IR 05000528/2016002
| ML16218A365 | |
| Person / Time | |
|---|---|
| Site: | Palo Verde |
| Issue date: | 08/05/2016 |
| From: | Geoffrey Miller NRC/RGN-IV/DRP/RPB-D |
| To: | Edington R Arizona Public Service Co |
| Charles Peabody | |
| References | |
| IR 2016002 | |
| Download: ML16218A365 (57) | |
Text
August 5, 2016
SUBJECT:
PALO VERDE NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000528/2016002, 05000529/2016002, AND 05000530/2016002
Dear Mr. Edington:
On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Palo Verde Nuclear Generating Station Units 1, 2, and 3. On July 14, 2016, the NRC inspectors discussed the results of this inspection with R. Bement and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.
NRC inspectors documented two findings of very low safety significance (Green) in this report.
Both of these findings involved violations of NRC requirements.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Palo Verde Nuclear Generating Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the at the Palo Verde Nuclear Generating Station.
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely, Geoffrey B. Miller, Branch Chief Project Branch D Division of Reactor Projects Docket Nos. 50-528, 50-529, 50-530 License Nos. NPF-41, NPF-51, NPF-74
Enclosure:
Inspection Report 05000528/2016002, 05000529/2016002, 05000530/2016002 w/ Attachment: Supplemental Information
/RA/ Agencywide Documents A
REGION IV==
Docket:
05000528, 05000529, 05000530 License:
NPF-41, NPF-51, NPF-74 Report:
05000528/2016002, 05000529/2016002, 05000530/2016002 Licensee:
Arizona Public Service Company Facility:
Palo Verde Nuclear Generating Station Location:
5801 South Wintersburg Road Tonopah, AZ 85354 Dates:
April 1 through June 30, 2016 Inspectors: C. Peabody, Senior Resident Inspector D. Reinert, PhD, Resident Inspector D. You, Resident Inspector L. Carson II, Senior Health Physicist J. Drake, Senior Reactor Inspector G. Pick, Senior Reactor Inspector I. Anchondo, Reactor Inspector N. Greene, PhD, Health Physicist G. Guerra, Emergency Preparedness Inspector D. Tailleart, Team Leader, Inspection and Regulatory Improvements Branch, Office of Nuclear Security and Incident Response Approved By:
Geoffrey B. Miller Chief, Project Branch D Division of Reactor Projects
- 2 -
SUMMARY
IR 05000528, 529, 530/2016002; 04/01/20106 - 06/30/2016; PALO VERDE NUCLEAR
GENERATING STATION INTEGRATED INSPECTION REPORT; Radiological Hazard Assessment and Exposure Controls; In-Plant Airborne Radioactivity Control and Mitigation.
The inspection activities described in this report were performed between April 1 and June 30, 2016, by the resident inspectors at Palo Verde Nuclear Generating Station and inspectors from the NRCs Region IV office and other NRC offices. Two findings of very low safety significance (Green) are documented in this report. Both of these findings involve violations of NRC requirements. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas.
Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.
Cornerstone: Occupational Radiation Safety
- Green.
The inspectors reviewed a Green, self-revealing, non-cited violation of Technical Specification 5.7.2, which was caused by the licensees failure to control a high radiation area with radiation levels greater than 1 rem per hour in the Unit 1 containment. A radiation protection technician received an unexpected dose rate alarm while conducting surveys on piping in the 87-foot elevation of the 2B reactor coolant pump bay area near a high efficiency particulate air unit in containment. Licensee personnel corrected the error by guarding the area, posting the area, and changing the pre-filters in the adjacent portable a high efficiency particulate air units to reduce the dose rates. This issue was entered into the licensees corrective action program as Condition Reports 16-06515 and 16-07479.
The inspectors determined that the failure to identify a locked high radiation area through timely surveys and adequate a high efficiency particulate air maintenance procedures that could have revealed changing radiological conditions was a performance deficiency. The performance deficiency was more than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation because licensee personnel did not implement barriers intended to prevent workers from receiving unexpected dose. Using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the violation had very low safety significance (Green) because: (1) it was not an as low as is reasonably achievable finding, (2) there was no overexposure, (3) there was no substantial potential for an overexposure, and (4) the ability to assess dose was not compromised. This finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, and procedures were available and adequate to support nuclear safety. Specifically, the licensee failed to ensure that procedures were adequate to ensure radiation levels around portable high efficiency particulate air units were monitored to evaluate changing radiological conditions in a timely manner such that hazards were appropriately controlled
[H.1]. (Section 2RS1)
- Green.
The inspectors identified a non-cited violation of 10 CFR 20.1701 due to the licensees failure to implement adequate processes and engineering controls necessary to reduce airborne radioactivity and prevent internal dose to workers in Unit 1. On April 20, 2016, inspectors identified that procedures and instructions for monitoring high efficiency particulate air ventilation filter unit to prevent worker exposures to radiation and airborne radioactivity were being inadequately implemented. On April 21, 2016, the licensees inadequate engineering and radiological controls during a high efficiency particulate air operations caused an airborne radioactivity event in containment, resulting in the evacuation of 41 potentially contaminated workers of whom 8 had measurable intakes of radioactive material. The licensees immediate corrective actions included stopping work in the Unit 1 containment, evacuating workers in containment, assessing workers for external and internal contamination, and investigating the cause and source of the contamination event. This matter was placed in the licensees corrective action program as Condition Reports16-06499 and 16-06578 and the licensee initiated a root cause investigation.
The inspectors determined that the failures to implement adequate engineering and radiological controls to reduce airborne radioactivity during a high efficiency particulate air unit operations in accordance with 10 CFR 20.1701 and radiation protection procedures were performance deficiencies. The performance deficiencies were more than minor because they were associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. This was evident by the Unit 1 containment airborne radioactivity event on April 21, 2016, that resulted in at least eight workers with unplanned intakes. Using Inspection Manual Chapter 0609,
Appendix CProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix C" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the finding had very low safety significance (Green) because: (1) it was not an as low as is reasonably achievable planning and controls finding, (2) there was no overexposure, (3) there was no substantial potential for an overexposure, and (4) the ability to assess dose was not compromised. The inspectors concluded that the finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, procedures, and other resources were available and adequate to support nuclear safety. Specifically, procedures and radiation exposure permits failed to have adequate instructions for ensuring a high efficiency particulate air filter loading and dose rates were monitored to prevent overloading, and safe handling of loaded a high efficiency particulate air filters [H.1]. (Section 2RS3)
PLANT STATUS
Unit 1 entered the inspection period at full power and was shutdown for a refueling outage on April 8, 2016. Unit 1 restarted from their refueling outage on May 14, 2016, and returned to full power on May 18, 2016. On May 19-24, 2016, power was reduced to 39 percent to repair a main condenser tube leak. On June 22-25, 2016, power was reduced to 82 percent to repair a heater drain pump discharge valve. Unit 1 operated at full power for the remainder of the inspection period.
Unit 2 operated at full power for the duration of the inspection period.
Unit 3 operated at full power for the duration of the inspection period.
REPORT DETAILS
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
.1 Summer Readiness for Offsite and Alternate AC Power Systems
a. Inspection Scope
On June 6, 2016, the inspectors completed an inspection of the stations off-site and alternate-ac power systems. The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment to verify that plant features and procedures were appropriate for operation and continued availability of off-site and alternate-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems. The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors verified that the licensees procedures included appropriate measures to monitor and maintain availability and reliability of the off-site and alternate-ac power systems.
These activities constituted one sample of summer readiness of off-site and alternate-ac power systems, as defined in Inspection Procedure 71111.01.
b. Findings
No findings were identified.
1R04 Equipment Alignment
.1 Partial Walkdown
a. Inspection Scope
The inspectors performed partial system walk-downs of the following risk-significant systems:
- April 11, 2016, Unit 1, containment purge A
- May 2, 2016, Unit 3, turbine driven auxiliary feedwater pump
- May 4, 2016, Unit 3, diesel generator A
- May 4, 2016, Unit 3, diesel generator B
The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.
These activities constituted four partial system walk-down samples as defined in Inspection Procedure 71111.04.
b. Findings
No findings were identified.
.2 Complete Walkdown
a. Inspection Scope
On May 27, 2016, the inspectors performed a complete system walk-down inspection of the Unit 3 fuel building essential ventilation system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed open condition reports, temporary modifications, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.
These activities constituted one complete system walk-down sample, as defined in Inspection Procedure 71111.04.
b. Findings
No findings were identified.
1R05 Fire Protection
.1 Quarterly Inspection
a. Inspection Scope
The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on five plant areas important to safety:
- April 18, 2016, Unit 2 high pressure safety injection room, fire zone 31B
- April 25, 2016, Unit 3 auxiliary feedwater pump N, fire zone TB-1
- April 26, 2016, Unit 1 containment building SI-651 work area
- May 10, 2016, Unit 3 fuel building 100 elevation, fire zone 27
- June 21, 2016, Unit 1 cable spreading room 140 elevation, fire zone 14 For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
These activities constituted five quarterly inspection samples, as defined in Inspection Procedure 71111.05.
b. Findings
No findings were identified.
1R06 Flood Protection Measures
a. Inspection Scope
On June 27, 2016, the inspectors completed an inspection of the stations ability to mitigate flooding due to internal causes. After reviewing the licensees flooding analysis, the inspectors chose a plant area containing risk-significant structures, systems, and components that were susceptible to flooding:
- Unit 3 condensate storage tank tunnel
The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.
These activities constitute completion of one flood protection measures sample as defined in Inspection Procedure 71111.06
b. Findings
No findings were identified.
1R07 Heat Sink Performance
a. Inspection Scope
On June 7, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed the licensees implementation of biofouling controls for the Unit 2 spray pond. Additionally, the inspectors walked down the Unit 2 train A and B Essential Cooling Water heat exchangers to observe their performance and material condition.
These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
b. Findings
No findings were identified.
1R08 Inservice Inspection Activities
The activities described in Subsections 1 through 4 below constitute completion of one inservice inspection sample, as defined in Inspection Procedure 71111.08.
.1 Non-destructive Examination Activities and Welding Activities
a. Inspection Scope
The inspectors directly observed the following nondestructive examinations:
System Weld Identification Examination Type Steam Generator SGE L008-W2 Ultrasonic Steam Generator SGE L008-W3 Ultrasonic Charging CHE W28 Penetrant Charging CHE W29 Penetrant Reactor Coolant System 1PRCEL046 Visual 3 Reactor Coolant System 1PRCEL036 Visual 3 Feedwater 1PSGE011 Weld 59-24 Magnetic Particle Feedwater 1PSGE011 Weld 59-25 Magnetic Particle Steam generator SGE L008-W6 Radiograph
The inspectors reviewed records for the following nondestructive examinations:
System Weld Identification Examination Type Steam Generator SGE L008-W2 Radiograph Steam Generator SGE L008-W3 Radiograph Feedwater 1PSEIL223 Weld 11-10/24-1 Penetrant Safety Injection Weld 15-9 Penetrant Safety Injection UV-651 Visual 3 Essential Cooling Water EWB-E01-W Visual 1 System Weld Identification Examination Type Essential Chill Water ECB-E-1-W Visual 1
During the review and observation of each examination, the inspectors observed whether activities were performed in accordance with the American Society of Mechanical Engineers (ASME) Code requirements and applicable procedures. The inspectors also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current.
The inspectors directly observed a portion of the following welding activities:
System Weld Identification Weld Type Steam Generator W-6 Gas Tungsten Arc Welding
The inspectors reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code Section IX requirements.
The inspectors also determined whether the essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications.
b. Findings
No findings were identified.
.2 Reactor Vessel Upper Head Penetration Inspection Activities
a. Inspection Scope
No inspection of the reactor vessel upper head penetrations was performed in this outage.
b. Findings
No findings were identified.
.3 Boric Acid Corrosion Control Inspection Activities
a. Inspection Scope
The inspectors reviewed the licensees implementation of its boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walk-down as specified in Procedure 73DP-9ZC01, Boric Acid Corrosion Control Program, Revision 7. The inspectors reviewed whether the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components, and whether engineering evaluation used corrosion rates applicable to the affected components and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity. The inspectors observed whether corrective actions taken were consistent with the ASME Code, and 10 CFR 50, Appendix B requirements.
b. Findings
No findings were identified, there was one unresolved item.
c.
Unresolved Item 05000528/2016002-01, Leakage from Reactor Coolant Pump 2B Discharge Pipe Instrument Nozzle
Introduction.
The inspectors identified an unresolved item for pressure boundary leakage from reactor coolant pump 2B discharge pipe instrument nozzle.
Description.
On April 10, 2016, during the Unit 1 Refueling Outage 19, the licensee discovered reactor coolant system pressure boundary leakage at instrument nozzle 1JRCETW0121Y on the 2B reactor coolant pump discharge piping. The leakage was discovered during a planned visual inspection of Unit 1 hot and cold leg nozzles. The leak was not detectable by either the reactor coolant system leak rate procedure or the containment radiation monitor trend reviews while the unit was operating. Additionally, the leak had not been visually detected during the previous refueling outage. The leakage was consistent with a small leak characterized by moderate boric acid accumulation at the leakage site. The licensee determined that the cause of the leakage was primary water stress corrosion cracking of the Alloy 600 instrument nozzle. The licensee corrected the leakage using a mechanical nozzle seal assembly repair method utilizing ASME Code Case N-733, Mitigation of Flaws in NPS 2 (DN 50) and Smaller Nozzles and Nozzle Partial Penetration Welds in Vessels and Piping by Use of a Mechanical Connection Modification,Section XI, Division 1. The evaluation of the 2B cold leg RTD nozzle leakage is being evaluated by the licensee as part of Palo Verde Action Request 15-01640-012. The inspectors reviewed the circumstances surrounding the discovery of the leak and observed portions of the repair activity during the refueling outage. Once the licensee completes their evaluation, the inspectors will review and complete an inspection to determine if a performance deficiency exists as a result of the nozzle failure.
.4 Steam Generator Tube Inspection Activities
a. Inspection Scope
The inspectors reviewed the steam generator tube eddy current examination scope and expansion criteria to determine whether these criteria met technical specification requirements, Electric Power Research Institute (EPRI) guidelines, and commitments made to the NRC. The inspectors also reviewed whether the inspection scope included areas of degradations that were known to represent potential eddy current test challenges such as the top of tube sheet, tube support plates, and U-bends. The licensee plugged 23 tubes in each steam generator.
Steam Generator Inspection
- Inspectors verified that the number and sizes of steam generator tube flaws/degradation identified was consistent with the licensees previous outage operational assessment predictions.
- Inspectors verified that steam generator eddy current examination scope and expansion criteria met technical specification requirements.
- Inspectors verified that eddy current probes and equipment configurations used to acquire data from the steam generator tubes were qualified to detect the known/expected types of steam generator tube degradation in accordance with Appendix H, Performance Demonstration for Eddy Current Examination of EPRI Document 1013706.
The inspectors reviewed the licensees identification of the following tube degradation mechanisms:
- Mechanical wear at tube support structures
Tube Repair
- The inspectors verified that the licensee implemented repair methods which were consistent with the repair processes allowed in the plant technical specification requirements and determined qualified depth sizing methods were applied to degraded tubes accepted for continued service.
Secondary Side Inspections
- The inspectors reviewed secondary side inspection results and verified the licensee took corrective actions in response to the observed degradation.
- At the time of the inspection, no loose parts or foreign material on the steam generator secondary side were identified or left in place.
b. Findings
No findings were identified.
.5 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed 23 Palo Verde action requests which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. From this review the inspectors concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection operating experience. Specific documents reviewed during this inspection are listed in the attachment.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
.1 Review of Licensed Operator Requalification
a. Inspection Scope
On May 31, 2016, the inspectors observed simulator training for an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the training activities.
These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11
b. Findings
No findings were identified.
.2 Review of Licensed Operator Performance
a. Inspection Scope
On April 9-10, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity due to a plant shutdown for refueling outage. The inspectors observed the operators performance of the following activities:
- Plant shutdown briefs, including the pre-job brief, turnover brief, and reactivity maneuver plan brief, reactor trip brief, and plant cooldown brief
- Control rod bank insertions
- Reactor coolant system borations
- Main turbine load reductions
- Manual reactor trip from 30 percent reactor power
- Initiation of reactor cooldown following reactor trip
In addition, the inspectors assessed the operators adherence to plant procedures, including the conduct of operations procedure and other operations department policies.
These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed three instances of degraded performance or condition of safety-related structures, systems, and components (SSCs):
- May 3, 2016, Units 1, 2, and 3, emergency lighting charge card unreliability issues due to obsolescence
- May 25, 2016, Unit 1 spent fuel pool cooling heat exchanger unavailability due to inability to complete eddy current testing
- June 28, 2016, Units 1, 2, and 3, essential cooling water system ability to transfer heat from the reactor coolant system to the spray pond system The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
These activities constituted completion of three maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
- April 14, 2016, Unit 1 outage daily risk assessment
- May 10, 2016, Unit 1 outage daily risk assessment
- June 20-26, 2016, Unit 1 weekly risk assessment
- June 20-26, 2016, Unit 3 weekly risk assessment
The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.
The inspectors also observed portions of two emergent work activities that had the potential to cause an initiating event or to affect the functional capability of mitigating systems:
- May 17, 2016, Unit 1 diesel generator A emergent troubleshooting work activities following failed surveillance test
- May 20, 2016, Unit 1 downpower for circulating water leak in condenser and startup transformer work The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components (SSCs).
These activities constitute completion of six maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
The inspectors reviewed six operability determinations and functionality assessments that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):
- April 4, 2016, Unit 3 operability determination of spray pond conduit bolts
- April 23, 2016, Unit 1 operability determination of pressurizer safety valve pipe stress impact evaluation following a rigging error
- May 18, 2016, Units 1, 2, and 3, operability determination regarding containment radiation monitor surveillance testing validation of technical specification 3.4.16 required safety functions
- May 24, 2016, Unit 1 operability determination of safety injection piping following detection of gas void
- June 1, 2016, Unit 2 operability determination of diesel generator A degraded fuel oil surge tank bolting
- June 26, 2016, station blackout generators 1 and 2 functionality assessment following loss of battery charger The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable or functional, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded SSC.
These activities constitute completion of six operability and functionality review samples, as defined in Inspection Procedure 71111.15.
b. Findings
No findings were identified.
1R18 Plant Modifications
a. Inspection Scope
On May 11, 2016, the inspectors reviewed a permanent modification to Unit 1 shutdown cooling suction isolation valve SI-651.
The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified.
These activities constitute completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed five post-maintenance testing activities that affected risk-significant structures, systems, or components (SSCs):
- May 13, 2016, Unit 1 post maintenance testing of high pressure injection check valve SIE-V133
- May 24, 2016, Unit 1 control element assembly rod drop testing following assembly replacement
- June 7, 2016, Unit 3 battery charger PK11 relay replacement
- June 10, 2016, station blackout generator 1 testing following replacement of the fuel oil transfer pump
- June 22, 2016, Unit 2 post maintenance testing of auxiliary feedwater B injection valve to steam generator 2 following lubrication and electrical testing The inspectors reviewed licensing-and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.
These activities constitute completion of five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
During the stations refueling outage that concluded on May 14, 2016, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions.
This verification included the following:
- Review of the licensees outage plan prior to the outage
- Review and verification of the licensees fatigue management activities
- Monitoring of shut-down and cool-down activities
- Verification that the licensee maintained defense-in-depth during outage activities
- Observation and review of fuel handling activities
- Monitoring of heat-up and startup activities
These activities constitute completion of one refueling outage sample, as defined in Inspection Procedure 71111.20.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:
In-service tests:
- June 6, 2016, Unit 2 bypass steam Supply to turbine driven auxiliary feedwater pump DC motor operated valve static test
Containment isolation valve surveillance tests:
- April 26, 2016, Unit 1 high pressure nitrogen supply containment penetration 30 Other surveillance tests:
- May 2, 2016, Unit 1 containment sump calibration
- May 18, 2016, Unit 2 containment atmospheric radioactivity monitor quarterly functional test
- May 27, 2016, Unit 3 fuel building essential ventilation B operability
- June 6, 2016, Unit 1 control element assembly operability The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
These activities constitute completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22
b. Findings
No findings were identified.
1EP2 Alert and Notification System Evaluation
a. Inspection Scope
The inspectors verified the adequacy of the licensees methods for testing the primary and backup alert and notification system (ANS). The inspectors also reviewed the licensees program for identifying emergency planning zone locations requiring tone alert radios and for distributing the radios. The inspectors interviewed licensee personnel responsible for the maintenance of the primary and backup ANS and reviewed a sample of corrective action system reports written for ANS problems. The inspectors compared the licensees alert and notification system testing program with criteria in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1; FEMA Report REP-10, Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants; and the licensees current FEMA-approved alert and notification system design report, Palo Verde Nuclear Generating Station FEMA 350 Report, revised July 2014.
These activities constituted completion of one alert and notification system evaluation sample as defined in Inspection Procedure 71114.02.
b. Findings
No findings were identified.
1EP3 Emergency Response Organization Staffing and Augmentation System
a. Inspection Scope
The inspectors verified the licensees emergency response organization on-shift and augmentation staffing levels were in accordance with the licensees emergency plan commitments. The inspectors reviewed documentation and discussed with licensee staff the operability of primary and backup systems for augmenting the on-shift emergency response staff to verify the adequacy of the licensees methods for staffing emergency response facilities, including the licensees ability to staff pre-planned alternate facilities.
The inspectors also reviewed records of emergency response organization augmentation tests and events to determine whether the licensee had maintained a capability to staff emergency response facilities within emergency plan timeliness commitments.
These activities constituted completion of one emergency response organization staffing and augmentation testing sample as defined in Inspection Procedure 71114.03.
b. Findings
No findings were identified.
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspectors performed an in-office on-site review of Palo Verde Emergency Plan, Revision 56. This revision included the description of changes to 10 CFR Part 50, Appendix E, related to emergency plan change submittals.
This revision was compared to its previous revision, to the criteria of NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the requirements of 10 CFR 50.54(q)(3) and 50.54(q)(4). The inspectors verified that the revision did not reduce the effectiveness of the emergency plan. This review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.
These activities constituted completion of one emergency action level and emergency plan changes sample as defined in Inspection Procedure 71114.04.
b. Findings
No findings were identified.
1EP5 Maintenance of Emergency Preparedness
a. Inspection Scope
The inspectors reviewed the following for the period February 2014 to April 2016:
- After-action reports for emergency classifications and events
- After-action evaluation reports for licensee drills and exercises
- Independent audits and surveillances of the licensees emergency preparedness program
- Self-assessments of the emergency preparedness program conducted by the licensee
- Licensee evaluations of changes made to the emergency plan and emergency plan implementing procedures
- Drill and exercise performance issues entered into the licensees corrective action program
- Emergency preparedness program issues entered into the licensees corrective action program
- Records of evacuation time estimate population evaluation and annual evaluation reviews of the emergency planning zone population
- Maintenance records for equipment supporting the emergency preparedness program
- Emergency response organization and emergency planner training records
The inspectors reviewed summaries of 1,060 corrective action program reports associated with emergency preparedness, and selected 43 to review against program requirements, to determine the licensees ability to identify, evaluate, and correct problems in accordance with planning standard 10 CFR 50.47(b)(14) and 10 CFR Part 50, Appendix E, Section IV.F. The inspectors verified that the licensee accurately and appropriately identified and corrected emergency preparedness weaknesses during critiques and assessments.
These activities constituted completion of one sample of the maintenance of the licensees emergency preparedness program as defined in Inspection Procedure 71114.05.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Public Radiation Safety and Occupational Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
The inspectors evaluated the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, performed independent radiation dose rate measurements, and observed postings and physical controls. The inspectors reviewed licensee performance in the following areas:
- Radiological hazard assessment, including a review of the plants radiological source terms and associated radiological hazards. The inspectors also reviewed the licensees radiological survey program to determine whether radiological hazards were properly identified for routine and non-routine activities and assessed for changes in plant operations.
- Instructions to workers including radiation work permit requirements and restrictions, actions for electronic dosimeter alarms, changing radiological conditions, and radioactive material container labeling.
- Contamination and radioactive material control, including release of potentially contaminated material from the radiologically controlled area, radiological survey performance, radiation instrument sensitivities, material control and release criteria, procedural guidance, and control and accountability of sealed radioactive sources.
- Radiological hazards control and work coverage. During walk downs of the facility and job performance observations, the inspectors evaluated ambient radiological conditions, radiological postings, adequacy of radiological controls, radiation protection job coverage, and contamination controls. The inspectors also evaluated dosimetry selection and placement as well as the use of dosimetry in areas with significant dose rate gradients. The inspectors examined the licensees controls for items stored in the spent fuel pool and evaluated airborne radioactivity controls and monitoring.
- High radiation area and very high radiation area controls. During plant walk downs, the inspectors verified the adequacy of posting and physical controls, including areas of the plant with the potential to become risk-significant high radiation areas.
- Radiation worker performance and radiation protection technician proficiency with respect to radiation protection work requirements. The inspectors determined if workers were aware of significant radiological conditions in their workplace, radiation work permit controls/limits in place, and electronic dosimeter dose and dose rate set points. The inspectors observed radiation protection technician job performance, including the performance of radiation surveys.
- Problem identification and resolution for radiological hazard assessment and exposure controls. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
These activities constituted completion of the seven required samples of radiological hazard assessment and exposure control program, as defined in Inspection Procedure 71124.01.
b. Findings
Introduction.
The inspectors reviewed a Green, self-revealing, non-cited violation of Technical Specification 5.7.2, which was caused by the licensees failure to control a high radiation area with radiation levels greater than 1 rem per hour in the Unit 1 containment.
Description.
On April 20, 2016, while performing a pre-job survey to characterize the radiological conditions associated with a valve-repacking job, a radiation protection technician (RPT) received a dose rate alarm on the 87-foot elevation of the containment building in the 2B reactor coolant pump (RCP) bay area. According to his alarming dosimeter, the maximum dose rate encountered by the RPT was 595 millirem per hour.
The RPT entered the area on Task 2 of Radiation Exposure Permit (REP)1-3502, Valve, Flange, and Pump Maintenance and Inspection. Task 2 of this REP allowed entry into a high radiation area, but did not allow entry into a locked high radiation area (LHRA). This REP also had a dose rate alarm setpoint of 120 millirem per hour.
As the RPT was surveying the piping area around valve 1PRECEV332, he noticed a high-efficiency particulate air (HEPA) unit sitting off by itself near one of the piping structures. The HEPA unit was stationed off the steam generator 2 exhaust. As the RPT leaned toward the HEPA unit, he received the dose rate alarm. The RPT measured the HEPA pre-filter with a survey meter and it read 5 rem per hour on contact and 1.2 rem per hour at 30 centimeters. This was confirmed by a second RPTs independent measurement. As instructed by the REP, the RPT stopped his work and informed RP supervision and the Unit 1 containment desk that LHRA conditions (dose rates greater than 1 rem per hour) were unexpectedly identified in the 2B RCP bay area.
The RPT guarded the area until other Palo Verde RPTs took over. These dose rates were documented on Survey 1-M-20160420-38, dated April 20, 2016.
According to the Exposure Evaluation Form from the dose rate alarm and the Unit 1 containment desk and rover logs, as documented in Condition Report (CR) 16-007479, this LHRA condition was identified around 9:46 p.m. (when the dose rate alarm occurred) and documented at 10:14 p.m. on April 20, 2016. The desk logs stated that three radiation protection technicians were briefed to enter the LHRA, in the 1B and 2B reactor coolant pump bay areas of the Unit 1 containment, to change the pre-filters around 10:17 p.m. on April 20, 2016. No log entries confirmed that the licensee had routinely stationed a radiation protection technician or guarded the LHRA until 7:02 p.m.
on April 22, 2016. However, verbal discussions indicate that radiation protection coverage occurred prior to this log entry.
Because it is unknown how long the LHRA conditions existed prior to discovery, the inspectors concluded that LHRA conditions existed in the 2B RCP bay area for an undetermined amount of time. As documented in the logs, the pre-filters on the HEPA unit were changed at 10:05 p.m. on April 22, 2016. The LHRA guards were released shortly after this time. The inspectors concluded that this issue may have been prevented if procedures were implemented to maintain dose rates on the portable HEPA units lower. The licensee had not provided specific instructions to monitor dose rates to allow for timely filter change-outs before the HEPA filters became excessively loaded with radioactivity.
Section 4.4 of licensee procedure 75RP-9OP02, Control of High Radiation Areas, Locked High Radiation Areas, and Very High Radiation Areas, Revision 27, requires that access controls to locked high radiation areas are maintained by LHRA doors being locked to prevent unauthorized entry or LHRA flashing lights are installed and functioning. The procedure requires physical barriers to provide assurance that the LHRA is secure against unauthorized access that cannot be easily circumvented. As stated above, the NRC inspectors could not confirm the LHRA identified was properly controlled for a period of time.
As immediate corrective actions, the radiation protection technician informed the radiation protection supervision of the issue, radiation protection technicicans guarded the LHRA until the HEPA pre-filters were removed, and the LHRA was eventually properly posted and controlled. This issue was entered into the licensees corrective action program as Condition Reports 16-06515 and 16-07479.
Analysis.
The inspectors determined that the failure to identify a LHRA through timely surveys and adequate procedures for HEPA unit operations that could have revealed changing radiological conditions was a performance deficiency. The performance deficiency was more than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation because licensee personnel did not implement barriers intended to prevent workers from receiving unexpected doses. Using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the violation had very low safety significance (Green) because:
- (1) it was not an ALARA finding,
- (2) there was no overexposure,
- (3) there was no substantial potential for an overexposure, and
- (4) the ability to assess dose was not compromised. This finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, and procedures were available and adequate to support nuclear safety. Specifically, the licensee failed to ensure that procedures were adequate to ensure radiation levels around portable HEPA units were monitored to evaluate changing radiological conditions in a timely manner such that hazards were appropriately controlled [H.1].
Enforcement.
Technical Specification 5.7.2 states, in part, that individual areas with radiation levels greater than or equal to 1 rem per hour (at 30 centimeters from the radiation source), accessible to personnel, that are located within large areas such as reactor containment, where no enclosure exists for purposes of locking, or that is not continuously guarded, and where no enclosure can be reasonably constructed around the individual area, shall be barricaded and conspicuously posted, and a flashing light shall be activated as a warning device. Contrary to the above, on April 20, 2016, an area with radiation levels greater than 1 rem per hour (at 30 centimeters from the radiation source), accessible to personnel, located within the Unit 1 reactor containment where no enclosure existed for purposes of locking, was not barricaded and conspicuously posted and a flashing light was not activated as a warning device for the area. Specifically, LHRA controls were not established in the piping area around valve 1PRECEV332 near a HEPA unit in the 2B RCP bay area in the 87-foot elevation of the Unit 1 containment. NRC inspectors concluded this condition existed for an undetermined amount of time before radiation protection established adequate controls.
The licensee documented the event in the corrective action program and logged the occurrence in their Unit 1 containment desk logs. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy. The violation was entered into the licensees corrective action program as CR 16-06515 and 16-07479: NCV 05000528/2016002-02, Failure to Implement High Radiation Area Controls in an Area with a Dose Rates Greater Than 1 Rem per Hour.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
a. Inspection Scope
The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, and reviewed licensee performance in the following areas:
- Engineering controls, including the use of permanent and temporary ventilation systems to control airborne radioactivity. The inspectors evaluated installed ventilation systems, including review of procedural guidance, verification the systems were used during high-risk activities, and verification of airflow capacity, flow path, and filter/charcoal unit efficiencies. The inspectors also reviewed the use of temporary ventilation systems used to support work in contaminated areas such as HEPA/charcoal negative pressure units. Additionally, the inspectors evaluated the licensees airborne monitoring protocols, including verification that alarms and set points were appropriate.
- Use of respiratory protection devices, including an evaluation of the licensees respiratory protection program for use, storage, maintenance, and quality assurance of NIOSH certified equipment, air quality and quantity for supplied-air devices and self-contained breathing apparatus (SCBA) bottles, qualification and training of personnel, and user performance.
- Self-contained breathing apparatus (SCBA) for emergency use, including the licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, hydrostatic testing of SCBA bottles, status of SCBA staged and ready for use in the plant including vision correction, mask sizes, etc., SCBA surveillance and maintenance records, and personnel qualification, training, and readiness.
- Problem identification and resolution for airborne radioactivity control and mitigation. The inspectors reviewed audits, self-assessments, and corrective action documents to verify problems were being identified and properly addressed for resolution.
These activities constituted completion of the four required samples of in-plant airborne radioactivity control and mitigation program, as defined in Inspection Procedure 71124.03.
b. Findings
Introduction.
The inspectors identified a non-cited violation of 10 CFR 20.1701 due to the licensees failure to implement adequate processes and engineering controls necessary to reduce airborne radioactivity. Subsequently, an airborne event in the Unit 1 containment building resulted of 41 individuals being evacuated from containment, eight of whom had measureable intakes of radioactive material.
Description.
On April 20, 2016, the inspectors identified that procedures and instructions for monitoring portable high efficiency particulate air (HEPA) ventilation filters to prevent worker exposures to radiation and airborne radioactivity were not being implemented adequately. On April 21, 2016, the licensees inadequate engineering and radiological controls during HEPA filtration unit operations caused an airborne radioactivity event in the Unit 1 containment, resulting in the evacuation of 41 potentially contaminated workers.
During the Unit 1 Refueling Outage 19, the inspectors reviewed the licensees implementation of radiation protection Procedure 75DP-0RP05, Revision 6, Control of Portable Air Filtration Systems. The inspectors focused on the following parts:
- Section 4.4, Portable Filter System Operational Checks
- Section 4.5, Radiological Controls for Portable Filtration
- Section 5.3, Records
- Appendix A, Portable Filtration Unit Daily Operational Checks
The inspectors reviewed six operational checklists from HEPA units that were in-service during the Unit 1 outage or that had been recently placed in-service during April 2016.
The records (Appendix A Checks) reviewed included HEPA filter installations in the following locations:
- Unit 1 steam generator 1 and 2 on the 87-foot elevation
- Unit 1 shutdown heat exchanger on the 70-foot elevation
- Unit 1 hot machine
- Dry active waste process and storage facility
Inspectors noted that licensee radiation protection technicians, generally, had entered the daily HEPA unit differential pressure data on the checklist and initialed this task as an indication that pre-filter and HEPA units were not loaded up, blocked, and had no filter breakthrough. Initials on the checklists were indications that radiation protection technicians (RPTs) had:
- Performed a radiation survey of the filter housing to ensure that general area dose rates are not affected
- Assessed the need for a filter change based on differential pressure and impact on general area dose rates
The inspectors reviewed radiation surveys, contamination surveys, and air sample results associated with HEPA unit operations for the week of April 18-22, 2016.
Inspectors found that RPTs had not initialed the daily HEPA unit data checklist on April 20 and April 21 for the HEPA unit located at the Unit 1 steam generator 2 area.
Additionally, radiation protection technicians did not initial the daily HEPA unit differential data checklist on April 21 for the HEPA unit located at the Unit 1 steam generator 1 area.
These omissions by the radiation protection technicians were not in accordance with Procedure 75DP-0RP05, Section 4.4.
Section 4.5, Radiological Controls for Portable Filtration, and Subsection 4.5.1 of this procedure stated, Verify efficiency of the HEPA filter daily when in service by one or more of the following methods:
- Portable air sampling in the affected room or area
- Continuous air sampling in the affected room or area using an AMS-4 or equivalent
- Contamination survey at the discharge of the portable filtration unit
The inspectors asked how RPTs specifically decided when to change out pre-filter and HEPA filters based on radiation surveys and general area dose rates. Licensee staff explained that RPTs would change the HEPA filter based on the results of their filter checks, surveys, and monitoring. The inspectors noted that none of the radiation exposure permits associated with the Unit 1 steam generators or shutdown heat exchangers provided specific instructions on changing pre-filter and HEPA filters based on radiological conditions. Procedure 75DP-0RP05 was not specific on changing filters based on radiological conditions.
The inspectors examined two radiation and contamination survey records, dated April 20, 2016, that were performed. Survey 1-M-20160420-22 recorded data for the steam generator 1 and steam generator 2 HEPA units at 3:39 p.m. The steam generator 1 pre-filter had a contact reading of 3,500 millirem per hour on contact and a 550 millirem per hour reading at 30 centimeters. The steam generator 1 HEPA filter had a contact radiation reading of 500 millirem per hour and a 30 centimeters reading of 100 millirem per hour. The HEPA filter also had a discharge contamination reading of 5,000 disintegrations per minute. During this same time (3:39 p.m.), the steam generator 2 pre-filter had a contact radiation reading of 2,400 millirem per hour and a 30 centimeters reading of 350 millirem per hour. The steam generator 2 HEPA filter measured 350 millirem per hour on contact and 100 millirem per hour at 30 centimeters.
The steam generator 2 HEPA filter had a discharge contamination reading of 50,000 disintegrations per minute. By 10:53 p.m. on April 20, 2016, the steam generator 2 pre-filter and HEPA filter assembly had a contact radiation reading of 5,000 millirem per hour and a 30 centimeters reading of 1,200 millirem per hour.
Licensee supervision explained that it would have been their expectation that the pre-filter and HEPA filter change-outs would have occurred before the discharge contamination levels reached 5,000 dpm and before the radiation levels in the area approached 1,000 millirem per hour. However, radiation protection management acknowledged that Procedure 75DP-0RP05 and radiation exposure permits did not have specific instructions on when pre-filter and HEPA filter change outs were required.
Overall, the inspectors determined that the portable filtration unit daily operational check frequencies were insufficient radiological controls. The inspectors concluded that the lack of specific instructions in Procedure 75DP-0RP05 and the radiation exposure permits used to monitor and change out HEPA pre-filters represented a lack of practical processes or other engineering controls necessary to reduce the concentration of radioactive material in air.
At 10:17 p.m. on April 20, 2016, the licensee had an ALARA pre-job meeting to change out the pre-filters to the steam generator 1 and steam generator 2 HEPAs in the Unit 1 containment building, on the 87-foot elevation. Early in the morning of April 21, 2016, the licensee changed out the pre-filters to the steam generator 1 and steam generator 2 HEPA units. However, there were indications of elevated airborne radioactivity in containment. The Unit 1 plant vent radiation monitor RU-143 went into an alarming mode. Simultaneously, several continuous air monitors located in Unit 1 containment went into the alarm mode. The licensee evacuated at least 41 workers from the containment building. Nine workers alarmed the personnel contamination monitors and eight workers were sent to dosimetry for whole body counting. Unit 1 outage work in the containment building was suspended pending an investigation to identify the actual source of the airborne contamination event. The licensees initial investigation identified the following:
- The source of the radioactivity was the pre-filter HEPA unit at steam generator 2 associated with eddy current testing sludge material overloading
- A radiation protection technician had placed a plastic bag over the Y-connector that later got sucked into the HEPA filter, disabling the unit
- Procedure 75DP-0RP05, Appendix A, Portable Filtration Unit Daily Operational Checks, failed to identify a reduction in the HEPA units performance
- The radiation protection technicians monitoring of radiological indicators associated with the HEPA units operations failed to identify any problems
The inspectors also determined that radiation protection Procedure 75DP-0RP05, Revision 6, Control of Portable Air Filtration Systems, as written was inadequate.
Engineering and radiological controls that the licensee had implemented in accordance with RG 8.8, Section 2(d), and 10 CFR 20.1701 were insufficient to mitigate and control the concentration of radioactive material in air. Pre-filter and HEPA unit checks, monitoring, and surveys were untimely and too infrequent to properly assess HEPA unit performance. The licensees immediate corrective actions included stopping work in the Unit 1 containment, instructing individuals to report to dosimetry for monitoring and conducting an extensive root cause investigation of the event. The licensee entered this issue into their corrective action program as Condition Reports 16-06099, 16-06578, 16-06593, and 16-06594.
Analysis.
The inspectors determined that the failures to implement adequate engineering and radiological controls to reduce airborne radioactivity during HEPA unit operations in accordance with 10 CFR 20.1701 and radiation protection procedures was a performance deficiency. The performance deficiency was more than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of program and process (exposure control) and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. This was evident by the Unit 1 containment airborne radioactivity event on April 21, 2016, that resulted in at least eight workers with unplanned intakes. Using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, dated August 19, 2008, the inspectors determined the finding had very low safety significance (Green) because:
- (1) it was not an ALARA planning and controls finding,
- (2) there was no overexposure,
- (3) there was no substantial potential for an overexposure, and
- (4) the ability to assess dose was not compromised. The inspectors concluded that the finding has a cross-cutting aspect in the human performance area, associated with the resources component, because the licensee leaders failed to ensure that personnel, equipment, procedures, and other resources were available and adequate to support nuclear safety. Specifically, procedures and radiation exposure permits failed to have adequate instructions for ensuring HEPA filter loading and dose rates were monitored to prevent overloading, and safe handling of loaded HEPA filters
[H.1].
Enforcement.
Title 10 CFR 20.1701 states, in part, that the licensee shall use, to the extent practical, processes or other engineering controls necessary to reduce the concentration of radioactive material in air. Contrary to the above, on April 20, 2016, the licensee failed to use, to the extent practical, processes or other engineering controls necessary to control the concentration of radioactive material in air within the Unit 1 containment building. Specifically, the licensee failed to implement portable HEPA filtration unit daily operational checks, radiological surveys, and timely monitoring processes in order to identify decreased HEPA unit performance in the steam generator 1 and steam generator 2 areas of the Unit 1 containment. Consequently, these failures to use adequate radiological and engineering controls resulted in an airborne radioactivity event on April 21, 2016, in the Unit 1 containment, causing the evacuation of 41 potentially contaminated workers, eight of whom had measureable intakes of radioactive material.. Because the violation is of very low safety significance (Green) and the licensee has entered the issue into their corrective action program, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000528/2016002-03, Inadequate Engineering and Radiological Controls Resulting in a Unit 1 Containment Building Airborne Radioactivity Event with Unplanned Intakes.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
4OA1 Performance Indicator Verification
.1 Mitigating System Performance Index: Emergency AC Power Systems (MS06), High
Pressure Injection Systems (MS07), Heat Removal Systems (MS08), Residual Heat Removal Systems (MS09), and Cooling Water Systems (MS10)
a. Inspection Scope
The inspectors reviewed the licensees mitigating system performance index data for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the mitigating system performance index for emergency ac power systems, high pressure injections systems, heat removal systems, residual heat removal systems, and cooling water systems for units 1, 2, and 3, as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.2 Drill/Exercise Performance (EP01)
a. Inspection Scope
The inspectors reviewed the licensees evaluated exercises and selected drill and training evolutions that occurred between July 2015 and March 2016 to verify the accuracy of the licensees data for classification, notification, and protective action recommendation (PAR) opportunities. The inspectors reviewed a sample of the licensees completed classifications, notifications, and PARs to verify their timeliness and accuracy. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.
These activities constituted verification of the drill/exercise performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.3 Emergency Response Organization Drill Participation (EP02)
a. Inspection Scope
The inspectors reviewed the licensees records for participation in drill and training evolutions between July 2015 and March 2016 to verify the accuracy of the licensees data for drill participation opportunities. The inspectors verified that all members of the licensees emergency response organization (ERO) in the identified key positions had been counted in the reported performance indicator data. The inspectors reviewed the licensees basis for reporting the percentage of ERO members who participated in a drill.
The inspectors reviewed drill attendance records and verified a sample of those reported as participating. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.
These activities constituted verification of the emergency response organization drill participation performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.4 Alert and Notification System Reliability (EP03)
a. Inspection Scope
The inspectors reviewed the licensees records of Alert and Notification System tests conducted between July 2015 and March 2016 to verify the accuracy of the licensees data for siren system testing opportunities. The inspectors reviewed procedural guidance on assessing alert and notification system opportunities and the results of periodic alert and notification system operability tests. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.
These activities constituted verification of the alert and notification system reliability performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.5 Occupational Exposure Control Effectiveness (OR01)
a. Inspection Scope
The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period of April 1, 2015, through March 31, 2016. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 millirem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.6 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual
(ODCM) Radiological Effluent Occurrences (PR01)
a. Inspection Scope
The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred between April 1, 2015, and March 31, 2016, and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the radiological effluent technical specifications (RETS)/offsite dose calculation manual (ODCM) radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution
.1 Routine Review
a. Inspection Scope
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.
b. Findings
No findings were identified.
.2 Semiannual Trend Review
a. Inspection Scope
The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, station-wide and departmental performance improvement reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends.
These activities constitute completion of one semiannual trend review sample, as defined in Inspection Procedure 71152.
b. Observations and Assessments The licensee is currently monitoring five station-wide performance trends that are considered to be adverse to quality.
- Hazard identification and acceptance
- Station program and procedure non-compliances
- Procedural guidance and quality
- Human performance tool usage
- Implementation of corrective actions With regard to all of these trends, the inspectors concluded that the licensee is identifying, monitoring, and correcting these trend behaviors adequately and effectively.
The inspectors also observed that the results of the trend analysis were consistent with station performance indicators.
The inspectors did not identify any additional adverse trends, however inspector observations have contributed to some of the trends identified by the licensee.
c. Findings
No findings were identified.
.3 Annual Follow-up of Selected Issues
a. Inspection Scope
The inspectors selected two issues for an in-depth follow-up:
- From April 4, 2016, through June 3, 2016, during an in-office inspection, the inspectors reviewed the six cyber security issues documented in Inspection Report 05000528; 05000529; 05000530/2013405 for an in-depth follow-up. The inspectors reviewed procedures, digital asset listings, and corrective action documents. The inspectors interviewed personnel involved in implementing the corrective actions.
The inspectors assessed the licensees cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were appropriate.
- On May 12, 2016, the inspectors reviewed an instance of reactor coolant pressure boundary leakage at the Unit 1 reactor coolant loop 2B cold leg resistance temperature detector nozzle.
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.
These activities constitute completion of two annual follow-up samples as defined in Inspection Procedure 71152.
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On April 21, 2016, the inspectors presented the inservice inspection results to Mr. R. Bement, Senior Vice President, Site Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On April 22, 2016, the inspectors presented the radiation safety inspection results to Mr. R. Bement, Senior Vice President, Site Operations, and other members of the licensee staff.
The licensee acknowledged the issues presented. In addition, the inspector conducted a telephonic final exit with Mr. M. Lacal, Vice President, Regulatory Affairs and Plant Improvement, and other members of staff on June 9, 2016. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On May 5, 2016, the inspectors presented the results of the on-site inspection of the emergency preparedness program to Mr. R. Bement, Senior Vice President, Site Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On June 3, 2016, the inspectors presented the inspection results to Mr. R. Bement, Senior Vice President, Site Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors destroyed proprietary information that had been reviewed.
On July 14, 2016, the inspectors presented the inspection results to R. Bement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- R. Bement, Senior Vice President, Site Operations
- M. Lacal, Senior Vice President of Regulatory and Oversight
- J. Cadogan, Vice President, Engineering
- C. Kharrl, Plant General Manager for Operations
- M. McLaughlin, Plant General Manager of Site Support
- D. Vogt, Assistant Plant Manager
- H. Ridenour, Director Maintenance
- G. Andrews, Director Regulatory Affairs
- D. Wheeler, Director Performance Improvement
- K. Graham, Director Plant Engineering
- K. House, Director Design Engineering
- D. Arbuckle, Manager, Unit Operations/Emergency Preparedness
- M. McGhee, Department Leader, Nuclear Regulatory Affairs
- G. Cameron, Section Leader, Nuclear Regulatory Affairs
- H. Lesan, Section Leader, Performance Improvement
- G. Jones, Supervisor, Radiation Protection
- S. Lantz, Dosimetry Section Leader, Radiation Protection
- C. Moeller, Director, Technical Support (Acting)
- R. Routolo, Manager, Radiation Protection (Acting)
- R. Atkisson, Manager, Cyber Security Project
- S. Bittner, Senior Engineer and Cyber Security Specialist
- A. Swirlbul, Section Leader, Cyber Security
- J. Bettencourt, Senior Health Physicist, Radiation Protection
- M. Cosenza, Manager, Security Programs
- T. Dickinson, Unit 3 RMC Supervisor, Radiation Protection
- D. Heckman, Senior Consultant, Nuclear Regulatory Affairs
- H. Jackson, Health Physicist, Radiation Protection
- M. Mahoney, Senior Program Advisor, Nuclear Security Programs
- R. Neville, Senior Reactor Engineer
- D. Ricks, Senior Reactor Engineer, Special Nuclear Material Custodian
- J. Sowers, Department Leader, Nuclear Engineering Design
- D. Whitehead, Section Leader, Operations Computer Systems Engineering
- R. Carbonneau, Director, Nuclear Assurance
- T. Weber, Department Leader, Nuclear Regulatory Affairs
- T. Gaffney, Department Leader, Program Engineering
- B. Loyd, Department Leader, Maintenance/Welding
- D. Naughton, Program Engineering Section Leader
- M. Brannin, Engineering Program Owner
NRC Personnel
- D. Garmon, Health Physicist, Office of Nuclear Reactor Regulation
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
- 05000528/2016002-01 URI Leakage From Reactor Coolant Pump 2B Discharge Pipe Instrument Nozzle
Opened and Closed
- 05000528/2016002- 02
NCV Failure to Implement High Radiation Area Controls in an Area with a Dose Rates Greater Than 1 rem per Hour
- 05000528/2016002- 03 NCV Inadequate Engineering and Radiological Controls Resulting in a Unit 1 Containment Building Airborne Radioactivity Event with Unplanned Intakes