Letter Sequence RAI |
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Initiation
- Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request
- Acceptance...
- Supplement
Results
Other: ML071900365, ML11090A078, ML11109A067, ML12199A025, ML13043A527, ML13067A315, ML13077A284, ML13134A367, ML13155A504, ML13270A248, ML14217A206, ML15007A430, ML15055A004, ML15055A014, ML15268A128, NL-07-078, Station Blackout (SBO) / Appendix R Diesel Generator Commitment, Response to NRC Review Status of License Renewal Application, NL-10-054, Correction to License Renewal Application, NL-12-037, License Renewal Application - Revised Reactor Vessel Internals Program and Inspection Plan Compliant with MRP-227-A, NL-14-013, Additional Information Regarding the License Renewal Application - Action Item 7 from MRP-227-A
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MONTHYEARNL-07-056, Supplement to License Renewal Application2007-05-0303 May 2007 Supplement to License Renewal Application Project stage: Supplement ML0729601252007-06-21021 June 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for June 21 2007 Project stage: Request NL-07-078, Station Blackout (SBO) / Appendix R Diesel Generator Commitment, Response to NRC Review Status of License Renewal Application2007-06-21021 June 2007 Station Blackout (SBO) / Appendix R Diesel Generator Commitment, Response to NRC Review Status of License Renewal Application Project stage: Other ML0719003652007-07-25025 July 2007 Determination of Acceptability and Sufficiency for Docketing, Proposed Review Schedule, and Opportunity for a Hearing Regarding the Application from ENO, Inc. for Renewal of the Operating License for the Indian Point Nuclear Generating Unit Project stage: Other ML0727804392007-10-16016 October 2007 Summary of Telephone Conference Call with Entergy Nuclear Operations, Inc., Requests for Additional Information Project stage: RAI NL-10-054, Correction to License Renewal Application2010-05-27027 May 2010 Correction to License Renewal Application Project stage: Other ML11090A0782011-04-19019 April 2011 Safety Project Manager Change for the License Renewal Project for Indian Point Nuclear Generating Unit Numbers 2 and 3 Project stage: Other ML11109A0672011-04-19019 April 2011 Lr Hearing - FW: OAR - Safety PM Change for the License Renewal Project for Indian Point...(Tac Nos. MD5407 & MD5408) Project stage: Other CNRO-2011-00006, Request for Approval of Change to the Entergy Quality Assurance Program Manual (QAPM) and Associated Plant Technical Specifications Regarding Staff Qualifications2011-12-13013 December 2011 Request for Approval of Change to the Entergy Quality Assurance Program Manual (QAPM) and Associated Plant Technical Specifications Regarding Staff Qualifications Project stage: Request ML12048B4082012-02-17017 February 2012 State of New Yorks Answer to Entergys Motion in Limine to Exclude Portions of Pre-Filed Testimony and Exhibits for Contention NYS-37 (Entergy Alternatives) Project stage: Request NL-12-037, License Renewal Application - Revised Reactor Vessel Internals Program and Inspection Plan Compliant with MRP-227-A2012-02-17017 February 2012 License Renewal Application - Revised Reactor Vessel Internals Program and Inspection Plan Compliant with MRP-227-A Project stage: Other CNRO-2012-00004, Request for Additional Information Regarding Changes to the Entergy Quality Assurance Program Manual (QAPM) and Associated Plant Plant Technical Specifications Regarding Staff Qualifications2012-05-21021 May 2012 Request for Additional Information Regarding Changes to the Entergy Quality Assurance Program Manual (QAPM) and Associated Plant Plant Technical Specifications Regarding Staff Qualifications Project stage: Request ML12184A0372012-06-14014 June 2012 Reply to Request for Additional Information Regarding the License Renewal Application Project stage: Response to RAI ML12199A0252012-07-30030 July 2012 Project Manager Change for the License Renewal of Indian Point, Units 2 & 3 Project stage: Other ML12223A3882012-09-10010 September 2012 RAI for the Review of the Indian Pont Nuclear Generating Unit Nos. 2 and 3, LRA Set 2012-02 Project stage: RAI ML12223A3672012-09-12012 September 2012 Summary of Telephone Conference Call Held Between NRC and Entergy Nuclear Operations, Inc., Concerning RAI Set 2012-02, Reactor Vessel Internals Program Pertaining to the Indian Point, Units 2 & 3, License Renewal Application Project stage: RAI ML12270A3842012-09-26026 September 2012 Lr Hearing - Meeting Summary Project stage: Request ML12278A0772012-10-16016 October 2012 Request for Additional Information for the Review of the Indian Point Nuclear Generating Units 2 and 3, License Renewal Application, Set 2012-03 Project stage: RAI NL-12-140, Reply to Request for Additional Information Regarding the License Renewal Application2012-10-17017 October 2012 Reply to Request for Additional Information Regarding the License Renewal Application Project stage: Response to RAI NL-12-166, Reply to Request for Additional Information Regarding the License Renewal Application2012-11-20020 November 2012 Reply to Request for Additional Information Regarding the License Renewal Application Project stage: Response to RAI CNRO-2012-00009, Entergy Responses to Request for Additional Information Regarding Changes to the Quality Assurance Program Manual & Associated Plant Technical Specifications Re Staff Qualifications2012-11-20020 November 2012 Entergy Responses to Request for Additional Information Regarding Changes to the Quality Assurance Program Manual & Associated Plant Technical Specifications Re Staff Qualifications Project stage: Response to RAI ML13015A1752013-02-0606 February 2013 Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, LRA, Set 2013-01 Project stage: RAI ML15335A2722013-02-0606 February 2013 Official Exhibit - NRC000187-00-BD01 - Letter from John Daily, NRC, to Entergy, Request for Additional Information for the Review of the IP Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2013-01 (TAC Nos. MD5407 and Project stage: RAI ML15334A2562013-02-0606 February 2013 Official Exhibit - ENT000660-00-BD01 - Letter from J. Daly, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the IP Nuclear Generating Unit Nos. 2 and 3 LRA, Set 2013-01 (TAC Nos. MD5407 and Project stage: Request ML15223A2632013-02-0606 February 2013 NRC000187 - Letter from John Daily, NRC, to Entergy, Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2013-01 (TAC Nos. MD5407 and MD5408) Feb. 6, Project stage: RAI ML15222A8962013-02-0606 February 2013 ENT000660 - Letter from J. Daly, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3 License Renewal Application, Set 2013-01 (TAC Nos. MD54 Project stage: Request ML13043A5272013-02-26026 February 2013 PM Change Letter - February 2013 Project stage: Other ML13077A2842013-03-0808 March 2013 Correction PM Letter Indian Point Project stage: Other ML13067A3152013-03-0808 March 2013 Correction to Project Manager Change for the License Renewal of Indian Point, Units 2 and 3 (TAC Nos. MD5407 & MD5408) Project stage: Other ML13127A3762013-05-0707 May 2013 Errata to NRC Staff'S Proposed and Reply Findings of Fact and Conclusions of Law on Contention NYS-5 (Buried Piping and Tanks) Project stage: Request NL-13-052, Reply to Request for Additional Information Regarding the License Renewal Application2013-05-0707 May 2013 Reply to Request for Additional Information Regarding the License Renewal Application Project stage: Response to RAI ML13155A5042013-06-11011 June 2013 IP2-32-390 Request to Withhold-NL-12-166 Project stage: Other ML13162A6062013-06-12012 June 2013 Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2013-02 Project stage: RAI ML13186A1692013-07-17017 July 2013 Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2013 03 Project stage: RAI ML13134A3672013-07-19019 July 2013 PM Change Letter Project stage: Other ML13205A0222013-07-24024 July 2013 Lr Hearing - Telecon Summary for 7-19-13 Call on Drais for Rvi Program and Inspection Plan Project stage: Request ML15222A8982013-07-26026 July 2013 ENT000661 - Letter from K. Green, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3 License Renewal Application, Set 2013-04 (TAC Nos. MD5 Project stage: Request ML15334A2572013-07-26026 July 2013 Official Exhibit - ENT000661-00-BD01 - Letter from K. Green, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the IP Nuclear Generating Unit Nos. 2 and 3 Lr Application, Set 2013-04 (TAC Nos Project stage: Request ML13204A1992013-07-26026 July 2013 RAI for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2013-04 Project stage: RAI ML13240A0762013-09-0303 September 2013 RAI Set 2013-5 follow-up RAI on CP Project stage: RAI ML13270A2482013-09-27027 September 2013 Lr Hearing - IPEC License Renewal - Response to Set 2013-04 RAIs Project stage: Other ML13318A4502013-11-19019 November 2013 Request for Additional Information for the Review of the Indian Point Nuclear Generating, Units 2 and 3, License Renewal Application, Set 2013-06 Project stage: RAI NL-14-010, Units, 2 & 3 - Reply to Request for Additional Information Regarding the License Renewal Application2014-01-16016 January 2014 Units, 2 & 3 - Reply to Request for Additional Information Regarding the License Renewal Application Project stage: Response to RAI ML14027A4152014-01-16016 January 2014 Enclosure 2 to NL-14-010, Attachment 2, Final Response to U.S. NRC RAI 6-A Items 1 and 2 on the Rvi Program and Rvi Inspection Plan Project stage: Request NL-14-013, Additional Information Regarding the License Renewal Application - Action Item 7 from MRP-227-A2014-01-28028 January 2014 Additional Information Regarding the License Renewal Application - Action Item 7 from MRP-227-A Project stage: Other ML15160A2002014-01-28028 January 2014 NYS000503 - Dacimo, Fred, Entergy, Letter to Document Control Desk, USNRC, Reply to Request for Additional Information Regarding the License Renewal Application, NL-14-013 (January 28, 2014) (ML14038A150) Project stage: Response to RAI ML14084A3872014-04-0101 April 2014 Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2014-01 Project stage: RAI ML15334A2582014-04-0909 April 2014 Official Exhibit - ENT000662-00-BD01 - Letter from K. Green, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the IP Nuclear Generating Unit Nos. 2 and 3 LRA, Set 2014-02 (TAC Nos. MD5407 and Project stage: Request ML15222A9012014-04-0909 April 2014 ENT000662 - Letter from K. Green, NRC, to Vice President, Operations, Entergy, Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3 License Renewal Application, Set 2014-02 (TAC Nos. MD5 Project stage: Request ML14094A1732014-04-0909 April 2014 Request for Additional Information for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3, License Renewal Application, Set 2014-02 Project stage: RAI 2012-09-26
[Table View] |
Text
January 30, 2018 LICENSEE:
Entergy Nuclear Operations, Inc.
FACILITY:
Indian Point Unit Nos 2 and 3
SUBJECT:
SUMMARY
OF TELEPHONE CONFERENCE CALLS HELD ON NOVEMBER 30, 2017 AND DECEMBER 19, 2017, BETWEEN THE U.S.
NUCLEAR REGULATORY COMMISSION AND ENTERGY NUCLEAR OPERATIONS, INC., CONCERNING REQUESTS FOR ADDITIONAL INFORMATION PERTAINING TO THE INDIAN POINT LICENSE RENEWAL APPLICATION (TAC. NOS. MD5407/MD5408)
The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of Entergy Nuclear Operations, Inc. ( the applicant) held telephone conference calls on November 30, 2017, and December 19, 2017, to discuss and clarify the staffs requests for additional information (RAIs) and audit information concerning the Indian Point, license renewal application. The telephone conference calls were useful in clarifying the intent of the staffs RAIs and audit information.
provides a listing of the participants and Enclosure 2 contains a summary of the key issues addressed during the conference calls with the applicant.
The applicant had an opportunity to comment on this summary.
Sincerely,
/RA/
William Burton, Senior Project Manager License Renewal Project Branch Division of Materials and License Renewal Office of Nuclear Reactor Regulation Docket Nos.: 50-247 and 50-286
Enclosures:
- 1. List of Participants
- 2. Summary of Key Issues cc w/encls: See next page
ML18002A256 OFFICE PM:MRPB:DMLR LA:MRPB:DMLR BC:MRPB:DMLR NAME WBurton YEdmonds EOesterle DATE 1/30/2018 1/30/2018 1/30/2018
TELEPHONE CONFERENCE CALL INDIAN POINT LICENSE RENEWAL APPLICATION LIST OF PARTICIPANTS NOVEMBER 30, 2017 AND DECEMBER 19, 2017 November 30, 2017 Conference Call PARTICIPANTS AFFILIATION Charlie Caputo Entergy Nuclear Operations, Inc. (Entergy)
Alan Cox Entergy Tom Orlando Entergy Jim Gavula Nuclear Regulatory Commission (NRC)
Bill Holston NRC Brian Allik NRC
December 19, 2017 Conference Call PARTICIPANTS AFFILIATION Robert Walpole Entergy Nuclear Operations, Inc. (Entergy)
Alan Cox Entergy Tom Orlando Entergy Charles Caputo Entergy Steve Bloom Nuclear Regulatory Commission (NRC)
William Burton NRC Eric Oesterle NRC Jim Gavula NRC Bill Holston NRC Brian Allik NRC
TELEPHONE CONFERENCE CALL INDIAN POINT LICENSE RENEWAL APPLICATION NOVEMBER 30, 2017 AND DECEMBER 19, 2017 The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of Entergy Nuclear Operations, Inc. (Entergy) held telephone conference calls on November 30 and December 19, 2017, to discuss and clarify the staffs requests for additional information (RAIs) and audit information concerning the Indian Point license renewal application.
By letter dated May 8, 2017, Entergy provided responses (ADAMS Accession No. ML17132A175) to the NRC staffs Request for Additional Information (RAI) SET 2017-01 (ADAMS Accession No. ML17046A231). After reviewing Entergys RAI responses, the NRC staff conducted a supplemental, onsite regulatory audit from August 1 - 3, 2017, to gain a better understanding of Entergys RAI responses, and new plant-specific operating experience related to the Service Water Integrity aging management program. The NRC staffs audit report can be found at ADAMS Accession No. ML17250A244.
By [[letter::NL-17-127, Supplemental Information Regarding the Service Water Integrity Aging Management Program for the Review of the Indian Point Nuclear Generating Unit Nos. 2 and 3 License Renewal Application (LRA)|letter dated November 8, 2017]], Entergy provided supplemental information in response to the onsite regulatory audit (ADAMS Accession No. ML17321A079). After reviewing the supplemental information, the NRC staff held a teleconference with Entergy on November 30, 2017, to clarify Entergys responses to Audit Items 3 and 6. The specific discussion topics are provided below.
Audit Item 3: Entergys response states that the galvanic corrosion rates of carbon steel are expected to be similar when coupled to superaustenitic stainless steels (AL-6XN and Avesta 254 SMO) and 300-series stainless steels, because the corrosion potentials for superaustenitic stainless steels and 300-series stainless steels are similar. The staff notes that the magnitude of the difference in corrosion potential alone is not sufficient to predict the risk of galvanic corrosion, because there are a number of factors that affect the severity of galvanic corrosion (e.g., ratio of cathodic to anodic areas, temperatures, flow rates, conductivity of the electrolytes). Consequently, additional considerations may be needed if the various materials (AL-6XN, Avesta 254 SMO, and 300-series stainless steel) are combined into a single population. In order to be consistent with other IP AMPs, it is not clear to the staff whether the sample selection for galvanic corrosion will focus on the bounding or lead components that are most susceptible to aging based on time in service and severity of operation.
During the teleconference, Entergy stated that a sample will be selected that focuses on the bounding or lead components most susceptible to the aging mechanism.
Audit Item 6: Although Entergy developed new acceptance criteria for maintaining containment integrity due to potential service water leaks, the associated report (IP-RPT-17-00062) is not included as part of the Service Water Integrity Program. This is inconsistent with other aspects of the program where commitments were made to enhance the program to include other recently developed guidance documents. (See Audit Item 5 and the corresponding commitment associated with IP-RPT-16-00046).
During the teleconference, Entergy stated that IP-RPT-17-00062 will be included as part of the Service Water Integrity Program.
By letter dated December 14, 2017, Entergy provided additional information to clarify the areas identified in the audit report and that were discussed during the November 30, 2017, teleconference.
The NRC staff reviewed the responses in Entergys December 14, 2017, letter and held a teleconference with Entergy on December 19, 2017, to discuss final clarifications related to external carbon fiber repair and the definition of significant as it relates to additional volumetric non-destructive (NDE) to identify loss of material. The specific discussion topics are provided below.
- 1. For the weld location PAB-204 external carbon fiber repair, Entergy stated that (based on the proposed end date of April 30, 2025 for the renewed license for Indian Point Unit 3), the internal surface of the carbon fiber reinforced epoxy is not expected to be in contact with raw water prior to the end of the renewed license term. Entergy based its statement on a conservatively assumed corrosion rate of approximately 0.012 inches per year starting at the minimum measured wall thickness of 0.121 inches. However, LER 386/2002-001 describes a leaking service water pipe that did not provide sufficient structural integrity after 27 years, yielding a corresponding corrosion rate of approximately 0.014 inches per year. It is not clear to the staff that there is no need to manage aging effects associated with carbon-fiber wrap exposed to raw water. The staff and Entergy discussed potential periodic inspections to ensure that either the fiber-wrap is adhering to steel base metal or that loss of material in the welds has not gone through-wall.
Entergy stated that it will perform a volumetric examination at the location identified with the minimum wall thickness in 2016 to confirm that the carbon steel piping is not degrading at a rate that will result in exposure of the internal surface of the carbon fiber-reinforced epoxy to raw water prior to the end of the renewed license term. The volumetric examination will be performed prior to 12/31/21.
- 2. For the enhancement to the Service Water Integrity program associated with galvanic corrosion at flanged joints where insulating kits are not installed, Entergy stated that additional volumetric NDE will be performed if visual inspection identify significant loss of material. However, the applicant does not define significant.
During the teleconference, Entergy stated that it would consider clarifying the corrective actions in response to findings of visual inspections. In clarifying the criteria, Entergy indicated that it would consider the response to RAI 3.0.3-8 in letter dated December 16, 2014, regarding the response to findings of visual inspections.
- 3. The staff discussed information that they would need to complete their evaluation of aging effects associated with the internal coating on the steam jet air ejector piping discussed in the recent annual update letter. The staff noted that the coating is exposed to steam, an environment not covered in AMP XI.M42. Entergy stated that they would provide the type of coating material and a basis for why loss of coating integrity would not need to be managed (i.e., basis for no downstream flow effects, basis for no safety-related components in the vicinity that could be impacted by through-wall leakage). LRA BTable 3.3.2-19-4-IP2 will be updated.
On January 11, 2018, the NRC staff held a brief call with Entergy to clarify the timing of the volumetric examination. The staff noted that conducting a volumetric wall thickness inspection in the vicinity of weld PAB 204 prior to 12/31/21, could result in the inspection being conducted without a sufficient incubation period. The intent of conducting the examination is to be able to project the wall thickness to the end of the period of extended operation. Given the variability in wall lose rate throughout the service water system, the staff believes that the inspection should occur in the 2020 or 2021 time frame. Entergy agreed to perform the inspection in the 2020 or 2021 time frame.