ML19347F144
| ML19347F144 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 05/08/1981 |
| From: | Sarsour B TOLEDO EDISON CO. |
| To: | |
| Shared Package | |
| ML19347F138 | List: |
| References | |
| NUDOCS 8105150321 | |
| Download: ML19347F144 (5) | |
Text
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AVERAGE DAILY UNIT POWER LEVEL 50-346 DOCKET NO.
UNIT Davis-Besse U #1 May 8, 1981 DATE Bilal Sarsour COMPLETED BY TELEPilONE (419) 259-5000 Ext.251 MONTil April, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe Net) 801 0
I 37 0
2 828 gg 0
3 769 g9 0
4 549 20 408 0
5 21 375 0
6 22 0
0 7
23 0
0 8
24 0
0 9
25 0
0 10 26 O
390 II 27 0
789 12 28 0
850 13 29 0
881 14 30 0
15 3l 0
16 INSTRUCTIONS On this format.hst the average daily und power leselin MWe. Net for each day in the reporting month. Compute to the nearest whole nwgawatt.
(9/771 l
8105150 %
OPERATING DATA REPORT DOCKET NO.
DATE May 8, 1981 COMPLETED BY @Bilal Sarsour TELEPilONE m 259-5000 Ext.
~
251 OPERATING STATUS Davis-Besse Unit #1 Nots April, 1981
- 2. Reporting Period:
2772
- 3. Licensed Thermal Power (SIWr):
925
- 4. Nameplate Rating (Gross $1We):
906
- 5. Design Electrical Rating (Net SIWE):
934
- 6. Maximum Dependable Cap.1 city (Gross SlWe):
890
- 7. Maximum Dependablu'apacity (Net SlWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
~
- 9. Power Level To Which Restricted. If Any (Net S!We):
- 10. Reasons For Restrictions.If Any:
This Month Yr.-to Date Cumulative 719 2,879 32,188 II. Hours in Reporting Period 269.5 1,731.7 16,115.9
- 12. Number Of flours Reactor Was Critical 0
34.8 2,916.9
- 13. Reactor Reserve Shutdown llours
- 14. liours Generator On Line 240.8 1.593.4 14,641.2
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0 0
1.731.4
- 15. Unit Resene Shutdown llours 509,t05 3,743,803 30,648,609
- 16. Gross Thermal Energy Generated ISlWil)
- 17. Cross Electrical Energy Genented ISIWif >
170,048 _,_,
1,250,814 10.226,148 155,299 1,165,669 9,430,170
- 18. Net Electrical Energy Generated (SIWil)
- 19. Un;t Senice Factor 33.5 55.3 46.1 33.5 55.3 51.9
- 20. Unit Availability Factor
- 21. Unit Capacity Factor IUsing alDC Net) 24,3 45.5 34.7
- 22. Unit Capacity Factor (Usir:g DER Net) 23.8 44.7 34.1 7.0 34.1 25.8
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Oser Next 6 Stonths (Type. Date.and Duration of Each t:
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status Irrior o Commercial Operation):
Forecast Achiesed INITIA L CRITICA LITY INITIAL ELECTRICITY CO%l%IERCIAL OPER ATION (9/77i L
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50-346 DOCKET NO.
Davis-Besse U #1 UNIT SHUTDOWNS AND POWL:t REDUCTIONS UNIT NAME DATE Mav 8 I381 4
i COMPLETED BY Bilal Sarsour TELEPilONE (419) 259-5000 Ext.251
{
REPORT MONT!!
April, 1981 l
I 1
e s
E 4._. 3 l U""S##
5%
o"3 Cause & Correetive c
r.
c=
$3 Action to No.
Date E.
k _$
?ge Event g,7 g.
B3 C
E co Prevent Recurrence z
Report a mv g
ac ;5 =g o=
e O
5 81 04 04 S
0 A
NA NA NA NA Reactor Power was reduced to 50%
due to an indicated increase in c
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the steam generator tube Icak.
6 81 04 06 S
460.0 A
NA NA NA NA A planned shutdown was initiated to repair the SG tube leak.
7 81 04 26 F
18.2 A
1 NA CH NA The Reactor was tripped following e
a full SFRCS trip T
,O (See operational sumary for Q
further details)
C
- C Q@
8>
P 3
4 l
2 Method:
Exhibit G instructions F: Forced Reason:
1 Manual for Preparation of Data S: Schedu!cd A Equipment Failure (Explsin)
B. Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee 3-Automatic Scram.
Event Report (LER) File (NUREG-C-Refueling 0161)
D-Regulatory Restrictiam I~. Operator Training a l_icense Examinstion 4-Continuation 5
l F-Administrative 5-Reduction Exhibit I - Same Sourec.
G-Operaiional Estor (lixplain) 6-Other ty??)
it-Other (lisplain)
April, 1981 DATE:
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REFUELING INFORMATION_
Davis-Besse Nuclear Power Station Unit 1 1.
Name of facility:
March, 1982 Scheduled date for next refueling shutdown:
2.
May, 1982 Scheduled date for restart following refueling:
3.
hi l
Will refueling or resumption of operation thereaf ter require a tec n caIf a specification change or other license amendment?If answer is no, has the rel 4.
in general, will these be?
i w Committee and core configuration been reviewed by your Plant ~ Safety Rev e i
d with
- to determine whether any unreviewed safety questions are assoc ate the core reload (Ref.10 CFR Section 50.59)?
1981. No Reload analysis is scheduled for completion as of December, d nts identified technical specification changes or other license amen me to date.
a ting
__ Scheduled date(s) for submitting proposed licensing action and suppor 5.
January, 1982
.inforention.
Important licensing con'siderations associated with refueling, e.g., new or l
i different fuel design or supplier, unreviewed design or performance ana 6.
d res.
methods, significant changes in fuci design, new operating proce u None identified to date.
a fuel The number of fuel assemblics (a) in the core and (b) in the spent 7
storage pool.
44 - Spent Fuel Assemblies 8 - New Fuel Assemblics (a) 177
_ (b)
- l f any The present licensed spent fuel pool storage capac 8.
j
/
in number of fuel assemblies.
0 (zero)
Increase size by_
735 Present The projected datc of the last refueling that can be discharged to the fuel pool assuming the present licensed capacity.
9.
k fuci 1988 (ansuming ability to unload the entire core into the spent Date pool is maintained)
OPERATIONAL
SUMMARY
APRIL, 1981 4/1/81 - 4/5/81 The reactor power was maintained at approximately 90% with the turbine generator gross load at 835 + 10 MRe, until 1225 hours0.0142 days <br />0.34 hours <br />0.00203 weeks <br />4.661125e-4 months <br /> on April 4, 1981 when the reactor power was reduced to 50% due to an indicated increase in the steam generator tube leak which was detected on March 23, 1981.
4/6/81 - 4/24/81 The reactor power was maintained at 50% until 2323 hours0.0269 days <br />0.645 hours <br />0.00384 weeks <br />8.839015e-4 months <br /> on April 6, 1981 when a planned shutdown was initiated to repair the steam generator tube leak.
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4/25/81 The reactor was critical at 0729 hours0.00844 days <br />0.203 hours <br />0.00121 weeks <br />2.773845e-4 months <br />.
4/26/81 The turbine generator was synchrcnized on line at 0327 hours0.00378 days <br />0.0908 hours <br />5.406746e-4 weeks <br />1.244235e-4 months <br />.
Reactor power was slowly increased to 17% until the morning of April 26, 1981 when a feedwater transient was experienced.
While stroking main feed block valve for the #2 side, startup feedwater valve went fully closed due to excessive leakage through the main feedwater control valve. The main feedwater block valve was then manually closed to stop the leakage, how-ever, the startup feedwater valve could not respond quick enough to open and ensure adequate flow to the #2 steam genera-tor. A full Steam and Feedwater Rupture Control System trip occurred on low steam generator level which caused an antici-patory reactor trip on a turbine trip.
The reactor returned to criticality at 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br /> on April 26, 1981.
The turbine generater una synchrcnized on line at 2306 hours0.0267 days <br />0.641 hours <br />0.00381 weeks <br />8.77433e-4 months <br />.
4/27/81 - 4/30/81 The reactor power was slowly increased and attained 99% full power on April 30, 1981.
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