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Category:E-Mail
MONTHYEARML24025A1592024-01-25025 January 2024 NRR E-mail Capture - Shearon Harris Nuclear Power Plant, Unit 1 - Request for Additional Information - Rvi AMP and Inspection Plan (L-2023-LLL-0016) ML23177A1992023-06-26026 June 2023 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-23-0005 - LAR to Align Certain TSs with ISTS (L-2023-LLA-0078) ML23172A0132023-06-20020 June 2023 Duke Fleet - Correction to June 2, 2023, Request for Additional Information Proposed License Amendment Request to Revise Restrictive Surveillance Requirement Frequencies ML23153A1892023-06-0202 June 2023 Duke Fleet - Request for Additional Information Proposed License Amendment Request to Revise Restrictive Surveillance Requirement Frequencies ML23151A3482023-05-30030 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML23142A2732023-05-22022 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) ML23124A1212023-05-0404 May 2023 Acceptance of Requested Licensing Action Duke Fleet Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML23082A0432023-03-23023 March 2023 002 Radiation Safety Baseline Inspection Information Request Final ML23073A2282023-03-13013 March 2023 Duke Fleet- Adoption of TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements - Acceptance Review ML23065A0942023-03-0606 March 2023 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-22-0081 - LAR to Address Administrative Changes to the Operating License and Technical Specifications (L-2023-LLA-0020) ML23058A0562023-02-27027 February 2023 Acceptance of Amendment to Revise Surveillance Frequencies for RCS Pressure Isolation Valve Operational Leakage Testing and Reactor Trip System Instrumentation ML23048A1512023-02-16016 February 2023 Acceptance Review - Proposed Alternative for Steam Generator Welds (L-2023-LLR-0003) ML22237A1632022-08-25025 August 2022 004 Radiation Safety Baseline Inspection Information Request ML22115A1412022-04-25025 April 2022 NRR E-mail Capture - Duke Common EOF Relocation - Request for Addition Information ML22108A0182022-04-15015 April 2022 NRR E-mail Capture - Accepted for Review - Duke Energy Relief Request for Harris Nuclear Plant Inservice Testing Program Plan - Fourth Ten-Year Interval to Extend Type C Test to 75 Months ML22083A0702022-03-24024 March 2022 NRR E-mail Capture - Catawba Nuclear Station, Units 1 and 2, Shearon Harris Nuclear Power Plant, Unit 1, and McGuire Nuclear Station, Units 1 and 2 - Acceptance Review for TSTF-569 LAR ML22083A0282022-03-23023 March 2022 Email Snsb Safety Evaluation for Harris LAR to Revise Reactor Protection System TS ML22038A1572022-02-0707 February 2022 NRR E-mail Capture - Duke Energy Fleet - Acceptance of License Amendment Request Regarding Adoption of TSTF-541, Revision 2 ML22018A0272022-01-18018 January 2022 2022 All RFI Responses - Exercise and Program Inspections - Revl ML21361A0122021-12-23023 December 2021 NRR E-mail Capture - Accepted for Review - Duke Energy Fleet License Amendment Request to Relocate Emergency Operations Facility ML21354A8612021-12-15015 December 2021 NRR E-mail Capture - Request for Additional Information - Duke Fleet Request RA-19-0352 - Alternative for RPV Closure Stud Exams (L-2020-LLR-0156) ML21321A3782021-11-16016 November 2021 NRR E-mail Capture - Energy Harbor Fleet, Beaver Valley Units 1 and 2 and DAVIS-BESSEL Unit 1 - Acceptance of License Amendment Request Adoption of TSTF-554 EPID-L-2021-LLA-0193 ML21288A0802021-10-15015 October 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-21-0213 - Remove Limitations to Perform Certain SRs During Shutdown (L-2021-LLA-0167) ML21295A0372021-10-0505 October 2021 NRR E-mail Capture - Accepted for Review - Duke Energy Fleet License Amendment Request to Adopt TSTF-577 Revised Frequencies for Steam Generator Tube Inspections ML21252A0112021-08-30030 August 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1- RA-21-0191 - Revised TS Related to Reactor Trip System Instrumentation (L-2021-LLA-0149) ML21189A0282021-07-0101 July 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-21-0112 - Revise TS to Reflect Development of TRM (L-2021-LLA-0108) ML21172A2432021-06-21021 June 2021 NRR E-mail Capture - Request for Additional Information - Harris RA-20-0252 - LAR to Remove Extraneous Requirements from OL and TS (L-2021-LLA-0027) ML21106A0112021-04-15015 April 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-21-0052 - Revise Containment Spray Nozzle Surveillance Frequency (L-2021-LLA-0058) ML21084A2492021-03-24024 March 2021 Notification of Inspection and Request for Information ML21084A2512021-03-22022 March 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-20-0252 - LAR to Remove Extraneous Content and Requirements from the OL and TS (L-2021-LLA-0027) ML21039A6382021-02-0808 February 2021 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1-RA-20-0311 - 10 CFR 50.69 Categorization Process to Reflect an Alternative Seismic Approach (L-2021-LLA-0003) ML21036A1142021-02-0505 February 2021 NRR E-mail Capture - Request for Additional Information - Harris - Relief Request RA-20-0312 - SW Pinhole Leak (L-2020-LLR-0143) ML21049A2632021-02-0404 February 2021 NRR E-mail Capture - Request for Additional Information - Duke Energy Fleet License Amendment Request to Revise Emergency Plan ML21033A8452021-02-0202 February 2021 NRR E-mail Capture - State Notification of Amendments to Shearon Harris Nuclear Power Plant, Unit 1 - Revision Minimum RCS Flow Rate and Update COLR References ML21033B1062021-02-0202 February 2021 NRR E-mail Capture - (External_Sender) (External) State Notification of Amendments to Shearon Harris Nuclear Power Plant, Unit 1 - Revision Minimum RCS Flow Rate and Update COLR References ML21032A0492021-02-0101 February 2021 NRR E-mail Capture - Request for Additional Information - Duke Fleet RA-20-0263 - Use of Later ASME B&Pv, XI for Repair - Replacement (L-2020-LLR-0124) ML21025A2922021-01-25025 January 2021 NRR E-mail Capture - (External_Sender) State Notification of Amendment to Shearon Harris Nuclear Power Plant, Unit 1 - Revise TS 3/4.4.9, Pressure/Temperature Limits - Reactor Coolant System ML21007A3722021-01-0707 January 2021 NRR E-mail Capture - Acceptance Review - Duke Fleet - RA-19-0352 - Proposed Alternative for Reactor Vessel Close Stud Examinations (L-2020-LLR-0156) ML21006A4302021-01-0606 January 2021 Acceptance Review - Duke Fleet RA-20-0207 Request to Revise the Technical Specification for Engineered Safety Feature Actuation System (ESFAS) Instrumentation ML21006A4042021-01-0606 January 2021 NRR E-mail Capture - State Notification of Amendment to Shearon Harris Nuclear Power Plant, Unit 1 - Revise TS 3/4.4.9, Pressure/Temperature Limits - Reactor Coolant System ML20345A3052020-12-10010 December 2020 NRR E-mail Capture - (External_Sender) (External) State Notification of Amendments to Shearon Harris Nuclear Power Plant, Unit 1 - Revise TS 3.3.3.6 and TS 3.9.2 ML20344A4192020-12-0909 December 2020 NRR E-mail Capture - State Notification of Amendments to Shearon Harris Nuclear Power Plant, Unit 1 - Revise TS 3.3.3.6 and TS 3.9.2 ML20328A0802020-11-23023 November 2020 NRR E-mail Capture - Acceptance Review - Shearon Harris Nuclear Power Plant, Unit 1 - RA-20-0312-Relief Request, Service Water Pinhole Leak in a Socket Weld, Inservice Inspection (L-2020-LLR-0143) ML20323A4072020-11-18018 November 2020 NRR E-mail Capture - Request for Additional Information - Brunswick License Exemption Request from 10CFR73 Annual Force on Force Exercise Requirements (EPIC L-2020-LLE-0180) ML20297A3102020-10-13013 October 2020 NRR E-mail Capture - Acceptance Review - Duke Fleet - RA-20-0191 - Request to Use a Provision of a Later Edition of the ASME B&PV Code, Section XI - IWA-5120, IWA-5213, IWA-5241, IWA-5242, and IWA-5250 (L-2020-LLR-0126) ML20297A3072020-10-13013 October 2020 NRR E-mail Capture - Request for Additional Information - Shearon Harris Nuclear Power Plant, Unit 1 - RCS Flowrate Reduction/Lbloca LAR ML20297A3082020-10-0707 October 2020 NRR E-mail Capture - Acceptance Review - Duke Fleet - RA-20-0263 - Request to Use a Provision of a Later Edition of the ASME B&PV Code, Section XI for Repair/Replacement (L-2020-LLR-0124) ML20297A3092020-10-0606 October 2020 NRR E-mail Capture - Acceptance Review - Duke Fleet - RA-20-0262 - Request to Use a Provision of a Later Edition of the ASME B&PV Code, Section XI - IWA-4540(b) (L-2020-LLR-0125) ML20274A0462020-09-29029 September 2020 Request for Additional Information Regarding License Amendment Request to Adopt TSTF-505, Revision 2 ML20247J3822020-09-0303 September 2020 Request for Additional Information - Shearon Harris Nuclear Power Plant, Unit 1 - Revise TS Related to Accident Monitoring and RFO Instrumentation 2024-01-25
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Worosilo, Jannette From: Wade Loo / 2 Sent: Wednesday, April 29, 2009 5:28 PM To: Brian Bonser; Randy Musser Cc: Ruben Hamilton; George Kuzo; Donald Forbes; Patrick Lessard; Joseph Austin; Jannette Worosilo
Subject:
RE: Update on Groundwater Monitoring/Blowdon Line at Harris Need to clarify one point. MPC inspected over 5,000 feet of pipe from the cooling tower to the last manway which is located a few feet where the land meets the lake reservoir and not the opening because the opening is in the middle of the lake.
From: Wade Loo Sent: Wednesday, April 29, 2009 3:59 PM To: Brian Bonser; Randy Musser Cc: Ruben Hamilton; George Kuzo; Donald Forbes; Patrick Lessard; Joseph Austin; Jannette Worosilo
Subject:
Update on Groundwater Monitoring/Blowdon Line at Harris Just to let you know where we are at regarding the cooling tower blowdown line with regards to HP issues in short. We have had several meetings with the various licensee staff and walked down the various areas of the blowdown line and have the following information:
- 1) Silar Services, who conducted the groundwater site characterization study and installed monitoring wells (Silar did work for Brunswick)*, subcontracted with Miller Pipeline Corporation (MPC) to inspect the condition of the inside of the pipe. MPC inspected over 5,000 feet of the fiberglass pipe from the cooling tower to the pipe discharge opening into the lake reservoir (one area of the pipe was not inspected, -300 feet downstream from the cooling tower to cistern #1 due to low oxygen concentrations and the ability of the workers to egress from that area of the pipe safely due to large amounts of mud in one section of the pipe, they are referring to it as the "dead end pipe"). MPC completed that inspection and its preliminary report identified numerous cracks, space between joints, and roots growing on the inside of the pipe all along the entire length of the pipe where the discharge could potentially leak into the surrounding ground.
- 2) With regards to the elevated tritium levels observed and reported in accordance with the Groundwater Protection Initiative, the licensee had MPC repair a pipe crack -200 ft downstream cistern #2 using a "Weco Seal" (metal bands that hold a rubber gasket in place over the crack and entire diameter of the pipe area).
Based on the slope of the downstream portion (did not slope down downstream direction but sloped down upstream direction), the amount of water found in it (water filled in upstream in valley between cistern #1 and manhole which is downstream of cistern #2), and condition of the inside pipe (entire circumference of pipe is dirty and not clear) they believe this crack is the one that has the highest potential for leaking the tritium to the monitoring wells and needed an immediate fix via this "Weco Seal".
- 3) The licensee only repaired one crack in the pipe. There are other large cracks and spaces in joints identified in the pipe downstream but due to the oval or egg shape of the inside diameter of the pipe this "Weco Seal" is not an option for repair (good for repairing round pipes but not oval shaped pipes). In addition, there were areas of the pipe that had horizontal and vertical cracks together (cross shaped). These cracks were not repaired with the "Weco Seal" because the pressure from the "Weco Seal" to seal the vertical crack could propagate and cause more damage to the horizontal cracks in that same area.
- 4) MPC has not finalized their report but the licensee is hoping to have a draft report by next week (tMPC just completed their pipe inspection late yesterday). The licensee is awaiting MPC's report so that Engineering can evaluate it and determine from that report what actions to take with regards to addressing how to fix the pipe.
There are several options on the table: a) repair the cracks that can be repaired with the "Weco Seal"; b) 1
replace portions of the pipe that need to be fixed; c) place an inner sleeve in the areas of the pipe that need to be fixed; or 4) just put in a whole new blowdown line. This has not been decided at this time.
- 5) The licensee is awaiting this report so that they can evaluate if they will need additional monitoring wells installed (which they most likely will need to do since they have identified numerous cracks and open joints in the pipe) and if so, where to install them.
- 6) We have reviewed liquid release permits for discharges made since discovery of the pipe cracks. All were within the confines of the permit that allowed the release and were within their ODCM limits.
- 7) We have lots of documents to bring back for everyone to look at if there are any questions (release permits, diagrams of the blowdown line, pictures of the inside of the pipe and "Weco Seal", NCRs associated with this issue, monitoring well sample results, composite sampler results, etc.
- 8) The licensee is planning to have a conference call with the region and residents next Tuesday at -10:00 AM to discuss the status of the blowdown line.
- 9) We have reminded Plant Personnel not to forget about areas that should be added to decommissioning plans.
Hope this is what you are looking for as far as a summary. We could not get electonic copies of the pictures so that you could look at them now but I have color copies of some of them that I will bring back next week. May be kinda hard to understand what I am talking about above but hopefully, with the pictures and diagrams, they can help you understand it.
Let me know if you have any questions. Otherwise, we can talk more on this next week. Thanks.
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