ML18102A643

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Insp Repts 50-272/96-15 & 50-311/96-15 on 960915-1102. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support
ML18102A643
Person / Time
Site: Salem  PSEG icon.png
Issue date: 12/03/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102A641 List:
References
50-272-96-15, 50-311-96-15, NUDOCS 9612090265
Download: ML18102A643 (50)


See also: IR 05000272/1996015

Text

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Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/96-15, 50-311/96-15

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

September 15, 1996 - November 2, 1996

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

T. H. Fish, Resident Inspector

E. B. King, Physical Security Inspector

E. H. Gray, Project Manager

Larry E. Nicholson, Chief, Projects Branch 3

Division of Reactor Projects

9612090265 961203

PDR

ADOCK 05000272

G

PDR

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EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272/96-15, 50-311 /96-15

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support.

Operations

Operators* isolated service water to an available emergency control air compressor.

Operators missed several opportunities to identify the degraded condition. The operations

corrective action staff performed an inadequate evaluation of the occurrence and failed to

identify that operators ran the emergency control air compressor without service water

(SW) cooling (Section 02.1 ).

Inspectors discovered that operators used informal methods to control valve manipulations,

and an incorrect procedure revision to perform charging pump performance testing.

Operators also performed procedure steps out of sequence when removing a vital bus from

service, did not adhere to the alarm response procedure for the no. 1 station air

compressor, and did not document degraded equipment condition. Operations managers

initiated appropriate corrective measures in each of the above circumstances, however,

poor operator performance in procedure adherence and use remains an NRC concern

(Section 04. 1 ) .

Due to inadequate preparation and incomplete system knowledge, operators did not

anticipate depressurizing the no. 4 SW header. In response, the operators failed to follow

procedures to restore pressure, and prevented safety related equipment from automatically

functioning to mitigate the pressure loss. Instead, they restored pressure through

application of inappropriate. procedures and use of SW support systems in an unevaluated

manner. The operator performance and the initial corrective action was poor (Section

04.2).

The LERs and supplements identified in Section 08.13 identify 26 Technical Specification

(TS) related problems exemplary of a programmatic failure. Taken collectively, they form

the basis for concern regarding the adequacy of Salem procedures and controls to assure

compliance with TS requirements. The PSE&G initiative to identify and correct similar

deficiencies via the Technical Specification Surveillance Improvement Project (TSSIP)

indicates a positive attitude toward corrective action. Notwithstanding, the adequacy of

procedures and controls, as identified in NRC restart inspection item 111.3 remains to be

resolved (Section 08. 13).

Maintenance

Operators and technicians accomplished a carefully controlle~ test of the Salem Unit 2

phase "A" containment isolation valves. They precisely recorded the minor discrepancies

observed during the test. The plant staff did not thoroughly insure resolution of

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disagreement between plant design and Technical Specification 3.6.3 requirements for

  • valves 2CV68 and 2CV69.(Section M1 .2)

Engineering

The Salem Steam Generator Replacement Project staff demonstrated effective control of

planning and transportation of the steam generators (Section E1 ). The inspectors

considered the corrective action taken to date to resolve concerns with the Emergency

Diesel Generator Air Start System acceptable. The Salem staff produced a thorough and

technically sound resolution for this restart issue.

Engineering acknowledged continued station air and control air deficiencies, however, they

did not affect corrective measures to ensure reliable operating performance (Section E8.1 ).

Plant Support

Radiation Protection took prompt and appropriate action in response to contamination

found outside the radiologically controlled area (Section R2.1 ).

The Salem Unit 1 steam generators met most of the requirements for an SCO class II

shipment. The contamination level on the channel head and tube sheet areas appeared to

be above the DOT limits and the steam generators were not packaged into IP~2 containers.

Accordingly, the licensee applied for exemption to these requirements, which were

subsequently approved by the DOT.

Security personnel complied with the requirements of the security plan for access control

in response to door alarms. Although security supervisors and managers might have been

more aggressive in implementing compensatory measures and initiating maintenance

efforts, the inspectors did not find any degradation of access control (Section S2.1).

During receipt of replacement steam generators, Salem security staff properly and

effectively implemented compensatory measures associated with temporary changes to the

perimeter intrusion detection systems, and protected area barrier. Additionally, the

inspector determined that measures were in place to ensure proper restoration of the

barriers and intrusion detection systems as required by the approved security plan (Section

S8.1).

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TABLE OF CONTENTS

EXECUTIVE SUMMARY

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TABLE OF CONTENTS .............................................. iv

I. Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

16

Ill. Engineering

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

IV. Plant Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

28

V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 42

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Report Details

Summary of Plant Status

Unit 1 and Unit 2 remained defueled for the duration of the inspection period.

I. Operations

01

Conduct of Operations

01 . 1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations are detailed in

the sections below.

01.2 (Update) LER 50-311196-009 : fourteen day follow-up report regarding 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

shifts for operations personnel. This Licensee Event Report (LER) identified a

conflict between Salem's practice of 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> work shifts for operations personnel

versus an Operating License requirement of 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shifts. PSE&G presently utilizes

this work schedule for operations personnel at the Hope Creek plant and the Hope

Creek Technical Specification (TS), Section 6, permits that practice. PSE&G has

submitted* a Licensing Change Request to address this issue for Salem and is

tracking a commitment to resolve this issue with the NRC prior to entering Mode 2.

The inspector found the resolution to this specific licensing condition issue

satisfactory.

Part of the corrective action for this LER required PSE&G to review all Salem Unit 2

license conditions to verify they have been, or are being satisfied.

The inspector

learned that a report was being prepared to document the review and the results

but the final report was not available at the time of the inspection. This LER will

remain open pending review of the final report.

02

Operational Status of Facilities and Equipment

02.1

Emergency Control Air Compressor Control, NRC Restart Items Ill. 7 and 111.10

(Open)

a.

Inspection Scope (71707)

b.

The inspector reviewed the Salem corrective action in response to an operator-

identified near miss involving the no. 2 emergency control air compressor (ECAC).

Observations and Findings

On September 26, 1996, in preparation for starting no. 2 ECAC, the Unit 2 reactor

operator (RO) reviewed the off-normal Tagging Request and Inquiry System (TRIS)

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report in accordance with S2.0P-SO.CA-0001, Control Air System Operation. The

RO identified that technicians had previously tagged out essential service water

(SW) supply valves to the ECAC on September 13, 1996. The operator placed the

no. 2 ECAC in manual to prevent an automatic start and initiated a corrective action

request (AR 960926067).

Operations management preliminarily attributed the root cause of the tagged SW

valves to a tagging process deficiency. An Operations Planning and Scheduling

Senior Reactor Operator (SRO) reviewed the SW tagout and failed to identify the

impact on no. 2 ECAC. Operations staff believed that the no. 2 ECAC was in

automatic when equipment operators (EO) tagged the SW valves on September 13

and remained aligned without SW cooling until September 26. They believed that

operators did not run the ECAC during this period. On September 27, the station

management team assigned a significance level 1 condition resolution (CR) to AR

960926067, requiring plant staff to complete a root cause investigation within 3.0

days.

Early in the evaluation, the operations reviewer determined that this event had

similarities to 18 other tagging events subject to a level 1 root cause evaluation

initiated in January 1996 (960109205).

On day 26 of 30, the specialist had

completed a one page justification that this event did not require a separate root

cause evaluation. He planned to present the justification to station management on

day 27 of 30. As a result of this conclusion, the reviewer had not identified several

conditions adverse to quality. The inspector noted that the "specialist" assigned to

perform the root cause analysis had not completed the PSE&G root cause training,

and had never performed a level 1 root cause analysis.

Based on independent review, the inspector identified the following facts not found

as a result of the root cause:

On 9/2 and 9/12, the Operations Planning and Scheduling SRO approved a

SW tagging request (103109) that isolated cooling to the no. 2 ECAC. The

SRO failed to identify that the no. 2 ECAC remained available to start

automatically on low air header pressure.

Unit 2 operators placed no. 2 ECAC in manual at 5: 11 a.m. on September

13, in preparation for a no. 2C vital bus outage. Fortuitously (due to the

vital bus outage), the ECAC was unavailable prior to tagging the SW valves

on September' 13.

On 9/15, following restoration of no. 2C vital bus the operators ran no. 2

ECAC for six minutes without cooling water available. The operator did not

insure the availability of SW to cool the ECAC, as required by S2.0P-SO.CA-

0001.

On 9/16, prior to removing no. 1 station air compressor (SAC) from service,

operators verified valves 2SW401 and 2SW119 open to ensure SW available

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to no. 2 ECAC. They did not identify that upstream SW valves (2SW300

and 2SW90) were tagged and isolated SW to the ECAC.

Procedures SC.OP-AP.ZZ-0107, Revision 3, Shift Turnover Responsibilities,

step 3.7.1 and S2.0P-D2.ZZ-0014, Revision 4, Shift Routines, step 5.14.2

require the RO to review the Tagging Request Inquiry System off-normal

report. From September 13 to September 26, no RO identified that 2SW300

and 2SW90 were tagged closed.

On October 24, the inspector presented the above observations and findings to

station management. Operations management promptly provided additional

guidance on procedure compliance and management expectations concerning less

than adequate operator performance to all operators. The engineering staff

determined that running the no. 2 ECAC for six minutes without SW cooling did not

adversely affect the ECAC. Operations management maintained the ECAC CR as a

level 1.

The inspector determined that the tagged SW valves and operators failure to

identify the condition in a timely manner resulted in running the ECAC without SW

cooling and increased outage risk. From September 17-19, both ECACs and two

out of three SACs were unavailable. SC.SA-AP.ZZ-0055, Outage Risk

Management, requires a contingency plan for this degraded condition. Failure to

identify and take prompt and appropriate actions to correct conditions adverse to

quality is a violation of 10 CFR 50, Appendix 8, Criterion XVI (VIO 50-272&311 /96-

15-01 ).

Conclusions

An alert operator prevented operation of the no. 2 ECAC without cooling water. He

identified that several barriers to insure cooling water had failed. In response to the

identified failure, the plant staff did not effectively implement the corrective action

program. As a result, the reviewers did not identify that operators had previously

run the compressor for six minutes without cooling water. In addition, the

reviewers did not identify that operators missed several opportunities to identify

that the compressor remained available to start automatically without available

cooling water.

02.2 (Closed) LER 50-272/96-011: pressurizer safety relief valves found outside of

technical specifications limit. The TS requires the relief valve lift point to be within

plus or minus 1 percent of the set point. Three of the pressurizer relief valves failed

this requirement during testing. The deviations were plus 1.28, 1.32, and 3.90

percent. The inspector reviewed documentation that verified the valves were

refurbished and successfully retested. The inspector reviewed the approved root

cause analysis for this event and found it acceptable. The corrective actions

resulting from this are either complete or are being tracked to completion by

Performance Improvement Number 960621244. The inspector considered the

corrective actions appropriate. This LER is closed.

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04

Operator Knowledge and Performance

04.1

Procedure Use and Adherence

a.

Inspection Scope (71707)

b.

The inspector observed control room activities to ensure operators adhered to

approved procedures and that procedures were of the correct revision, useful, and

complete.

Observations and Findings

During the inspection period, the inspectors observed daily operator activities to

assess operator use and adherence to procedures. The Salem operators typically

used approved procedures to control equipment manipulations, responses to alarms,

and other safety related activities. The operators appropriately used procedures and

closely adhered to the procedures in most instances. The inspectors noted that in

the following examples, however, operators did not adhere to procedures.

On September 18, 1996, Unit 2 operators conducted S2.0P-PT-CVC-0002,

Charging Pump Flow Test. The inspector observed that operators did not sign off

each procedure step as they completed it. Subsequently, the reactor operator

documented all completed steps in the procedure. In addition, the operators used a

"post-it" note attached to the procedure to control closing two valves

(2SJ12/2SJ13). Operators closed the valves during shift turnover to preclude

gravity fill of the refueling cavity from the refueling water storage tank. The

Operations Manager directed operators to annotate the control room narrative log to

indicate operator action, reason for action, and senior reactor operator concurrence

when conducting activities not specifically covered by procedures. The inspector

determined that the 2SJ 1 2/2SJ 13 narrative log entry provided adequate control for

the closed valves. The inspectors considered operator use of informal control of

plant equipment an example of poor performance.

On October 1, 1996, the inspector found that Unit 2 operators performed

approximately half of procedure TS2.0P-PT.CVC-0002, Troubleshooting on 21 or

22 Charging Pump With Temporary Modifications of Plant Configuration, without

noting that it contained a combination of revision 0 and revision 1 . The Unit 2 SRO

promptly stopped the troubleshooting activity and initiated a CR report (CR

961002063). The SRO found that the operators missed an independent verification

of an instrumentation alignment as a result of the mixture of procedure revisions.

Operators subsequently performed the independent verification and found the

instrumentation properly aligned. The inspector noted that the operating shift did

not demonstrate a questioning attitude when presented several opportunities to

identify an incorrect procedure revision. The inspector considered the lack of

attention to detail an additional example of poor operator performance.

On October 21, 1996, the inspector observed that, when removing the no. 1 C

460V/230V vital bus from service, the RO performed procedure S1 .OP-S0.4KV-

0003, 1C 4KV Vital Bus Operation, step 5.2.4 before performing step 5.2.3. The

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RO and SRO determined that they should reverse the sequence to protect plant

equipment. The inspector concluded that no immediate threat to equipment existed

and the operators proceeded without using an approved method to change the

procedure. The inspector noted that performing the steps out of sequence resulted

in an additional 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> without the no. 1 emergency control air compressor, 1

hour without no. 11 and no. 12 service water pumps, and 40 minutes without no.

1 C emergency diesel generator. The reduced availability did not impact plant safety

due to the Unit 1 condition (shutdown and defueled). Operations management

counseled the RO and SRO concerning procedure adherence. Operators submitted a

request to change S1 .OP-S0.4KV-0003 to provide additional equipment protection.

Failure to adhere to procedures for control of safety related equipment is a violation

of TS 6.8.1 requirements (VIO 50-272&311/96-15-02).

On October 23, 1996, personnel in Unit 1 turbine building reported a high water

level in separator alarm on no. 1 SAC. The EO informed the RO that he performed

the steps in the alarm response procedure (ARP), and could not resolve the problem.

The SRO and RO recalled previous problems with the drain line clogging and that

cycling the drain valves closed then open again had successfully cleared the

blockage. The SRO directed the EO to cycle the drain valves. The EO cycled the

drain valves and reported that the alarm cleared. The inspector observed that,

although not specified by the alarm response procedure, the EOs routinely cleared

the alarm by cycling SAC valves 11SA1 5 and 11 SA 17 to dislodge corrosion

products from the drain lines. They did not initiate an AR to document the plugged

drain line on those occasions. In addition, the operators did not place another

compressor in service, and no. 1 SAC in manual, when they could not control

separator water level, as required by procedure SC.OP-AR.SA-0001, Revision 5,

Station Air Compressors Control And Alarm Panel. On October 23, 1996, the

inspector presented the above observations to the Senior Nuclear Shift Supervisor

(SNSS). *As of October 24, the operating shift did not initiate an action request (AR)

to document the degraded SAC piping, or the ARP non-compliance. This is an

additional example of failure to identify degraded plant conditions.

Conclusions

In most cases during daily plant activities, operators closely adhered to procedures.

Inspectors discovered that operators used informal methods to control valve

manipulations, and an incorrect procedure revision to perform charging pump

performance testing. Operators also performed procedure steps out of sequence

when removing a vital bus from service, did not adhere to the alarm response

procedure for the no. 1 station air compressor, and did not document degraded

equipment condition. Operations managers initiated appropriate corrective

measures in each of the above circumstances, however, poor operator performance

in procedure adherence and use remains an NRC concern.

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  • 04.2 Service Water (SW) Bay Depressurization, NRC Restart Items Ill. 7 and 111.10.1

(Open), Inspector Follow-up Item 50-272 and 311 /96-12-02 (Closed)

a.

Inspection Scope (92901 l

The inspector evaluated corrective actions for an operator-induced SW bay

depressurization.

b.

Observations and Findings

On September 3, 1996, Unit 2 operators closed 22SW17, SW pump discharge

header crossover valve, in preparation for 21SW17 valve maintenance. Due to the

SW system alignment, closing the 22SW17 resulted in no. 4 SW bay

depressurization. Within an hour, operators restored no. 4 SW bay pressure and

reopened the 22SW17. Operators cross-connected the SW nuclear headers in the

auxiliary building prior to closing 22SW17 and did not expect to depressurize no. 4

SW bay. Operators did not account for a SW check valve that prevented flow

backward from the auxiliary building to the SW bay. Cross-connecting the SW

nuclear headers in the auxiliary building prevented depressurization of the no. 22

SW nuclear header and resulted in no safety consequence. The Unit 2 SRO initiated

a CR report (960903068). The inspector considered the item open pending

operations' completion and NRC review of corrective actions .

On October 16, 1996, operations staff completed an apparent cause evaluation.

The evaluator attributed the apparent cause to control room crew failure to use

procedure S2.0P-SO.SW-0005, Service Water System Operation, or SW system

drawings for guidance in closing 22SW17 and ensuring adequate SW flow to no. 4

SW bay. He noted that failure of the Planning and Scheduling Group to consider

the 22SW17 closure a complex evolution and the resulting lack of special

instructions in the maintenance tagging request ( 10481 2) a contributing cause.

He

also identified the failure of the control room crew to follow the ARP for overhead

annunciator (OHA) B-24 (no. 24-26 SW pumps low bearing cooling pressure) a

contributing cause. The B-24 OHA ARP directed operators to open 22SW250 to

restore bearing cooling, however, operators opened both 21 SW250 and 22SW250

to re-pressurize no. 4 SW bay. The operations staff concluded that the SW bay

depressurization had no safety significance due to the plant condition (shutdown

and defueled with no. 2 SW bay supplying both nuclear headers), and since the

control room crew took immediate action to restore no. 4 SW bay pressure.

Operations management took corrective action for human performance deficiencies.

The Operations Department newsletter emphasized the need for personnel to

comply with procedures. Operations supervision planned to provide all Operations

Department personnel a copy of the Apparent Cause Report as required reading to

reinforce management expectations regarding station operating practices. In

addition, they planned to provide additional instructions on 22SW17 tagging

requests.

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Inspectors found that apparent cause evaluation by the operations staff overlooked

or failed to address a number of significant concerns. These included:

The Unit 2 operator, after closing the 22SW17, took no. 24 SW pump out of

automatic as SW header pressure started to decrease. The operator believed

that SW pressure would stabilize and did not want an automatic pump start

(pump auto starts at 95.5 psig). The automatic pump start would have

prevented no. 4 SW bay depressurization.

Operators did not comply with OHA 8-14 ARP. When the bay depressurized,

OHA 8-14 ARP directed operators to abnormal procedure S2.0P-A8.SW-

0001, Loss of Service Water Pressure. Procedure S2.0P-A8.SW-0001 step

3.5 directs the operator to start a service water pump to restore pressure.

Operators did not start a service water pump to restore pressure.

The on-shift SRO was not familiar with the availability of safety related

equipment. He stated that the degraded condition of the no. 4 bay pumps

(pumps 24, 25, 26) prevented operators from placing these pumps in

service. Contrary to his belief, SW pumps no. 24 and no. 26 SW were

available and no. 24 SW pump was in automatic when the operators closed

22SW17.

Operators did not fully understand operation and design of the SW system .

The Unit 2 operator and NSS did not anticipate that 24" check valve 24SW5

would prevent SW flow from the pressurized auxiliary building nuclear

headers back to the no. 4 SW bay. Several operators stressed the

importance of providing SW for no. 24 SW pump motor upper bearing

cooling. The upper bearing is air-cooled and needs no SW supply. In

addition, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after bay depressurization, the SRO did not know if any of

the no. 4 SW bay pumps were in automatic prior to 22SW17 closure.

Operators did not realize that they connected the Unit 2 SW system to the

Unit 1 SW system. The operating shift reviewed Unit 1 and Unit 2 SW

system prints and created a method to re-pressurize the SW bay through the

21 SW250 and 22SW250. These valves are normally locked closed and

operated individually under abnormal conditions, to provide alternate SW

pump bearing cooling. Although OHA 8-24 ARP directed-operators to open

only the 22SW250, operations opened 21 SW250 and 22SW250 in an

attempt to re-pressurize the bay. The SRO and RO stated that they knew

that the 8-24 ARP directed opening only the 22SW250, however, they

considered the bay re-pressurization a priority. The inspector identified that

opening the 21 SW250 and 22SW250 placed the SW system in an

unanalyzed condition.

Operators did not adequately document the transient in control room

narrative logs. The logs stated: Closed 22SW17, no. 4 bay depressurized to

11 psig, opened 21 and 22SW250s. Re-opened 22SW17, no. 4 bay re-

pressurized, closed 21 and 22SW250s."

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On September 10, plant staff used special tagging instructions to control

22SW17 closure. The inspector noted, however, that no controls exist in

maintenance procedures, the tagging process, or operating directives to

ensure that operators use these special tagging instructions in the future for

similar valve strokes that impact plant operation.

The inspectors concluded:

Some operators involved did not understand the requirements for procedure

adherence, as required by TS 6.8.1.

Operators inappropriately allowed the perceived urgency to restore SW

header pressure to override their safety focus. Even with no. 4 SW bay

depressurized the SW system continued to supply adequate cooling for plant

conditions (shutdown and defueled). Operators had no reason based on

plant or worker safety to deviate from procedure requirements.

Operations and plant managers did not insure appropriate or timely corrective

action. It took 7 days to initiate a significance level 2 CR. Once assigned as

a level 2, the evaluator took 36 days to complete the evaluation. Licensee

procedure NC.NA-AP.ZZ-0006, Corrective Action Program, states that

management expects that evaluators complete level 2 evaluations within 30

days .

The Condition Resolution evaluator was not qualified to determine the cause

or corrective action for the inappropriate operator performance. He had very

little operations experience and less than one year experience at the Salem

station.

PSE&G failed to identify and evaluate operator action taken to disable

automatic actuation of a safety-related component during an operational

transient. Failure to identify and correct conditions adverse to quality is a

violation of 10 CFR 50, Appendix 8, Criterion XVI "Corrective Action"'

requirements (VIO 50-272&311 /96-15-01 ).

On October 24, the inspectors discussed the above observations and findings with

station management. Operations management acted promptly to address corrective

action program concerns. A significance level 1 CR was initiated on the adequacy

of operations corrective action process (961025129) and issued a Standing Order

was issued on performance of fact-finders following significant events. (SOD-96-

122). On October 28, the operations manager issued a memorandum to all

personnel concerning procedure use and adherence, and detailed the many

operations shortcomings over the inspection period (see sections 02.1, and 04.1 ).

The memorandum provided candid self-assessment and focused lessons learned.

The October 24 Standing Order directed operations personnel to perform the

following steps for all human performance errors that result in the issuance of a CR:

c.

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(2)

(3)

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Notify one of the four senior operations department representatives,

assemble a fact finding team, and

interview involved individuals prior to end of shift and before individuals

leave site.

The inspector noted that the Standing Order provided adequate interim guidance,

however, it did not adequately ensure a long-term solution to operations'

performance weaknesses. Reliance on four personnel does not ensure appropriate

operating shift response during operational transients and provide real time safety

focus twenty-four hours a day. On October 29, Unit 2 operators attempted to start

no. 21 containment spray pump. The pump did not start because.the pump's 125

VDC control power breaker was open and its 4KV breaker was racked down. The

operating shift identified human performance issues and initiated a CR

(961029270), however, contrary to management's expectations the fact finding

team did not interview involved individuals before individuals departed the site. In

addition, the involved SNSS and SRO were members of the fact finding team. The

inspector noted that this approach, similar to the initial 22SW17 fact finding, did

not contain sufficient independence.

Conclusions

Due to inadequate preparation and incomplete system knowledge, operators did not

anticipate depressurizing the no. 4 SW header. In response, the operators failed to

follow procedures to restore pressure, and prevented safety related equipment from

automatically functioning to mitigate the pressure loss. Instead, they restored

pressure through application of inappropriate procedures and use of SW support

systems in an unevaluated manner. The operator performance and the slow and

ineffective corrective was cause for concern. Although plant staff initiated the

corrective action process, the resulting apparent cause investigation failed to

identify multiple operator performance problems. In addition, the corrective action

process did not involve the appropriate levels of management. As a result, the

initial corrective actions were incomplete and ineffective. Plant managers

implemented measures to address the performance deficiencies and to insure

appropriate management involvement in future operator performance problems.

(Closed) LER 50-311195-001: manually initiated engineered safety feature actuation

to effect a main steam isolation signal in order to increase reactor coolant system T-

avg above 541 degrees (F). While reducing power, operators allowed the reactor

coolant system Tavg to decrease below the TS minimum value, 540.5 degrees

versus 541 degrees (F). The operators responded by initiating a manual main steam

isolation from the "Safeguards" bezels to increase Tavg. The operators were able

to return Tavg above the TS minimum value in approximately one minute, well

within the 15 minutes allowed by TS 3.1.1 .4.

The inspector determined that this event was minor and did not constitute a

violation of NRC requirements. This LER is closed.

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07

Quality Assurance in Operations

07 .1

Operating Experience Feedback (OEFJ, NRC Restart Inspection Item 111.9 (Closed)

Inspectors previously reviewed the OEF effectiveness in NRC Inspection Report 96-

06. The inspector did not close the NRC Restart Inspection item as a result of

discrepancies between the requirements of procedure NC.NA-AP.ZZ-0054(Q),

Operating Experience Program and actual program implementation. The inspector

reviewed NC.NA-AP.ZZ-0054(Q), Revision 4, dated 10/24/96 and determined that

plant staff had effectively revised section 3.8, responsibilities of the General

Managers, Salem and Hope Creek to reflect the actual practice. In addition, the

inspector reviewed the OE program response to NUREG CR-6245, NUREG 1522,

and Westinghouse Owners Group recommendations for EOPs. The inspector

considered the OE program treatment of these items appropriate. The NRC Restart

item is closed:

08

Miscellaneous Operations Issue

08.1

(Closed) Unresolved Item 50-272 and 311 /92-12-01: EO log falsification. The issue

remained open pending resolution of EO tour conduct and security card system

effectiveness. Salem Quality Assurance (QA) conducted frequent assessments of

EO conduct and log-taking. Quality Assurance inspectors stated that EOs

demonstrated good performance in this area. Security supervisors determined that

no deficiency existed within the security key card system. The NRC inspector

reviewed station QA Surveillance Report 92-666, conducted over the period

September 16, 1992 - September 21, 1992, and concluded that QA appropriately

determined that equipment operators conducted proper rounds and security key

card readers functioned as designed. The inspector frequently reviewed EO logs

and observed EO tours. The inspector found no evidence of EO misconduct and

observed that the security key card system functioned to record access information.

This item is closed.

08. 2

(Closed) Unresolved Item 50-27 2 and 311 /93-21-03: potential technical

specification noncompliance due to solid state protection system (SSPS) train B in

operability. Operators had indications that SSPS train B did not function properly,

however, they failed to pursue those indications in a timely manner commensurate

with the potential safety consequence. This is a violation of 10 CFR 50 Appendix B

Criterion XVI, Corrective Action, requirements. Since the NRC has taken significant

enforcement action for Salem's failure to identify and correct conditions adverse to

quality, and since PSE&G voluntarily maintained both Salem units shut down to

address equipment and enforcement deficiencies, the NRC will not take additional

enforcement action in these cases. In particular, Salem management took extensive

measures to retrain all licensed operators to improve plant knowledge, operator

performance, and safety culture. This item is closed.

08.3 (Closed) Violation 50-311/94-06-01: failure to comply with TS for power operated

relief valves (PORVs). Operation's management determined that inadequate

procedural guidance directly attributed to the TS noncompliance. The inspector

I

I

08.4

11

reviewed PSE&G's response to the violation and determined that the licensee took

appropriate corrective actions. The inspector verified that the licensee completed

the associated TS amendment and operating procedure changes addressed in their

response letter. This violation is closed.

(Closed) Violation 50-272&311 /94-80 (EA 94-112-03013): loss of control room

command and control. The control room senior reactor operators (SNSS, NSS) did

not maintain appropriate command and control of the reactor at all times.

Management took actions to improve shift supervisory personnel performance,

especially with regard to control room leadership. Management reinforced

command and control expectations through written guidance, shift training, and

control room observations. In particular, Salem management took extensive

measures to retrain all licensed operators to improve plant knowledge, operator

performance, and safety culture. The inspector reviewed shift guidance provided

through Night Order Book entries and observed SROs at the training center and in

the control room. The inspector concluded that management affected significant

improvements in SRO performance relative to command and control. The NRC

restart inspection issue will address any additional issues of command and control

prior to restart. This violation is closed.

08.5 (Closed) Unresolved Item 50-272&311 /94-13-02: repeated entry into Technical

Specification LCO. This item remained unresolved pending inspector review of the

details of previous SA-118 valve manipulations. T.he inspector could not

substantiate any TS 3.6.3.1 noncompliance associated with opening SA-118. The

inspector discussed repeated entries into TS LCOs with operations personnel and

concluded that personnel maintained an appropriate safety awareness to such

potential LCO abuse. This item is closed.

08.6 (Closed) Violation 50-272&311 /95-07-01: control room emergency air conditioning

system TS noncompliance. Operations management determined that the Nuclear

Shift Supervisor and Nuclear Control Operator failed to properly verify redundant

channel operability and failed to adequately maintain administrative control of

inoperable control room instrumentation. The licensee initiated actions to improve

procedural guidance, control room console log TS references, and TS tracking. The

inspector verified that operations revised console logs to provide appropriate TS

references and implemented a TS tracking log. The inspector determined that the

licensee took appropriate corrective actions. This violation is closed.

08. 7

(Closed) Deviation 50-272&311 /95-07-02: concurrent testing of redundant

emergency diesel generators (EOG) during normal plant operation. Operations made

procedure changes to prohibit operation of more than one EDG paralleled to the

electrical grid at any one time. This practice is consistent with Regulatory Guide

1.108 recommendations. The inspector verified that operations revised the

associated EDG procedures for both units to preclude concurrent testing of the

EDGs. This deviation is closed.

e.

A

.

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12

08.8 (Closed) Follow-Up Item 50-272&311 /94-19-01: definition of controlled leakage.

08.9

08.10

08.11

Salem TS defined controlled leakage as " ... seal water from the reactor coolant

pump seals." This definition differed from other Westinghouse plants TS that

defined controlled leakage as " ... seal water to the reactor coolant pump seals."

The Salem staff addressed this issue through a TS amendment that eliminated the

term controlled leakage and established a new TS that limits seal injection flow

rather than seal leakoff flow. The NRC approved the amendments October 30,

1995, and the inspectors confirmed Salem staff implemented the amendments in

station procedures. This item is closed.

(Closed) Unresolved Item 50-311/94-08~01 : steam generator depressurization

during simulator scenario. NRC examiners observed operators perform a simulator

scenario that involved steam generator depressurization. During the exercise, the

Emergency Operating Procedures (EOPs) directed the operators to depressurize an

intact steam generator by opening its associated atmospheric steam dump.

Although the crew performed this step, they first shut all main steam isolation

valves (MSIVs), an action not in the step. Subsequently, the examiners questioned

operator compliance with the EOP step. The noncompliance did not constitute a

violation, however, because the operators were operating the simulator, not the

plant. The examiners also questioned the technical adequacy of the EOP step

because an unmonitored release could occur if operators used atmospheric steam

dumps instead of available main condenser steam dumps .

Salem staff addressed the procedure compliance aspects of this item through

operator requalification training. In addition, NRC Restart Issue Ill. 7, Operator

Performance, also addresses procedure adherence as well as other generic aspects

of operator performance. The staff addressed EOP technical aspects through a

major revision to the EOPs (NRC Inspection Report 96-08 has details), including the

steps that give operators direction on steam generator depressurization and whether

to close the MSIVs. The inspectors determined the revisions were adequate and

that the operators completed training on the revised procedures. This item is

closed.

!Closed) Violation 50-272&311 /96-05-01: failure of Offsite Safety Review

(OSR) and Onsite Safety Review Group personnel to meet the number and

qualification requirements of Technical Specification 6.5.2.2. The inspector

determined the corrective actions described in PSE&G's response letter,

dated May 22, 1996, were acceptable. This item is closed.

(Closed) Violation 50-27 2&311/95-17-01 : failure of electricians to reinstall

tags. This item concerned a maintenance activity where electricians

removed a red-tagged 460 volt breaker from its cubicle, but failed to reinstall

the tags on the breaker racking device handle. In response, Salem staff

revised the tagging procedure to clarify tagging requirements, and to restrict

moving red blocking tags to Operations personnel only. The inspectors

determined Salem operators implemented the revised procedure. This item is

closed.

I

08.12

08.13

13

(Closed) Violation 50-272&311/96-08-01: failure of plant staff to update the

Tagging Request Inquiry System (TRIS). This item concerned two examples

where operators repositioned valves but did not update TRIS to reflect the

off-normal position. In response, Salem staff initiated a TRIS training course

for operators and limited TRIS system use to those qualified on the system.

The inspectors verified Salem staff implemented TRIS training and that only

operators qualified on TRIS can update the system. This item is closed.

Review of Licensee Event Reports related to Technical Specification

Implementation

a. Inspection Scope

The inspectors reviewed the following LERs to determine whether the licensee took,

or planned to take, appropriate corrective action to resolve the issues. The

inspectors also assessed adequacy of the licensee response to the events, and

determined if the licensee complied with regulatory requirements.

Unit 1

Number

LER 95-004

LER 96-003

LER 96-004

LER 96-005

Event Date .

May 15, 1995

February 20, 1996

March 7, 1996

March 25, 1996

Description

Unacceptable approach to

determine containment air

temperature for TS requirement

TS radiation monitor sampling non-

compliance

Containment isolation valve missed

TS surveillance

Failure to perform channel checks

for Tavg as required by TS

Note : LER 96-005, Supplements 1. through 5 to documented additional TS related

incidents identified by the Salem Technical Specification Surveillance Improvement

Program (TSSIP)

LER 96-006

April 21, 1996

LER 96-007

May 24, 1996

Missed independent verification of

release lineup on waste gas decay

tanks required by TS

Engineered Safety Feature

Actuation System (ESFAS) above

TS value

'

14

LER 96-008

June 13, 1996

Failure to meet TS requirement

while in Mode 5 for natural -

recirculation

LER 96-016

July 19, 1996

Missed surveillance for residual

heat removal pump dynamic head

prior to entering Mode 4

LER 96-017

July 25, 1996

Missed surveillance for plant vent

flow

LER 96-022

September 1 2, 1996

Containment radiation monitor

setpoints not in accordance with

technical specifications

LER 96-023

August 22, 1996

Surveillance for MSIVs not

performed prior to entry into Mode

3 as required by TS

LER 96-024

August 28, 1996

Surveillance requirement not met

for time response of motor driven

auxiliary feedwater pumps

Unit 2

LER 95-007

May 3, 1995

Missed diesel surveillance required

by TS

LER 95-008

December 15, 1995

Missed verification of containment

isolation as required by TS

LER 96-001

January 9, 1996

Failure to perform chemistry

sampling within TS required time

frame

LER 96-002

July 1, 1996

Waste gas decay tank oxygen

concentration exceeded TS limit

LER 96-003

May 15, 1996

Failure to perform surveillance for

fuel handling building ventilation

system auto start

LER 96-004

May 15, 1996

Missed TS action statement,

compensatory survey

LER 96-005

June 27, 1996

Missed TS surveillance of fuel

I

handling building ventilation

system charcoal

6

I

15

LER 96-007

July 16, 1996

LER 96-010

August 19, 1996

Missed TS surveillance of

containment penetration over-

current protection device

Missed TS surveillance for two

pressurizer welds

Inspectors selected these LERs for a collective review because each involved some

degree of failure to implement TS requirements. The inspector also reviewed the

Salem Technical Specifications Surveillance Improvement Program (TSSIP) scope,

and reviewed related TSSIP documents provided by PSE&G.

b. Observations and Findings

Salem Unit 2 LER 95-008 discussed the TSSIP. The licensee initiated the program

due to previous LERs that indicated a weakness in TS compliance. The program

consists of two stages of implementation. The licensee designed the first stage to

improve TS surveillance testing administrative controls, and to assure adequate

scheduling and tracking of surveillance requirements. The TSSIP first stage also

validates that implementing procedures contain adequate purpose statements and

adequately maintained and updated acceptance criteria. In the TSSIP second stage,

Salem staff plans to review applicable licensing and regulatory basis and design

documents to verify the technical adequacy of TS surveillances. The licensee

required completion of the first stage of TSSIP prior to restart. The plant managers

targeted completion of the second stage for late in 1997.

To date, TSSIP has identified many problems; some have resulted in LERs listed

above. The inspector reviewed thirty deficiency documents initiated as a result of

the TSSIP. The inspector found examples of the following problems:

Some TS surveillance requirements had no implementing procedure.

In some cases, TS surveillance procedures had inadequate purpose and/or

acceptance criteria.

Operating procedures did not adequately reference TS surveillances required

for the associated plant conditions.

Scheduling or tracking mechanisms did not assure TS surveillance

implementation.

In some instances, procedure revisions inappropriately deleted TS

surveillance requirements.

Some Technical Specification surveillance requirements existed for features

not installed in the plant.

Personnel errors resulting in missed TS surveillance.

The inspector reviewed the TSSIP charter and scoping document. The program

included plans to evaluate and enhance station processes, administrative

procedures, and controls that govern the TS program. Plant staff intends to review

the TS surveillance cross reference matrix to verify that implementing procedures

I

16

exist for all TS requirements. The inspector found the program provided a

comprehensive and thorough approach to resolving the problems identified.

The inspector's review of the LERs did not identify new problems or problems that

would not be resolved by effective implementation of the TSSIP. The inspector

considered the licensee responses to the individual events adequate. Since the

licensee implemented acceptable corrective actions for each of the identified

problems the LERs identified above are closed.

The inspector determined that Unit 1 LERs95-004, 96-007, and 96-023; and Unit 2

LERs96-003 and 96-007, described examples of problems that the second stage of

the TSSIP is designed to identify and correct; that is, they are examples of design

information not adequately captured by TS implementing documents.

The

inspectors concluded that, prior to Salem Unit 2 restart, the NRC should assess the

acceptability of the basis for not completing the second phase of TSSIP in

conjunction with NRC restart inspection item 111.3, Procedure Adequacy and

Adherence.

c. Conclusions

The LERs and supplements identified in Section (a) above identify 26 TS related

problems exemplary of a programmatic failure. Taken collectively, they form the

basis for concern regarding the adequacy of Salem procedures and controls to

assure compliance with TS requirements. The PSE&G initiative to identify and

correct similar deficiencies via the Technical Specification Surveillance Improvement

Project (TSSIP) indicates a positive attitude toward corrective action.

Notwithstanding, the adequacy of procedures and controls, as identified in NRC

restart inspection item 111.3 remains to be resolved.

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

a.

Inspection Scope (62707)

The inspectors observed all or portions of the following work activities:

Unit 2 WO 960712062:

No. 22 fuel handling building exhaust

filter/replace charcoal filters

Unit 2 WO 960912219:

No. 22 component cooling water pump - correct

oiler size

Unit 2 WO 950407193:

service water bay station air filter replacement

The inspectors observed that the plant staff performed the maintenance effectively

within the requirements of the station maintenance program.

I

b.

17

Inspection Scope (61726)

The inspectors observed all or portions of the following surveillances:

  • *

S2.0P-ST.DG-0003:

S2.0P-ST.DG-0001:

2C diesel generator surveillance test

2A diesel generator surveillance test

The inspectors observed that plant staff did the surveillance safely, effectively

proving operability of the associated system.

M1 .2 Testing of Containment Isolation Valves

Inspection Scope (71707)

The inspectors reviewed the surveillance procedure to determine compliance with

Technical Specification requirements. In addition, they observed the test to verify

that Salem staff performed it in accordance with the procedure, that plant

equipment operated as designed, and that plant staff appropriately documented the

test results.

Observations and Findings

Operators proceeded carefully and deliberately during the test. The Senior Nuclear

Shift Supervisor and the Salem Unit 2 Nuclear Shift Supervisor conducted a test

brief that included operators and technicians. Operators held up start of the test to

make several changes to the procedure for clarity.

The procedure had two other problems previously identified by plant staff. It

permitted Salem operators to perform the test in mode 5 (shutdown), mode 6

(refueling) and defueled. Technical Specification 4.6.3.2 requires that plant staff

perform the test in mode 5 or mode 6. Although Salem Unit 2 remained defueled at

the time of the test, Salem managers decided to do the test to determine if the

isolation valves functioned as designed after the extensive outage activities. Plant

staff also identified that the test procedure did not verify that valves 2CV68 and

2CV69 close on a phase A isolation signal. The staff changed the procedure to

note that it tested the phase A isolation valves with the exception of 2CV68 and

2CV69. In addition, PSE&G submitted a license change request to remove

Technical Specification Table 3.6.-1, Phase A Containment Isolation Valves, out of

the Technical Specifications and into the Updated Final Safety Analysis Report. The

NRC had not approved the LCR at the time of the test, and approval of the LCR will

not resolve the conflict between the TS and the plant design. Inspectors observed

that the operators and technicians carefully conducted the test and precisely

documented the minor equipment discrepancies.

In response to identifying that 2CV68 and 2CV69 did not receive a phase "A"

isolation, the plant staff did not thoroughly insure resolution of the discrepancy

between plant design and NRC requirements. Until questioned by the inspector, the


1

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18

plant staff did not insure that they would demonstrate the operability of valves

2CV68 and 2CV69 as required by Technical Specification 3.6.3.

Conclusions

Operators and technicians accomplished a carefully controlled test of the Salem Unit

2 phase "A" containment isolation valves. They precisely recorded the minor

discrepancies observed during the test. The plant staff did not thoroughly insure

resolution of disagreement between plant design and Technical Specification 3.6.3

requirements for valves 2CV68 and 2CV69.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 (Closed) LER 50-311 /96-008: inoperable battery chargers due to manufacturing

discrepancies. The inspectors did not identify any failures to meet regulatory

requirements. The inspector verified, by a documentation review, that the

deficiencies have been corrected for Unit 2 and the corrective action implementation

documents are being tracked for Unit 1 . The licensee completed reporting required

by 1 OCFR21. This LER is closed.

M2.2 (Closed) LER 50-272/96-009: potential common mode failure for 4KV Magna-Blast

breakers. This event was the subject of an NRC inspection in June 1996. That

inspection was documented in Inspection Report 50-272&311/96-07. No new

issues were revealed by the LER. This LER is closed.

MS

M8.1

Miscellaneous Maintenance Issues

(Closed) LER 50-272/95-013: On July 3, 1995, Instrumentation and Controls (l&Cl

technicians performed TS 4.3.3.3.1 surveillance requirements approximately 6.5

hours late. Technicians satisfactorily completed TS 4.3.3.3.1 and demonstrated

continued operability of the instruments. The licensee attributed the occurrence to

personnel error. The l&C TS surveillance coordinator did not understand

surveillance tracking codes and the Station Planning and Scheduling Group failed to

adequately review the TS surveillance schedules. The licensee human-factored the

surveillance tracking codes, identified clear responsibilities for TS tracking, and

established. a station Planning and Scheduling Group TS coordinator.

The inspector reviewed the TS tracking codes and discussed TS surveillance

tracking with the surveillance coordinator. The licensee took appropriate actions to

prevent recurrence. Failure to perform the required surveillance within the

appropriate interval is a violation of TS 4.3.3.3.1. This licensee identified and

corrected violation is being treated as a non-cited violation, consistent with section

Vll.B.1 of the NRC Enforcement Policy.

M8.2 (Closed) LER 50-272/95-018: improper range gauges used for inservice testing. In

July 1995, QA inspectors identified that inservice testing (IST) technicians did not

use properly ranged gauges for pump testing. The licensee identified this deficiency

I

19

as a violation of TS 4.0.5 in that IST technicians did not test certain components in

accordance with ASME Section XI requirements.

The licensee attributed the root cause to less than adequate IST program

maintenance, implementation processes, and associated controls. On July 31,

1995, QA issued a stop work order for all IST surveillance testing. On December

12, 1995, QA lifted the stop work order, specifying interim work controls until IST

made needed procedure revisions to IST controlling documents. The licensee

conducted an assessment of the entire IST program and implementing procedures

and identified numerous deficiencies, however, the deficiencies did not constitute

reportable conditions. The licensee planned to revise the IST manual prior to

restart.

The inspector reviewed the licensee's IST program assessment. The licensee

initiated appropriate corrective actions. The licensee-identified violation of TS 4.0.5

requirements is being treated as a non-cited violation, consistent with Section

Vll.B.1 of the NRC Enforcement Policy.

M8.3 (Closed) Unresolved Item 50-311194-14-01: Flange Leak Repair Root Cause

Analysis

In July, 1994, the licensee attempted to perform an inservice temporary leak repair

for Unit 2 on a small steam leak from a flange joint on a one inch pipe connected to

No. 22 reactor coolant pump seal. During the repair, the leak quickly increased to

14 gallons per minute. The leak was unisolable, so the workers terminated the

repair. Personnel exited the containment, and the operators proceeded with a

reactor coolant system (RCS) cooldown to cold shutdown as required by Technical

Specification 3.4.7.2. Inspectors *concluded that operators and management

responded appropriately to the event, and subsequently implemented an acceptable

flange repair. Inspectors considered the problem unresolved pending NRC review of

the licensee's root cause investigation.

The inspector reviewed the root cause analysis and considered it satisfactory. The

analysis conclusion stated that loss of the joint preload over the 1 5 year service life

combined with the increased internal pressure on the flange face from the leak

repair sealant injection caused the sudden increase in leakage. The root cause

analysis also specified corrective action that included procedure changes and

contingency plans. The inspector reviewed procedure SC.MD-GP.ZZ-0188(Q),

lnservice Temporary Leak Repair, Revision 0, dated April 28, 1996 and found that it

satisfactorily addressed actions to prevent potential problems similar to those

encountered during the failed leak repair. This item is closed.

E1

a.

b.

20

Ill. Engineering

Conduct of Engineering

Inspection Scope (50001)

Inspectors reviewed the steam generator replacement project (SGRP) to obtain an

overview of current and planned work, related procedures, documentation, quality

inputs and progress of the Salem Unit 1 SGRP. This inspection included

.observation of the replacement steam generator (RSG) staging area, walking the

haul routes for both the RSGs and old steam generators (OSG) with the responsible

engineers and observation of conditions inside the containment building.~ Inspection

on October 29, 1996, focused on the analysis, planning and controls on piping

stress related to the SGRP process. It included ASME Code related inspection of

the project and the oversight (self-assessment) process.

Observations and Findings

By October 29, 1996, the four RSGs had been prepared for shipment at the

Seabrook site, transported by barge to the Salem plant, offloaded and moved to the

RSG staging area. The primary and secondary sides of each steam generator were

maintained under a nitrogen inert gas purge until the start of nozzle machining to

minimize material degradation. Work in the RSG staging area and preparations in

the containment building were observed to be proceeding in an orderly manner with

appropriate supervision and work control packages. A walkdown of the OSG and

RSG haul paths with the responsible reviewing engineers indicated that

consideration had been given to potential haul route problems and related factors.

The inspector reviewed the licensee stress analysis considerations given the steam

generator and its related piping system to ascertain conformance with ASME Code

requirements. The review resulted in the following observations:

The "spring back" of the piping to the OSG was small (0.022-0.038") when

the reactor coolant piping (RCS) was cut loose from the first steam

generator. This movement, when coupled with the relatively low level of

jacking force present during cutting, indicates that significant piping loads

have not been exerted on OSGs during operation.

The inspector observed the computer-based locating equipment used in

matching the steam generator nozzles with corresponding pipe system

attachment such that stresses due to welding of the pipe to the nozzles

would not require excessive cold springing of the pipe. This locating system

is state-of-the-art and has been used successfully in other critical alignment

applications. Alignment of multi-nozzle components with this system allows

precision adjustments to be made that satisfy all locations simultaneously.

Consideration has been given to the weld shrinkage in computing the

dimensions and alignment of the matching parts.

21

The stresses resulting from installation of the RSGs are limited to a small

fraction of the ASME Code operational levels. Conservative analyses have

been performed by the licensee to show that the effect of the loadings on

the RSG shell is small.

Independent design reviews scheduled include the feedwater and RCS

thermal hydraulic modifications, haul path, and an overall 10 CFR 50.59

project review.

c.

Conclusions

E2

The inspections found a generally high level of project performance in the areas

inspected and identified no safety significant project deficiencies.

Engineering Support of Facilities and Equipment

E2.1

NRC Restart Issue 11.5 - Moisture in the Emergency Diesel Generator Air Start

System (Open Unit 1 , Closed Unit 2)

The EOG Air Start System has a history of repetitive maintenance problems that

PSE&G has attributed to rust entrained in the system. This includes problems such

as leaking drain valves and check valves. In addition, the air receivers had a low air

pressure alarm setting of 90 psig, yet past testing indicated that a least 140 psig is

required for successful start testing. The NRC documented these problems in

Inspection Report 50-272,311/94-19, dated October 12, 1994. The licensee has

initiated a significant redesign of this system to reduce or eliminate these and other

operating problems, and to replace obsolete components and parts. PSE&G

submitted this change to the NRC pursuant to 1 OCFR50.90, and the NRC accepted

this alternate design in a letter dated March 21, 1996.

a. Inspection Scope

The inspectors reviewed the closure package that had been reviewed and accepted

by the Salem Management Review Committee. The package identified six Design

Change Packages (DCPs) for implementation on Salem Unit 1 and 2. The inspectors

reviewed the DCPs to determine the scope of the design and to identify related

procedural changes necessitated by the design changes. The inspectors reviewed

the work orders and toured the EOG rooms to determine the status of

implementation of the DCPs. The inspectors also reviewed the test results for

testing performed on the Salem Unit 2 EDGs following implementation of the design

changes. Finally, the inspectors sampled related procedures to determine if the

required changes had been incorporated.

b. Observations and Findings

The inspectors considered the scope of the design change extensive. In addition to

resolving the problems identified by the NRC, PSE&G addressed other maintenance

and operational problems that they had experienced with the Air Start and Turbo

22

Boost systems. For example, the redesign added replacement compressor

start/stop pressure switches to improve setpoint stability and eliminate unwanted

relief valve lifting. Also, they replaced obsolete model EDG air start motors with a

newer model used at Diablo Canyon. PSE&G considers the newer model an

improved design.

The scope of the six DCPs includes:

1 EC-3533 and 2EC-3456

1.

Installs improved Starting Air and Turbo Boost Compressor

pressure control switches.

2.

Installs flexible hose to isolate the switches from compressor

vibration.

1 EC-3387 and 2EC-3335

1 .

Adds an air receiver low air pressure alarm with a 182 psig

setpoint.

1 EC-3401 and 2EC3349

1 .

Replaces all air receiver drain valves with stainless steel ball

valves.

2.

Upgrades piping and valves between the Air Start and Turbo

Boost compressor and receiver tanks to stainless steel.

Eliminates the air dryers and provides moisture separators.

3.

Increases air receiver relief valve setpoint and replaces relief

valves.

4.

Upgrades piping and components between air receiver and air

start motors to corrosion resistant materials. Adds flexible

connections in the system piping at the EDGs to isolate the

system from engine vibration.

5.

Upgrades air start motors and pressure regulators to a newer

design.

6.

Upgrades inlet check valves to a soft seat design for improved

leak tightness. A pulsation damper was added to the Turbo

Boost compressor discharge to prevent check valve chatter

(The Air Start compressor is already equipped with this

device).

The engineers identified procedure changes required as a result of the DCPs. The

inspectors sampled three procedures identified in 2EC-3349 and found that plant

staff had incorporated the required changes. For 2EC3456, the inspectors verified

that plant staff revised the pressure switch calibration data sheets to reflect new

setpoints. The implementing work orders were also included in the DCPs. The work

order documentation indicated that plant staff completed the work for Unit 2 and

had not completed the work for Unit 1. The inspectors performed a field walkdown

of the Air Start and Turbo Boost System and confirmed that the licensee had

completed modification installation for Unit 2. Inspectors also confirmed that a

significant amount of work still remained to complete the Unit 1 modifications.

23

The inspectors determined that DCP-2EC3349, Package #1, contained test

procedure STP-3349-001, Special Test Procedure, designed to verify that all

affected portions of the 2A Diesel Generator Air Start and Turbo Boost Air systems

function properly following the modifications. The inspectors verified that Package

  1. 2 and #3 contained similar procedures for the 2B and 2C systems. The test

procedures included component functional tests for valves, switches and

instruments, as well as integrated start tests to demonstrate the ability of the EDG

to start and come up to speed within 10 seconds. The inspectors reviewed the

completed test results for the 2A, 2B, and 2C systems and found that the

acceptance criteria had been satisfied.

From discussions with the system manager, the inspectors learned that the work

reduced system air leakage, reduced air compressor run time, and that blowing

down the air receivers yielded very little water.

c. Conclusions

E3

E3.1

ES

E8.1

The inspectors considered the corrective action taken to resolve the identified

concerns with the EDG Air Start System adequate. In addition, PSE&G took steps

to correct other problems in order to reduce maintenance and to improve operability

and reliability of the EDG Air Start and Turbo Boost System. The inspectors

concluded that PSE&G produced a thorough and technically sound resolution to this

restart issue. This NRC restart issue is closed for Salem Unit 2. However, the issue

will remain open for Unit 1 because a substantial amount of modification installation

work and post modification testing has yet to be completed.

Engineering Procedures and Documentation

(Closed) LER 50-311195-003 : failure to perform type C local leak rate testing

following piping modification to 21. containment spray piping system. This failure

occurred in March, 1989. In April, 1990, Salem staff performed routine type C

leak rate testing on the new piping section. The result was satisfactory.

Salem management determined that a design change preparer did not properly rout

a design change interface sheet to the In-Service Inspection (ISi) group.

Consequently, they did not identify the test requirement. Since the event, Salem

enhanced the procedures to clearly identify specialty reviews such as ISi

requirements. Additionally, plant engineering management stressed the importance

of design change package quality and attention to detail to engineering personnel.

This licensee identified and corrected violation is being treated as a Non-Cited

Violation consistent with Section Vll.B.1 of the Enforcement Policy.

Miscellaneous Engineering Issues

Reliability of Station Air Compressors, NRC Restart Item 11.2 (Open)

On October 7, 1996, no. 2 SAC tripped on high vibration. The no. 1 ECAC and no.

2 ECAC started automatically as designed. The no. 2 ECAC tripped on low lube oil

,'

) w

E8.2

24

pressure 22 seconds after the auto start. The no. 1 and no. 2 SACs started

automatically. Control air pressure fluctuated slightly (4 psig drop) and quickly

stabilized at normal operating pressure. Operators initiated action requests to

resolve 'the deficient conditions (961007058 for no. 2 ECAC and 961007060 for

no. 2 SAC). Engineering planned corrective measures for both previously

documented deficiencies. They had not yet implemented the corrective actions.

The inspector noted that Salem had not yet established sustained reliable station air

and control air operating performance.

(Closed) Unresolved Item 50-272 and 311 /93-15-03: Salem Unit 2 fuel rod defects.

This item was unresolved pending licensee's evaluation, assessment and

reportability review. Reactor engineering determined that flow induced vibration

caused the fuel rod failures. The vibration only manifested itself on core peripheral

locations due to the clearances required. Fuel manufactured after May 1993 is not

susceptible to flow induced vibration due to Westinghouse V5H fuel redesign (mid-

grid rotation). Engineering determined that a 10 CFR 21 report was not required

because the leaking fuel rods and coolant activity levels were adequately addressed

by Technical Specifications and did not present a substantial safety hazard. Since

1993, the licensee has not experienced additional fuel rod defects due to mid-grid

fretting. The inspector discussed the failures with reactor engineers and observed

failed fuel inspections for Salem Unit 1 and 2. The inspector considered the Salem

response to the fuel rod defects acceptable. This item closed .

E8.3

(Closed) LER 50-272/95-014: safety injection throttle valve inoperability. In

November 1995, engineering determined that erosion of the intermediate head

safety injection (IHSI) throttle valves, in service after a large break loss of coolant

accident (LOCA), could lead to loss of IHSI to the cold legs and hot legs and

potentially impact adequate core cooling.

In 1985 and 1986, Salem maintenance replaced a total of eight high head safety

injection (HHSI) throttle valves due to failures .. In October 1985, engineering

determined that the IHSI valves were not susceptible to accelerated erosion because

they believed that none of the valves were adjusted to a position less than 50%

open. In August 1995, engineering identified that all of the cold leg IHSI throttle

valves at Salem Units 1 and 2 were open less than 30%, and three of the four hot

leg IHSI valves were open less than 50%. At the time of the 1985 HHSI throttle

valve replacements, most of the IHSI throttle valves were less than 50% open. In

1985, engineering failed to take appropriate corrective action to preclude IHSI

throttle valve degradation.

In 1996, maintenance installed orifices in the hot and cold legs to eliminate the

need to throttle the IHSI less than 50% (DCP 2-EC-3461 ). Engineering evaluated

throttling valves in safety-related systems.

In addition, engineering conducted

lessons-learned training and reviewed related safety injection throttle valve

operating experience feedback (OEF).

E8.4

25

The inspector concluded that engineering, in 1985, relied on unproven assumptions

and failed to take appropriate corrective action to preclude IHSI throttle valve

degradation. Since the NRG has taken significant enforcement action for Salem's

failure to identify and correct conditions adverse to quality, and since PSE&G

voluntarily maintained both Salem units shut down to address equipment and

enforcement deficiencies, the NRG will not take additional enforcement action in

these cases. The inspector discussed throttle valve degradation and corrective

actions with the safety injection system manager. The inspector determined that

engineering, in 1996, thoroughly evaluated throttle valve concerns and took

appropriate actions to prevent recurrence.

(Closed) LER 50-272/95-017:failure of control room emergency air conditioning

system to meet GDC 19 criteria.

On July 18, 1995, engineering determined that

Salem Unit 1 would have exceeded the GDC 19 requirements for control room

habitability following a LOCA.

The UFSAR assumed value for control room air in-leakage, used to calculate thyroid

dose, was much less than expected in-leakage. In 1988, engineering reconstituted

the emergency air conditioning design basis, however, they did not provide

supporting information for the assumed air in-leakage. In 1994, engineering

calculated the air in-leakage, using Standard Review Plan guidelines, and determined

that the in-leakage value was much higher than originally assumed in the UFSAR.

Engineering did not determine the effect on thyroid dose from the calculated higher

air in-leakage.

Engineering identified an alternative operating mode for the emergency air

conditioning system to ensure compliance with GDC 19 requirements. Engineering

planned to implement those changes prior to restart. Quality Assurance made

changes to NC.NA-AP.ZZ-0000, Action Request Process, to ensure senior reactor

operator approval of action requests and senior nuclear shift supervisor notification

of potential operability concerns.

The inspector reviewed NC.NA-AP.ZZ-0000 and engineering's 10 CFR 50.59

evaluation and determined that engineering took appropriate corrective action

following their July 1995 identification of the issue. Engineering's failure to take

appropriate actions to resolve the issue in 1988 and 1994 is a violation of 10 CFR

50 Appendix B Criterion XVI, Corrective Action, requirements. Since the NRG has

taken significant enforcement action for Salem's failure to identify and correct

conditions adverse to quality, and since PSE&G voluntarily maintained both Salem

units shut down to address equipment and enforcement deficiencies, the NRG will

not take additional enforcement action in these cases. This LER is closed.

E8.5

(Open) Inspector Follow-up Item 50-272&311 /95-21-02: service water reliability

issues. This item remained open pending NRG review of (1) licensee's siltation

control program, (2) susceptibility of SW traveling screens to debris clogging, (3)

licensee's interpretation of UFSAR (section 9.2.1.2) statement "The SWS is

r

1

designed for class I (seismic) conditions except for the turbine area service water

"

piping outside of the service water intake structure" relative to seismic classification

E8.6

E8.7

' *

26

of SW components in the intake structure. This item remains open pending NRC

review of Restart Plan Ill 19.2, Service Water Reliability.

(Open) Inspector Follow-up Item 50-311 /94-24-02: auxiliary feedwater (AFW) pump

surveillance adequacy. This item remained open pending inspector review of the

licensee's evaluation of the AFW pump surveillance activity. This item remains

open pending NRC review of Restart Plan II 42, AFW Performance and Reliability.

(Open) Inspector Follow-up Item 50-272&311 /96-07-03: breaker testing and

analysis. Inspection Reports 50-272/96-07, 50-311 /96-07 discussed "failure to

latch closed" the problems experienced with General Electric (GE) 4.16kV Magne-

Blast circuit breakers. To alert other licensees of this problem, the NRC issued

Information Notice 96-43, "Failure of General Electric Magne Blast Circuit Breaker,"

on August 2, 1996. To correct this problem at Salem, the licensee adjusted (1) the

opening spring tension, (2) the length of the opening spring, and (3) the primary

contact wipe. GE's proposed action to correct the same problem was a

combination of ( 1) replacing the current second prop spring with a stiffer one, (2)

installing a prop stop block to restrict the prop movement on the left hand side, and

(3) adjusting the wipe on the main contacts.

On September 23-24, 1996, NRC inspectors witnessed GE Philadelphia Operations

(GE PO), where the circuit breakers were manufactured, conduct life tests on two

4.16kV GE circuit breakers that had been in operation at Salem and failed to latch

closed earlier this year. The purpose was to (1) determine if GE PO's proposed

modification to correct "the failure to latch closed" problem will enable the breaker

to close reliably, even if the breaker is adjusted to worst-case (but still acceptable)

tolerances, and (2) determine if adjustments made by the licensee are sufficient to

provide reliable breaker operation without implementing GE's hardware modification.

The details of the breakers are as follows:

Breaker #1: Serial No. 0224A6259-007. This breaker had been in service at Unit 2

first to operate a reactor coolant pump motor and then as a Vital Bus 1 A 41 60/480-

230V transformer breaker, when it failed to latch closed in March 1996. Salem

used this breaker at its training center to demonstrate the "failure to latch closed"

syndrome before it was sent to GE PO for testing. After adjusting the primary

contact wipe to 1 /4" and the opening spring tension to intentionally make the

breaker fail to latch closed, GE PO installed their proposed modification.

This

breaker was installed in a skeleton cubicle during tests. GE PO was operating the

breaker at two cycles per minute.

Breaker #2. Serial No. 0224 A 6257-003. On January 5, 1996, while this breaker

was being used as the 15 service water pump, it failed to latch closed on demand.

Salem was unable to duplicate this failure (non-repeatable) when this breaker was

initially tested. However the breaker did fail after subsequent testing. Salem sent

this breaker to GE PO where the ML-13 operating mechanism was completely

rebuilt using new parts. The breaker was aged by operating it for 4,000 cycles to

E8.8

27

represent a typical breaker installed at Salem. After aging, GE PO incorporated the

Salem modification. GE PO was operating the breaker at two cycles per minute.

On October 4, 1996, after GE PO completed the aging operations, the NRC

inspectors witnessed the continuation of the life cycle testing of the two Magne

Blast circuit breakers. GE PO performed routine maintenance on the two breakers

every 1,000 cycles. GE PO tested the two breakers and captured the motion of the

prop and the prop pin to demonstrate that the breakers did not fail to latch close

after 4000 cycles. As of October 22, 1996, the two breakers operated more than

5,000 cycles without a failure demonstrating that both the modifications were

reliable.

The limiting conditions of acceptability of the reliable operation of the circuit breaker

are:

The opening and closing velocities of the breaker should be more than 15 and 14

feet per second respectively.

The high speed video should indicate that ( 1) the prop pin bounce does not occur in

the wrong place, (2) the prop bounce should not be excessive, (3) the prop kick

back should be limited, and (4) the prop stop pin is fully forward.

The tests demonstrated that the separate corrective actions implemented by Salem

and GE PO eliminated the failure to latch closed problem and enabled the breakers

to operate reliably. This item will remain open until Salem has had sufficient

operating experience to conclude that breaker performance problems do not recur.

GE PO issued a service advice letter (SAL) 351 .1 A on October 18, 1996 on this

subject. GE PO estimates that it will take a few weeks before it could translate the

corrective actions into design drawings and manufacture the items for installation.

(Closed) LER 50-272/96-001 : insufficient thermal overload relay heater margin. In

January 1996, the licensee issued a calculation to perform sizing determinations for

selected rotating equipment thermal overload heaters (TOLs). The results of the

calculation showed that 36 electrical loads had undersized TOLs. The original sizing

of TOLs was performed by selecting the heater from the vendor catalog using

vendor recommended selection criteria. That method did not fully consider the

possibility of degraded voltage conditions or high ambient temperatures within

cabinets. The inspector verified that PSE&G engineering has issued a Technical

Standard providing guidance for design and sizing of motor starters, circuit

breakers, and thermal overload relay heaters. Additionally, the inspector verified

that engineering issued calculations for the sizing of all TOLs for safety related

rotating equipment loads and for all safety related motor operated valve loads.

The

inspector also confirmed that the incomplete modifications are being tracked as

"required for restart" for Salem Unit 1 and 2.

Since the NRC has taken significant enforcement action for Salem's failure to

identify and correct conditions adverse to quality, and since PSE&G voluntarily

maintained both Salem units shut down to address equipment and enforcement

E8.9

28

defici.encies, the NRC will not take additional enforcement action for the previous

failure to adequately size thermal overload heaters.

(Closed) LER 50-272/96-010 : inadequate pressurizer relief tank (PRT) supports.

During an engineering review, it was determined that the support design provided

by Westinghouse for the PRT did not consider hydrodynamic loads that would be

created if all three safety relief valves lift simultaneously. The locked reactor

coolant pump rotor and loss of turbine load accident analysis take credit for the

safety relief valves operating at the same time.

The corrective action for this LER was to revise the design and to install the

modification prior to entering mode 3. Also, since the design was provided by a

supplier, the shortcoming was reported in accordance with 1 OCFR21 .

The inspector reviewed documentation that verified the Salem Unit 2 modification is

installed and the Unit 1 modification is scheduled for installation prior to mode 3.

This LER is closed.

IV. Plant Support

R2

Status of RP&C Facilities and Equipment

R2.1

Radioactive Material Found Outside of the Radiological Controlled Area !RCA)

a.

Inspection Scope (71707)

Inspectors verified radiation protection (RP) controls .and corrective measures

following a RP technician's discovery of contaminated material outside of the RCA.

b.

Observations and Findings

At 1 :00 a.m. on October 16, a Salem radiation protection technician, performing a

normal quarterly survey of plant areas outside the RCA, discovered six discrete

areas in one location of fairly high contamination. Technicians had not discovered

contamination on previous quarterly surveys, however, recent construction activities

necessitated a change in survey location. Technicians identified contamination

down to about 4 inches deep at direct frisk levels of 5,000 to 80,000 dpmiprobe

area (32,000 - 500,000 dpm/100 cm 2) with one area reading 2 mrem/hr on contact.

The material was not readily dispersible and required mechanical means for removal.

No personnel contaminations resulted.

The SNSS determined that the discovered contamination was not reportable in

accordance with Salem Emergency Classification Guide (ECG) Section 7.

Technicians surveyed the surrounding area and found no contamination. By 10:00

a.m. on October 16, technicians removed the radioactive material from the area,

performed a 100 percent direct frisk, and released the area. Radiation Protection

management assessment indicated that the material had been present in this

29

location for some time based on the stable and nondispersible nature of the

material. Radiation Protection management initiated action to perform more

comprehensive site surveys to provide complete site coverage on a biennial

periodicity.

The inspector verified the radioactive material area posting and SNSS ECG

classification and reviewed contamination surveys. Radiation Protection personnel

acted promptly to post the area, remove the contamination, investigate possible

sources, and enhance contamination surveys. In addition, they planned to modify

the survey process to insure that they survey all areas of the protected area outside

the radiologically controlled area in each two year period.

c.

Conclusions

R3

R3.1

a .

b.

Radiation Protection took prompt and appropriate action in response to

contamination found outside the radiologically controlled area.

RP&C Procedures and Documentation

DOT Exemption Request and Steam Generator Characterization Documentation

Scope(86750)

On April 1, 1996, a new revision to Title 49 Code of Federal Regulations became

effective. A new radioactive shipment classification, Surface Contaminated Objects

(SCO) was established by the new regulations. 49 CFR 173.403 defines SCO and

stipulates the limits for SCO I and SCO II. The SCO II definition provides for

contamination concentration limits for both accessible and .inaccessible areas. As

the steam generators will be seal welded shut, only the inaccessible area SCO II

limit applies. The limit is 20 microcuries/cm 2 total contamination (fixed and non-

fixed) beta/gamma and 2 microcuries/cm 2 alpha averaged over 300 cm

2

The inspector reviewed documentation submitted to the DOT which requested

approval for shipment of 4 steam generators under the SCO II classification. This

report documents the NRC review of the licensee's characterization and a

determination of applicability of the SCO II classification and related requirements.

Observations and Findings

On August 5, 1996, the licensee submitted to the DOT an exemption request from

the packaging requirements of 49 CFR 173.427(b)(1) for the shipment of four

steam generators as SCO 11 from Salem Generating Station Unit 1 . This refers to

the requirement that surface contaminated objects are to be packaged in industrial

packaging (for greater than A 2 quantities). The exemption application, stated that

the steam generators themselves offered equivalent or better packaging than that

required for an IP-2 package and requested relief from that requirement. Also

contained in the August 5th exemption request was the licensee's characterization

basis for demonstrating compliance with the limits of SCO II.

30

The information provided indicated that a swipe sample was taken for complete

radiochemical analysis of radionuclide content and a series of contact radiation

surveys were taken along the external surfaces of each steam generator. This data

was used to determine an average surface area concentration inside of each steam

generator.

The inspector indicated that the licensee utilized a simplified computer model of the

steam generator. The steam generator geometry was simplified to that of a cylinder

containing a homogenous source mixture of air and' iron molecules. The total curie

values were calculated from the maximum external contact dose rate determined

from each steam generator. Total activities of 143, 129, 122, and 126 curies were

calculated for the four steam generators. The inspector calculated the total A 2

quantities for each steam generator and determined that they ranged from 7.45 to

8.8 times A 2 quantities. The DOT regulations require an IP-2 package for SCOs

with quantities greater than 1 A 2 quantity not to exceed 100 times the A 2 quantity

limit. Based on knowledge of the total primary side internal surface area of a

Westinghouse Model 51 steam generator, the licensee derived an average

contamination concentration for each steam generator. The steam generators were

determined by the licensee to represent an average surface contamination level of

approximately 3 microcuries/cm 2 beta/gamma and 2.24E-4 microcuries/cm 2 alpha.

The inspector questioned the evaluations of uncertainty in the results and the

availability of benchmarking the results by comparison to steam generator tube

  • samples in order to validate the characterization.

Revision 1 of the Salem Unit 1 Steam Generator Characterization Report was issued

on August 20, 1996. This report stated that "It is impossible to quantify the

percent error associated with an analysis of this type without additional empirical

data." The report continued providing a benchmark evaluation using dose rate data

obtained from individual tube samples from Salem's steam generators and compared

these dose rates with a computer-derived estimate of dose rates based on the

previously determined surface contamination level of 3 microcuries/cm 2 * This

comparison indicated that the actual dose rates were between 2 and 27 % higher

than predicted.

The inspector questioned the variability of contamination inside the steam

generators. Thus far, the licensee had only made an average surface contamination

determination, however, the regulations specify that the sea limits apply to each

300 cm

2

  • The inspector referred the licensee to EPRI Report NP-3107, May 1983,

entitled, "Gamma-Ray Exposure Rate Distribution in a Steam Generator". This

report indicated that contamination is not uniformly distributed inside of a steam

generator, but that the contamination on the channel head bowl and tube sheet

regions was approximately 14 times greater than the contamination found in the

steam generator tubes. The inspector indicated that if the licensee's average

contamination level was 3 microcuries/cm 2, then this study suggests that the

channel head bowl and tube sheets may be expected to exceed the SCO II limit of

20 microcuries/cm 2 *

31

The licensee issued revision 2 of the Salem Unit 1 Steam Generator Characterization

Report on September 20, 1996 to address the variability of contamination inside

Salem's steam generators. Based on a review of the EPRI report, the licensee

revised their characterization approach into a two-step process. The original dose-

to-curie calculation approach was used to determine the activity in the tube bundle

areas and a separate set of calculations (following the EPRI methodology) was

utilized to determine the contamination levels outside the tube bundle areas. The

licensee's results indicated that the tube bundle contamination level was 3

microcuries/cm 2 and the channel head bowl area was 15 microcuries/cm

2

  • Both

sets of calculations utilized the radionuclide ratios determined from a swipe sample.

Due to the close proximity to the SCO II limit, the inspector reviewed the use of the

swipe sample for radionuclide characterization. The inspector noted that, due to the

dominance of the radionuclides of Co-58 and Co-60 found in the swipe sample, and

the relatively short half-life of Co-58 (70.8 days versus 5. 7 years for Co-60), the

variability of the cobalt 58 constituent could greatly affect the contamination

concentration found in the steam generators, particularly since Salem Unit 1 had

been shut down for 20 months. The inspector noted that, the licensee back-

decayed the swipe data to the April 18, 1995 shutdown date and used this

information as the basis for all other characterization results. At shutdown, the

Co-58/Co-60 ratio was 3.15; at 20 months, 0.01.

The inspector questioned whether a swipe sample would accurately represent the

total contamination radionuclide ratios. Reason suggests that deeper into th_e

corrosion film may represent older corrosion deposits and much less Co-58.

Therefore, a higher percentage of longer lived radionuclides may be expected in the

total contamination layer corresponding to a higher surface contamination level at

the time of shipment.

The licensee indicated that a metal hand-held implement was used to abrade the

surface and then a swipe of this material was taken. Therefore, the swipe sample

was intended to represent the total contamination present. The inspector

questioned whether the previously utilized steam generator tube samples could be

utilized for direct gamma analysis of the total contamination present. On

October 7, 1996 the licensee provided the inspector with this information and

additional swipe samples. Comparisons of Co-58/Co-60 ratios of these samples are

provided below.

Sample Description

Tube sheet swipe

Channel head bowl swipe

Divider plate swipe

Abraded swipe used for S/G characterization

Shot peen swipe (abrasive blasting)

Tube sample direct gamma scan

Co-58/C0-60

3.87

3.38

3.36

3.15

2.79

2.41

c.

32

In utilizing the direct gamma scan data for the gamma contributors and the

radiochemical results of the abraded sample for the difficult-to-measure

radionuclides, the inspector (utilizing the same EPRI methodology as the licensee)

calculated that the channel head bowl and tube sheet area contamination levels

were approximately 30 microcuries/cm 2 over an area of 2.1 E5 cm

2 for each steam

generator. Therefore, the channel head bowl and tube sheet portions of the steam

generators are apparently above the limits for SCO 11. These findings were

discussed with the licensee (J. Burford, H. Cruickshank), NMSS (E. Easton, J. Cook,

R. Lewis), and DOT (R. Boyle) on October 8, 1996 via telephone conference. As a

result of the discussion, the licensee submitted a letter dated October 10, 1996 to

DOT requesting relief from the SCO 11 limits in the channel head sections for all four

steam generators as these areas comprise less than 1 % of the surface

contaminated area of each steam generator. On November 6, 1996 the DOT issued

an exemption approval (DOT-E-11745), which allows the licensee to transport the

four Salem steam generators as surface contaminated objects with exemptions to

the industrial packaging requirement and contamination level limits in the channel

head sections.

Conclusions

The inspector determined that the Salem Unit 1 steam generators met most of the

requirements for an SCO class II shipment. The contamination level on the channel

head and tube sheet areas appeared to be above the DOT limits and the steam

generators were not packaged into IP-2 containers. The licensee applied for

exemption to these requirements, which were subsequently approved by the DOT.

P1

Conduct of Emergency Preparedness (EP) Activities

P1 .1

Effectiveness of Licensee Controls

a.

b.

Inspection Scope (82701 l

The inspectors reviewed the licensee's tracking systems used for tracking EP related

action items. Also, the EP self-assessment program was reviewed to determine the

effectiveness of licensee controls.

Observations and Findings

Procedure NC.NA-AP-ZZ-000(0), PSE&G Nuclear Business Unit, Action Request (AR)

Process, describes the licensee's method for reporting conditions requiring corrective

action, program enhancement or interdepartmental support. A newly developed

automated system called the Performance Improvement Review System (PIRS) tracks

ARs. The system is maintained by the audit department staff who screen, classify and

distribute the ARs. ARs are assigned significance levels (one to four, in descending

priority) depending on circumstances, conditions or at management discretion. All ARs

are given significant management attention and the highest significance levels (one and

two) require a root cause analysis .

-1

c .

33

The inspectors requested a demonstration of the PIRS but the licensee was not able to

locate any recently closed ARs. The licensee stated that PIRS is not user-friendly and

has the potential for losing data if a user incorrectly inputs information. Due to these

problems, the EP staff utilizes three other internal office systems for tracking repetitive

EP activities required by E-Plan commitments, procedure/E-Plan changes, drill/exercise

critiques, training classes reviews and EP administrative review items. The inspectors

discussed the problems noted during the demonstration of the PIRS with members of the

audit department. They stated that they were aware of the computer program problems

and are currently modifying the program for easier and more efficient use. Once the

problems are resolved, it is the licensee's inte.nt that the PIRS will become the sole

tracking system for Salem and Hope Creek.

The inspectors reviewed several ARs and found th~m to be very detailed, thorough and

were reviewed by management.

The licensee had recently implemented an "EP Group Planned Self-assessment Program"

to evaluate the effectiveness and performance of the EP program. The inspectors

reviewed several self-assessment reports and found them to include evaluation plans,

strengths, weaknesses and/or potential areas for improvement. As the self-assessment

program develops, the licensee plans to become more self- critical, establish trending

data and closely evaluate repeat findings.

Conclusions

The EP staff uses the AR process plus three other automated systems for tracking issues

such as audit findings, procedure changes and self-assessment findings. The systems

are effective and ensure adequate management attention. The recent addition of a self-

assessment program is a good initiative for the EP program.

P1 .2

Relationship with Offsite Agencies

a.

Inspection Scope (82701)

The inspectors interviewed state and county representatives from the States of

New Jersey and Delaware to assess the licensee's relationship with offsite agencies.

b.

Observations and Findings

The inspectors interviewed the Radiological Administrator for the Delaware Emergency

Management Agency, and the Manager, Bureau of Nuclear Engineering (BNE),

New Jersey, and contacted by telephone, the Deputy Coordinator for the Department of

Emergency Services, Salem County, New Jersey, to discuss the licensee's relationship

with those agencies. Both Delaware and Salem County, NJ representatives stated that,

overall, the licensee worked hard to maintain an excellent rapport with their agencies.

However, the Manager, BNE stated that while the communications and information flow

between the licensee and the State has improved since October, 1995, further

improvement is needed in the following areas: 1) planning of the Emergency Operational

c.

34

Facility (EOF) renovation; 2) quality of the station status checklists used for transmitting

event information; and 3) the verification of information contained in press releases from

the licensee's emergency news center. He further stated that recent communications

with the licensee on the proposed NUMARC EALs was constructive.

Conclusions

Overall, the licensee maintained good rapport with the offsite agencies. However, the

Manager, BNE identified some issues where coordination and communication between

the licensee and the State of New Jersey could be improved.

P2

Status of EP Facilities, Equipment, and Resources

P2. 1

Operational Readiness of Emergency Facilities

a.

Inspection Scope (82701 l

b.

The inspectors toured the following Salem facilities: the EOF, Control Room (CR),

Technical Support Center (TSC), Operations Support Center (OSC), and Control Point.

The Hope Creek facilities were evaluated during the May, 1996 annual exercise and

found to be operationally ready. The inspectors also reviewed 1996 facility equipment

inventories and surveillance tests for completeness and accuracy .

Observations and Findings

The inspectors checked the inventory of several emergency equipment lockers and one

field monitoring team emergency kit for completeness and equipment readiness. One

locker contained two radiation survey instruments with dead batteries, that were

immediately replaced. All other survey meters inspected were calibrated and operational.

The inspectors found two unshielded Cesium-137 check sources in supply lockers

located in the EOF and TSC, used for verifying instrument response. The check sources

are routinely stored near a supply of personnel thermo-luminescent dosimeters (TLDs)

used for offsite field monitoring teams. These sources could potentially produce an

erroneous radiation dose to the field TLDs prior to use in an actual emergency. The

licensee acknowledged this problem and agreed that the check sources and TLDs should

be stored in separate lockers.

While touring the TSC, the inspectors noticed that a key for a radiation protection (RP)

locker was missing. Apparently, an RP staff member had changed the lock, without

informing the EP staff, and stored the key at the Salem control point. According to the

licensee's emergency plan implementing procedure (EPIP) 203S, the key is to be stored

near the locker. Relocation of the key could potentially result in the locker being

inaccessible to field teams during an emergency. The licensee initiated a procedure

change to ensure that during emergency conditions, an RP technician, assigned to the

TSC, would bring the locker key from the control point and unlock the locker.

35

The licensee was in the process of constructing a new OSC inside the CR ventilation

boundary and renovating the existing EOF. During construction, a temporary OSC,

outside the CR, was being utilized in case of an actual emergency event. The inspectors

concluded that the EOF and temporary OSC were adequate if needed for this purpose.

The inspectors determined that equipment inventories, communication surveillance tests,

and siren surveillance tests were conducted at correct frequencies, and inventory

checklists were properly completed and reviewed. Identified deficiencies and corrective

actions were well documented.

c.

Conclusions

The inspectors concluded that the licensee maintained an effective inventory and

surveillance test program and that the Salem/Hope Creek emergency facilities and

equipment were operationally ready.

P3

EP Procedures and Documentation

a.

Inspection Scope (82701)

The inspectors reviewed emergency plan (E-Plan) and EPIP revisions in the regional

office, prior to the inspection, to determine if the changes reduced the effectiveness of

the E-Plan. While onsite, the inspectors reviewed the documentation for the last E-Plan

changes.

b.

Observations and Findings

The inspectors reviewed the licensee's 10 CFR 50.59 safety evaluation and 10 CFR

50.54(q) licensee review for Revision 5 to Section 2 of the E-Plan. The inspectors

concluded that these were thorough, well-documented, and adequate for making this

revision. EPIP revision changes were documented in NRC Inspection Report 50-354/96-

01, 50-272 & 311 /96-01 and no additional revisions were reviewed prior to this

inspection.

c.

Conclusions

The inspectors determined that the reviewed E-Plan and EPIP changes did not reduce the

effectiveness of the E-Plan. Also, the licensee's procedure change process was good.

P5

Staff Training and Qualification in EP

a.

Inspection Scope (82701)

The inspectors reviewed EP training records, training procedures, lesson plans, EPIPs and

the licensee's E-Plan to evaluate the licensee's EP training program. The inspectors also

conducted interviews with Salem Senior Reactor Operators (SROs) to assess the

licensee's EAL classification training.

b.

"

36

Observations and Findings

The EP off-site supervisor maintained the EP training records for emergency response

organization (ERO) responders. The inspectors randomly selected the training records of

approximately 75 responders from Salem and Hope Creek and verified that the ERO

responders were qualified to fill their assigned emergency response positions.

Approximately a quarter of the responders are required to have respirator training that is

provided by RP. EP does not routinely track the RP training to ensure that all responder

training requirements are met. In early 1996, the EP off-site supervisor, accidently

discovered that respirator training for 9 out of 16 maintenance workers on the ERO list

had elapsed. Also, in August 1996, it was reported in the licensee's morning

management meeting, that an Instrument and Control technician was reported not to

have current respirator qualifications and was listec:l on the current ERO list. The EP staff

appeared to be unaware of this incident and committed to writing an AR for further

review.

The inspectors stated to the licensee that although the RP Department is responsible to

provide respirator training, the EP staff is responsible to ensure that all members on the

ERO list meet the required qualifications stated in the Emergency Plan and EPIPS. The

licensee initiated a review of the RP records to ensure that all individuals on the current

ERO list meet all training requirements. Additionally, the licensee mentioned plans to

have one automated training tracking system for better utilization by the EP staff .

The licensee had made changes to their EP training program due to problems identified in

drills and exercises. The licensee was conducting quarterly unannounced call-out muster

drills, weekly pager tests, and were completely revising procedures and EP overview

lesson plans. In addition, a letter was sent from upper management to the ERO

members addressing their EP roles and responsibilities.

The inspectors interviewed two Salem SROs to assess the quality of the licensee's

present EAL training. Both SROs stated that the NUMARC EAL training was good,

however, they did not think the one-hour training session on the present EAL scheme

was very thorough or detailed. They both stated that if the NUMARC EALs are not

approved prior to restart of Salem 1 & 2, they would expect comprehensive retraining on

the present EALs. *

The inspectors stated to the licensee that until the NUMARC EALs are approved,

adequate and appropriate training should be provided to the SRO's for classifying events

using the present EALS.

The inspectors reviewed training records for annual offsite emergency response training

for medical, fire-fighting, and media personnel. The inspectors found that the required

drills had been conducted and were well-documented. Media training was offered by the

licensee, but may not have been implemented in accordance with the E-Plan (see Section

PS). With this one exception, all on-site and off-site required drills, exercises and

training were conducted in 1995 and 1996 in accordance with the licensee's E-Plan .

37

The licensee conducted monthly pager drills for all four duty ERO teams and weekly drills

for the on-call duty team. Additionally, they conducted quarterly muster exercises where

the duty team must actually report to the site, alternating between Salem and Hope

Creek. The inspectors noted that documentation regarding these drills and exercises

indicated an overall improvement in ERO response. However, in May 1996, NRC

inspectors attended an unannounced call-out drill and observed poor drillmanship and

command and control. (See Section P8.3)

The inspectors reviewed the training records for annual EAL training with the states and

counties and found them to be satisfactory.

c.

Conclusions

The inspectors determined that the ERO members, for whom training was reviewed,

were currently qualified. However, the licensee needs to ensure that individuals listed on

the ERO list meet all training requirements to fill their position. Training of offsite

agencies and support organizations is of good quality and completed as required.

The inspectors concluded that the periodic pager tests and mustering drills, as well as

holding ERO responders accountable for their responsibilities is a positive step to upgrade

their overall emergency response capability. Overall, the inspectors assessed this area

as adequate .

PG

EP Organization and Administration

a.

Inspection Scope (82701)

The inspectors reviewed the licensee's EP staffing and management to determine the

changes that have occurred since the last program inspection (August 1994), and to

assess if those changes had any adverse effect on the EP program.

b.

Observations and Findings

The EP Department has had several management and organization changes in the past

year. In January 1996, the Manager, EP & Radiological Safety was replaced. In

September 1996, this position is being eliminated and split into two management

positions. The intentions are to add an experienced EP manager and an experienced

radiological health manager. In July, the EP and Radiological Support Division was

moved from Site Support Services and placed in the Nuclear Training Center (NTC)

Division. The Director, NTC reports directly to the Sr. Vice President, Nuclear

Operations. The licensee is planning additional changes in the responsibilities of the EP

staff members.

Discussions with the Sr. Vice President and Director, NTC indicated that management is

committed to bringing a serious EP attitude to the ERO members. They also stated that

the addition of a manager with EP experience will enhance EP staff performance .

c .

38

Conclusions

Discussions with the members of the EP staff, the inspectors determined that the recent

organizational changes have not had an adverse effect on the EP staff. At this time, it

does not appear that these changes have reduced the ability to administer the EP

program effectively.

P7

Quality Assurance in EP Activities

a.

Inspection Scope (82701)

The inspectors reviewed Audit Reports No.95-030 and 96-030, of the EP Department,

conducted in 1995 and 1996, respectively. The inspectors also reviewed audit plans,

checklists procedures and interviewed personnel from the QA Department regarding the

process for conducting a program audit.

b.

Observations and Findings

c.

Based on document review and interviews, the inspectors determined that the audits

were conducted utilizing an audit plan and checklists, and that the audit team included

several technical specialists from other nuclear utilities with EP experience. The audit

reports were appropriately detailed and met the requirements specified in 1 0 CFR

50.54{t)._ No programmatic problems were identified .

Conclusion.

The audit reports were comprehensive and the audit plan was extensive. The use of

independent technical specialists is particularly noteworthy. The reports met the

requirements of 10 CFR 50.54(t) and the inspectors assessed this area as very good.

PS

Miscellaneous EP Issues

P8.1

Updated Final Safety Analysis Report (UFSARl Inconsistencies

A recent discovery of a licensee operating its facility in a manner contrary to the UFSAR

description highlighted the need for a special focused review that compares plant

practices, procedures, and/or parameters to the UFSAR description. Since the UFSAR

does not specifically include EP requirements, the inspectors compared licensee activities

to the E-Plan, that is the applicable document. The following inconsistences were noted

between the E-Plan and licensee activities by the inspectors.

1.

Section 9, paragraph 4.4 of the E-Plan discusses additional radiological

instrumentation located in the licensee's Training Center laboratory to be available

as backup to the EOF. The inspectors determined that the instrumentation had

never been calibrated and the laboratory is currently being dismantled .

2.

39

The inspectors discussed this with the licensee, and an E-Plan change has been

submitted to delete the use of the Training Center laboratory as a backup to the

EOF. (URI 50-272&311/96-15-03)

Section 8, paragraph 3.0 of the E-Plan, states that annually, an information program

is provided to local news representatives and covers specific outlined topics on

nuclear energy, radiation and emergency planning. It also states that this program

may take place as part of the annual exercise. A public information (Pl)

representative stated that media training actually consisted of an information

calendar sent to local media personnel, followed by a phone call, inviting them to

the licensee's annual exercise. This is inconsistent with the commitments in the E-

Plan. A change to the E-Plan describing the current media training program has

been submitted. (URI 50-272&311/96-15-04).

P8.2

Missed Alert Declaration

a.

Observations and Findings

On July 12, 1996, a new shift technical advisor (STA) reviewing a reactor trip event

report from June 7, 1995, found that the licensee had not made an alert declaration in

accordance with the emergency classification guide (ECG), Section 4A. The report

stated that, on that date, at 6:28 p.m., Salem Unit 2 began a reactor shutdown in

accordance with Technical Specification (TS) 3.03, due to the inoperability of both

Residual Heat Removal (RHR) trains. At 5:42 a.m., on June 8, 1995, Unit 2 entered

Mode 4, that, concurrent with the inoperability of both RHR trains, met the criteria for an

alert declaration. Although both RHR trains were inoperable by TS, they were functional,

and RHR was used for shutdown cooling. Based on the STA's finding, the licensee

made a "one-hour report" in accordance with ECG, Section 17D, "Emergency Conditions

Discovered After-the Fact," to inform the NRC of the missed classification and an AR

was written for additional review.

The inspectors reviewed the licensee's Significant Event Review Team (SERT) report that

followed the 1995 event and determined that the SERT did not identify the missed

classification. It was also noted, that the licensee's AR report did not address the

SERT's failure to identify the missed classification. The inspectors questioned the

licensee about this. The licensee believed that the SERT missed the classification due to

the confusion with the present EALS. Since this has been a continuing problem

identified for other missed classifications, the licensee did not address it in the AR. The

inspectors stated that the recent review of the SERT should have included investigation

into other possible contributors to the EAL classification problems, for example, the

quality of EAL training or if scenarios are realistic and challenging. The licensee initiated

an AR to review this matter further.

The missed alert declaration was licensee-identified. It could not have been prevented

by corrective actions for any previous violation. The licensee's AR, that initiated a

reevaluation of the event, prescribed adequate remedial and corrective actions to prevent

recurrence. Additionally, the safety significance of the event was negligible. Both RHR

trains were functional at all times, and RHR was used for shutdown cooling, i.e., to cool

I

,I

b.

40

the reactor core by removing decay heat, even though both RHR trains were inoperable

according to TS. The inspectors concluded that the licensee's ECG is restrictive by

using the term "inoperable" when referring to the RHR trains in the initiating conditions

for the alert. NUREG-0654, "Criteria for Preparation and Evaluation of Radiological

Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," uses

the term "non-functional" when describing the initiating conditions for a loss of decay

heat removal capability (alert). This term is less restrictive in that a system can be

ii:ioperable, but still functional. The licensee had the capability at all times to use RHR

for decay heat removal, and protect the core from overheating.

Conclusions

The NRC Enforcement Policy states that the failure to declare an alert is a Level Ill

violation. However, due to the mitigating circumstances discussed above, this licensee-

identified item is being treated as a Non-Cited Violation, consistent with Section Vll.B.1

of the NRC Enforcement Policy.

P8.3

Unannounced Off-hours Call-out Drill

a.

Observations and Findings

On May 14, 1996 the licensee conducted an unannounced off-hours call-out drill for

staffing all Salem emergency response facilities. NRC inspectors observed player

performance at the EOF and the TSC. The licensee successfully staffed the facilities in a

timely manner. However, at the EOF, many of the players did not take play seriously

and some appeared unfamiliar with their position responsibilities. No command and

control was exhibited by the Emergency Director (ED) and that contributed more to a

"laissez-faire" atmosphere. A member of the technical support team was told to fill the

technical support manager position, and informed the ED that she had not received the

required training for filling that position.

The ED had her assume the role of technical

support manager anyway. Also, the EP staff played dual roles of observer and referee

that caused them to coach and demonstrate to players their responsibilities. Similar

observations were made at the TSC.

During this inspection, the inspectors reviewed the licensee's drill critique in that the

above observations were documented. In discussions with the licensee, the EP staff

believed many of the identified problems were due to the EP staff not stating the

objectives of the drill, therefore, many of the players thought it was just a "muster" drill.

They also stated that the lack of command and control was due to the ED being told

minutes prior to his arrival, that this was just a muster drill. No action report was

written for these observations.

The inspectors noted that* no additional training was provided to those players that

weren't familiar with the responsibilities of their position. Also, the licensee gave no

consideration to whether poor player performance was due to the fact that this drill was

"unannounced" .

b.

41

Conclusions

The licensee has performed numerous drills during the past year and licensee critiques

indicated that player performance was serious and responsible. However, for the May

1996 drill, players did not perform their duties seriously as they would if it were a real

event, until informed otherwise.

S2

Status of Security Facilities, Equipment, and Resources

S2.1

Security Door Material Condition

Inspection Scope (71707)

The inspectors reviewed the adequacy of the security staff's response to door alarms.

Observations and Findings

The inspector reviewed the record of alarms for security doors in some high traffic areas.

In one case, a door alarmed nineteen times in one day. The record indicated that, in

each case, security personnel responded to the alarms. Based on the record and

discussions with security and other plant personnel, a number of factors caused the door

alarms, including ventilation effects, equipment problems, and plant staff not correctly

operating the security features. The inspector noted that, after a few days of door

alarms, security managers implemented compensatory measures for the doors and

insured that maintenance staff corrected the identified hardware discrepancies. In the

case of one door, the staff replaced major components to insure proper door operation.

Conclusions

The inspectors concluded that security personnel complied with the requirements of the

security plan for access control. Although security supervisors and managers might

have been more aggressive in implementing compensatory measures and initiating

maintenance efforts, the inspectors did not find any degradation of access control.

S8

Miscellaneous Security and Safeguards Issues

S8.1

Security Support of Replacement Steam Generator Transportation

a.

Inspection Scope

On October 3, 1996, a regional security specialist was dispatched to the site to review

the security considerations associated with the movement of the RSGs. The RSGs were

received at the Salem barge slip, transported through the vehicle barrier system,

protected area barrier, and intrusion detection systems, into the protected area (PA),

maneuvered, transported out of the protected area and taken to the temporary storage

facility. Entry into, and then out of, the PA was necessitated to make use of an existing

construction roadway for the transporter vehicle .

b.

42

Observations and Findings

The inspector determined by observations, procedural reviews, interviews with security

force members, and discussions with security management, that security considerations

associated with the RSGs, as described in the Salem Unit 1 Steam Generator Entry

Security Plan, dated October 2, 1996, Revision 1, was properly implemented. The

inspector verified that compensatory measures associated with the removal of the

vehicle barrier system, perimeter intrusion detection systems, and protected area barrier

were effective and properly implemented. Additionally, the inspector determined by

reviewing Security Procedure SP12, dated March 9, 1996, Revision 9, and discussions

with security management, that measures were in place to ensure that the barriers

would be properly re-installed and that all applicable intrusion detection systems re-

installed and reactivated, and tested in accordance with the requirements of the NRC-

approved security plan prior to removing compensatory measures. No weaknesses or

discrepancies were noted.

V. Management Meetings

X 1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on November 8, 1996. The licensee acknowledged the

findings presented .

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified .

INSPECTION PROCEDURES USED

IP 50001:

IP 61726:

Steam Generator Replacement Inspection

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 86750:

Solid Radioactive Waste Management and Transportation of Radioactive

Material

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-272&311/96-15-01

VIO

50-272&311 /96-15-02

VIO

50-272&311 /96-15-03

URI

50-272&311 /96-15-04

URI

Closed

50-272&311/92-12-01

URI

50-272&311/93-15-03

URI

50-27 2&311 /93-21-03

URI

50-311 /94-06-01

VIO

50-272&311/E03013

VIO

50-311 /94-08-01

URI

50-272&311/94-13-02

URI

50-272&311/94-14-01

URI

50-272&311/94-19-01

IFI

50-272&311/95-07-01

VIO

50-272&311 /95-07-02

DEV

50-272&311 /95-17-01

VIO

50-272&311/96-05-01

VIO

50-272&311 /96-08-01

VIO

50-272&311 /96-12-02

IFI

50-272/95004

LER

50-272/95013

LER

50-272/95014

LER

50-272/95017

LER

Corrective action for operator performance problems

Operator failure to adhere to procedures

Acceptability of change to EOF backup facility

Acceptability of lack media training vs. E-plan

description.

equipment operator log falsification

Salem Unit 2 fuel rod defects

potential TS noncompliance due to SSPS train B

inoperability

failure to comply with TS for power operated relief

valves

loss of control room command and control

steam generator depressurization during simulator

scenario

repeated entry into TS LCO

flange leak repair root cause

definition of controlled leakage

control room emergency air conditioning system TS

noncompliance

concurrent testing of redundant EDGs during normal

plant operation

failure of electricians to reinstall tags

failure of Offsite Safety Review and Onsite Safety

Review Group personnel to meet the number and

qualification requirements of TS 6.5.2.2

failure of plant staff to update Tagging Request Inquiry

System

service water bay depressurization

inadequate containment air temperature surveillance

TS 4.3.3.3.1 surveillance requirements late

safety injection throttle valve inoperability

failure of control room emergency air conditioning

system to meet GDC 19 criteria

2

50-272/95018

LER

improper range gauges used for inservice testing

50-272/96001

LER

insufficient thermal overload heater margin

50-272/96003

LER

missed radiation monitor sampling

50-272/96004

LER

missed containment isolation valve surveillance

50-272/96005

LER

failure to perform Tavg channel checks

50-272/96006

LER

missed independent verification of waste gas alignment

50-272/96007

LER

ESFAS values greater than TS allowed

50-272/96008

LER

failure to meet mode 5 requirements for natural

circulation

50-27 2/9.6009

LER

potential common mode failure for 4KV Magna-Blast

breakers

50-272/96010

LER

inadequate pressurizer relief tank supports

50-272/96011

LER

pressurizer safety relief valves found outside of TSs

limit

50-272/96016

LER

missed RHR pump surveillance

50-272/96017

LER

missed plant vent surveillance

50-272/96022

LER

incorrect radiation monitor setpoints

50-272/96023

LER

failure to perform MSIV surveillances

50-272/96024

LER

failure to meet AFW pump response times

50-311/95001

LER

manually initiated engineered safety feature actuation

50-311 /95003

LER

failure to perform type C local leak rate testing

50-311 /95007

LER

missed emergency diesel generator surveillances

50-311 /95008

LER

missed verification of containment isolation

50-311/96001

LER

failure to perform chemical sampling when required

50-311 /96002

LER

waste gas decay tank oxygen greater than limit

50-311 /96003

LER

failure to perform fuel handling building auto start

surveillance

50-311 /96004

LER

description missed compensatory survey

. 50-311 /96005

LER

missed fuel handling building charcoal surveillance

50-311 /96007

LER

missed over current protective device surveillance

50-311 /96008

LER

inoperable battery chargers due to manufacturing

discrepancies

50-311/96010

LER

missed pressurizer weld surveillances

Discussed

50-311 /94-24-02

IFI

auxiliary feedwater pump surveillance adequacy

50-272&311 /95-21-02

IFI

service water reliability issues

50-272&311/96-07-03

IFI

breaker testing and analysis

50-311 /96009

LER

fourteen day followup report regarding 1 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> shifts

for operations personnel

LIST OF ACRONYMS USED

AFW

Auxiliary Feedwater

AR

Action Request

ARP

Alarm Response Procedure

CR

Condition Resolution

DCPs

Design Change Packages

EPRI

Electric Power Research Institute

DOT

U.S. Department of Transportation

ECAC

Emergency Control Air Compressor

ECG

Emergency Classification Guide

EDG

Emergency Diesel Generator

EO

Equipment Operator

EOPs

Emergency Operating Procedures

ES FAS

Engineered Safety Feature Actuation System

GDC

General Design Criterion

GE PO

General Electric Philadelphia Operations

GE

General Electric

HHSI

High Head Safety Injection

l&C

Instrumentation and Controls

IHSI

Intermediate Head Safety Injection

IP

Industrial Packaging

ISi

In-Service Inspection

IST

lnservice Testing

LCO

Limiting Conditions for Operation

LCR

License Change Request

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

MSIVs

Main Steam Isolation Valves

NRC

Nuclear Regulatory Commission

OEF

Operating Experience Feedback

OSG

Old Steam Generator

OSR

Offsite Safety Review

OTSC

On-The-Spot-Change

PA

Protected Area

PDR

Public Document Room

PO RVs

Power Operated Relief Valves

PRT

Pressurizer Relief Tank

PSE&G

Public Service Electric & Gas

QA

Quality Assurance

RCA

Radiological Controlled Area

RCP

Reactor Coolant Piping

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RO

Reactor Operator

RP

Radiation Protection

RSG

Replacement Steam Generator

SAC

Station Air Compressor

sco

Surface Contaminated Object

,,

SGRP

SNSS

SRO

SSPS

SW

TDR

TO Ls

TRIS

TS

TSSIP

UFSAR

WO

2

Steam Generator Replacement Project

Senior Nuclear Shift Supervisor

Senior Reactor Operator

Solid State Protection System

Service Water

Technical Document Room

Thermal Overload Heaters

Tagging Request Inquiry System

Technical Specification

Technical Specifications Surveillance Improvement Program

Updated Final Safety Analysis Report

Work Order