05000272/LER-1981-075-03, /03L-0:on 810809,containment Fan Coil Unit 13 Declared Inoperable Due to No Svc Water Flow Indication. Caused by Equipment Failure.Flow Transmiter FA-3543Z-1 Sensing Line Blown Clear & Transmitter Recalibr

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/03L-0:on 810809,containment Fan Coil Unit 13 Declared Inoperable Due to No Svc Water Flow Indication. Caused by Equipment Failure.Flow Transmiter FA-3543Z-1 Sensing Line Blown Clear & Transmitter Recalibr
ML20010F158
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/28/1981
From: Dickey F
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010F150 List:
References
LER-81-075-03L-01, LER-81-75-3L-1, NUDOCS 8109090441
Download: ML20010F158 (1)


LER-1981-075, /03L-0:on 810809,containment Fan Coil Unit 13 Declared Inoperable Due to No Svc Water Flow Indication. Caused by Equipment Failure.Flow Transmiter FA-3543Z-1 Sensing Line Blown Clear & Transmitter Recalibr
Event date:
Report date:
2721981075R03 - NRC Website

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EVENT OESCR.PTION AND PROB ABLE CONSEQUENCES h g l On August 9, 1981, the control room operator noticed that there was no service water j (CFCU). The CFCU was declared l

g ) flow indication on No.13 containment fan coil unit 3.6.2.3.a was entered at 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br />, August 9, 1981.j

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