IR 05000219/1972002

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Insp Rept 50-219/72-02 on 720223-25,29 & 0301. Major Areas Inspected:Torus to Drywell Vacuum Breaker Check for BWRs
ML20107C764
Person / Time
Site: Oyster Creek
Issue date: 05/16/1972
From: Cantrell F, Robert Carlson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18039A986 List: ... further results
References
FOIA-95-258 50-219-72-02, 50-219-72-2, NUDOCS 9604170528
Download: ML20107C764 (19)


Text

{{#Wiki_filter:, d I o U. S. ATOMIC ENERGY COMMISSION ' DIVISION OF COMPLIANCE - . REGION I > CO Inspection Report No.' -50-219/72-02-Subject: Jersey Central' Power & Linht Comoany Oyster Creek License No.

DPR-16- , - Location: Forked River, New Jersey Priority i Category C = Type of Licensee: BWR (1930 MWt) Type of Inspection: Routine

, Dates of Inspection: February 23, 24, 25, 29_ and March 1. 1972 ' Routine * July 2, 1971 - Dates of= Previous Inspection: Special February 7, 1972 b-ff . .,.. ' P , * * -l' t / ~-A / -

~ Principal Inspector: ( - F. S. Cantrell, ReactorA nspector Da t'e / Accompanying Inspectors: None Date Date-Other Accompanying Personnel: None j Date

, 7t' b"' /6 77_ Reviewed By: ' R. T. Carlson, Senior Reactor Inspector date/ Proprietary Information: 'de 9604170528 960213 PDR FOIA

DEKOK95-258 PDR , m _ _ _, , - -. . . - -

- - _ ._ _... _. . __ . - _ . ~ _. - .- . .- -Section I Enforcement Action: A.- Technical Specification 3.4.C.5 specifies in'part, "During the period when ciin diesel is inoperabit, the containment spray' loop'.... connected i to the operable diesel shall have no, inoperable components".

- On Janu ary l14, 1972,' while'the No. I containment ^ spray system (which , Jis - connected to the No.1 emergency diesel generator) was. inoperable in the course of:a scheduled'surveill'ance test, the No. 2 emergency , diesel generator was made inoperable to permit adding oil. This condi-tion existed for'45 minutes.

(Paragraph 7) ' B.

Technical Specification 6.6.B requires in'part, "The events: listed below require reports within 24 hours by telephone or telegraph to-Region I Compliance office followed by a written report within 10 days to the Director, Division.of Reactor Licensing... 2.Any abnormal occurrence as'specified in Section 1.15..". Section 1.15.B defines an abnormal occurrence as " Violates a limiting' condition for operation as established 'in Section 3 of the Tachnical Specifications, or..". Contrary to the above requirement, the written report of the violation was not submitted until February. 22, 1972.

(Paragraph 7 and Management

Interview) Licensee Action ~on Previously Identified Enforcement Matters: i As a follow up to.the April 1971 inspection, a formal enforcement letter-was sent to the licensee from CO:HQ on August 25, 1971 identifying three items of noncompliance with Regulatory requirements pertaining to the i rslease and storage of liquid radioactive waste-and two other, issues j involving variances in the operation of the facility from information j . presented in the FD&SAR.

l In a letter dated September 16, 1971, JCP&L replied'to the enforcement action as~follows: , A.

Corrections were made in 'the sampling and analytical techniques ] ' (discussed in CO. Report No. 219/71-2). Corrected figures for total ' radioactivity' released were supplied to the Division of Reactor Li-censing in a letter dated September 22, 1971 that accompanied Semi- , Annual Report No. 4 Revised-pages for Seni-Annual Reports Nos.

" 1, :2, and 3 were included. This item is considered resolved.

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The source of the excessive background radiation in the vicinity of the liquid effluent monitor was removed. This item is considered resolved.

C.

Jersey Central did not agree with the requirement to report any substan-tial variance disclosed by operation of the facility from performance specifications contained in the Facility Description and Safety Analysis Report (FD&SAR) or the Technical Specifications (TS). This item was resolved in a letter to Jersey Central from L. D. Low, Director, Division of Compliance, dated December 30, 1971, re-affirming the requirement to report any substantial variances.

As a result of the June 23 - 25, 1971 and July 2, 1971 inspection, two items , of noncompliance with Regulatogrrequirements were identified in a letter from J. P. O'Reilly, Director, Region I, to JCP&L on September 14, 1971.

In a letter dated October 1,1971, JCP&L replied to the enforcement action as follows: A.

The incorrect trip point setting for the radiation monitor in the main steam line tunnel was detected by a General Office Review Board (GORB) audit and was corrected prior to the inspection.

Item resolved at time of subject inspection, as noted in September 14, 1971 letter.

i B.

New administrative procedures were reported to have been instituted which require the General Public Utilities Safety and Licensing Group to review all CORB audit reports for licensing violations and to report the results , . to the Chariman, CORB. The Chairman reports separate violations to the President, JCP&L as necessary.

' The JCP&L letter further stated, "With respect to Item No. 2 of your 1etter, an investigation will be conducted and the results reviewed at the next GORB meeting.... ". Contrary to the above cannitment, the minutes of the next GORB meeting, which was on November 23, 1971, did not show that the investigation had been conducted or that the results had been reviewed. Records did not indicate any other meeting had been held subsequent to October 1,1971.

As a follow up to the November 19, 1971 inspection, one item of noncompliance with Regulatory requirements.vas identified in a letter to JCP&L from J. P. O'Reilly, Director, Region I on December 23, 1971. No reply was requested since corrective i action was initiated and the violation was reported in a letter from JCP&L dated December 14, 1971.

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-3-Unresolved Itans: None Status of Previously Reported Unresolved Items: . A.

QA records for the installation of relief valve No. NR108E are at the site. No deficiencies were noted. This item is considered resolved.

(Paragraph 5.1) B.

QA records are at the site for: 1.

the six new 10 inch swing check valves in the core spray system (Paragraph 5.h); 2.

two new Powell valves in the poison system (Paragraph 5.ky, 3.

eight isolation condensers drain valves (two each drain line) (Paragraph 5.g).

These valves were installed during the September - November 1971 outage. This item is considered resolved.

C.

A new isokinetic probe was installed in the plant stack. This area was not inspected.

D.

A jockey pump (to keep the piping system filled) has been installed on both core spray loops. A preliminary report of the investigation of the core spray water hammer was submitted to the Division of Reactor Licensing on June 25, 1971.

(Paragraph 8) E.

Reactor vessel level instrumentation - The "A" GE/MAC level indicator does not. agree with the "B" GE/MAC or the Yarway level indicators (1.3 feet lower). This problem is still unr.esolved.

(Paragraph 9) F.

The basis for setting the 45% bypass device for turbine scrams was provided in Amendment No. 65 (Application to Increase Power Level), approved on November 5, 1971. This item., considered resolved.

G.

The protective devices for the emergency diesel generator (EDG) when in the fast start mode were functionally tested during the annual inspection.

These devices for the No. 1 EDG were calibrated in February 1972.

No. 2 is scheduled in April 1972.

(Paragraph 12) Unusual Occurrences: A.

The generator load rejection and turbine trip anticipatory scram bypass switch failed due to a packing leak on'the root valve on August 2, 1971 (Letter, JCP&L to DRL, dated September 9, 1971).

B.

The standby gas treatment system train No.1, minimum flow valve failed to open due to a solenoid valve failure on July 6, 1971 (Letter, JCP&L to DRL, dated September 9,1971).

C.- One of the four scram dump volume level switches failed due to binding during a surveillance test on August 17, 1971 (Letter, JCP&L to DRL, , dated September 9, 1971).

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While performing a surveillance test on the B isolation condenser line break

isolation sensors, the time delay feature of both isolation relays was found inoperable thus negating the automatic isolation function la the event'of a line break (Letter, JCP&L to DRL, dated September 30, 1971).

(Paragraph 10) , E.

As a result of an accident involving one of the mobile nitrogen evaporators used to inert containment and severe weather conditions where the backup nitrogen evaporator was located, equipment was not available to inert the

containment within 24 hours after the reactor was placed in the run mode on November 23, 1971. A temporary Technical Specification change was approved by the Division of Reactor Licensing to permit operation at up to 50% of full power with the 02 content greater than 5% for an additional 24 hours.

(Letter, JCP&L to DRL, dated November 22, 1971 and letter, DRL to JCP&L, dated November 22, 1971) (Paragraph 11) F.

Following the annual. inspection on September 9,1971, the generator breaker-was inadertantly closed on a live bus with the diesel engine at a standstill.

- (Letter, JCP&L to DRL, dated December 13, 1971) 't G.

The vent line-from the isolation condenser to one of the main steam lines broke, downstream of the isolation valves in both the vent line and the main , i steam line. The reactor was shutdown and the line was repaired by welding.

(Letter, JCP&L to DRL, dated January 12, 1972) H.

During a~ closure test of the main steam isolation valves on September 18, 1971, one of the inside. valves closed faster than desired (3.2 seconds).

' An oil leak in the hydraulic dash pot adjustment leg was determined to be the cause. During a subsequent test, the leakage through the valve was r greater than TS limits. The valve stem was straightened and the main and . pilot valve seats were lapped (Letter, JCP&L to DRL, date d December 13, 1971).

' I.

During a routine surveillance test on December 28, 1971, the No. 1 emergency ' diesel generator (EDG) tripped off when it ran out of fuel in the " day tank".

i The starting switch on both transfer pumps was dirty and corroded.

(Letter, , JCP&L to DRL, dated January 5,1972) (Paragraph 12) J.

The radionuclide inventory in the outside tank farm exceeded 0.7 Ci on several occasion (TS limit 0.7 C1) and was recycled until compliance with the TS limit was achieved as required by the TS.

Due to problems with the waste , concentrator plugging, rapid depletion of the rad waste demineralizer and

the large inventory remaining from the September - November 1971 outage, the inventory of the tank farm exceeded 0.7 Ci from November 29 to December 17, 1971.

(Letter, JCP&L to DRL, dated December 22, 1971) (Paragraph 13) 1 - e f / - .

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While the No.1 containment spray system was out of service for surveillance j testing, the No. 2. emergency diesel generator that powers the No. 2 contain-j ment spray system was removed from service for servicing.

(Letter, JCP&L to DRL, dated February 22, 1972) (Paragraph 7) , l L.

While testing the " normal emergency power DC interlock failure" alarm on ! -January 22, 1972, DC power was transferred from 12SV DC Bus A to 125V DC ' Bus B.

The momentary loss of power. caused a trip of three of the five s recirculation pumps and one feeduater pump.

Plant power dropped from 642 MWe to'316 MWe and leveled at 336 MWe.

(Letter, JCP&L to DRL, dated

February 22, 1972)

M.

While removing the "A" battery motor generator set from service for main-tenance, the main breaker was opened before the static charger was , closed in on the bus. The loss of DC voltage on A bus caused three of the

" 'five recirculation pumps, and one feedwater pump to trip. Reactor power .[ ' dropped from 640 MWe to 346 MWe and leveled off at 400 MWe.. (Letter, JCP&L to DRL,. dated February 23, 1972) i N. -During a check out of repairs to the current transformers that supply

overload = protection to the 1A auxiliary transformer, power to the 1C emer- . i gency bus tripped off due to an error in setting.up the test. The operator attempted to restore power by reclosing the normal supply at the same time

the. emergency diesel generator (EDG) phased on line. The EDG tripped on

reverse current and the normal supply tripped because the fault that was set up in the' transformer check out was still in the system.

(Paragraph 14) l

0.

One of the four scram' dump volume level switches failed during a surveillance check on March 1, 1972 due to dirt and water in the switch assembly that

. prevented full travel of the switch arm.

(Letter, JCP&L to DRL, dated l March.10, 1972) ! i l Persons Contacted: T. J. McCluskey, Station Superintendent J. T. Carroll, Operations Supervisor R. M. McKeon, Shift Foreman R. VanBrakle, Control Room Operator J. Glendenning, Control Room Operator D. A. Ross, Technical Supervisor E. I. Riggle, Maintenance Supervisor , J.

L.~ Sullivan, Technical Engineer D. Petrine, Chemical Supervisor D. E. Kaulback, Radiation Protection Supervisor . K. O. Fickeissen, Assistant Technical Engineer

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\\ l . -6-y agement Interview: M .The inspector conducted an exit interview on March 1, 1972 with Messrs.

McCluskey, Ross, Carroll and Riggle.

. A.

Comments on Discussion with operators Mr. McCluskey stated that he was not aware of any problems from the inspector's discussion with two operators on the loss of the IC bus that ' occurred on l December 22, 1971. The two operators were on duty at the time.

Mr. McCluskey asked the inspector if he had any problem. The inspector stated that the ! two men had been very cooperative and to the best of the inspector's under-

standing, verified the information in the OC internal report to the PORC.

] I B.

Violation of LCO No. 1, Containment Spray System, and No. 2, EDG Out of ! Service Simultaneously (1/14/121 l ! (Letter, JCP&L to DRL, dated rebruary 22, 1972) J l According to plant re ords, the violation was discovered on January 15, 1972, but was not reported to Region I until January 26, 1972, and as of the date the inspector left his office on February 22, 1972, the written j report had not been received by Region I.

l I Mr. McCluskey stated that normally when testing the core spray system, the core spray system is not inoperable - an initiation signal will' override ! the test signal; however, for this particular test, it was necessary to , close and de-energize a valve that made the system inoperable. He stated l that even though he was informed on January 15, 1972 that both systems were ' l off line at the same time, he did not realize that a LCO was violated ! until a full investigation was completed on January 25, 1972 and at that i time he reported the violation to Compliance. He stated he could not j explain the reason for the delay in the written report other then the time necessary to get a report through the necessary channels.

Mr. Ross , obtaired a copy of the written report (dated February 22, 1972) that was l sent to DRL. After some discussion, the inspector stated he accepted the i explanation for the delay in the verbal report to Compliance; however, ( the failure to submit a written report of the violation of an Leo within l 10 days after it was discovered was considered in noncompliance with the Technical Specifications.

(Paragraph 7) C.

Exceeding TC Limits (0.7 Ci) for Tank Farm Inventory The inspector discussed the present controls which require the plant chemist to notify the shift foreman when the results of his analysis show that the 0.7 Ci limit is exceeded.

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( Mr. Carroll stated that additional-information would be provided to the shift. foreman in order -to reduce the nusber of violations.

(Mr. McCluskey , - subsequently informed the inspector by telephone that the ~results of the ' Monday 4 Wednesday - Friday inventories are reported to the shi foreman to; help him plan his reprocessing ' schedule.)

(Paragraph 13) Do Loss of 4160 Volt Emergency bus IC The inspector stated that paragraph 3.7.A.I.a of the Technical Specifications (TS) requires the 1C breaker to be energized and paragraph 3.7.B requires l placing the reactor in a cold shutdown condition if the requirements of !

paragraph 3.7.A are not. met.

Since a violation of a limiting condition for

operation (LCO)' is defined as an abnormal occurrence, the event requires a 24 hour telephone or telegraph report to compliance, and a 10 day written report to DRL.

Mr. McCluskey stated that the event had been investigated by the Plant

Operations Review Committee (PORC) and the cmmnittee had concluded that the-event was not a violation of an LCO. The basis for the TS states that the objective'is to assure an adequate supply of power with at least one active

' and one standby source of power for operation of equipment that is required for a safe plant shutdown and to operate the required engineered safety equipment. In light of the safety analysis that one standby source of power (emergency diesel generator) will supply adequate power to place the plant in a safe conditfbn, the PORC interpreted that Specification 3.7.B only applied to the availability of outside power supplies as specified in paragraphs 3.7.A.2 and 3, and station batteries as specified in paragraph 3.7.A.4.

The inspector stated that he felt the words of the TS vere specific; however, he would review this matter with his supervision to determine the intent of the specification and how it should be applied. Assuming the specific requirements apply, the following comments are applicable: 1.

Emergency procedure No. 502, which covers the loss of power, was revised as a result of the loss of bus IC: however, neither the old nor the revised procedure recognized the TS requirement to place the plant in a cold shutdown condition when a LCO is exceeded.

I 2.

Written procedures were not used to check out the modifications to the auxiliary transformer.

3.

There was no record that the modifications to the auxiliary transformer were approved by the PORC or that the change did not involve an un-reviewed safety question. Prior to this event, we probably would have agreed that this type change could have been made without a written safety evaluation as required by 10 CFR 50.59; however, D _- --- - -_--_ -_. .-

. . -9-The inspector stated that PORC meeting minut es did not indicate that the problem of the difference in the reactor level as sensed by the two GE/MAC level indicators had been discussed.. Mr. M;Cluskey stated that this was apparently an oversight in the minutes since the problem had been assigned to one of Mr. Ross's engineers as an " action item" and that he is required to report his findings to the PORC.

Mr. Ross stated the problem was still active. This explanation was accepted.

(Paragraph 15) F.

Information Recorded in the Shift Foreman's Log and the Control Room Log The inspector stated that he did not feel that sufficient information was being recorded in these two logs to serve as a record of significant events.

Neither log indicated the reason for the January 27, 1972 shutdown (the unexplained leakage rate increased to 4 gpm) and neither log showed that the stack release rate increased to 142,000 uCi/sec for a short period on January 23, 1972.

(The release rate had been about 55,000 uCi/second.)

Mr. Carroll agreed more information should be entered in these two log books and that he would initiate the necessary action.

(Paragraph 16) G.

Additional Areas Reviewed to Determine Compliance with Regulations The inspector stated that he had made a specific review of logs, charts an&. records to verify: 1.

that reactor power had not been increased above 50% until the oxygen in the drywell was less than 5% on November 23, 1972 (Paragraph 11), ar.d 2. that an additional operator was present to act in place of the ipo' _rable rod worth minimizer during the reactor startup on November 11, 1971. The review did not show any items of noncompliance in these two areas.

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_ . . -8-in retrospect the events that occurred demonstrated that modifications in the power supply area can directly affect plant safety equipment.

The inspector asked if Jerse Central would operate with only the EDG supplying either of the emergency buses (Bus 1C or 1D). After a brief discussion Mr. McCluskey stated that the plant would not be operated with only the EDG available to supply power to its associated emergency bus.

He pointed out, however, that the TS permit a startup transformer and an EDG to be out of service simultaneously for seven days. The inspector stated he intended to pursue this subject to determine the intent of the specification.

After reviewing the above event, the inspector called Mr. McCluskey on March 6,1972 and informed b tm that TS 3.7.A and B must be interpreted as written and that a written report of the event must be made to DRL.

The review indicated that there is some inconsistency between the basis for the TS and the words in TS 3.7.A and B.

He was told that Compliance was not implying that with the IC bus de-energized for five minutes he should have shut down the reactor; however, if the bus had been lost for five hours, the reactor should have been in the process of shutting down.

The inspector stated that as long as the present specifications were applicable, Jersey Central will be expected to follow the specification as written; however, if the written report is made within 10 days of the present date, there would be no citation for failure to report this event.

(A written report was submitted to DRL on March 10, 1972.)

- The inspector pointed out that if there is any doubt as to whether an event is reportable that if the Regional Compliance office is notified within 24 hours, the licensee automatically has at least 10 days by his TS to make up his mind as to whether a written report to DRL is required.

(Paragraph 14) E.

Plant Operations Review Committee The inspector stated he was concerned with the poor attendance of the representatives of the General Office Review Board (GORB) at the PORC meetings. The records indicated that the GORB members only attended two of the monthly meetings during the period July - December 1971.

Mr. McCluskey stated that the inspector's comments would be relayed to the appropriate people. He stated that the investigation of the loss of emergency bus 1C had been delayed a few days to permit the GORB members to be present at the investigation (PORC meeting on January 11, 1972).

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_ __ . .. . Section II.

Additional Subjects Inspected, Not Identified in Section I, Where No D-ficiencies or Unresolved Items were -Found. 1.

' General Since the July 2, 1971 inspection, the reactor has experienced one scram (complete loss of instrument air on November 16, 1971), two unplanned shutdowns (broken isolation condenser vent line on December 11, 1971 and an increase in unidentified leakage in the drywell on January 28, 1972) and one scheduled shutdown. (September 18 through November 11, 1971).

During the September - November outage, the licensee completed the following-tasks: removed all poison curtains, performed incore sipping of 548 of 560 fuel bundles, inspecte.d 33 suspected leaking fuel bundles, recon-stituted 20 fuel bundles, installed 24 new fuel bundles, replaced 7 local

power range monitor strings, replaced 1 control blade, replaced 3 control rod drives, inspected the high pressure. turbine and the "A" low pressure turbine, replaced 6 of the 9 main steam bypass valve seats, and installed L a fif th main steam relief valve in the drywell.

I Amendment No. 3 to the facility license was approved on November 5, 1971 permitting operation at 1930 MWt. During the power ascension program, the main steam bypass valves started opening at 1850 MWt indicating that the stean produced at that level was the maximum that could pass the control valves without completion of modifications to the second stage reheaters.

This' work was started during the September - November outage. Comple' tion ' is now scheduled for the April 1972 refueling outage. All of the testing that was scheduled for 1930 MWt was then performed at approximately 1830 MWt except for the five recirculation pump trip test and the turbine trip test. The five recirculation pump trip test was performed on January 27, 1972 just prior to the shutdown for high drywell leakage on January 28, 1972. The turbine trip test is scheduled to be performed just prior to the shutdown for refueling (April 1972). Following the January 28, 1972 shutdown, the effluent cooling water dropped to approximately 350 F, a decrease of 250 F during the shutdown. A sudden change in the weather prior to the shutdown dropped the cooling water temperature approximately 10 F during the two days just prior to the shut-down. Newspapers in the area reported thousands of dead fish as a result of the plant shutdown (C0 Report No. 50-219/72-01).

Records show that the stack release rate, which was approximately 50,000 uCi/second prior to the September 1971 shutdown, decreased during steady state operation af ter the September - November 1971 outage to approximately 40,000 uCi/second, but has since increased to approximately 55,000 uci/second with peaks as high as 142,000 uCi/second after moving control rods (for flux shaping and reactivity control).

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Administration and Organization a.

Parsonnel changes, b.

Plant Operations Review Committee (PORC) meeting minutes July 29, 1971 through February 10, 1972. (except as noted in paragraph 15) c.

General Office Review Board (GORB) meeting minutes and GORB audit reports August 17, 1971 through February 10, 1972.

3.

Operations 'a.

Abnormal Occurrence Records - August 1971 through February 1972.

b.

Plans to examine main steam line flow restrictor sensing lines.

c.

Program for testing torus to drywell vacuum breaker valves.

d.

Records of reactor vessel thermal cycles.

Procedures Small, Leak Detection (No. 515) a.

, b.

Dmergency Diesel Generator Monthly Inspection (No. 726.2) c.

Diesel Generator 20% Plue load Test 5.

Maintenance a.

Modifications to electromatic relief valves.

b.

Plans to replace two control rod drives that failed to insert.

c.

Plans to inspect the baffles in the torus during the April 1972 refueling outage, d.

Installation of a " jockey pump" for the No.1 core spray loop.

e.

Depth of lifting holes in the standby liquid control pump, f.

Off gas isolation circuit, g.

Quality control records for installation of isolation condenser drain valves.

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Quality control records for installation of core spray system check valves.

i. Quality control records for installation of the fifth relief valve in the main steam system.

j. Repairs to the isolation condenser vent line.

k.

Quality control records for the installation of two valves in the poison system.

1.

Modification to the electromatic relief valves.

6.

Surveillance Testing a.

Main steam isolation valve closure time test.

b.

Records of reactor pressure vessel thermal cycles.

c.

Testing of torus to drywell check valve, d.

Emergency service water pumps.

Details of Subiects Discussed in Section I 7.

Violation of LCO No. 1 Containment Spray System and No. 2, EDG Out of Service Simultaneously (Letter, JCP&L to DRL, dated February 22, 1972) The control room log shows that the No. I containment spray system was taken out of service at 8:10 a.m. on January 14, 1972, the No. 2 EDG mode switch was placed in the "off" position at 8:20 a.m., and the No. I con-tainment spray system was returned to service at 9:05 a.m. on January 14, 1972.

Technical Specification paragraph 3.4.C.5 specifies in part, "During the period when one diesel is inoperable, the containment spray loop.... connected to the operable diesel shall have no inoperable components." The No. I containment spray loop is powered by the No. 1 EDG.

This violation was reported to Region I by telephone on January 26, 1972.

A written report was made to DRL on February 22, 1972.

8.

Core Spray Jockey Pump A field inspection showed that JCP&L has completed the installation of a jockey pump (to keep the system filled) on both core spray loops.

(Reference CO Report 219/71-2, paragraph 11). This item is considered complete.

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9.

Reactor Vessel Level Instrumentation (C0 Report 219/71-2, paragraph 20) The A GE/MAC level indicator indicates that water level is approximately 1.3 feet lower than either the B GE/MAC or the Yarway indicators. This was discussed with Mr. Riggle. The two systems were recalibrated completely during the September - November 1971 outage, the difference remains. The venting of the condensing pots was discussed - the pots are not vented.

Mr. Riggle said the problem had been reviewed with tne PORC; however, meeting ' minutes did not confirm this statement. During the exit interview, other members were aware of the problem and agreed that the PORC minutes should have included a discussion of the work on the level indicators, since one of Mr. Ross's engineers had been assigned to investigate the problem and report back to the PORC. The issue is still unresolved.

10.

Isolation Condenser Relay Failure (Letter, JCP&L to DRL, dated September 30, 1971) The relays that failed were initially described as GE CR120 type relays with a time delay addition. This information was provided in a telephone report to Compliance on September 9, 1971 (Inquiry Report 219/71-05). Jersey Central was asked by telephone on February 9,1972 to provide more specific information as to the type of relay replaced. On February 14, 1972, the inspector was told that the relay specifically was a CR122A-09041AA (time delay) relay.

. - - ~ In response to a question as to how the wrong information was provided, Mr. Riggle stated that the CR120 relay was the basic relay and the modification made for Oyster Creek made the relay a CR122A-09041AA. The initial look had just shown the CR120 designation. GE literature describing CR120 and CR122 relay was reviewed; however, the literature did not include a des-cription of the above numbered relay.

Mr. Riggle stated that numerous other CR120 type relays are used at Oyster Creek but no CR120's are used directly in the reactor protection system. CR120's as used in allied systems such as the reactor manual scram indicating lights circuit, scram relay resets circuits, scram di charge volume high level bypass ~ circuit, and condenser low vactum bypass circuit.

11.

09 Concentration in Drywell A temporary TS change dated November 23, 1971 permitted operation at 507 of licensed power with 0 concentration in the drywell - torus greater than 5% for 48 hours untli 2:11 a.m. on November 24, 1971.

(Weather condi-tions and a wreck prevented getting "N2 pumps" to the site within the prescribed 24 hours.)

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- 14 - The control room log showed that the oxygen content of the drywell I decreased to (5% at 1.0:18 a.m. on November 23, 1971 and that reactor power

was at 935 MWt ~ (approximately 48%) until 10:18 a.m.

At that time, a power

increase was initiated using recirculation flow controls. Recorder charts and data sheets for November' 23,1971 verified the entry in the control room log book.

Plans for the installation of permanent equipment at the site for inerting the - drywell and torus were discussed.

Mr. Riggle stated that all of the equip-l ment needed was at the site and was in the process of being installed.

i 12.

Emergency Diesel Generator out of Fuel (Letter, JCP&L to DRL, dated January 5, 1972) The subject failure was discussed with Mr. McKeon and Mr. Carroll, and the equipment involved was inspected. A review of the procedure for the monthly inspection verified that the procedure had been modified to check the fuel oil transfer pumps and to verify that the trouble alarm (for the EDG) , l operated in the control room as was reported in the referenced letter.

In response to a question abouc protective devices on the EDG and the testing calibration of same, 'Ar. McCluskey provided the following in a -

subsequent telephone cal'. ! ! Shutdown devices that are bypasse'd in the fast start mode: ' i a.

Engine temperature high switch " b.

Main bearing oil pressure high switch c.

Main bearing oil pressure low switch , i d.

Overspeed trip limit switch (back up)

e.

Lube oil temperature low switch f.

Low water pressure switch

Devices that unload diesel, open generator breaker and *hrottle diesel back to " idle" speed: g.

1.

No starter pinion engagement

2.

No engine start i 3.

No voltage buildup 4.

Generator overvoltage 5.

No generator circuit breaker closed i Devices that open generator breaker: , h.

Generator breaker relay 1.

Undervoltage relay 2.

Leading vars relay i .

q [ a , /

- _ - - ... O r.

. ' '.. - 15 - ! 3..: Reverse power. relay ~ 4.. Phase-differential relay .5... Engine'overspeed. relay iDevices;that stop;the~ diesel:

1.

Overspeedf trip.on the ' diesel The devices in.g, h and i were fast start' tested during'the annual inspection in September 1971~. The relays for No.1 EDG were calibrated during February '1972 by the JCP&L Relay Department. The relays in No. 2 EDG are scheduled . to be calibrated during Apri1 ~ 1972.

13. Rad Waste Tank Farm Inventory-(Letter, Jersey Central to DRL, dated December 22, 1971)l Technical Specifications limit the inventory to 0.7 C1 (traragraph 3.6.C).

'If 'the limit ui,s exceeded,- TS require reprocessing until the inventory is less than 0.7 Ci.

This limit is exceeded frequently according to the records; however, nor-mally the condition is corrected within a few hours by recycling. As this is an LCO, a written report is required to be sent to DkL. Following the September - November 1971 outage,-larger than normal amounts of liquid rad. waste were-on hand.- When the inventory was calculated beginning No-

vember-14' (calculated Monday-Wednesday-Friday), the limit was exceeded.

This continued'through December'17, 1971. On November 29, 1971, the contents of the tank farm could not be recycled due to the plugging of the L tubes of the waste concentrator and the rapid depletion of the rad waste demineralizer.. Three tank truckloads (3700 gallons each) were transferred to:a licensed carrier for disposal by Nuclear Engineering Company in Kentucky, releases were made to the environment in accordance with the TS, the tubes of the waste. concentrator were drilled out, and the danineralizer was re-l generated. z The inventory was reduced to less than 0.7 Ci on December 20, 1971.

Plant operation was allowed to continue with the verbal concurrence of CO and DRL for the following reasons: a.. Jersey Central indicated.they were doing all possible to get the waste

' concentrator and the demineralizer back in service.

b.

The inventory was being reduced by off plant shipments.

- l I c. - A' reactor ~ shutdown would not have stopped additions to the rad

  • waste system.

j d.

The condition cou.d have been corrected by releases - to the environment Lat the maximum rate permitted by the TS.

. t .

0

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. .. . . .. '. - 16 - It was concluded that the proper action in light of the requirement to keep , releases "as low as practical" was to allow the inventory in the tank farm to renain above 0.7 Ci while the waste concentrator and demineralizer were repaired o* regenerated.

Records show that an inventory is calculated Monday, Wednesday and Friday (TS 4.6.D requires analysis every 72 hours). If the results indicate the limit is exceeded, a report is sent to the shift foreman with recommendation as to the priority of reprocessing the various tanks.

In response to questions by the inspector, Mr. Carroll stated that additional information would be provided to the shift foreman to enable them to reduce the number of violations.

(Previously the shift foremen were not advised of the in- , ventory status until the limit was exceeded.)

14. Loss of 4160 Volt Emergency Bus IC (Letter, JCP&L to DRL, dated March 10, 1972) The reactor control room log showed that the IC breaker opened at 11:45 a.m.,' December 22, and initiated a "1/2 scrmn" on the No. I reactor pro-tection system. The log showed that the electrical system was returned to normal at 12:10 p.m. the same day. The two operators that were on duty when the IC breaker opened were interviewed as were Mr. Carroll and Mr.

Riggle.

While checking circuit continuity for a spare set of current transformers = to be used as replacements for the burned out units associated with the auxiliary transformer, the proper fuses were not removed to isolate the circuit. When a voltage signal was applied to the circuit, protective relay actions occurred that tripped the IC breaker. Emergency diesel generator No. I was initiated in the " fast start" mode and had just re-energized the IC bus when a reclosure of the IC breaker was attempted.

The IC breaker was only closed for a few cycles since the false signal had not been removed; however, during that time, the voltage and frequency mismatch activated the EDG reverse power relay, tripping the unit. As a result, the 1C bus was de-energized for approximately five minutes while the false signal was removed and normal power was being restored to the bus.

The remainder of the twenty-five minutes was consumed in restarting equip-ment.

According to Mr. Riggle, a written procedure was not prepared for check out of the current transformer since written procedures are not specifically required in the area of power distribution. The mechanics involved in the check out pulled the wrong fuses and failed to isolate the circuit.

In response to a specific question, the persons interviewed stated that no consideration was given to shutting down the reactor during the period the IC bus was de-energized. Both emergency buses are required to be energized in TS 3.7.1 (limiting condition for operation - LCO).

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W l.

. 17 - The loss of the 10 bus was investigated by the Plant Operations Review Committee (PORC) on January 13, 1972. A report was prepared and the PORC concluded that the event did not reduce the-availability of power as provided for in the Technical Specifications.

i As a result of this event, the emergency procedure. (No. 502) for Loss of Power was revised. Neither the original procedure or the revised procedure acknowledge the loss of an emergency bus as a violation of a LCO. This subject was discussed during the exit interview.

15.

Plant Operations Review Committee (PORC) Meetings . Meeting minutes show that 18 meetings were held during the period July 1971 to February 1972,' which adequately met the TS requirement (paragraph 6.1.C).

1Two members of the General Office Review Board (GORB) are appointed by the ' . Chairman of the GORB as members of the PORC. The PORC meeting minutes showed that the GORB members ' vere present at two of the meetings during - 'the period July 1971 to December 1971.

(GORB was represented at two of the i-three meetings in 1972.) The TS do not specifically require the GORB

members to be present.

The PORC meeting minutes did not show that the differences in reactor level ' instrumentation had been reviewed by the PORC. The members of the staff

stated during the exit interview that this was an oversight in keeping the minutes. Mr. Ross etated that one of his engineers had been assigned to - - this problem by the PORC.

q 16.

Shift Foreman's Log and Control Room Log Portions of these two logs were read for the period June 25, 1971 through February 27, 1972. The information provided was sketchy. Two noteworthy events were not recorded: a.

the reason for the planned shutdown on January 27,1972 (an increase to 4 gpm in the unexplained leak rate), and i b.

an approximate 150% increase in stack release rate to 142,000 uCi/sec on January 23, 1972 (previous release rate was 50 - 60,000 uCi/sec).

t i This item was discussed with Mr. Carroll and he agreed that more information should be recorded in the two logs. He stated that he had recently discussed this subject with the shift foremen and believed the logs now reflect < better coverage of the plant operation, and he would continue to push for improvement in this area.

l i

r / ..,..

\\ ' * ". - 18 - 17._ Failure of Two Control Rods to Fully Insert -(18-11 and 30-31) -(Letter, JCP&L to DRL, dated January 25, 1972).

Mr..!cCluskey re-affirmed plans to replace the drives for these two rods - during the outage scheduled to start approxLmately April 22, 1972.

Re-built drives will be installed. The two drives will be dismantled.and inspected'after the outage.

18. Stack Release Rates-Release records were reviewed and the stack monitor chart for January 1972 was' unrolled.and inspected. The records show a maximum stack release rate of 142,800 uCi/second for about one hour on January 23, 1972.

'This rate occurred following the return to power fran a runback on ' January 22, 1972 (loss of three recirculation pumps-and one feedwater

pump). During routine level operation, the release rate has been approxi-mately 55,000_uci/second.

The release rate as shown on the stack activity recorder is recorded hourly in counts per second (cps) along with wind speed and direction. The re- ' corder is set to alarm when the cps increase to' the equivalen of 50% of the maximum allowable release rate. An off gas sample is analyzed at least weekly to calibrate the stack monitor. This calibration is used to determine the stack release rate in uCi/second. The rates shown on the attached table are typicil for January - February 1972. ' '" The inspector questioned the lack of any none in the Control Room Log or the Shift Foreman's Log about the increase in release rate to 142,800

uci/second. This type increase is normal following a return to power according to Mr. Carroll, and this was probably why a special note was not made in the log books.

z- , / . -

.. . = _. _, _ . i .*

',..

. c !:- r . Stack Release Rates i(Typical Rates for -January - February 1972) 4. Date'

Release Rate (uCi/cc)

1/5 " 56,700 j - . 1712 40,400 - 1/20 65,100-

1/21-62,500 / Lost 3 "Recirc"'and 1 - ' feedwater pumps '1/22 .136,000

1/23: 142,800 '2/2 43,900 2/8L .55,000 t . . - . 2/16~ 55,400 .2/23-55,400 - , i i . ' - ,

. - ., _

! - . .g ' 3944 May 9 1972 J. G. Keppler, Chief, Reactor Testing & Operations Br.

Regulatory operations, Headquarters RO INQUIRY REPORT No. 50-219/72-12 JERSEY CENTRAL POWER & LIGHT COMPANY OYSTER CREEK ~1 - BWR HUMAN ERROR - FUEL BUNDLE FOUND WITH A 90 MISORIENTATION The' subject inquiry report is forwarded for your information.

Our preliminary review of this matter, which included the licensee's FSAR, disclosed that operation with fuel assembly misorientations of i 90 are lass severe in consequences than the analyzed case involving , 1800 misorientations. We believe the licensee's intended course of j action is appropriate.

We vill continue to follow this matter and keep you informed as appropriate.

In addition, our inspector will review this matter, as well as any noncompliance aspects, during the next site inspection.

.Ww The licenses will submit a written report (10-day) to RL.

J l l , R. T. Carlson Senior Reactor Inspector Enclosure: Subject Inquiry Report

cc: E. G. Case, RS (3) R. S. Boyd, RL (2) R. C. DeYoung, RL (2) D. J. Skovholt, RL (3) j H. R. Denton, RL (2) , Regional Directors, RO j R0 Files DR Central Files , L. Kornblith, RO-l ' R. H. Engelken, RO E.

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c. _... . -. . .. -. - -. ~. . - - - , .. . ~. .. . -.. P .. > t 3 i 'l RO Inquiry Report No. 50-219/72-12 i ! -t

+ - Subj ect : - Jersey Central Power'& Light Company .

License Not DPR-16 ' i Facility; Oyster Creek-1 ' BWR - , . , Title: Human Error - Fuel Bundle Found with a 90 Misorientation= ' l j i ' Prepared by: l l T. Young,.Jr., Reactor Inspector Date.

] i l A.

Date & Manner AEC was Infot1ned:

By telephone call from Mr. Tom McCluskey, Station Superintendent, on , ' i Hay 8, 1972 I i a B. ' Description of Particular Event or Circumstance: During the current outage while performing fuel sipping operations, , one fuel bundle (25-08) was found in a position of 90o misorientation.

  • i

. This bundle was last handled on October 31, 1971. OC-1 procedures call l for a verification of fuel bundle orientation before vessel head closure, i-l' This check was made by T.V., recorded on film, and the film was reviewed.

j j A subsequent _ review of the. film on May 8, 1972, clearly showed'the bundle . with the 900 minorientation.

!rue., t l C.

Action by Licensee:

1.

The licensee is making an analysis of the consequences of operating with i .the fuel bundle in the 900 misoriented position.

!

i 2.

A visual inspection of the bundle will be conducted.

. 3.

A 10-day written report will be made to RL.

t i i i ! , .

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. _ _ _ _.. __ _ .. _.. I

3944' MnY 81972 , .

J. G. - Reppler, Chief, Reactor Testing.& Operations Br.

Regulatory Operations, HQ RO INQUIRY REPORT No. 50-219/72-11 JERSEY CENTRAL POWER & LIGiff COMPAIN OYSTER CREEK - BWR EQUIPMENT FAILURE - LOOSE BAFFLES IN TORUS The subject inquiry report is forwarded for your infomation.

.This inspection was made in response to a written request from RL, and the inspection results will be reported in writing to RL as re-quested in their letter.

We plan to review this matter during the next site inspection.

%ey R. T. Carlson Senior Reactor Inspector Enclosure: Subject Inquiry Report cc: E. G. Case, RS (3) R. S. Boyd, RL -(2) R. ' C. DeYoung, RL (2) D. J. Skovholt, LRL (3) 11. R. Denton, RL (2) L. Kornblith, RO R.11.' Engelken, RO Regional Directors, RO RO Files DR Central Filen 3 3G-S3 l--M .1 L / . OFFICE >.L ......, ,,, .[. .i ... .J. .... . , . Spes s'ard: smg Carlson t , , .SURNAMEp- ,. . . . . . .. ' ,c,i15/8/72 " ~ ' ~ " " rurm di'!Euiuvis 4, ~ a r.s w muo.o mico...o un '" ' ' ' ~ ' > ,

.___ _ _ _.-

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RO Inquiry Report No. 50-219/72-11 ? ! Stbjects-Jersey Central Power & Limht Company i License No.: DPR-16 i Facility:: Oyster Creek - BWR

'. Title: Equipment Failure -'140se Baffles in Torus Prepared by: T. Young, Jr., Reactor Inspector Date i .

I

A. - Date end Manner AEC was Informed: '~

By telephone call from Mr. Tom McCluskey, Station Superintendant, at

11:40 a.m.

on May_4, 1972.

, i B.

Description of Particular Event or Circtanstance: ? An inspection of the torus during the current outage disclosed that five d bafflee were loose and laying on the floor of the torus; two baffles in ! the area of one downcomer and three in the area of a second downcomer.

> The 3/8" bolts that hold the baffles in place were broken.

C.

Action by Licensee: l The inspection of the torus is continuing and the licensee is evaluating his findings. A written report will be made to DRL.

.

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-. .- . ~. .- . - -.. - - .-. . - - .. s i .1-(Q l- . ' APR 2 419E , ,

1 ~ J. G. Keppler, Chief, Reactor Testing & Operations Br.

-Division of Compliance, HQ CO INQUIRY REPORT No. 50 219/72-10 .: JERSEY CENTRAL POWER & LIGHT COMPANY OYSTER CREEK - BWR . .CPIHER - LABOR PROBLDiS RESULTING IN A DELAY OF THE SCHEDULED REFUELING OUTAGE The subject inquiry report is forwarded for your information.

The full implication of the subject issue is not apparent at this = time,~but from the information we have received from the licensee, it appears they plan to take a firm stand against the use of the construction craft union to perform the turbine overhaul.

, ' . We plan to follow developments closely and will keep you advised . as is appropriate.

Misji R. T. Carlson ~ Senior Reactor Inspector . Enclosure:

Subject Inquiry Report cc: E. G. Case, DRS (3) ! R. S. Boyd, DRL (2) R. C. DeYound, DRL (2) ' D. J.-Skovholt, DRL (3) i-H. R. Denton, DRL (2) i L. Kornblith, CO

R. H. Engelken, CO CO Files DR Central Files - @Y ,pti o o o s O .Lg.

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- -. .. . -. - - . -.. ... - -.. - .. -. --- -- - ..... - - ! O

CO Inquiry Report No. 50-219/72-10 , Subject:' Jersey Central Power & Light Company ] Licensa No.1 DPR-16 i ! l Facility: Oyster Creek - BWR l I Title: Other - Labor Prob 1sas Resulting in Delay of Scheduled Refueling Outage I i j i j Prepared by . j F. S. Centrell, Jr., Reactor Inspector Date , .'! A.

Date and Manner AEC was Informed: , I d By telephone call from Mr. T. J. McCluskey, Station Superintendent, to -

the inspector lswatel at 9:00 pm on April 21, 1972.

! l B.

Description of Particular Event or Circumstance: i

Mr. McCluskey stated that the refueling outage scheduled to start at , ' i 10:00 pm on April 21, 1972 had been pettponed due to a breakdown in ' , l labor negotiations between JCP&L, the International Brotherhood of ' Electrical Werkers (IBEW), which represents Oyster Creek's hourly

! i empicyees, and the local' construction trade unions. According to ' ' Mr. McCluskey, JCP&L entered into a contract with a New Jerry firm

We,J,1 to perfoss the turbine overhaul using local iebor * Ger.w:ist Electric supervision. The local labor would belong to the IBEW.

, I The local construction trade union previously objected to the use of , ! outspde CE employees for the turbine overhaul and established a picket ' li$ttheplantsite(InquiryReport 50-219/71-07, October 23, 1972).

, Contrary to their understanding, JCP&L was informed on April 21, 1972 i that if the construction trade unionsestablished a picket line around ' the plant, the IBEW anployees would honor the picket line.

Information ! available i.o JCP&L indicated a picket line would be established on j j April 24, 1972.

i

C.

Action by Licensee: i l JCP&L elected to continue operation for another week while labor nego-

tiations continued.

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3944 ppp g.j - . .-

- J. G. Keppler, Otief, Reactor Testing & Operations Br.

Division of Compliance, BQ CO INQUIRY REPOKr NO. 50-219/72-09 JERSEY CENTRAL POWER & LICHT CWPANY OYSTER CREEK - BWR EQUIPMENT DEFICIENCY - CRACKS IN SAFETY VALVE SEAT BUSHING The subject inquiry report is forwarded for your action, since the problen may be generic. We understand that facilities _ equipped with ' this type valve include Dresden 2 and 3 Quad Cities 1 and 2 Tsurugs and Nuctenor.

(M111st Jue 1 was ' originally scheduled to have this type valve; however, 8 hey subsequently changed to a combination safety / relief valve - Target Rock.)

-Jersey Central appears to be waiting for the results of GE metallurgical analysis prior to making any further coments as to what direction their progem will take.

We plan to follow this matter closely and will keep you informed of 44J siedequent developments, es is appropriate.

R. T. Carlson Senior Reactor Inspector Enclosure: Subject Inquiry Report (18 cys) . cct L. Kornblith, CO R. H. Engelken, CO < C0 Files

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_. _ _ _. _ _ ._.. __ _ _ _ _. _ __ __. , , i . , !.g

l CO Inquiry Report No. 50-219/72-09 . ! Subject: Jersey Central Power & Light Company i License No.: DPR-16 , ,, : * Facility: Oyster Creek - BWR Title: Equir-aat Deficiency - Cracks in Safety Valve Seat Bushing ,

Prepared by: F. S. Centre 11, Jr., Reactor Inspector Date i A.

Date and Hanner AEC was Informed: By the Station Superintendent, Mr. T. J. McCluskey, during a special i inspection at the site on April 21, 1972.

B.

Description of Particular Event or Ciretsnatances ,

j During the September - Noveder 1971 outage, five safety valves were ! replaced with five clean tested spara valves. The plans were to test 'the five valves removed using nitrogen; however, a correlation betwoon

testing with cold nitrogen and hot steam was not availabia. As a result, it was necessary to send the valves to tie manufacturer's shop for testing a and to detemine the correlation between cold nitrogen and hot staan for

! future testing. Efforts to decontaninate the valves to suitable levels f for shipement to the manufacturer's shop (less then 2 mR/hr) 1 pere un-successful until the valve seat bushing was unscrewed from the valve , body.. When initial decontamination efforts on the seat bushing of the ! , first valve were unsuccessful, a dye check showed radial cracks en

the seat and a circumferential crack approximately 4.4 inches from the - j base, at a point where the wall thickness completed the transition from j 1.4 inches to 0.75 inches.

It was necessary to grind to a maximum J depth of 0.12 inches to remove the circumferential crack (Atte % t No. 1).

. n Without any further attempt to decontaminate, the seat bushing was removed from the second valve and was dye checked. Cracks were detected at the sane locations as in the first valve examined. In addition, +

.

several vertical cracks about 1/2 inch long were noted about ten j inchs above the base (The point at which water could have been standing if the valves were cold).

<

The remaining three valves were disassembled and dye checked but did not show the crack indications found on the first two valves.

. e e m n fl d .v. fQ O )t,,O V V " 3l0f-i . . .., . . .

. i

-2-

We subject valves are Dresser "Maxiflow Safety Valves", Model 6-3777QA, with a six inch inlet and an eight inch outlet (Attachment 2). We seat bushing is ASTM A182, Guide F304 stainless _ stool. The base (or valve housing) is ASTM A216, Guide WCA carbon ' ' ' steel.

C.

Action by Licensee: The valve seat of the second valve was shipped to General Electric, San Jose, California by air freight for metallurgical analysis, on April 20, 1972. The results are currently being evaluated by General Electric.

Ten safety valve repair kits were ordered from GE (all that were available) to use in replacing cracked seats.

'4 The General Office Review Board (CORB) held a special meeting on April 21, 1972 to review the scheduled turbine trip test in light of the cracks , found in the safety valves. The GBRB approved the test as scheduled.

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