ML13329A147

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SALP Repts 50-206/90-02,50-361/90-02 & 50-362/90-02 for Oct 1988 - Jan 1990
ML13329A147
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 04/11/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13329A148 List:
References
50-206-90-02, 50-206-90-2, 50-361-90-02, 50-361-90-2, 50-362-90-02, 50-362-90-2, NUDOCS 9005240294
Download: ML13329A147 (45)


See also: IR 05000206/1990002

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION V

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SALP BOARD REPORT

Nos. 50-206/90-02, 361/90-02, 362/90-02

SOUTHERN CALIFORNIA EDISON COMPANY

SAN ONOFRE NUCLEAR GENERATING STATION

OCTOBER 1, 1988 THROUGH JANUARY 31, 1990

9 00

C24294

- C

900411

PDR

ADOCK 05:00206.

PDLEc:

TABLE OF CONTENTS

Page

I.

Introduction.

.

..............

.

. . . . ..

1

II. Summary of Results.

............. ....

. . . .

2

A.

Effectiveness of Licensee Management.........

.

2

B.

Results of Board Assessment.

............. .

3

C.

Changes in SALP Ratings. ........... .

. . . .

3

III. Criteria.

.

... ..............

..

. . . .

4

IV.

Performance Analysis.

............ .....

. . .

5

A.

Plant Operations. . . . ................ 5

B. Radiological Controls . ................

8

C. Maintenance/Surveillance................

10

D. Emergency Preparedness. . . . . . . . . ........ 13

E. Security.

.

..............

15

F. Engineering/Technical Support . . .

. . ........ 17

G.

Safety Assessment/Quality Verification. ........

20

.

V.

Supporting Data and Summaries. . . ............. 23

A.

Licensee Activities . . . . .

.23

B. Direct Inspection and Review Activities ........

25

C.

Enforcement Activity.................

25

D. Confirmation of Action Letters . . . . ........ 25

E. Orders..........

25

F. AEOD Assessment of Licensee Event Reports .. .. ....

26

TABLES

Table 1 -

Inspection Activities and Enforcement Summary

Table 2 -

Enforcement Items

Table 3 -

Synopsis of Licensee Event Reports

ATTACHMENT

AEOD Analysis of Licensee Event Reports

U. S. NUCLEAR REGULATORY COMMISSION

REGION V

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SALP BOARD REPORT

Nos. 50-206/90-02, 361/90-02, 362/90-02

SOUTHERN CALIFORNIA EDISON COMPANY

SAN ONOFRE NUCLEAR GENERATING STATION

OCTOBER 1, 1988 THROUGH JANUARY 31, 1990

TABLE OF CONTENTS

Page

I. Introduction.

.

...............

...

. .

1

II. Summary of Results........... ......

. . . . .

2

A.

Effectiveness of Licensee Management.....

. . . . .

2

B.

Results of Board Assessment......... ..

. . . .

3

C.

Changes in SALP Ratings........... .

. . . . .

3

III. Criteria.......

..............

.

. .

4

IV.

Performance Analysis..........

......

. . . . .

5

A.

Plant Operations..5

B.

Radiological Controls. .. ....... .........

8

C. Maintenance/Surveillance. .. ... ........ ...

10

D.

Emergency Preparedness. .. ... ........ ....

13

E. Security.....15

F.

Engineering/Technical Support. .. ...... ...... 17

.

Safety Assessment/Quality Verification....

. . . . ..

20

V. Supporting Data and Summaries . . ...............

23

A.

Licensee Activitiess. . . . . .

. . . . ..... ...

23

B.

Direct Inspection and Review Activities .. ... ....

25

C.

Enforcement Activity . .

. .

. . . . . . . ... ...

25

D.

Confirmation of Action Letters .. ....... ....

25

E. Orders.

25

F. AEOD Assessment of Licensee Event Reports.... ..

.

26

TABLES

Table 1 -

Inspection Activities and Enforcement Summary

Table 2 -

Enforcement Items

Table 3 -

Synopsis of Licensee Event Reports

ATTACHMENT

AEOD Analysis of Licensee Event Reports

.1.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an NRC staff

integrated effort to collect available observations and data on a

periodic basis and to evaluate licensee performance based on this

information. The program is supplemental to normal regulatory processes

used to ensure compliance with NRC rules and regulations. It is intended

to be sufficiently diagnostic to provide a rational basis for allocating

NRC resources and to provide meaningful feedback to the licensee's

management regarding the NRC's assessment of their facility's performance

in each functional area.

An NRC SALP Board, composed of the members listed below, met in the

Region V office on March 15, 1990, to review observations and data on the

licensee's performance in accordance with NRC Manual Chapter 0516,

"Systematic Assessment of Licensee Performance," dated August 16, 1989.

The Board's findings and recommendations were forwarded to the NRC

Regional Administrator for approval and issuance.

This report is the NRC's assessment of the licensee's safety performance

at San Onofre for the period October 1, 1988 through January 31, 1990.

The SALP Board for San Onofre was composed of:

  • R. P. Zimmerman, Director, Division of Reactor Safety and Projects,

(Board Chairman)

  • A. E. Chaffee, Deputy Director, Division of Reactor Safety and

Projects

E. W. Merschoff, Deputy Director, Division of Reactor Safety,

Region II

  • C. M. Trammell, Acting Director, Project Directorate V, NRR
  • S. A. Richards, Chief, Reactor Projects Branch

Protection Branch

  • P H. Johnson, Chief, Reactor Projects Section 3

F. A. Wenslawski, Chief, Facilities Radiological Protection

Section

  • F. R. Huey, Chief, Engineering Section

M. D. Schuster, Chief, Safeguards Section

  • J. E. Tatum, Unit 1 NRR Project Manager
  • L. E. Kokajko, Units 2 and 3 NRR Project Manager
  • C. W. Caldwell, Senior Resident Inspector

K. Prendergast, Emergency Preparedness Analyst

A. McQueen, Safeguards Inspector

  • Denotes voting member (in all functional areas).

Other persons

advised the Board in areas of cognizance.

  • S

2

OI.

SUMMARY OF RESULTS

A. Effectiveness of Licensee Management

Notable licensee achievements were observed during this SALP period.

Overall plant performance was good, with few transients and no

significant complications. The number of reactor trips and other

significant events was slightly higher than during the previous

period, but still relatively low. Weaknesses were noted in the

Plant Operations area involving insufficient attention to detail and

inadequate training in normal operations, resulting in several

operational errors during the assessment period. Other weaknesses

were observed in association with non-conservative application or

interpretation of Technical Specification (TS) requirements, and the

staffing level of licensed operators was impacted by a higher than

normal attrition rate.

In the Maintenance/Surveillance functional area, the Board

considered the licensee to have defined a very effective Maintenance

and Surveillance program, although minor weaknesses in program

implementation were observed during the performance of maintenance

activities. The licensee has also shown initiative in the

Maintenance area by the use of innovative analysis techniques (e.g.,

Electronic Characterization and Diagnostics (ECAD) System). In

addition, the licensee has demonstrated an aggressive Radiological

Controls program which has served as an industry leader in several

respects. Effective management controls, ample and capable

staffing,. and self-critical attitudes also provided good overall

performance in the Emergency Preparedness and Security areas.

Strengths were also observed in other functional areas. In

particular, the licensee was aggressive in upgrading programs to

enhance the effectiveness of Engineering/Technical Support and

Safety Assessment/Quality Verification activities. These efforts

reflected strong management support of initiatives in these

functional areas.

Results were being achieved, as exemplified by

significant design problems identified by Engineering and by

meaningful audit/surveillance findings by the Quality Oversight

organizations. However, weaknesses were also observed in these

areas. In the Engineering/Technical Support area, problems were

observed with regard to inadequate translation of the design bases

to component setpoints, and in the lack of formal calculations for

key design parameters related to some of the electrical distribution

systems. In addition, there were a few examples of problems with

design changes that manifested themselves in plant events. With

regard to the Safety Assessment/Quality Verification area,

weaknesses were observed in the adequacy of the corrective action

program, safety evaluations, and licensing submittals.

The weaknesses noted above were discussed during periodic meetings

with licensee management. These discussions emphasized a need for a

continued self-critical attitude by SCE in addressing areas of

weakness, particularly involving attention to detail during the

3

performance of work activities. In a manner indicative of such a

self-critical attitude, senior SCE management recognized the

significance of weaknesses observed during the last SALP period and

initiated comprehensive actions to improve performance in the

Engineering/Technical Support and Safety Assessment/Quality

Verification functional areas. These efforts included a corporate

reorganization to put all such activities under one Vice President,

a move of the Engineering department closer to the San Onofre

Station, relocation of all quality oversight organizations to the

site, and initiation of a comprehensive review and updating of the

plant's design basis documents.

B. Results of Board Assessment

Overall, the SALP Board found the performance of NRC licensed

activities by the licensee to be acceptable and directed toward safe

operation of the San Onofre Station. The SALP Board has made

specific recommendations in most functional areas for licensee

management consideration. The results of the Board's assessment of

the licensee's performance in each functional area, along with the

previous assessments, are as follows:

Rating

Rating

Last

This

Functional Area

Period

Period

Trend*

A. Plant Operations

1

2

B. Radiological Controls

1

1

C. Maintenance/

2

1

Surveillance

D. Emergency Preparedness

1

1

E. Security

1

1

F. Engineering/Technical

3

2

Support

G. Safety Assessment/

3

2

Quality Verification

The SALP report may include an appraisal of the performance

trend in a functional area for use as a predictive indicator.

Licensee performance during the assessment period should be

examined to determine whether a trend exists. Normally, a

performance trend will be indicated only if (1) a definite

trend is discernible and (2) continuation of the trend could

result in a change in performance rating. The performance

trend is intended to predict licensee performance during the

next assessment period and should be helpful in allocating NRC

resources.

C. Changes in SALP Ratings

Changes to the SALP ratings occurred in the Plant Operations,

Maintenance/Surveillance, Engineering/Technical Support, and Safety

Assessment/Quality Verification functional areas. Performance in

4

Plant Operations declined from the previous Category 1, primarily

due to instances of non-conservative application or interpretation

of Technical Specification requirements, and several events

involving operator error. These events appeared to result from

insufficient attention to detail and inadequate training in normal

operations. A decreased licensed operator staffing level on Units 2

and 3 (due to a higher than normal attrition rate) also warrants

management attention because of its potential impact on future plant

performance in the Plant Operations area.

Performance in the Maintenance/Surveillance functional area was

concluded to have improved due to a well-defined program and

significant licensee initiatives in this area, including

improvements in the control and scheduling of work, and the use of

innovative maintenance techniques. Performance in this area was

assessed as Category 1; nevertheless, the SALP Board noted several

examples of problems associated with the implementation of that

program. As a result, the Board recommends that the licensee

continue to promote the concept of attention to detail during the

performance of work, and strengthen supervisory review of work

(including work plans) to assure that maintenance activities are

performed safely and efficiently.

Performance was -found to have improved in the Engineering/Technical

Support and Safety Assessment/Quality Verification functional areas

due to the licensee's aggressiveness in upgrading programs to

enhance the effectiveness of these areas. These involved relocation

of cognizant organizations closer to (or at) the site, additional

staffing, and improved processes for performing and managing related

activities. The Board noted strong management support of

initiatives in these functional areas. The higher ratings reflect

the Board's perception that desired notable improvements have been

made in these areas, as discussed further in Sections IV.F and G,

although a need for additional improvement was observed.

III. CRITERIA

Licensee performance is assessed in functional areas described in NRC

Manual Chapter 0516. Appendix A to this manual chapter describes a

number of attributes for each evaluation criterion and provides guidance

on using these criteria to assign a performance rating. The evaluation

criteria were as follows:

1. Assurance of quality, including management involvement and control.

2. Approach to the identification and resolution of technical issues

from a safety standpoint.

3. Responsiveness to NRC initiatives.

4. Enforcement history.

5

5. Operational events (including response to, analysis of, reporting

of, and corrective actions for events).

6. Staffing (including management).

7. Effectiveness of the training and qualifications program.

On the basis of the NRC assessment, each functional area evaluated was

rated according to three performance categories. The definitions of

these performance categories are as follows:

Category 1:

Licensee management attention and involvement are

readily evident and place emphasis on superior performance of

nuclear safety or safeguards activities, with the resulting

performance substantially exceeding regulatory requirements.

Licensee resources are ample and effectively used so that a high

level of plant and personnel performance is being achieved. Reduced

NRC attention may be appropriate.

Category 2:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are good.

The licensee has attained a level of performance above that needed

to meet regulatory requirements. Licensee resources are adequate

and are reasonably allocated so that good plant and personnel

performance is being achieved. NRC attention may be maintained at

normal levels.

Category 3:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are not

sufficient. The licensee's performance does not significantly

exceed that needed to meet minimal regulatory requirements.

Licensee resources appear to be strained or not effectively used.

NRC attention should be increased above normal levels.

IV. PERFORMANCE ANALYSIS

The following is the Board's assessment of the licensee's performance in

each of the functional areas, along with the Board's conclusion for each

area and its recommendations with respect to licensee actions and

management emphasis.

A. Plant Operations

1. Analysis

During the SALP period, approximately 1770 hours0.0205 days <br />0.492 hours <br />0.00293 weeks <br />6.73485e-4 months <br /> of direct

inspection effort were applied in the Plant Operations area.

The licensee's strengths continued to be in well-written

operating procedures, administrative controls, and operations

support. A noteworthy accomplishment was a new site record for

continuous operation set by Unit 3 shortly after the end of the

assessment period. Weaknesses identified were associated with

attention to detail and training in normal operations,

6

involving several personnel errors and instances of improper

application of Technical Specification (TS) requirements. In

addition, the staffing level of licensed operators was impacted

by a high attrition rate.

The licensee responded to these

weaknesses, and corrective action plans were being developed at

the end of the assessment period.

In response to the last SALP recommendations, the licensee took

action to strengthen housekeeping and the interface among

Operations, Maintenance, and Technical groups. Safety policies

were reinforced through formal training and periodic reviews.

Management continued to emphasize strict compliance with

procedures, and took other actions to heighten the safety

sensitivity of the operating staff. Corporate management was

effectively involved in site activities and their presence in

the plant was observed regularly, including during backshift

hours. The licensee lowered the threshold for initiating

operating incident investigations. This resulted in the

assessment of more minor events for lessons learned. A general

absence of recurring problems indicated that corrective actions

for events and violations were effective.

The licensee's responses to NRC identified issues were

technically sound, and implementation was timely and effective.

One example was the development of a program, pursuant to an

NRC Bulletin, to control plant evolutions with reduced reactor

coolant system (RCS) inventory.

The trip reduction program appeared to remain effective,

although the number of trips increased slightly over the

previous period. Most were caused by equipment failures, such

as those associated with Units 1 and 3 (as summarized in

paragraph V.A). The Unit 2 CPC trip during startup, on the

other hand, was attributed to operator error and training

weaknesses. In addition, noise in the Unit 1 nuclear instru

mentation system was identified by Operations, but was not

effectively resolved with Engineering, later resulting in a

reactor trip. In the case of manual trips, the operators took

conservative actions and followed the procedures promptly when

the adverse conditions were identified. The licensee's actions

to analyze these events were aggressive and corrective actions

were effective. In addition, the licensee initiated a

professional operator development program to monitor and

enhance operator performance.

In the licensee's approach to the identification and resolution

of technical issues, there were several examples of

non-conservative interpretation or implementation of TS

requirements. Examples of this included (1) management

misinterpretation of NRC Generic Letter 87-09, inappropriately

allowing Unit 2 to be kept at power by invoking a 24-hour

allowance to complete an overdue surveillance test, (2) not

understanding that Unit 1 hot leg recirculation (HLR) was a

7

TS-required feature and that TS 3.0.3 was applicable when

CV-304 failed, and (3) failure to reduce reactor power by 30%

within an hour after a Unit 2 control element assembly slipped

into the core. On the other hand, the facility staff did

exhibit conservatism by shutting down Unit 1 to implement

necessary modifications to the HLR system and shutting down

Unit 2 when it was necessary to perform leak rate testing on

the fuel transfer canal.

In addition, equipment operability

determinations made by Operations, in collaboration with

Station Technical, were generally thorough and conservative.

Other weaknesses were observed in the Plant Operations area, as

evidenced by occasional significant operating events that were

attributable to causes under the licensee's control.

One such

event was a hydrogen ignition and fire in the radwaste building

that resulted partly from program weaknesses and insufficient

training for the control of combustible gases in plant systems.

A number of personnel errors during routine plant evolutions

were also attributed to insufficient attention to detail or to

weaknesses in training on normal operations. Examples were a

misunderstanding by the operators which led to Unit 2 being

taken critical with all four channels of the core protection

calculators (CPCs) indicated as being inoperable, and a

draindown of approximately 700 gallons from the Unit 2 RCS by

an equipment operator who manipulated the wrong valve during a

reduced inventory condition.

With respect to staffing, responsibilities were well defined.

To support the on-shift operators, the licensee had an

experienced equipment control and procedure writing group that

produced quality operating procedures and work requests in

almost all cases.

However, during this assessment period, the

attrition rate for Unit 2 and 3 licensed operators increased to

about double that of the previous year. While some of these

operators were promoted within the Edison organization, thereby

enhancing the depth of other organizations such as QA, many

left the company. This caused some reduction in the experience

base and increased the demand on the remaining operators. NRC

enforcement action also focused attention on excessive use of

overtime, by both Unit 2 and Unit 3 personnel, during the Unit

2 refueling outage. Toward the end of the period, the licensee

initiated recruitment and training actions to improve licensed

operator staffing levels.

The licensee's training and qualification program was well

defined and implemented with dedicated resources and with

effective means for feedback of industry and internal operating

experiences. In particular, the program was effective in

preparing personnel for NRC license examinations, as evidenced

by near 100% pass rates for initial operating license

candidates. Additionally, the administration of the licensee's

requalification program received a satisfactory rating.

However, while many operators examined exhibited strong

8

performance in handling abnormal operations, their performance

for normal operations at times appeared to be weak, as

evidenced during the requalification exams and by some of the

events previously discussed. The licensee initiated corrective

actions to address this deficiency.

The performance of the licensee's fire protection program

during this period was consistent with NRC requirements,

although resolution of several technical issues from the 1988

fire protection team inspection is still in progress. The

licensee has maintained an effective firefighting capability,

including a very capable onsite fire department, and has

.conducted frequent drills to ensure firefighter proficiency.

Inspection activities during the SALP period identified five

severity level IV violations.

Root cause analyses and

corrective actions for the enforcement issues were timely and

effective.

2. Conclusion

Performance Assessment -- Category 2

3. Board Recommendations

The Board recommends that management ensure continued use of a

conservative interpretation and application of TS requirements.

In addition, the licensee should provide continued management

emphasis on procedure compliance, work control, and attention

to detail.

Continuing emphasis should also be given to

strengthening licensed operator training and performance in

routine plant evolutions, and to augmenting licensed operator

staffing levels.

B. Radiological Controls

1. Analysis

This functional area was reviewed routinely during the

assessment period by both regional and resident inspection

staff. Approximately 530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> of direct inspection effort

were expended in this area. Strengths identified included

comprehensive management control systems, particularly for

ALARA (as low as reasonably achievable exposure) planning; many

highly qualified staff personnel; an effective chemistry

control program; and a commitment at the highest levels of

management to improvements in quality. Housekeeping was

aggressive, resulting in minimization of contaminated areas.

Observed weaknesses evolved around inspector identified

problems in the respiratory protection program, including

training for dosimetry personnel, health physics department

auditing techniques, and maintenance of respirators. The

licensee aggressively pursued root cause evaluation and

9

correction of programmatic aspects of this issue. One

additional weakness observed was the control of radioactive

material, as indicated by several licensee-identified unplanned

releases of low-level radioactive material and one instance of

radiation dose rates in an unrestricted area above the limit.

No problems were indicative of programmatic weaknesses in

radiological controls.

Management control of planning activities continued to play a

significant role in identifying problems before they became

critical factors during maintenance. Health Physics management

continued to meet frequently with their personnel, and

conducted weekly tours of the plant and of ongoing work.

Management commitment to improvement programs and to resolution

of technical issues was responsible for a significant reduction

in the failure rate for effluent and process monitors,

resulting in increased availability of the monitors and fewer

spurious challenges to engineered safety feature systems.

The licensee's staff continued to be a strength, with a low

turnover rate, resulting in retention of highly qualified

personnel.

With the exception of supervision of the respira

tory protection program, which had been delegated to personnel

with other duties, responsibilities were well defined and

personnel in staff positions demonstrated thorough knowledge of

the technical aspects of their areas.

The licensee's training program remained accredited by the

Institute for Nuclear Power Operations (INPO), with many

instructors certified by the National Registry of Radiation

Protection Technologists (NRRPT), and with a high number

(near 100%) of ANSI qualified health physics technicians. The

licensee has approximately 10 American Board of Health Physics

(ABHP) certified health physicists. Management encouragement

of personnel, through company-wide and departmental incentive

programs for excellence and for ALARA improvement suggestions,

maintained a high level of commitment to excellence by the

plant staff.

Programs for chemistry analysis were very good as demonstrated

by staffing, equipment, and procedures. Effective use and

maintenance of condensate polishing demineralizers resulted in

minimal chemical excursions in secondary systems. Routine

quality control methods and fully independent measurement

standards were effective, as demonstrated by a 98% success rate

for initial analyses of NRC Confirmatory Measurements Program

test standards.

The licensee's commitment to improvements in quality was

exemplified by the correction of findings from internal audits,

which were comprehensive. In the instance of a respiratory

protection program audit which was found not to have been

thorough in scope and depth, the licensee promptly instituted

II

10

changes to the program forconduct of health physics audits to

improve audit techniques. Responses to NRC identified problems

were timely and comprehensive, indicating a self-critical and

conservative approach to correcting those problems.

Two cited violations were identified during this assessment

period, as indicated in Table 2. This was a reduction from the

three violations identified during the last SALP period. One

was an isolated incident involving worker instructions in high

radiation areas, which did not indicate a programmatic

deficiency and was expeditiously corrected. The second was

associated with respiratory protection problems, as mentioned

earlier. However, the licensee's comprehensive commitments to

correcting the root causes of the problem appeared to be

sufficient to prevent recurrence.

The station's collective occupational radiation exposure for

1988 was 781 person-rem. This was up somewhat from the station

goal of 750 person-rem, and the 697 person-rem achieved in

1987. The increase was attributed to extensive outage

maintenance and plant aging. The licensee's solid radioactive

waste disposal during 1988, of 97 cubic meters average per

unit, was down slightly from recent previous years.

2. Conclusion

Performance assessment --Category 1

3. Board Recommendations

The Board recommends that the licensee continue efforts to

assure active participation of all site organizations in a

quality Health Physics program, to improve the quality of

health physics audits, and to maintain periodic retraining for

health physics disciplines such as respiratory protection.

C. Maintenance/Surveillance

1. Analysis

During the SALP period, approximately 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br /> of direct

inspection effort were applied in the maintenance/surveillance

area. In addition to routine inspections, a special

maintenance team inspection was conducted to provide for an

in-depth assessment of this area. An electrical Safety System

Functional Inspection (SSFI) also reviewed the licensee's

maintenance activities. The licensee's strengths continued to

be in maintenance expertise, effective scheduling of surveil

lance tests, implementation of an effective computerized

scheduling and work control system, and use of innovative

maintenance technology applications. A noteworthy

accomplishment was the well-executed transshipment of spent

fuel from Unit 1 to the Units 2 and 3 fuel pools. The major

11

weakness identified was associated with continued instances of

inattention to detail during the performance of work

activities. The licensee recognized this weakness and

continued to strive for excellence in this area.

In the previous SALP report, the Board recommended that

emphasis on a high standard of performance by maintenance

supervision and other personnel be continued, that better

control over the conduct of maintenance activities be exer

cised, and that special attention be given to evaluation and

documentation of discrepant conditions. In response to these

recommendations, the licensee implemented several initiatives

to perform tasks such as improving the quality of procedures

(e.g., using more precise acceptance criteria) so that they

were easier to use and understand. In addition, training was

provided to promote a "do it right the first time" attitude, a

self-assessment task group was formed within the Maintenance

Division to continuously evaluate the quality of activities,

and a review was conducted of discrepant conditions found by

Division Incident Investigations and the nonconformance report

(NCR) process. This appeared to result in the development of

additional rigor in the maintenance process.

With regard to efforts to resolve technical issues, the

licensee has been innovative in many cases by applying state

of-the-art technology and programs for maintenance. For

example, SCE was one of the first utilities to use the

Electronic Characterization and Diagnostics (ECAD) System.

This was successfully used to locate an intermittent instrument

cable ground fault that caused a reactor trip in Unit 1. This

fault would have been almost impossible to locate without ECAD

and could have caused another reactor trip later. The ECAD

system was also used in the preventive maintenance program for

the monitoring of electrical cables. The licensee also

supported NRC initiatives by dedicating resources to assist the

NRC's Office For Analysis And Evaluation Of Operational Data

(AEOD) in development of maintenance performance indicators.

The licensee maintained a very effective surveillance

scheduling program during this period, with only three missed

surveillance tests for the three units.

A maintenance team inspection was conducted in July 1989 to

determine the effectiveness of the maintenance program by

applying Maintenance Tree methodology to the licensee's

activities. The team found that the maintenance process for

San Onofre was well defined and incorporated many current

industry initiatives, reflecting strong management support and

involvement. The team also considered that implementation of

the program was satisfactory, but could be further streng

thened. This was evidenced by several examples of inattention

to detail in the development of maintenance work plans, failure

to fully implement all steps of maintenance work instructions,

12

poor or untimely root cause analyses, and insufficiently

developed or comprehensive corrective action plans. In

addition, a weakness was also noted in pre-job walkdowns by

planners. An example of this included the hydrogen fire that

occurred during maintenance work on a waste gas relief valve.

The licensee acknowledged these weaknesses and was addressing

their resolution.

The maintenance team considered the licensee's training and

qualification program to be well defined and to exceed

established industry training criteria. The program provided

good scheduling, documentation, feedback mechanisms, involve

ment of instructors in field activities, and training of

supervision. In addition, the resident inspectors found the

licensee's maintenance training facility to be well equipped

for hands-on training. With respect to staffing, the

maintenance team considered staffing for activities to be

satisfactory, with some reservation regarding the adequacy of

resources to address the workloads of work planners.

During this period, there were several operational events which

occurred as a result'of errors in the Maintenance/Surveillance

functional area. In particular, a reactor trip in Unit 3

resulted from a non-1E uninterrupted power supply (UPS) fault

because a temporary grounding cable was not removed upon

completion of work performed during a previous SALP period

(June 1988). In addition, several engineered safety feature

(ESF) inadvertent actuations (other than emergency core cooling

systems) occurred during the performance of surveillances as a

result of personal error or equipment failure. These events

were properly identified and analyzed, and were promptly

reported where required.

Nine severity level IV violations and two deviations were cited

in the Maintenance/Surveillance area during the assessment

period. However, none of these indicated a programmatic

breakdown and the licensee's root cause and corrective actions

were effective and timely in most cases as evidenced by lack of

recurrence.

2. Conclusion

Performance Assessment -- Category 1

3. Board Recommendations

The Board recommends that the licensee continue to improve

implementation of the maintenance program, especially regarding

attention to detail and procedural implementation. Efforts

should also continue to strengthen the work order preparation

and planning processes. Furthermore, the licensee should

continue to strengthen supervisory review of maintenance

13

activities to assure that they are performed safely and

efficiently.

D. Emergency Preparedness

1. Analysis

During this assessment period 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> of inspection effort

were devoted to assessing the licensee's emergency preparedness

program. This included two routine inspections and observation

of the 1988 and 1989 annual exercises. The licensee received a

SALP category 1 rating in this area during the last appraisal

period. The last SALP board encouraged improvement in the

areas of training and quality assurance.

Strengths identified during this assessment included upper

level management's continued support of the emergency

preparedness program. The only weak areas identified duri'ng

this assessment involved minor repeat exercise findings during

the 1989 exercise and some need for improvement in the shift

crew's familiarization with the Emergency Plan implementing

procedures. The licensee has been responsive to NRC concerns

in these areas and has implemented improvements to the Training

Program.

Management commitment to the Emergency Preparedness program was

demonstrated by continued support of and participation in the

licensee's drill and exercise program, and by significant

improvements to the licensee's emergency facilities, including

a new corporate support center, improvements to the Unit 1

operations support center, and improved telephone and compu

terized message systems. The actions by the Nuclear Affairs

and Emergency Planning (NA&EP) Department to cultivate a

cooperative interface with offsite agencies, including local

governments, the state of California, and the U. S. Marine

Corps, were also noted. This effort resulted in commendable

participation by these agencies during the 1989 exercise, even

though resources were then being expended in support of the San

Francisco Earthquake and a large forest fire in the area.

The licensee's efforts to resolve technical issues from a

safety standpoint have been conservative. For example, the

licensee initiated a program to perform root cause analyses on

all 1989 drill and exercise findings in an effort to improve

performance and resolve previous exercise weaknesses.

Licensee management has demonstrated responsiveness to NRC

initiatives. In response to Generic Letter 89-15, the licensee

volunteered to participate in the NRC's Emergency Response Data

System (ERDS). In addition, items identified by the NRC have

been evaluated by management and acted upon. During the exit

meeting for the 1989 exercise, several comments were brought to

licensee management's attention for their consideration. The

14

licensee received the comments in a cooperative manner and

responded promptly in writing by describing their evaluation

and corrective actions. During another inspection conducted in

1989, it was noted that the shift crews' familiarity with their

emergency procedures for classification and protective actions

were in need of improvement. To this end, the licensee has

provided a new full-time individual to the training program

with expertise in emergency planning. This individual is to

improve interface with the shift crews to increase their

familiarity with their implementing procedures and provide

feedback to Emergency Planning. The position also interfaces

with the managers of other disciplines, including Health

Physics and Maintenance, to insure their feedback and support

of the drill and exercise program.

The licensee's audit program for the Emergency Preparedness

area meets the regulatory requirements contained in 10 CFR

50.54(t) and was also noted to have improved in 1989. However,

inspection findings shortly after the end of the assessment

period indicated some weaknesses in the audit program.

Operational events were appropriately classified and no

violations of NRC requirements were identified in the Emergency

Preparedness functional area during this SALP period.

One Licensee Event Report (LER) was identified in the

Emergency Preparedness area. This LER dealt with improper

placement of fuse blocks for the emergency siren transfer

switch.

The licensee continues to maintain adequate staffing levels

with dedicated personnel to provide for the advancement of the

Emergency Preparedness Program and to sustain a cooperative

interface with local offsite agencies. Positions are ident

ified and authorities and responsibilities are well defined.

Few vacancies have occurred, and staffing continuity is

considered a strength. Expertise is available "in house";

consequently, there has been little need for outside contractor

support.

The licensee's training program is well defined, and utilizes

computer-based training supplemented by an ambitious quarterly

drill and exercise program. The drill program was observed to

have been improved during this SALP period by the utilization

of more challenging scenarios.

Increased emphasis was also

placed on the documentation of drill and exercise findings and

on the program to identify the cause of the finding to preclude

recurrence. Weakness was observed, however, in the licensee's

exercise critique program. As discussed during the NRC exit

for the 1989 exercise, providing the players with a copy of the

scenario prior to the critique may provide benefits.

15

2. Conclusion

Performance Assessment -- Category 1

3. Board Recommendation

Continued support of the licensee's drill and audit programs is

recommended to improve the implementation of corrective actions

and reveal areas for improved performance.

E. Security

1. Analysis

During this SALP assessment period, Region V conducted three

physical security inspections and one material control and

accountability (MC&A) inspection at the San Onofre Nuclear

Generating Station. Approximately 310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br /> of direct

inspection effort (including 68 hours7.87037e-4 days <br />0.0189 hours <br />1.124339e-4 weeks <br />2.5874e-5 months <br /> for MC&A) were expended

by regional inspectors. In addition, resident inspectors

provided continuing observations in this area.

Corporate and plant management continued to be involved in

assuring quality and in reviewing the operation of the overall

security program. This remained a strength, as in the previous

SALP period. This was further reflected in the licensee's

approach to the identification and resolution of technical

issues from a safety, as well as a security, standpoint.

Two violations, one licensee identified and not cited, were

indicated during the SALP period. One violation pertained to

an item of security equipment required to be protected as vital

being located outside vital areas, and the other pertained to

an individual being allowed access to a vital area without

appropriate processing. Both appeared to be isolated incidents

not previously encountered by the licensee. The licensee

reported 13 events, of which four pertained to security and

nine pertained to Fitness for Duty incidents.

The licensee submitted copies of the safeguards event log on a

quarterly basis as required, indicating a total of 411 logged

security events attributed to both human and hardware failures.

The licensee empaneled a Security Section Safeguards Event

Review Committee to meet regularly and review each of the

logged events. Trends were established and responsibility was

assigned to an appropriate individual for each type event to

perform the necessary study, design, engineering, construction,

training, or other action necessary to correct the problem and

preclude or reduce its recurrence.

Performance appeared mixed in the area of responsiveness to NRC

initiatives during the period. On one side, licensee action in

response to an NRC generic letter (requiring licensees to plan

16

to react to a vehicle bomb threat against their facility)

appeared outstanding. The licensee not only went to great

lengths to ensure a thorough and comprehensive response to such

a threat, but went on to physically test the entire response

plan and all elements. On the other hand, response to NRC

initiatives or findings pertaining to vital area (VA) barriers

at the site appeared less prompt. An NRC information notice

issued in 1987 advised all licensees to review their VA

barriers for suspected penetrations to assure conformance to

existing requirements. The licensee did an excellent job in

reviewing barriers and properly identified a number of openings

or penetrations through the barriers. Several of these

openings were concluded to require corrective measures. This

corrective action has been ongoing and is currently programmed

for completion during the next SALP period. Similarly, an NRC

Regulatory Effectiveness Review (RER) indicated weaknesses in

Unit 1 VA barriers in 1985. At that time, the licensee

concluded that the barriers had "been formally reviewed and

approved as described in the San Onofre Physical Security Plan"

and that the continued use of such barriers was reasonable. At

the end of this SALP period, the licensee indicated that they

would again review these barriers to assess the RER-indicated

weaknesses for possible amelioration.

Licensee staffing of the security program has been a strength

during this period as it was during the previous SALP period.

Personnel appeared to be carefully screened for experience and

training. The security organization appeared well defined,

with areas of responsibility and authorities appropriately

detailed. Decision making authority appeared to be properly

delegated to assure quick identification of and response to

problems and changes. A program of security manning reductions

was initiated during this SALP period. As of the end of 1989,

14 personnel reductions had been made in the security

organization, with a goal of 21 by the end of 1992. The

licensee indicated that these reductions are being closely

reviewed and managed to ensure that there is no impact on

compliance or security organization commitments.

Remaining a strength from the previous SALP period was the

licensee's security training and qualification program.

Instructors appeared highly qualified and motivated. The

licensee has also recently enhanced security training for armed

personnel by encouraging quarterly practice firing of assigned

response weapons.

2. Conclusion

Performance assessment -- Category 1

17

3. Board Recommendations

The Board recommends that the licensee continue to support

security program enhancements; e.g., the licensee initiative to

assess and ameliorate Unit 1 Vital Area barrier weaknesses.

F. Engineering/Technical Support

1. Analysis

During the SALP period, approximately 330 hours0.00382 days <br />0.0917 hours <br />5.456349e-4 weeks <br />1.25565e-4 months <br /> of direct

inspection effort were applied in the Engineering and Technical

Support area. In addition to this inspection effort by

resident and region-based inspectors, an NRC Safety System

Functional Inspection (SSFI) team performed an inspection of

Units 2 and 3. The major strength identified during this

assessment period was the licensee's aggressiveness toward

upgrading programs to enhance engineering and technical

performance. The major weaknesses in this functional area

involved inadequate translation of the design bases to com

ponent setpoints, and the lack of formal calculations for key

design parameters related to some electrical distribution

systems. In addition, there were a few examples of problems

with design change output that resulted in plant events.

In response to problems identified in this area during the last

SALP, licensee management initiated many enhancements to

improve engineering performance and the quality and complete

ness of design basis documentation. The Nuclear Engineering,

Safety, and Licensing (NES&L) organization was reorganized and

relocated to Irvine to enhance the effectiveness of the

engineering organization in communicating with the site. In

addition, the licensee was increasing the in-house design

effort to minimize the use of contractor engineering support,

and was expecting that all engineering work for the 1990 Unit 1

refueling outage would be performed in-house. An Engineering

Excellence program was also implemented during this assessment

period to promote development of engineering standards, expand

and formalize design review functions, improve communications

and work processes, enhance design engineer training programs,

and monitor the results of engineering work to assess the

degree of quality improvements.

The licensee also instituted a program for enhanced under

standing of the design basis. This design basis document (DBD)

review will include a review of the design basis for selected

systems and a design document transfer from vendors to SCE.

The licensee expects that approximately 94 systems and topical

areas will have been reviewed when the DBD effort is completed

after about five years.

With respect to design changes, problems became evident in the

middle of the assessment period due to three events related to

18

instrumentation upgrades performed during the Cycle X refueling

outage in Unit 1. These were (1) a reactor trip during restart

caused by electrical circuit noise in the new nuclear

instrument (NI) system (reflecting insufficient analysis of

conditions observed before startup); (2) an automatic actuation

of the auxiliary feedwater (AFW) system (because engineers

overlooked the dynamic flow effects in the steam generator and

had not properly involved the nuclear steam system supplier in

the design process); and (3) a manual reactor trip which had to

be initiated because of a loss of feedwater flow (due to

failure to properly reflect design change information in

surveillance procedures).

To improve engineering output, the design change process was

being revised to better define the scope of work and to provide

for more thorough reviews of each change from its initial

conception to final approval.

This program should be fully

implemented for the Unit 1 Cycle XI refueling outage scheduled

for the summer of 1990. Although the design change process was

still in transition at the end of the assessment period, it

appeared that the performance of design changes was under

effective control.

Staffing appeared to be strained at times during the assessment

period, as evident by the amounts of overtime used. However,

additional engineering personnel had been added by the end of

the period, in support of the licensee's efforts to assume a

stronger in-house engineering role.

The licensee was actively participating in industry efforts to

improve the scope and content of training for the design

engineering staff and has developed a Nuclear Engineering

Organization training plan. The licensee also developed a

cognizant (plant technical) engineer training program during

the period. Both training programs consist of general and site

specific training designed to provide information for all

disciplines. These actions were notable, although somewhat

slow in implementation.

The November 1989 electrical SSFI conducted for Units 2 and 3

identified a number of specific deficiencies and two general

areas of weakness in this functional area. These involved

(1) weaknesses in the translation of design bases into com

ponent setpoints (e.g., diesel day tank level setpoints that

were below the TS requirements), and (2) lack of formal

calculations for key design parameters related to several

electrical distribution systems (e.g., missing or inadequate

calculations for diesel generator load, 120 VAC control power

voltage regulation, and containment penetration sizing and

protection). Calculations also did not show that the D/G air

receivers had sufficient capacity to support five automatic

starts (an FSAR commitment).

19

The NRC maintenance inspection team reviewed several engineer

ing evaluations and found them to be adequate. The team con

sidered that the engineering/technical support program and its

implementation were satisfactory. However, some weaknesses

were noted in engineering performance, as evidenced in insuf

ficient design data or analyses. In addition, insufficient

attention to detail was noted involving pressure ranges used in

calibration of feedwater flow transmitters.

Weaknesses in safety evaluations were noted in several cases.

For example, during startup from the Unit 1 Cycle IX refueling

outage, the licensee determined that no unreviewed safety

question (USQ) existed for S/G tube sleeve deficiencies.

However, this determination was made without an assessment of

the thermal hydraulic response of an improperly sleeved tube

and the potential consequences during a steam line break ,

accident. A subsequent assessment during the Cycle X refueling

outage showed that operation in this manner was a USQ. A

second example concerned a safety evaluation for an inadequate

weld process that resulted in several leaking S/G tube plugs in

Unit 2. In this case, an evaluation was not prepared to

substantiate return to operation without repairing other plugs

that had potential for similar weld deficiencies. By the end

of this assessment period, the licensee was focusing attention

to improve the quality of safety evaluations.

NRC inspections identified one violation and two deviations in

this functional area, but these did not indicate significant

weaknesses. A total of 29 LERs were associated with

Engineering and Technical Support activities. Most of these

involved system design inadequacies or personnel errors in the

engineering process that led to deficiencies which were

primarily found in Unit 1. Many of these LERs reflected

deficiencies in early design work which were identified through

more aggressive efforts by engineering to verify the design

basis of systems, or by a more critical attitude during the

performance of design work. These efforts identified a number

of significant design inadequacies such as Unit 1 safety

injection alignment delays and a lack of backup nitrogen for

recirculation system and containment spray system valves.

2. Conclusion

Performance assessment -- Category 2

3. Board Recommendations

The Board recommends that the licensee continue to emphasize

the design basis update program and strengthening of in-house

engineering capabilities. In addition, efforts to improve

engineering and technical work should continue, and the

licensee should ensure that calculations in support of

20

setpoints and key design parameters of systems are accurate and

properly maintained.

G. Safety Assessment/Quality Verification

1. Analysis

During the SALP period, approximately 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> of direct

inspection effort were applied in this functional area. The

major strength identified during this assessment period was the

licensee's aggressiveness in upgrading programs to enhance

performance in this area. In addition, enhancements were made

in the communication of problems to the NRC. Weaknesses in

this functional area were associated with the adequacy of the

corrective action program, safety evaluations, and licensing

submittals.

In response to findings during the last SALP period, the

licensee implemented or upgraded several programs to enhance

performance in this area. The area monitoring program (AMP)

was enhanced to provide a systematic method for directly

observing the implementation of QA program requirements so that

all oversight organizations could participate in monitoring

activities. This included evaluations of material condition,

temporary modifications, and housekeeping of assigned areas.

In addition, monitoring programs were implemented to provide

more direct observation of work performance, and resulted in

meaningful findings (e.g., problems with pipe supports in the

turbine building). These programs reflected a more

performance-based review by quality oversight groups.

Increased presence of quality oversight personnel and

management was noted in the plant, and the remaining offsite

safety oversight groups were relocated to the site to enhance

their effectiveness.

The QA audit and surveillance programs were revised during this

period to focus more directly on performance. Audit plans

received more in-depth reviews, and the scope of audits was

better defined. Followup documentation for audits and

surveillances provided a more thorough evaluation of conditions

found during the review, and corrective action requests were

issued for findings.

Problems identified included inadequate

control of crimpers and improper overpressure mitigation system

setpoints for the Unit 1 power-operated relief valves.

Although these programs appeared to be developing well,

problems such as non-conservative TS interpretations by

Operations or deficiencies with the corrective action program

(discussed below) were not challenged by QA until after the NRC

raised concerns in these areas.

The licensee focused increased emphasis on training and

qualification, with particular emphasis on quality assurance

personnel.

All auditors and inspectors, including quality

21

control inspectors, were given additional training on the

conduct of performance based inspections. This training,

coupled with increased in-plant inspections and focus on

safety-significant matters, reflected substantial management

support for the enhancement of performance in this area.

Higher management expectations and identified weaknesses in

knowledge levels resulted in downgrading of the qualifications

of approximately 30% of the auditors. Retraining of the

personnel was in progress through the use of an auditor

certification program, which was implemented to enhance the

knowledge level of new personnel and to recertify previous

auditors. Staffing was also enhanced in most quality oversight

groups. This included raising the experience base by adding

some licensed operators and other experienced personnel to the

quality assurance organization.

The root cause assessment program was in the process of being

enhanced to increase effectiveness. Although root cause

assessments will continue to be performed largely by the

cognizant organizations, overall program responsibility was

assigned to the Manager of Oversight Engineering. This new

position was established within the Oversight Organization to

provide the methodology, training, and assistance for root

cause determinations, and to provide oversight of root cause

determinations conducted by the other organizations. This

manager will also direct the efforts of the Independent Safety

Engineering Group, the Nuclear Safety Group, and the Quality

Engineering Group. Although progress was initially slow,

momentum had been established by the end of the SALP period,

and this program is expected to be fully implemented by the

spring of 1990.

The maintenance team inspection found a number of examples of

weaknesses in this functional area. These examples included

weak root causes for several problem reports, excessive use of

the category "unknown" (in classifying root causes for some

nonconformance reports), and insufficient priority for and

tracking of the resolution of several NRC inspector-identified

findings, particularly involving in-service inspection (ISI)

issues in Unit 1. The licensee was actively pursuing

corrective actions to resolve these problems, as discussed

previously.

A problem concerning a solenoid valve failure (Unit 1 valve

CV-304) that resulted in a diversion path for hot leg

recirculation flow led to the identification of a number of

weaknesses with the licensee's corrective action program.

Reviews by the resident inspectors and the licensee's QA

organization found a number of related problems, including

inadequate dissemination of information about component

problems to the necessary organizations for review, lack of

timely resolution of root cause determinations, inadequate

follow-through on commitments made in LERs, improper oversight

22

of outstanding items, and inadequate review of component

failures for generic implications. In addition, it was noted

that the licensee did not routinely evaluate site component

problems for 10 CFR Part 21 applicability. The QA organization

performed an in-depth analysis of this issue and found

additional problems with the corrective action program. The

licensee was aggressively pursuing resolution of these issues.

A weakness was also identified with inadequate or non-conser

vative safety evaluations performed during the period. For

example, the licensee did not promptly document a wall thick

ness problem involving residual heat removal (RHR) system

piping (a condition identified by ultrasonic measurements), and

a 10 CFR 50.59 review for changes to the intermediate range

startup rate trip did not result in the submission of a

required TS amendment request for. system change which blocked

the trip function at less then 10 % power. The licensee was

working to enhance safety evaluations and was in the process of

implementing the associated guidance provided in Nuclear Safety

Analysis Center (NSAC)-125.

Problems were noted with the adequacy and control of LERs. In

particular, there were three LERs early in the period that did

not appear to have fully addressed the applicable root causes

and corrective actions for the associated events. In addition,

it was identified in association with the CV-304 solenoid valve

failure (discussed previously) that a relatively large number

of LERs requiring supplemental reports were long outstanding.

LER quality improved toward the end of the assessment period,

and the licensee was attempting to reduce the backlog of

supplemental LER reports due to the NRC.

Licensing submittals received at the beginning of the period

were at times lacking in thoroughness and depth, resulting in

the need for repeated submittals to and conferences with the

NRC.

Examples included the single failure analysis submittal

for the Unit 1 reactor protection system (RPS) and engineered

safety features (ESF), and the Unit 1 thermal shield degrada

tion submittal. In addition, the NRC noted instances of the

licensee's inability to adequately identify, plan, and track

licensing actions. Examples included the Units 2 and 3 spent

fuel pool re-racking amendment, and the Unit 3 low temperature

overpressure (LTOP) mitigation system amendment. Also, there

were delays in submitting many licensing documents and related

correspondence throughout the period. Improved quality of

licensing submittals was noted toward the end of the assessment

period. Among these was the licensee's October 2, 1989

submittal which addressed full term operating license (FTOL)

open items. In this submittal, the licensee provided a

schedule for resolution of these items. In addition, at their

own initiative, the licensee committed to make improvements to

both the recirculation portion and the injection portion of the

safety injection system.

23

During this period one level V and four level IV violations

were identified, but these did not indicate significant flaws

in the licensee's programs.

2. Conclusion

Performance assessment -- Category 2

3. Board Recommendations

The Board recommends that the licensee continue to implement

and improve the root cause assessment program. In addition,

efforts to improve 10 CFR 50.59 safety evaluations and the

corrective action program should continue to ensure that

problems are adequately and timely resolved. Continued efforts

should be devoted to ensuring that conservatism is exhibited in

the making of operational decisions. Continued emphasis should

also be given to the quality and timeliness of licensing

submittals.

V. SUPPORTING DATA AND SUMMARIES

A. Licensee Activities

In general, all three units operated satisfactorily during the

assessment period and were relatively free of problems. Specific

operational activities were as follows:

Unit 1

Unit 1 began the Cycle X refueling outage in November, 1988.

Some

of the major plant modifications completed during that outage

included the installation of a new nuclear instrumentation system

(NIS), reconfiguration of the auxiliary feedwater (AFW) system to

include a dedicated safe shutdown train, installation of upgraded

steam generator (S/G) instrumentation, and upgrades to other systems

which were identified as being vulnerable to single failure. The

licensee attempted to return the Unit to service in May, 1989;

however, a number of difficulties were encountered over a period of

three months. Those difficulties included the following:

-

An automatic reactor trip (while in Mode 2) due to electrical

noise in the newly installed NIS;

-

A manual shutdown during power ascension due to a level anomaly

in the modified S/G instrumentation, which resulted in an

automatic initiation of AFW;

-

A manual shutdown from power to repair the cause of a high

bearing temperature in one of the reactor coolant pumps (RCPs);

-

A manual trip from power when a loss of feedwater occurred

during a surveillance test;

24

  • -

An automatic trip from an erroneous reactor coolant system low

flow signal, caused by a grounded instrument cable; and

-

A manual trip when multiple rods dropped into the core due to

faulty relays.

After these problems were corrected (each in turn) the Unit operated

trouble-free at power from September through November, at which time

it was shut down to make modifications to the hot leg recirculation

flow path (after design deficiencies were identified). After the

Unit was returned to service, it was again shut down in December to

correct problems with backup nitrogen for a safety injection valve.

The Unit was subsequently restarted and operated at power through

the remainder of this assessment period.

Unit 2

Unit 2 operated at power from the beginning of this SALP period

until January 1989, when it was shut down to repair an AFW pump

motor. The Unit was restarted in February even though lighted

annunciators indicated all four Core Protection Calculators (CPCs)

to be inoperable. This was recognized by operators during the

startup, and a shutdown was initiated. The CPCs were fully

operable, however, and initiated a reactor trip as the reactor was

being shut down (because operators did not place the trip function

in bypass). After restart, Unit 2 operated at power until May 1989

when it was shut down to repair a S/G tube leak. The Unit was

subsequently returned to service in June and was operated at power

until September, when it was shut down for the Cycle V refueling

outage. As the reactor was being shut down for the refueling

outage, it had to be manually tripped from 25% power when operators

realized that the axial shape index was approaching the CPC

automatic trip setpoint. A number of major activities were per

formed during the 97-day refueling outage, including the following:

-

Control room modifications for human factors improvements;

-

Turbine overhaul;

-

Installation of an anticipated transient without scram (ATWS)

diverse reactor trip;

-

Overhaul of main feedwater heaters; and

-

Main transformer replacement.

In December 1989, shortly after startup following the refueling

outage, the Unit was shut down to repair a main feedwater flow

venturi flange leak. The Unit was then returned to service and

operated at power through the remainder of this assessment period.

25

Unit 3

Unit 3 was operating at power at the beginning of this period. An

automatic reactor trip occurred in January 1989, due to a low S/G

level caused by a loss of non-1E power for the feedwater controller.

After return to service from the short outage, the Unit operated

until April 1989, when it tripped automatically due to a low voltage

condition associated with power to the control element drive

mechanism relays. After return to power operation, the Unit was

shut down in July to repair a low pressure safety injection (LPSI)

pump seal leak. After the return to service following this repair,

the Unit operated continuously at power for the remainder of this

assessment period. Shortly after the end of this SALP period, the

Unit exceeded the site's continuous operation record of 218 days set

by Unit 1 in 1976.

B. Direct Inspection and Review Activities

Approximately 6570 inspection hours were expended during this

assessment period in performing a total of 46 inspections by

resident, region-based, headquarters, and contract personnel.

Inspection activity in each functional area is summarized in

Table 1.

C. Enforcement Activity

Three resident inspectors were onsite during the SALP assessment

period. A total of 46 inspections, including a maintenance team in

June and July 1989, and an electrical SSFI in October and November

1989, were conducted during this period for a total of 6395 inspec

tor hours (plus 259 hours0.003 days <br />0.0719 hours <br />4.282407e-4 weeks <br />9.85495e-5 months <br /> invested in exit and management meetings).

A summary of inspection activities is provided in Table 1, along

with a summary of enforcement items identified during these inspec

tions. A description of enforcement items is provided in Table 2.

A synopsis of licensee event reports is included as Table 3.

D. Confirmation of Action Letters

One Confirmation of Action Letter was issued during this assessment

period, on January 31, 1989. This letter confirmed the licensee's

plans to resolve questions regarding Unit 1 thermal shield integrity

and other technical issues, and to obtain NRC concurrence before

restart of Unit 1 from its Cycle X refueling outage.

E. Orders

An Order requiring full compliance of Unit 1 with Generic Letter 82-28, "Inadequate Core Cooling Instrumentation System" was issued

on May 5, 1989.

An Order Confirming Licensee Commitments On Full-Term Operating

License Open Items For Unit 1 was issued on January 2, 1990. This

order confirmed SCE's commitment to complete the full-term operating

26

license open items pursuant to the schedule described in a letter

from the licensee dated October 2, 1989. In addition, this Order

modified the NRC's previous order dated May 10, 1989, to require

that the reactor vessel level indication system be installed during

the Cycle XII refueling outage instead of the Cycle XI refueling

outage. This Order also confirmed that the licensee would conduct a

S/G tube inspection during the Cycle XI refueling outage.

F. AEOD Assessment of Licensee Event Reports

A review of licensee events at San Onofre, performed by the Office

for Analysis and Evaluation of Operational Data (AEOD), is included

as Attachment 1. AEOD reviewed the LERs and significant operating

events for quality of reporting and effectiveness of identified

corrective actions.

TABLE 1

INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY

Enforcement Items*

Functional

Inspection

Percent

Severity Level

Area

Hours

of Effort

I II III

IV V Dev

A.

Plant Operations

1772

26.7

5

B.

Radiological

530

8.2

2

Controls

C. Maintenance/

1751

26.7

9

2

Surveillance

D.

Emergency Prep.

180

2.7

E.

Security

310

4.7

1

F.

Engineering/

332

5.2

1

2

Technical Support

G. Safety Assessment/ 1697

25.8

4 1

Quality Verif.

Totals

6572

100.0

22

1 4

Severity levels are discussed in 10 CFR 2, Appendix C.

In addition, 259 hours0.003 days <br />0.0719 hours <br />4.282407e-4 weeks <br />9.85495e-5 months <br /> were expended in exit and management meetings.

This information is current through inspection reports 206/90-05;

361/90-05; and 362/90-05.

TABLE 2

ENFORCEMENT ACTIVITY

UNIT 1

Inspection

Severity

Functional

Report No.

Subject

Level

Area

88-24

Inadequate Control of Maintenance

IV

C

Activities on Environmentally

Qualified Equipment

88-28

Failure to Use Proper Procedure

IV

C

Revision for Performing Reactor

Coolant Chemistry Sampling

89-01

Failure to Comply with Foreign

IV

C

Material Exclusion Control

Requirement

89-03

Inadequate Nonconformance Report

IV

G

on Residual Heat Removal Pipe

Wall Thickness

89-08

Inadequate Control of Radioactive

IV

B

Material

89-09

Inadequate 10 CFR 50.59 Review

IV

G

Regarding Nuclear Instrumentation

System Block of Start-up Rate Trip

89-16

Emergency Lighting Not Performed

Dev

F

Per Updated Final Safety

Analysis Report

89-16

Nonconformance Report Failed to

IV

F

Identify Root Cause

89-16

Failure to Perform Calibration

IV

C

and Test

89-18

Temporary Cables Routed With

IV

C

Safety Related Cable Trays

89-28

Failure to Verify or Properly

IV

B

Maintain a Procedure for

Respirators #

89-31

Inadequate Corrective Actions

IV

G

Related to Failure of Automatic

Switch Corporation Solenoid Valves

-2

.

Table 2, Enforcement Items (Continued)

UNIT 1

Inspection

Severity

Functional

Report No.

Subject

Level

Area

89-31

Failure to Comply with Technical

IV

A

Specification 3.0.3 by Initiating

Plant Shutdown Within One Hour

When Normal Hot Leg Recirculation

Flow Path Inoperable

90-01

Failure to Resolve Issues of In-

Dev

C

service Testing Program For Pumps

Bounded By the Safety Analysis #

Applies to Units 1, 2, and 3

UNIT 2

Inspection

Severity

Functional

Report No.

Subject

Level

Area

88-25

Inadequate Calibration Program

IV

C

for Safety Related Alarm

Devices ##

89-06

Failure to Report Condition that

V

G

Resulted in Violation of Techni

cal Specification Requirements ##

89-09

Housekeeping in 2/3 Electrical

IV

C

Cabinets and Electrical

Maintenance (Unit 3) ##

89-11

Adequacy of Corrective Actions

IV

G

Regarding 10 CFR 50.49 Equipment

Qualification Discrepancy ##

89-16

Work Authorization Request

IV

C

Released Improperly and Poorly

Maintained

89-18

Atmospheric Dump Valve Inoperable

IV

A

for Automatic Operation

89-24

Failure to Declare Equipment

IV

A

Inoperable Due to Delinquent

Surveillance

-3

Table 2, Enforcement Items (Continued)

UNIT 2

Inspection

Severity

Functional

Report No.

Subject

Level

Area

89-24

Lack of Control Over Temporary

IV

C

Cables Routed through a Control

Room Emergency Air Cleanup

System Door ##

89-30

Failure to Implement Periodic

Dev

C

Ground Check on Reactor

Protective System and Engineered

Safety Feature Actuation System

89-33

Excessive Overtime Usage

IV

A

90-03

Security Equipment (Required To

IV

E

Be Protected) Located Outside

Vital Area

.

    1. Applies to Units 2 and 3

UNIT 3

Inspection

Severity

Functional

Report No.

Subject

Level

Area

89-06

Failure to Control Technical

IV

A

Specification Fire Doors

89-16

LPSI Pump Seal Leakage

Dev

F

Drain Piping Not Installed As

Indicated in the Updated Final

Safety Analysis Report

Functional Areas

A -

Plant Operations

B - Radiological Controls

C - Maintenance/Surveillance

D - Emergency Preparedness

E -

Security

F -

Engineering/Technical Support

G - Safety Assessment/Quality Verification

S P

O T A B L E 3 A - U n i t 1

SYNOPSIS OF LICENSEE EVENT REPORTS (LERs)

Functional

SALP Cause Code*

Area

A

B

C

D

E

X

Totals

A.

Plant Operations

4

7

11

B.

Radiological

2

2

Controls

C. Maintenance/

2

3

5

Surveillance

D. Emergency Prep.

1

1

E.

Security **

8

1

9

F.

Engineering/

7

14

1

22

Technical Support

G.

Safety Assessment/

1

1

Quality Verif.

Totals

23

14

5

9

51

  • Cause Code

A - Personnel Error

B - Design, Manufacturing or Installation Error

C -

External Cause

D - Defective Procedures

E - Component Failure

X -

Other

Security LERs are applicable to Units 1, 2, and 3, and include Fitness

for Duty (FFD) reports. As of January 3, 1990, FFD events are not

reportable as safeguards events (are reported pursuant to 10 CFR 26.73).

Functional Areas

A -

Plant Operations

B -

Radiological Controls

C - Maintenance/Surveillance

D -

Emergency Preparedness

E -

Security

F -

Engineering/Technical Support

G -

Safety Assessment/Quality Verification

The above data are based upon LERs 88-15 through 90-03.

TABLE 3B -

Unit 2

SYNOPSIS OF LICENSEE EVENT REPORTS (LERs)

Functional

SALP Cause Code*

Area

A

B

C

D

E

X

Totals

A.

Plant Operations

9

4

3

2

3

21

B.

Radiological

1

1

Controls

C. Maintenance/

3

1

2

6

Surveillance

D.

Emergency Prep.

E.

Security **

4

4

F. Engineering/

1

4

5

Technical Support

G.

Safety Assessment/

1

1

Quality Verif.

Totals

17

9

5

4

3

38

  • Cause Code

A -

Personnel Error

B - Design, Manufacturing or Installation Error

C -

External Cause

D - Defective Procedures

E - Component Failure

X -

Other

One Security LER is applicable to Unit 2 only; the remaining three are

applicable to Units 2 and 3. Security LERs include Fitness for Duty

(FFD) reports. As of January 3, 1990, FFD events are not reportable as

safeguards events (are reported pursuant to 10 CFR 26.73).

Functional Areas

A -

Plant Operations

B -

Radiological Controls

C - Maintenance/Surveillance

D - Emergency Preparedness

E -

Security

F - Engineering/Technical Support

G - Safety Assessment/Quality Verification

The above data are based upon LERs 88-27 through 89-23.

TABLE 3C - Unit 3

SYNOPSIS OF LICENSEE EVENT REPORTS (LERs)

Functional

SALP Cause Code*

Area

A

B

C

U

E

X

Totals

A. Plant Operations

1

3

1

1

6

B. Radiological

1

1

2

4

Controls

C. Maintenance/

2

1

3

Surveillance

D. Emergency Prep.

E. Security

F. Engineering/

2

2

Technical Support

G. Safety Assessment/

Quality Verif.

Totals

4

4

3

3

1

15

  • Cause Code

A

Psonnel Error

B - Design, Manufacturing or Installation Error

C - External Cause

D - Defective Procedures

E - Component Failure

X -

Other

Functional Areas

A - Plant Operations

B - Radiological Controls

C -

Maintenance/Surveillance

D -

Emergency Preparedness

E - Security

F - Engineering/Technical Support

G -

Safety Assessment/Quality Verification

The above data are based upon LERs 88-09 through 90-01.

ATTACHMENT 1

ANALYSIS OF LICENSEE EVENT REPORTS (LERs)

PREPARED BY THE

OFFICE FOR ANALYSIS AND EVALUATION OF OPERATIONAL DATA

Erclcsure

AEOD Input to SALP Review for San Onofre Unit 1

During the assessment period of October 1, 1988, to January 31,

1989, 34 LERs

were submitted to the NRC. Our review encompassed LERs 88-15 through 89-2F.

1. Important Operating Events

Utilizino AEOD's screening process, the following 14 Unit 1 LERs were categorized

as important events:

LER 88-18: The structural integrity of 156 sleeved steam generator tubes might

not have been in accordance with design requirements from the time

they were installed in 1981 until they were plugged in December

1988. Eddy current testing methods, utilized at the time of sleeve

installation, did not detect inadequate tube roll expansions.

State-of-the-art eddy current testing technology was utilized to

identify the problem tubes.

(Event date: 12/12/88).

LER 88-19:

Design deficiencies existed in the Train "B" automatic controls

for the electrical power distribution system. Upon actuation of

certain safeguard systems, unqualified non-safety related loads

would not be isolated from the safety related portions of the

distribution system. This condition could electrically overload

the emergency diesel generator. With a main steam lire break

occurring in certain locations outside containment, spurious

actuations and malfunctions of non-safety related loads could

result in Train "A" voltage degradation and failure of the safety

related Train "A" loads to start.

The design deficiencies were caused by placing excessive reliance

on multiple contractors, and the lack of programs to compile,

update, and verify design basis documents. A training program for

supervisory personnel performing the review of engineering and

technical work was initiated.

(Event date:

12/13/88).

LER 88-20: Design requirements of post-TMI Action Plan (NUREG-0737)

Item II.E.1.2, Part 2 were not fully implemented in the design of

the steam generator wide-range level indication system. The level

indicators (one per steam generator) were not powered from a

battery-backed electrical power source, and the associated level

transmitters, installed inside containment, were not environmentally

qualified. The level indication system serves as one of two means

providing auxiliary feedwater flow indication. The cause was

attributed to weaknesses in the licensee's commitment management

program. (Event date:

12/8/88).

LER 88-21: 8 of 33 contairment fire protection system spray nozzles were found

to be plugged, due to piping corrosion. Minor leakage of borated

water through a spray isolation valve might have accelerated the

-2

corrcsion. Corrective actions included blowing the system with air

to ensure corrosion products and blockage were completely removed,

replacing nozzles with a non-clocing type, and performing air flow

tests.

(Event date:

12/12/88).

LEP 89-01: Three reactor vessel thermal shield support block bolts were found

to be protruding from the inner surface of the core barrel in excess

cf normal tolerances. Failure of the bolts was believed to have

been caused by high-cycle flow induced vibration.

As corrective actions, accessible support features were inspected

by remote video camera, and an engineering analysis was performed

to support continued plant operation. Additionally, a conceptual

design and plan for restoring the thermal shield supports was

initiated. (Event date:

1/8/89).

LER 89-03:

In response to NPC Generic Letter 88-14, the licersee determined

that during a design basis LOCA, the component cooling water (CCW)

control valves to the RHR heat exchangers could fail open due to

either assumed 1) loss of instrument air or 2) loss of the electri

cal control power supply. This could result in a decrease in CCW

flow to the recirculation heat exchanger to a value below that

assumed in the safety analysis. Assuming a single failure which

renders two CCW pumps inoperable, the remaining CCW pump could

runout, creating a total loss of CCW.

The failure modes and effects analysis, performed in 1976, did

not recognize the effects of failure of the CCW control valves.

The licensee installed blocking devices on the control valves

to limit the degree to which they can open.

Flow tests were also

performed to verify adequate flow distributions of CCW with one

pump in operation. (Event date: 1/27/89).

LER 89-04: A design deficiency was identified ir the automatic loading circuitry

of the safety-related 4 kV buses. When the bus load sequencers

initiate in response to a safety injection signal concurrent with a

loss of offsite power, the loss of power latch is reset as soon as

the diesel generator output breaker closes and voltage to the bus

is restored. Consequently, if one bus is energized by a diesel

generator in a shorter time than the other diesel generator, the

loss of power latch in the load sequencer associated with the

lagging diesel generator will be reset, and the output of the

breaker for that diesel generator will not have the reouire logic

to close.

Deficiencies with engineering review, oesign basis documentation,

and post-modification testing caused the concern. A training

program for supervisory personnel was initiated, and a design basis

documentation program was established. (Event date: 3/2/89).

LER 89-07: Design provisions, intended to trip reactor in event of a reactor

coolant pump (RCP) locked rotor, did not satisfy single failure

criterion. The existing RCP over-current protection scheme was

set-up to trip the RCP after a 24 second time delay. The time delay

relay was not bypassed after the pump was running. Therefore, the

pump protection scheme would not respond to a locked rotor ccndition

for 24 seconds. Single failure analysis assumed the locked rotor

(high current) trip would occur within 6 seconds.

The RCP over current protection settings were not reviewed during

performance of the reactor protection system single failure analysis

performed in 1987.

Failure to detect the error resulted from

absence of clear design basis documentation.

(Event date: 2/27/F9').

LER 89-08: Containment fire suppression system pneumatic control valve CV-92

could fail open due to a single spurious failure of the solenoid

valve which controls CV-92. This failure could divert flow from

the containment spray system during a LOCA, and result in contain

ment pressure reaching a value greater than design pressure. The

single failure analysis of the ECCS, performed in 1987, did not

address failure of CV-92.

A design change was made to the CV-92 control circuitry to preclude

opening due to a single failure. A single failure re-analysis of

the ECCS and supporting systems was performed. A training program

for supervisory personnel was also initiated.

(Event date:

3/8/89).

LER 89-11:

Upon initiation of safety injection, the main feedwater pumps (MFPs)

realign to take suction from their respective SI trains and discharge

into the RCS. MFP minimum flow valves, assumed to close within 21

seconds following safety injection actuation with loss of offsite

power, would be delayed in closing due to wiring discrepancies,

contrary to safety analysis. Accordingly, delivery of safety

injection flow to the RCS would be below that assumed in the safety

analysis.

The cause of this condition was inadeouate implementation cf design

basis requirements. General engineering deficiencies, as described

in previous LERs, contributed to this situation. The minimum flow

system has been modified. (Event date:

3/23/89).

LER 89-14: Unlimited operation of the DC buses on cross-train chargers during

the period 1977 through early 1989 (as allowed by existing technical

specifications) was subsequently determined to have reduced the

reliability of the onsite emergency electrical system during

accident scenarios. In the event of a loss of offsite power,

concurrent with failure of an emergency diesel generator, having

the chargers previously aligned to the opposite trains could result

in reduction of battery voltage and loss of control power to the

other diesel generator within 90 minutes.

-4

Operation of the buses under these conditions was caused by failure

to develop appropriate technical specifications.

Design changes to separate the chargers have been completed.

Inadequate engineering and technical work were causes of this event.

(Event date: 4/5/89).

LER 89-24: The licensee deteriined that the plant could be placed in a

configuration which could result in degraded containment spray

system flow.

If the containment spray system flow restricting

valves were in a closed position, and a loss of non-safety related

instrument air occurred, the spray system would be unable to

perform its intended function. An emergency backup nitrogen supply

to open the valves upon loss of instrument air should have been

provided in the design.

Weak engineering design control and poor understanding of the

design basis of the valves contributed to the problem. Technical

specification changes were made to address the issue. Corrective

actions associated with engineering weaknesses were described in

similar LERs described above. (Event date:

9/29/89).

LER 89-25:

Similar to LER 89-24, it was determined that the primary hot leg

recirculation function was susceptible to loss of non-safety

related instrument air. Two valves in the hot leg recirculation

path would fail closed on loss of instrument air, resulting in a

condition where boron precipitation in the core region could

possibly occur. Weaknesses in licensing support to the plant were

identified as the root cause of the event. A nitrogen backup

supply to the instrument air system for the valves was added.

(Event date:

10/12/89).

LER 89-26:

Charging isolation valve CV-304 failed to close when provided with

a close sional, rendering the valve inoperable. Entry into

Technical

pecification 3.0.3 was required, as the appropriate

technical specification did not have an action statement for this

situation. However, the required entry into TS 3.0.3 was not

recognized until two days later.

In the event of a LOCA combined with a single failure of isolation

valve FCV 1112 (isolates the RCS loop "A" cold leg, and auxiliary

spray/hot leg recirculation paths) during the 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> CV-304 was

inoperable, inadequate core cooling would have occurred.

Failure of the valve to close was attributed to failure of an

Automatic Switch Co three-way solenoid air valve. The manufacturirg

process utilized Dow Corning 550 lubricant, which hardened with

elevated tempEratures. The valve was replaced. (Event date:

8/23/89).

2. Preliminary Nctifications

Eight preliminary notifications (PNs) pertaining to Unit 1 were issued by

Region V during the assessment period. For those events described in the PIs

which warranted LERs from the licensee, the LERs were verified to have been

submitted. No omissions were identified.

S. LER Overview

Causes of the events are distributed among various categories, however an

inordinate number of the LERs were associated with design and design change

programmatic deficiencies.

4. LER Timeliness and Quality

LERs submitted by the licensee were timely and of high quality, with the

exception of LER 89-11. LER 89-11 indicated a supplemental LER was expected

to be issued by June 16, 1989, however, it was not issued until December 5,

1989.

5. 10 CFR 50.72 Reports

Based upon preliminary information provided by the licensee in immediate

notification reports submitted pursuant to 1OCFR50.72, it appears additional

LERs should have been submitted to the NRC in accordance with 1OCFR50.73 on

the following events:

EN 14598:

Postulated overload of 480 volt switchgear 1 & 2 main feeder breaker

following initiation of safety injection without loss of offsite

power (Event Date:

1/30/89).

EN 15046:

Automatic start of an emergency diesel generator when restoring the

south circulating water pump to service (event date 3/17/89).

Region V should assess the need for additional 50.73 reports on these items.

6. Abnormal Occurrences and Other Events of Interest

No events occurring during this assessment period were classified as Abnormal

Occurrences for inclusion in the NUREG-0090 report to Congress.

7. AEOD Reports

No AEOD reports were issued regarding events occurring at San Onofre Unit 1

during this evaluation period.

ENCLOSURE

AEOD Input To SALP Review For San Onofre 2 & 3

The Southern California Edison Company submitted licensee event reports for

San Onofre Units 2 and 3 durine the assessment period from October 1, 1988 to

January 31, 1990. The reports for Unit 2 included LER numbers 361-88-028

through 361-88-037 and 361-89-001 through 361-89-011. The reports for Unit 3

included LER numbers 362-88-010 through 361-88-01? and 361-89-001 through

361-89-011. We reviewed those LERs and related event reports and our review

findings are as follows:

1. Significant Operdting Events

Based on the AEOD LER screening criteria, two of the unit 2 events during this

period were found to be important from the safety standpoint. The events are

as follows:

LER 361-88-034. On December 15, 1988, while operating at 100% power, it was

determined that the unit 2 component cooling water system (CCWS) did not meet

its design basis.

Specifically, safety related systems should be designed to

withstand the effects of natural phenomena such as earthquakes. However,

components in the component cooling water system were powered by non-1E, non

seismfic power supplies.

LER 361-89-004.

Or Feburary 9, 1989, unit 2 was taken critical with all four

channels of the Core Protection Calculators (CPCs) inoperable. This was the

result of a misunderstanding by the operators of the function of the CPC alarm

and annunciator lights.

None of the events at San Oriofre during this time period was determined to be

an abnormal occurrence.

2. Emergency Notification Reports

The 50.72 reports for this period were evaluated and compared to the LERs

submitted. It was found that LERs had been submitted where appropriate for

events described in 50.72 reports for San Onofre units 2 and 3.

3. AEOD Technical Study Reports

None of the events at San Onofre during the time period of this assessment

was the subject of an in-depth technical study by AEOD.

4. Preliminary Notifications of Event or Occurrence

Six PNOs were issued during the period of the assessment. They are as

follows:

.

PNO-V-88-062; on 881119, an earthquake occurred 30 miles west of San Clemente.

PNO-V-89-004; cn 890106, a reactor trip and safety injection actuation

occurred at Unit 3. It was caused by failure of a non-1E power supply due to

a ground jumper. The jumper was removed and steam generator level sensing

lines blown down for sludge accumulation. (This was later reported in LER

362-89-001.

PNO-V-89-006; on 890111, a plant shutdown of Unit 2 was required by technical

specifications due to an inoperable motor-driven auxiliary feedwater pump.

(This was later reported in LER 361-89-001.)

PNO-V-89-008; On 890118, a magnitude 5 earthquake occurred 8 miles south of

MalibL.

PNO-V-89-014; on 890209, panel annunciators illuminated before the Unit 2

startup which indicated the core protection calculators were inoperable, but

the crew observed that the console indications were normal.

(This was later

reported in LER 361-89-004.)

PNO-V-89-023; on 890407, a magnitude 4.6 earthquake occurred near Newport

Beach. Unit 1 reported no damage.

PNO-V-89-025; on 890407, Unit 3 went into an unscheduled shutdown for more

than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. This was caused by a reactor trip due to a drop in voltage on

the rod drive bus after a breaker trip, an atmospheric dump valve not

operating properly, and a leak in the vent line.

(This was later reported in

LER 362-89-006.)

PNO-V-89-028; on 890512, a primary-to-secondary leak rate of 117 gallons per

day occurred at Unit 3. On 890513, steam generator blowdown radiation monitor

indication increased one decade.

The reactor was to be shutdown and drained

to mid-loop tc repair the leaking tube(s).

PNO-V-89-038; on 890629, excessive shaft leakage was identified while

performing inservice testing of a LPSI pump at Unit 3. (This was reported in

LER 362-89-008.)

PNO-V-89-068; on 891201, a hydrogen fire in the radwaste building occurred

during changeout of a relief valve on a waste gas decay tank. There were

no injuries, no equipment damage, and no release of radioactive material.

It appears that LERs have been submitted where required for events described

by the Region in PNOs.

5. LER Quality

The LERs described the major aspects of the events, including component or

system failures that were contrituting factors.