Kossatz, Maintenance Foreman

Mr. J. Young, Control Room Operator

Mr. E. Vetz, Control Room Operator "B"

2.

Fuel Handling

The requirements of Oyster Creek procedure No. 212 (Revision 3 as

modified by a temporary procedure change dated April 24, 1973),

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Fuel Handling, were inspected to verify compliance with the procedure

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and the Technical Specification (TS) requirements (paragraph 3.9).

The following information was obtained by reviewing plant records, in

discussions with plant personnel and during observations in the field:

A detailed Refueling Work List was issued by the Technical Super-

a.

visor designating specific fuel moves. This was approved by the

Technical Supervisor as specified in a temporary procedure change

dated April 24, 1973.

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b.

The steps of the Refueling Work List were being followed and

signed off as completed.

A procedure was available for checkout of refueling equipment,

c.

and records indicated that the procedure was completed prior

to the start of the refueling operaton.

d.

The inspector observed visual and functional checks of some of

the refueling equipment at the start of the 8-4 shift on May 11, 1973

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as required by procedure 212-5.3; however, no specific record was

made of these checks.

Plants records showed that the refueling interlocks were verified

e.

to be operable weekly as required by TS paragraph 4.9.

f.

Flant records showed that the source range monitors (SRM) were

calibrated prior to refueling, checked each hour, and tested week-

ly.

This schedule met the surveillance requirements of TS para-

graph 4.9.

g.

If any of the source range monitors became inoperable during refuel-

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ing, the control room operators determined that the SRM nearest

the core alteration in progress was operable (Requirement of TS

paragraph 3.9D).

h.

The surveillance requirements of TS Table 4.1.1 are continued

during the refueling outage in order to a seura that the protec-

tive instrumentation meets the requirements of TS Table 3.1.1.

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1.

The Core Spray, the Containment Spray, the Emergency Service

Water, and the Fire Protection Systems are maintained operable

during refueling as required by TS paragraph 3.4.

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Secondary containment integrity is verified by the Shift Foreman

at shif t turnover, and he controls the keys to locks on doors that

could breech containment integrity (Ref. TS paragraph 3.5B) .

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TS paragraph 3.9 requires the reactor " mode switch" to be locked in

the " refuel" position during core alterations. The mode switch was

observed to be locked in the refuel position, but the key was left

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in the switch.

In response to questions, the Station Superintendent

agreed that the key would be removed when the switch is required to

be locked by procedure _or the TS.

The key will be controlled by the

shift foreman who is responsible for equipment or safety lock outs.

3.

Inspection of Control Rod (Position 18-15)

Control Rod in position 18-15 was stuck in the reactor and could~not be

withdrawn on January 10, 1973. The control rod drive (CRD) was re-

placed and a licensee representative stated that Jersey Central plan-

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ned to examine the drive to determine why the drive was inoperable;

however, because of personnel exposures involved in overhauling

irradiated CRDs, this examination would be performed after the refueling

outage.

The inspector witnessed the removal and inspection of the fuel support

castings and the control rod blade at position 18-15.

The inspection

was performed with an underwater TV camera.

Both appeared to be in

good condition.

A minor scrape was observed on the upper part of the

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control blade; however, an evaluation by Jersey Central indicated that

the scrape was not connected with the failure of the control rod to

withdraw.

(The control rod operated normally during a subsequent

operability check).

4.

Isolation Condenser Drain Valve

(Letter JCP&L to Licensing dated April 24, 1973)

During a weekly surveillance test with the plant at cold shutdown on

April 14, 1973, the B-isolation condenser condensate drain valve (V 14-35)

failed to open. This valve failed to operate on November 16, 1971 due

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to a burned out motor (JCP&L letter dated December 14, 1971), and

also, failed to open when initiated following a reactor trip on

December 29, 1973. The valve was disassembled and inspected; how-

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ever, no specific :ause was identified for the malfunction. The

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switch settings of the valve operator were checked and found set as

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specified by the manufacturer. The valve operated properly during

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each subsequent weekly test.

(Testing frequency was increased from

monthly to weekly because of the failures experienced). Following

the April 14, 1973 failure, a representative of the valve manufactur-

er inspected the valve and concluded that the shape of the disc guider

caused the disc to rotate as the valve approached the fully closed

position.

The valve is mounted in a horizontal position.

In the

horizontal position, the lower guide causes the disc to move up and

down about 1/8 inch just prior to seating. A demonstration with the

stem and disc moved by nand, with bonnet removed, showed that the

disc could rotate as it seated. The corrective action recommended

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by the vendor was to remove the hump on the lower guide and build

up the upper guide to prevent this rotation of the disc just prior

to seating.

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