ML101650723

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IR 05000317-10-006 and 05000318-10-006; on 02/22/2010 - 04/30/2010; Calvert Cliffs Nuclear Power Plant Special Inspection for the February 18, 2010 Dual Unit Trip, Inspection Procedure 93812, Special Inspection
ML101650723
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 06/14/2010
From: David Lew
Division Reactor Projects I
To: George Gellrich
Constellation Energy Nuclear Group
References
EA-10-080 IR-10-006
Download: ML101650723 (45)


See also: IR 05000317/2010006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406*1415

June 14, 2010

EA-10-080

George H. Gellrich, Vice President

Calvert Cliffs Nuclear Power Plant, LLC

Constellation Energy Nuclear Group, LLC

1650 Calvert Cliffs Parkway

Lusby, Maryland 20657-4702

SUBJECT:

CALVERT CLIFFS NUCLEAR POWER PLANT - NRC SPECIAL INSPECTION

REPORT 05000317/2010006 AND 05000318/2010006; PRELIMINARY WHITE

FINDING

Dear Mr. Gellrich:

On April 30, 2010. the U. S. Nuclear Regulatory Commission (NRC) completed a Special

Inspection of the February 18, 2010, dual unit trip at Calvert Cliffs Nuclear Power Plant

(CCNPP) Units 1 and 2. The enclosed report documents the inspection results, which were

discussed on April 30, 2010, with you and other members ofyour staff.

The special inspection was conducted in response to the dual unit trip with complications on

February 18, 2010. The complications included loss of a 500 kilovolt (kV) offsite power supply

to each unit, loss of power to a 4 kV safety bus on each unit, failure of the 2B emergency diesel

generator (EDG) to reenergize a 4 kV safety bus, loss of power to the Unit 24 kV non-safety

buses, loss of Unit 2 forced reactor coolant system (RCS) flow, and loss of the Unit 2 normal

heat sink. The NRC's initial evaluation of this event satisfied the criteria in NRC Inspection

Manual Chapter 0309, "Reactive Inspection Decision Basis for Reactors," for conducting a

special inspection. The Special Inspection Team (SIT) Charter (Attachment 2 of the enclosed

report) provides the basis and additional details concerning the scope of the inspection.

The special inspection team (the team) examined activities conducted under your license as

they relate to safety and compliance with Commission rules and regulations and with conditions

of your license. The team reviewed selected procedures and records, observed activities,

conducted in-plant equipment inspections, and interviewed personnel. In particular, the team

reviewed event evaluations (including technical analyses), causal investigations, relevant

performance history, and extent-of-condition to assess the Significance and potential

consequences of issues related to the February 18 event.

The team concluded that, overall, station personnel maintained plant safety in response to the

reactor trips. Nonetheless, the team identified several issues related to equipment performance

and human performance which complicated the event. The enclosed chronology (Attachment 3

of the enclosed report) provides additional details on the sequence of events and event

complications.

G. Gellrich

2

This report documents one self-revealing finding that, using the reactor safety Significance

Determination Process (SDP). has preliminarily been determined to be White, a finding with low

to moderatE~ safety significance. The finding is associated with the failure to perform appropriate

maintenanc:e activities to ensure 2B EDG reliability. Specifically, safety related time delay

relays in th~:: EDG low lube oil pressure trip circuit were used beyond the manufacturer

recommended service life. without an associated test or monitoring program to demonstrate_

their continued reliability. Consequently, when called upon to reenergize the 24 4 kV safety

bus, the time delay relay failed and the 2B EDG prematurely tripped in response to a low lube

oil pressure signal. The 24 4 kV safety bus was reenergized from an alternate feed source

approximately 30 minutes into the event. The significance determination of the event was

performed assuming that similar time-delay relays on other systems have not failed due to this

performance deficiency. Subsequent corrective actions included replacing and retesting the

associated time delay relays on all three EDGs susceptible to the low lube oil pressure trip.

There is no current immediate safety concern due to this finding. because all EDGs have

subsequently been demonstrated operable and long term corrective actions are being

implemente1d through the Calvert Cliffs corrective action program to address the extent-of

condition and extent-of-cause. The final resolution of this finding will be conveyed ina separate

correspondence addressing the final risk significance and disposition of any violations.

As discussed i~ the attached inspection report. the finding is also an apparent violation (A V} of

NRC requirements, involving Technical Specification 5.4.1, and is therefore being considered

for escalated enforcement action in accordance with the Enforcement Policy, which can be

found on NRC's Web site at http://www.nrc.gov/reading-rom/doc-cotlections/enforcementi.

In accordance with NRC Inspection Manual Chapter (lMC) 0609, we will complete our

evaluation using the best available information and issue our final determination of safety

significanc: within 90 days of the date of this letter. The significance determination process

encourages an open dialogue between the NRC staff and the licensee; however, the dialogue

should not impact the timeliness of the staffs final determination.

Before we make a final decision on this matter, we are providing you with an opportunity (1 ) to

attend a Regulatory Conference where you can present to the NRC your perspective on the

facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2)

submit your position on the finding to the NRC in writing. If you request a Regulatory

Conference, it should be held within 30 days of your response to this letter and we encourage

you to submit supporting documentation at least one week prior to the conference in an effort to

make the conference more efficient and effective. If a Regulatory Conference is held. it will be

open for public observation. If you decide to submit only a written response. such submittal

should be s,ent to the NRC within 30 days of your receipt of this letter. If you deCline to request

a Regulatory Conference or submit a written response, you relinquish your right to appeal the

final SDP dE~termination,in that by not doing either, you fail to meet the appeal requirements

stated in the Prerequisite and Limitation sections of Attachment 2 of IMC 0609. We request that

if you decide to attend a Regulatory Conference or provide a written response, that you address

the apparent violation, and that you also address the length of time that the 28 EDG was

considered inoperable.

Please contact Glenn Dentel at (610) 337-5233 in writing within 10 days from the issue date of

this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we

wHl continue with our significance determination and enforcement decision. The final resolution

of this matter will be conveyed in separate correspondence.

G. Gellrich

3

Because the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for these inspection findings at this time. In addition, please be advised that the

number and characterization of the apparent violation described in the enclosed inspection

report may change as a result of further NRC review.

In addition, the report documents two NRC-identified findings and two self-revealing findings,

each of very low safety significance (Green). Three of these findings were determined to

involve violations of NRC requirements. However, because of the very low safety significance

and because they are entered into your corrective action program, the NRC is treating these

findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement

Policy. If you contest any NCV, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, AnN.:

Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Calvert

Cliffs Nuclear Power Plant. In addition, if you disagree with the characterization of any finding in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your disagreement. to the Regional Administrator, Region I, and the NRC

Senior Resident Inspector at Calvert Cliffs Nuclear Power Plant. The information you provide

will be considered in accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system .(ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,

I:t.~Ml~

Division of Reactor Projects

Docket Nos.: 50-317. 50~318

License Nos.: CPR-53, DPR-69

Enclosure:

Inspection Report 05000317/2010006 and 05000318/2010006

w/Attachments: Supplemental Information (Attachment 1)

Special Inspection Team Charter (Attachment 2)

Detailed Sequence of Events (Attachment 3)

cc w/encl:

Distribution via ListServ

Enclosure:

Inspection Report 05000317/2010006 and 05000318/2010006

G. Gellrich

3

Because the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for these inspection findings at this time. In addition, please be advised that the

number and characterization of the apparent violation described in the enclosed inspection

report may change as a result of. further NRC review.

In addition, the report documents two NRC-identified finding and two self-revealing findings,

each of very low safety significance (Green). Three of these findings were determined to

involve violations of NRC requirements. However, because of the very low safety significance

and because they are entered into your corrective action program, the NRC is treating these

findings as non-cited violations (NCVs) consistent with Section Vl.A.1 of the NRC Enforcement

Policy. If you contest any NCV, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial. to the Nuclear Regulatory Commission, ATTN.:

Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Calvert

Cliffs Nuclear Power Plant. In addition, if you disagree with the characterization of any finding in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your disagreement. to the Regional Administrator, Region I. and the NRC

Senior Resident Inspector at Calvert Cliffs Nuclear Power Plant. The information you provide

will be considered in accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.. 390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html{the Public Electronic Reading Room).

Sincerely,

IRAJ

David C. Lew. Director

Division of Reactor Projects

Docket Nos.:

50~317. 50-318

License Nos.: OPR-53, DPR~69

Enclosure:

Inspection Report 05000317/2010006 and 05000318/2010006

w/Attachments: Supplemental Information

Special Inspection Team Charter

Detailed Sequence of Events

cc w/encl:

Distribution via ListServ

Distribution w/encl (see attached page)

SUNSI Review Complete:

GTD

(Reviewer'S Initials

ML 101650723

DOCUMENT NAME: G:\\DRP\\BRANCH1\\CalverLCllffs\\CC SIT Report 2010-06 Final.doc

After declarin this document "An OffiCial

enc Record*, it will be released to the Public.

OFFICE

R!/DRP

RI/DRS

RIIDRP

NAME

DKern/dk via

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06/14/10

RI/DRP

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NRR

JClifford~c

NColeman/nc via email SWeeerakkody!sw via

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06f14/10

06/14/10

06114/10

OFFICIAL RECORD COPY

G. Gellrich

Distribution:

S. Collins, RA

M. Dapas, DRA

L Trocine, RI OEDO

J. Lubinski, NRR

D. Pickett, PM, NRR

G. Dentel, DRP

N. Perry, DRP

J. Hawkins, DRP

D. Lew, DRP

J. Clifford, DRP

4

S. Kennedy, DRP, Senior Resident Inspector

M. Davis, DRP, Resident Inspector

C. Newgent, DRP, Resident M

Region I Docket Room (with concurrences)

ROPResources@nrc.gov

L Pinkham, DRP

D. Kern, DRP, Senior Resident Inspector

1

Docket No.:

license No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Team Leader:

Team:

Observers:

Approved By:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-317

50-318

DPR-53. DPR-69

05000317/2010006, 05000318/2010006

Constellation Generation Company

Calvert Cliffs Nuclear Power Plant (CC)

Lusby, Maryland

February 22, through April 30. 2010

D. Kem. Senior Resident Inspector, Division of Reactor Projects (DRP)

W. Cook, Senior Reactor Analyst, Division of Reactor Safety (DRS)

M. Patel, Reactor Inspector. DRS

P. Presby, Reactor Inspector, DRS

B. Smith, Resident Inspector, DRP

R. Montgomery, Reactor Engineer, Nuclear Safety Professional

Development Program, DRP (added subsequent to issuance of the

Inspection Charter)

S. Gray, Power Plant Research Program Manager, Department of Natural

Resources, State of Maryland

M. Griffen, Nuclear Emergency Preparedness Coordinator, Department of

the Environment, State of Maryland

Glenn T. Dentel, Chief

Projects Branch 1

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY OF FINDINGS .............................................................................................................3

REPORT DETAilS.........................................................................................................................7

1.

Background and Description of Events .,. ........................................................................7

2.

Equipment Performance .................................................................................................8

3.

Human Performance .....................................................................................................21

4.

Organizational Response ..............................................................................................25

5.

Risk Significance of the Event. ......................................................................................27

40A3

Follow~up of Events ......................................................................................................28

40A6 Meetings, Including Exit ................................................................................................28

SUPPLEMENTAL INFORMATION............................................................................................. 1-1

KEY POINTS OF CONTACT...................................................................................................... 1-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .......................................................... 1-1

LIST OF D()CUMENTS REVIEWED .......................................................................................... 1-2

LIST OF ACRONYMS ................................................................................................................ 1-5

SPECIAL INSPECTION TEAM CHARTER ................................................................................ 2-1

DETAILED SEQUENCE OF EVENTS ........................................................................................ 3-1

Enclosure

3

SUMMARY OF FINDINGS

IR 05000317/2010006 and 05000318/2010006; 02/22/2010 - 04/30/2010; Constellation

Generation Company, Calvert Cliffs Nuclear Power Plant; Special Inspection for the February

18,2010. Dual Unit Trip; Inspection Procedure 93812, Specia/lnspection.

A six-pe~on NRC team. comprised of resident inspectors, regional inspectors, and a regional

senior reactor analyst conducted this Special Inspection. The team was accompanied by two

engineers from the State of Mary/and, Department of Natural Resources and Department of the

Environment. One apparent violation with potential for greater than Green safety significance

and four Green findings were identified. The significance of most findings is indicated by their

color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609, 'Significance

Determination Process' (SOP); the crosscutting aspect was determined using IMC 0310,

'Components Within the Cross Cutting Areas;' and findings for which the SOP does not apply

may be Green or be assigned a severity level after NRC management review. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

NRC Identified and Self Revealing Findings

Cornerstone: Initiating Events

Criterion XVI "Corrective Actions," was identified, because auxiliary building roof leakage

into the Unit 1 and Unit 2 45 foot switchgear rooms was identified on several occasions

from 2002 to 2009, but was not thoroughly evaluated and corrective actions to this

condition adverse to quality were untimely and ineffective. This degraded condition led

to the failure of the auxiliary building to provide protection to several safety related

systems from external events, a ground on a reactor coolant pump (RCP) bus, and

ultimately a Unit 1 reactor trip. Immediate corrective actions included: repair of

degraded areas of the roof; walk downs of other buildings within the protected area that

could be susceptible to damage to electrical equipment due to water intrusion; issuance

of standing orders to include guidance regarding prioritizing work orders due to roof

leakage; and identifying further actions to take during periods of snow or rain to ensure

plant equipment is not affected. Constellation entered the issue into their corrective

action program (Condition Report (CR) 2010-001351). Long-term corrective actions

include implementation of improved plant processes for categorization, prioritization and

management of roofing issues.

The finding is more than minor because it is associated with the protection against

external factors attribute of the Initiating Events Cornerstone and affected the

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The

team determined the finding had a very low safety significance because, although it

caused the reactor trip, it did not contribute to the likelihood that mitigation equipment or

functions will not be available. The cause of the finding is related to the crosscutting

area of Problem Identification and Resolution, Corrective Action Program aspect P.1 (c)

because Constellation did not thoroughly evaluate the problems related to the water

intrusion into the auxiliary building

Enclosure

4

such that the resolutions addressed the causes and extent-of-condition. This includes

properly classifying, prioritizing, and evaluating the condition adverse to quality. (Section

2.1)

  • Green: The team identified a finding for failure to translate the design calculations of

phase overcurrent relays on 13 kV feeder breakers into the actual relay settings. The

overcurrent relays protect the unit service transformer against faults in the primary or

secondary side windings. The design specified limit of 1200 amps was determined

based on the breaker rating of the feeder breakers. Constellation determined the as

found relay setting for the feeder breakers was 1440 amps which exceeded the rating of

the feeder breakers. The team determined that due to the as-found relay setting, certain

phase overcurrent conditions could potentially cause the breakers to fail prior to the

phase overcurrent relay sensing the degraded condition. This condition could affect the

recovery of the safety buses from the electrical grid. Constellation entered this issue into

the corrective action program (condition report 2010-002123).

The finding is more than minor because it affected the Initiating Events Cornerstone

attribute of equipment performance for ensuring the availability and reliability of systems

to limit the likelihood of those events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. Also, this issue was

similar to Example 3j of IMC 0612, Appendix E, "Examples of Minor Issues," because

the condition resulted in reasonable doubt of the operability of the component, and

additional analysis was necessary to verify operability. This finding was determined to

be of very low safety significance because the design deficiency did not result in an

actual loss of function* based on Constellation's determination that the maximum load

current possible would not challenge the feeder breaker ratings. Enforcement action

does not apply because the performance deficiency did not involve a violation of a

regulatory requirement. The finding did not have a cross-cutting aspect because the

most significant contributor to the performance deficiency was not reflective of current

licensee performance. (Section 2.3)

Cornerstone: Mitigating Systems

Preliminary White: The NRC identified an apparent violation of Technical Specification 5.4.1 for the failure of Constellation to establish, implement, and maintain preventive

maintenance requirements associated with safety related relays. The team identified

that Constellation did not implement a performance monitoring program specified by the

licensee in Engineering Service Package (ES2001 00067) in lieu of a previously

established (in 1987) 1 O-year service life replacement PM requirement for the 28 EDG

T3A time delay relay. As a consequence, the 26 EDG failed to run following a demand

start signal on February 18, 2010. Following identification of the failed T3A relay, it was

replaced and the 28 EDG was satisfactorily tested and returned to service. In addition,

time delay relays used in the 1 Band 2A EDG protective circuits, that also exceeded the

vendor recommended 1 O-year service life, were replaced. Constellation entered this

issue, including the evaluation of extent-of-condition, into the corrective action program.

This finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and adversely impacted the objective of

ensuring the availability, reliability, and capability of the safety related 2B EDG to

Enclosure

5

respond to a loss of normal electrical power to its associated safety bus. This finding

was assessed using IMC 0609. Appendix A and preliminarily determined to be White

(low to moderate safety significance) based upon a Phase 3 Risk Analysis with an

exposure time of 323 days which resulted in a total (internal and external contributions)

calculated conditional core damage frequency (CCDF) of 7.1 E-6. The cause of this

finding is related to the crosscutting area of Human Performance, Resources aspect

H.2(a} because preventive maintenance procedures for the EDGs were not properly

established and implemented to maintain long term plant safety by maintenance of

design margins and minimization of long standing equipment issues. (Section 2.2)

Action," because Constellation did not thoroughly evaluate and correct a degraded

condition of a C0-8 relay disc sticking or binding issues which can adversely impact the

function of the EDGs and the electrical distribution protection scheme. Specifically,

following the February 18. 2010 event, Constellation did not identify and adequately

evaluate the recent CO*8 relay failures due to sticking or binding of the induction discs in

the safety related and non-safety related applications. Constellation entered this issue

into the corrective action program (CR 20100004673).

The finding is more than minor because it is associated with the equipment reliability

attribute of the Mitigating Systems Cornerstone, and it adversely affected the associated

cornerstone objective of ensuring the availability. reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (I.e., core

damage). This finding was determined to be of very low safety significance because

these historical relay failures did not result in an actual loss of system safety function.

The cause of the finding is related to the crosscutting area of Problem Identification and

Resolution, Corrective Action Program aspect P.1(c) because Constellation did not

thoroughly evaluate the previous station operating experience of CO-8 relay induction

disc sticking and binding issues such that resolutions addressed the causes and extent

of-condition. (Section 2.3)

identified for failure to establish adequate procedures for restoration of Chemical and

Volume Control System (CVCS) letdown flow. On February 18, 2010, an electrical

ground fault caused a Unit 1 reactor trip, loss of the 500 kV Red Bus, and cves letdown

isolation as expected on the ensuing instrument bus 1Y10 electrical transient. Deficient

operating instructions prevented timely restoration of letdown flow following the initial

transient. Pressurizer level remained above the range specified in Emergency

Operating Procedure (EOP}-1 for an extended period because of the operators' inability

to relstore letdown. This ultimately led to exceeding the TS high limit for pressurizer

level. CVCS Operating Instruction Ol-2A was subsequently revised, providing

necessary guidance for re-opening the letdown system excess flow check valve to

restore letdown flow. This event was entered into the licensee's corrective action

program (CR 2010-001378).

The finding is more than minor because it is associated with the procedure quality

attrilJute of the Mitigating Systems Cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences (Le., core damage). The finding is of very

low safety significance because it is not a deSign or qualification deficiency, did not

represent a loss of a safety function of a system or a Single train greater than its TS

Enclosure

6

allowed outage time, and did not screen as potentially risk significant due to external

events. This finding has a crosscutting aspect in the area of human petiormance,

resources aspect H.2(c), because Constellation did not ensure that procedures for

restoring eves letdown were complete and accurate. (Section 3.1)

Enclosure

7

REPORT DETAILS

1.

Background and Description of Events

In accordance with the Special Inspection Team (SIT) charter (Attachment 2), team

members (the team) conducted a detailed review of the February 18, 2010, dual unit trip

with complications at Calvert Cliffs Nuclear Power Plant including equipment and

operator response. The team gathered information from the plant process computer

(PPC) alarm printouts, interviewed station personnel, performed physical walkdowns of

plant equipment, and reviewed procedures, maintenance records, and various technical

documents to develop a detailed timeline of the event (Attachment 3). The following

represents an abbreviated summary of the Significant automatic plant and operator

responses which began at 8:24 a.m. on February 18, 2010, and ended on February 22,

2010, with both Unit 1 and Unit 2 in cold shutdown:

On February 18, 2010, at 8:24 a.m., the Unit 1 reactor automatically tripped from 93

percent reactor power in response to a reactor coolant system (RCS) low flow condition.

Water had leaked through the auxiliary building roof into the 45' elevation switchgear

room, causing an electrical ground on bus 14 which tripped the 12B reactor coolant pump

(RCP), thereby initiating the reactor protection system trip on RCS low flow. Three of the

four Unit 1 RCPs continued operating.

Ground overcurrent (O/C) relay 2RY251 G/B-22-2 failed to actuate as designed,

permitting the Unit 1 ground O/C condition to reach the Unit 2 2213 kV RCP bus and the

associated 500 kVl13 kV transformer (P-13000-2). Ground O/C protection for the P

13000-2 transformer actuated which deenergized the 500 kV "Red Bus" offsite power

supply. the 22 bus, and all four RCPs. At 8:24 a.m., the Unit 2 reactor automatically

tripped from full reactor power in response to the associated reactor protection system

trip on ReS low flow.

The P~13000-2 isolation also deenergized the 21 13 kV service bus, which deenergized

the Unit 1 144 kV safety bus, the Unit 2 24 4 kV safety bus, and several Unit 2 non

safety related 4 kV busses. The 16 emergency diesel generator (EDG) started as

designed and reenergized the Unit 1 14 bus. The 26 EDG started. but tripped 15

seconds later due to a low lube oil pressure signal and the 24 bus remained deenergized.

The electrical transient deenergized 120 volt instrument buses 1 Y1 0 and 2Y10. which

isolated the chemical volume control system (CVCS) and ~CS letdown for both units and

. complicated operators' control of pressurizer level.

Loss of power to the Unit 2 non-safety related buses resulted in loss of the normal RCS

heat removal path (main feedwater pumps, circulating water pumps, and condenser).

Operators used the turbine driven auxiliary feedwater pump and atmospheric steam

dump valves for decay heat removal.

At 8:48 a.m., Unit 2 operators exited emergency operating procedure (EOP)-O. "Reactor

Trip" and entered EOP-2, "Loss of Flow and Loss of Offsite Power." At 8:57 a.m.,

operators reenergized the 24 bus via the altemate feeder breaker. At 9;00 a.m., Unit 2

operators restored RCS letdown and maintained appropriate pressurizer level control.

At 1'I :17 a.m., Unit 2 operators started the 23 motor driven auxiliary feedwater (AFW)

pump and secured the turbine driven AFW pump. At 11:18 a.m., Unit 2 operators exited

Enclosure

8

the EOPs and returned to normal operating procedures. As of 12:02 p.m., Unit 1

Operl:ltors remained unsuccessful at restoring RCS letdown and exceeded the

pressurizer high level limits specified by both EOPs and TS. At 1 :09 p.m., Unit 1

operators restored RCS letdown and restored normal pressurizer level control. At 1 :38

p.m., Unit 1 operators exited the EOPs and returned to normal operating procedures.

At 2:07 p.m., Unit 1 vital 4 kV bus 14 was aligned to its alternate offsite source and the

18 EDG was secured. At 5:13 p.m., Unit 2 operators started 21B and 22A RCPs to

restore forced RCS circulation. On February 19, 2010, at 12:05 p.m., operators verified

two offsite power supplies were available, with the 21 13 kV service bus energized from

an alternate offsite source. On February 20,2010, at 10:31 p.m. repairs on the 2B EDG

were completed and the diesel generator was declared operable.

Unit 1 achieved cold shutdown at 5:38 a.m. on February 21, 2010, and 500 kV Red Bus

was restored at 5:50 a.m. Unit 2 achieved cold shutdown at 5:00 a.m. on February 22,

2010.

2.

Equipment Performance

2.1

Untimely Corrective Actions to Unit 1 45 Foot Elevation Switchgear Room Roof Leak

Cam,ed Reactor Trip

a.

Inspection Scope

Water leakage through the Unit 1 auxiliary building roof into the 45' elevation switchgear

room, caused an electrical ground on Bus 14 which tripped the 12B RCP, thereby

initiating a reactor protection system trip on RCS low flow. The team interviewed station

personnel, performed field walkdowns, and reviewed various records including

maintenance backlogs, maintenance history, operating logs, condition reports, and

maintenance rule program records to independently determine the cause of the event

and assess associated corrective actions. Constellation determined the root cause ot

the e:vent was that Calvert Cliffs lacked sensitivity to the consequences associated with

degr;sded roof conditions which led to a reactive rather than preventive strategy for

dealing with roof leaks. The team independently reviewed Constellation's Root Cause

Analysis Report (RCAR) for the Unit 1 reactor trip to determine the adequacy of the

evaluation, the extent-ot-condition review, and associated corrective actions.

b.

Findings

Introduction: A self-revealing non-cited violation (NCV) of very low safety significance

associated with 10 CFR Part 50, Appendix B, Criterion XVI "Corrective Actions," was

identified because Constellation did not promptly identify and correct degraded

conditions associated with the Unit 1 auxiliary building (45-foot elevation switchgear,

room) roof leakage. These degraded conditions led to the failure of the auxiliary building

to provide adequate protection to numerous safety related systems from external events

(adverse weather conditions) resulting in a ground on a reactor coolant pump (RCP) bus

and a consequential Unit 1 reactor trip on February 18, 2010.

Description: On February 18, 2010, Unit 1 tripped due to water from a roof leak entering

into the Unit 1 45-foot elevation switchgear (SWGR) room and causing a phase to

ground short near a current transformer (CT) for the 12B RCP bus 14P

Enclosure

9

differential/ground current protection devices. The ground fault was not isolated close to

the source, due to a failed ground protection relay in the feeder breaker to the Unit 1

RCP bus. The consequential trip of the 12B RCP led to the Unit 1 reactor protection

system (RPS) trip due to the a low reactor coolant system (RCS) flow signal.

While conducting a review of the dual unit trip, the team noted that in July of 2008,

condition report (CR) IRE-032-766 was written regarding rain water which had fallen onto

and into the emergency shutdown panel (ESOP) 1 C43, which is located in the Unit 1 45'

elevation SWGR room. Immediate actions were taken to notify the control room

supervisor of the condition as well as to clean up the pooled water around the panel.

Corrective actions were initiated to establish a program to maintain weather tight building

integrity. In June of 2009, CR 2009-004060 documented water dripping inside the

SWGR room just east of the No. 12 motor generator set. No immediate actions were

taken; however, recommended actions were to repair the roof. On August 8, 2009, a .

third CR (CR 2009-005508) was written, again regarding water leaking into the SWGR

room and onto the ESOP. Immediate actions were taken to cover the panel with

herculite and to direct the leaking water into a plastic bucket, as well as mopping up the

standing water. Despite the immediate actions taken to address the three rain water

issues, no additional actions were taken to properly prioritize, identify, and correct the

roof leakage. This is evident due to the fact that each CR was given the lowest priority

(category 4) as well as none of the work orders written to address the roof leakage* had

been approved. Additional safety related SWGR equipment in the SWGR room included

power supply breakers for the "B" train auxiliary feed water pump, high pressure safety

injection pump, low pressure safety injection pump and EDG.

, Based on the review of the RCAR, the team noted several missed opportunities from

2002 to 2009 to identify and evaluate the degraded condition prior to the dual unit trip.

During a periodic bus inspection in 2004, repairs were made to insulating material on the

power cables inSide the 14P01 cubicle to correct a water spot on the "B" phase of the

12B RCP bus. This cubicle is in the same SWGR enclosure as the 14P02 cubicle where

the water intrusion occurred that resulted in the February 18, 2010 trip. The work was

completed under the bus inspection work order; however, no CR was written

documenting the indicated water intrusion. This preventive maintenance activity should

have led to an investigation into the cause of the water intrusion as well as the extent of

the degraded condition. An apparent cause (IRE-007-705) was also completed in 2005

in response to a CR written by quality assurance personnel noting that there were 33

leaks identified during a walk down but no trend CR was written. Corrective actions were

proposed; however they were not adequately implemented.

The Calvert Cliffs' maintenance rule scoping document states that the function of the

auxiliary building is to provide structural support and separation to safety and non-safety

relatE~d equipment while accounting for the effects of certain extemal events. Rain

storms and heavy snowfall are eKamples of external events for which the auxiliary

building is designed to provide protection against. The Calvert Cliffs' structure

monitoring program did not effectively use the corrective action process to ensure this

function of the auxiliary building would be maintained. At the time of this special

inspe:ction, 58 work orders were open to repair roof leaks. None of these work orders

were planned or scheduled. Several of these work orders were over 2 years old.

Immediate corrective actions included: repairing degraded areas of the auxiliary building

roof; performing walk downs of other protected area buildings that could be susceptible

Enclosure

I

10

to damage to electrical equipment due to water intrusion; issuing standing orders to

include guidance regarding prioritizing work or.ders due to roof leakage; and identifying

furthE~r actions to take during periods of snow or rain to ensure plant equipment is not

affected. Long-term corrective actions include implementing improved plant processes

for categorization, prioritization, and management of degraded roof and water leakage

issues.

The team concluded that Constellation had numerous opportunities to have thoroughly

evaluated, classified, and prioritized the roof leakage, such that corrective actions could

have addressed the full extent of the auxiliary building roofing degraded condition and

prevented the water intrusion event and subsequent plant trip on February 18,2010.

. The team concluded that station personnel did not properly inspect and maintain the

roofs of several safety related structures to ensure the internal safety related and non

safety related components were protected from effects of the external environment (Le.,

rain, snow).

Analysis: The failure of Constellation to promptly identify and correct conditions adverse

to quality, associated with the auxiliary building roof leakage. is a performance

deficiency. The finding is more than minor because it is associated with the Initiating

Events Cornerstone and affects the cornerstone objective to limit the likelihood of those

external events that upset plant stability and challenge critical safety functions during

shutdown, as well as power operations. The inspectors evaluated this finding using IMe

0612 Attachment 4, "Phase 1- Initial Screening and Characterization of Findings," The

team determined the finding to have very low safety significance because, although it

contributed to a reactor trip, it did not contribute to the likelihood that mitigation

equipment would not be availab!e.

The cause of this finding is related to the Problem Identification and Resolution cross

cutting area. corrective action program, because Constellation did not thoroughly

evaluate the problems related to the water intrusion into the-auxiliary building such that

the resolutions addressed the causes and extent-of-condition. This included properly

classifying, prioritizing. and evaluating the condition adverse to quality (P.1{c)).

Enforcement: 10 CFR Part 50, Appendix B. Criterion XVI "Corrective Action," states, in

part, that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and non-conformances are promptly

. identified and corrected. Contrary to the above, from 2002 to February 18. 2010,

Constellation did not thoroughly evaluate and promptly correct degraded conditions

associated with auxiliary building roof leakage. This led to the failure of the auxiliary

building to provide protection to several safety related systems from external events (Le.

flooding), a ground on a reactor coolant pump bus, and ultimately a Unit 1 reactor trip.

Beccluse this violation was of very low safety significance and was entered into the

licensee's corrective action program as CR 2010-001351, this violation is being treated

as an NCV, consistent with the NRC Enforcement Policy." (NCV 0500317/318/2010006

01: Failure to Thoroughly Evaluate and Correct Degraded Conditions Associated

with Auxiliary Building Roof Leakage)

I

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Enclosure

11

2.2

Deficient Preventive Maintenance Program Procedures and Implementation for EDG

Aqastat Time Delay (TO) Relays

.

a.

InspE3ction Scope

On February 18, 2010, Unit 2 experienced an automatic reactor trip, loss of the P-13000

2 Service Transformer, and loss of the 500 kV Red Switchyard Bus. The loss of the Red

Bus resulted in loss of power to the No. 244 kV safety bus which caused an automatic

start of the 2B EDG. The 28 EDG tripped due to low lube oil (LO) pressure after running

for 15.2 seconds. The team reviewed the timing sequence, design requirements, relay

schematics, and surveillance and maintenance history for the 2B EDG. Failure of a T3A

time delay (TD) relay coincident with the 28 EDG LO low pressure protection logic not

having reset caused the low LO pressure protective trip of the engine. Constellation

identified two root causes for the EDG failure: (1) station personnel failed to recognize

and quantify the low margin in all aspects of the low lube oil.pressure trip set feature for

the EDG; and, {2} station personnel did not rigorously assess all failure modes of the

Agastat relays in the EDG protection circuitry prior to extending its service life beyond

the vendor qualified life.

The team reviewed Constellation's evaluation of the 28 EDG's failure, the adequacy of

proposed and completed corrective actions, and the appropriateness of the extent-of

condition review. Independent reviews of design documents, mock-Up testing. drawings,

surveillance testing, and field walk-downs were performed by the team to evaluate the

cause of the 2B EDG failure. In addition, the team reviewed Constellation's preventive

maintenance (PM) history and associated PM programs.

b.

Findings

Introduction. The NRC identified an apparent violation of Technical Specification 5.4.1

for the failure of Constellation to establish, implement, and maintain preventive

maintenance requirements associated with safety related relays. The team identified

that Constellation did not implement a performance monitoring program in lieu of a

previously established 10-year service life replacement PM requirement for the 2B EDG

T3A TD relay. As a consequence, the 2B EDG failed to run following a demand start

signal on February 18, 2010. This apparent violation is preliminarily determined to be of

low-to-moderate safety Significance {White}.

Description. The purpose of the T3A (Agastat 7000 series) TD relay in the EDG

protective circuit is to bypass the low lube oil trip on the EDG start to allow the EDG lube

oil pressure to initially build up to operating conditions. The relay begins timing when the

EDG speed reaches 810 rpm (approximately 6 seconds after EDG start). The relay

functions to bypass the low LO pressure trip <<17 pounds pressure sensed in the EDG

upper crankcase) for 15 seconds (a total of 21 seconds from EDG start). This time delay

allows LO pressure to build-up in the EDG upper crankcase high enough to reset the trip

logic (2 of 3 pressure switches reset at >20 pounds). The Unit 2 February 18, 2010,

sequence of events printout revealed that the T3A relay timed out early (after 9.2

seconds) at 15.2 seconds following the EDG start and prior to the low LO pressure

sensing trip logic being reset. Constellation determined that a typical fast, non-pre

lubricated EDG start results in LO pressure exceeding 20 pounds pressure

approximately 13 seconds following the start of the EDG. Accordingly, the early timeout

Enclosure

12

of the T3A relay was not the only degraded 28 EDG condition that presented itself on

February 18, 2010. Constellation attributed the February 18 delayed reset of the

pressure switches to "sticky lubrication oil" in the %-inch stainless steel pressure sensing

line to the pressure switches, vice an actual low LO pressure condition in the diesel

engine upper crankcase.

The team determined that the T3A relay, which timed-out early, had been in-service on

the 28 EDG for approximately 13.5 years, 3.5 years beyond its vendor recommended

10-year service life. In 2001, Constellation engineering discontinued the vendor

recommended 10-year replacement PM and substituted a performance monitoring

program envisioned to ensure Agastat relays (approximately 100 safety related

applications and 500 to 600 non-safety related applications in the two Calvert Cliffs units)

were appropriately monitored and replaced prior to failure (reference Engineering

Service Package ESP No. ES200100067, approved 03/06/2001). The team identified

that a relay performance monitoring program had not been establiShed since 2001 at

Calvert Cliffs. Constellation initiated CR 2010-04493 to address this performance issue.

The Shift Manager reviewed the immediate operability and determined that the other

safety-related components using Agastat relays remain operable because these relays

are installed in less harsh operational environments (e.g. vibrations) then the EDG

Agastat relays, and therefore, are less susceptible to age-related degradation. In

addition, CR 2010-01784 was written to address the extent-ot-condition of Agastat relays

used in other safety-related applications.

Constellation replaced the 28 EDG failed T3A relay and, via a single 'as-found' bench

test, validated its February 18, 2010, in-service failure, when the relay failed again,

timing out early at 11.6 seconds. Subsequent attempts by Constellation to adjust the

relay to within calibration tolerance were unsuccessful. The failed relay was shipped to

an independent laboratory for diagnostic testing and destructive examination. The

laboratory identified that, exercised over its furl range of operation, >40 percent of the TD

actuation results were out of tolerance. Internals examination identified three of six

screws on the flexible diaphragm retaining ring were loose, suggesting that the early

time-out of the relay was possibly due to excessive air bleed off (leakage passed the

diaphragm seal). Constellation concluded that the TD relay failure was a relatively

recent event (within the last 47 days) and attributable to the three 28 EDG starts and

approximately seven cumulative hours of operation that occurred in early January 2010.

The team concluded that Constellation provided no evidence to support the approximate

time of failure of the TD relay. However, the team determined that the failure and

probable failure mechanism may have occurred between the last successful calibration

of the TD relay (May 13,2008) and the observed failure on February 18,2010. In

addition, the team conCluded that therD relay early time-out was most likely a latent

failUre and masked by the monthly EDG surveillance test. Accordingly, the TD relay

failure was revealed by the fast, non-pre-Iubrication, demand start on February 18, 2010.

The basis for the team's conclUSion was as follows:

  • Constellation'S troubleshooting results were not conclusive regarding the lubricating

oil pressure sensing line "'sticky oil" theory, based upon the following: 1} the "sticky

oil" drained from the sensing line was not saved or analyzed for consistency or

contaminants (Constellation did not exercise appropriate quarantine practices); 2) the

%-inch LO pressure sensing line was not backfilled with oil and was therefore

susceptible to trapped air pockets that may tend to dampen accurate pressure

Enclosure

13

sensing and may result in a delayed pressure response; and, 3) Constellation's

routine (two-year calibration cycle) and post-event calibration checks of the pressure

switches did not record "as-found" values of the pressure switch reset values; this

information may have assisted in ruling out possible pressure switch setpoint drift or

malfunction.

The team acknowledged that Constellation's subsequent mock-up testing of the

pressure sensing line did show that lubricating oils of heavier viscosity tend to delay

the pressure sensing response. However, the 100W oil used to demonstrate the

phenomena (approximate 3 second pressure sensing delay) was considerably

heavier than the lubricating oil used in the 2B EDG {40W} and mayor may not have

re!flected the "sticky oil" viscosity observed by the technician responsible for the

pressure switch troubleshooting.

  • The fast, non-pre-Iube start of the 2B EOG contributed to the identification of the

failed relay; whereas the monthly pre-lube EDG starts likely masked the failure of the

TO relay. The team determined that for a typical fast, pre-lubricated EOG start, a

small pre-lube pump is run for 3 to 5 minutes prior to the EDG starting and fills the

upper crankcase with lubricating oil, but is not of sufficient capacity to pressurize the

upper crankcase. When the EOG starts, the engine driven LO pump functions to

complete the upper crankcase fill and pressurization (>20 pounds pressure) in

approximately 8 seconds. Accordingly, any relay failure (timing out early, <12

s,~conds) is masked by the fast, pre-lube EDG start because the relay actuates at 6

seconds and only has to satisfactorily function (block the low lube oil trip signal) for >2

seconds. The team noted that by the low LO pressure protective system design. the

fast pre-lube EOG starts allow for a significant margin to satisfactory build-up of lube

all pressure before the TO relay times out (a margin of approximately 13 seconds).

For the fast non-pre-Iube start, LO pressure typically exceeds 20 pounds pressure at

13 seconds after EDG start. This 13 second time interval similarly translates to the

TD relay having to function for >7 seconds from the time it actuates at 6 seconds from

EOG start. This 7 seconds minimal TO function also, by design, provides margin (an

additional 8 seconds) for satisfactory LO pressure bUild-Up.

The team concluded that the last known satisfactory relay calibration (setpolnt) check of

the T3A relay was the two-year calibration check completed on May 13, 2008. Based

upon Constellation records, the as-found setting was 17.5 seconds and the as-left was

16.5 seconds. All monthly surveillance tests of the 2B EDG since May 13, 2008, were

fast, pre-lube starts. There were no demand starts of the 2B EDG between May 13,

2008, and February 18, 2010, that would have proved or disproved that the T3A relay

was operable, and that the LO pressure senSing line issue was coincidental or

precipitous of a fast, non-pre-Iube start.

Following identification of the failed T3A relay. the licensee replaced the relay,

satisfactorily tested the 2B EDG, and returned the 2B EOG to service. In addition, time

delay relays used in the 1 B* and 2A EDG protective circuits, that also exceeded the

vendor recommended 10-year service life, were replaced. Constellation is evaluating the

continued use of Agastat relays beyond their vendor recommended 10-yr service life. As

previously noted, there are approximately 100 safety related applications and 500-600

non-safety related applications at the two Calvert Cliffs units.

Enclosure

14

Analysis. The team identified that the failure of Constellation to perform preventive

maintenance in accordance with vendor recommendations without adequate

performance monitoring on safety related Agastat 7000 series TO relays used in safety

relat~~d applications is a performance deficiency and violation of Technical Specifications

(TS). This violation of TS is more than minor because it is associated with the

equipment performance attribute of the Mitigating Systems Cornerstone and adversely

impacted the objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically, the

early timeout of the T3A relay caused the 2B EDG to trip prior to the low lube oil

pressure trip signal clearing (resetting) after a demand fast start on February 18, 2010.

The failure of the 2B EDG to run resulted in the continued loss of alternating current to

the No. 24 4 kV safeguards bus and its associated emergency core cooling systems.

In ac~cordance with Table 4a of IMC 0609, Attachment 04, "Phase 1

Initial Screening

and Characterization of Findings," this performance deficiency required a Phase 2 or 3

risk analysis because the issue resulted in an actual loss of safety function of a single

train for greater than its TS allowed outage time. A Phase 3 risk assessment was

perfc)rmed by a Region I Senior Reactor Analyst (SRA) using the SAPHIRE software and

Calvert Cliffs Unit 2 Standardized Plant Analysis Risk (SPAR) model, Revision 3.46,

dated February 2010.

To conduct the Phase 3 analysis, the SRA made the following modeling assumptions;

Exposure time was based upon a T/2 approximation. The team determined that

the 2B EDG exposure time is best approximated by a T/2 value, per the usage

rules of IMC 0308, Appendix A, "Technical Basis for At Power Significance

Determination Process." Specifically, if the inception of a condition is unknown,

the use of the mean exposure time (T/2) is a statistically valid time period

because it represents one-half of the time since the last successful demonstration

of the component's function and the time of discovery or known failure. The last

successful demonstration of the T3A relay was the calibration check performed

on May 13, 2008. The total time (T) between May 13, 2008 and February 18,

2010 is 646 days. Therefore, T/2 represents an approximate exposure time of

323 days or 7752 hours0.0897 days <br />2.153 hours <br />0.0128 weeks <br />0.00295 months <br />.

SPAR model basic event EPS-DGN-FS-2B, representing "Diesel Generator 2B

Failure to Start" was set to TRUE. The basis for the TRUE. vice a failure

probability of 1.0, is that common cause failure of the remaining Fairbanks-Morris

EDGs could not be conclusively ruled out. The same type Agastat 7000 series

TD relays, with comparable greater than 10 years in-service times were installed

on the 1Band 2A EDGs.

SPAR model basic event AFW-XHE-XM-FC8, representing operator failure to

open the Turbine Building to turbine driven auxiliary feed water (TDAFW) pump

room door within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of a station blackout event, was set to FALSE. The

basis for this change is that recent engineering analysis of the TDAFW pump

room heat-up (post Appendix R fire, LOOP/LOCA, SBO) identified no

dependency on operator action to open the door to the turbine building to ensure

adequate cooling of the TDAFW pumps.

Enclosure

15

No additional 2B EDG recovery credit was applied to the model based upon this

event. The SRA noted that 2B EDG non-recovery probability (0.772) in the SPAR

model is based upon industry statistical data. The SRA notes that Constellation

procedures have operators align the OC EDG (within 45 minutes) vice attempt to

troubleshoot and restart the failed EDG. Accordingly, any subsequent attempts

to restart the 2B EDG. after an approximate one hour delay (aligning the OC

EDG) would likely have the same result because all LO would have drained from

the upper crankcase.

Even though Agastat 7000 series relays are used in multiple safety related

applications (some beyond their vendor recommended service life), no broad

based increase in safety related systems' or components' failure probabilities was

applied for this Phase 3 risk assessment. As a consequence, the calculated risk

estimate for this condition may be a non-conservative value because the Agastat

relays are used in multiple other safety related applications beyond the

manufacturers recommended 1 O-year service life.

Truncation for the SPAR model analysis was set at 1E-13.

USing the above stated assumptions. the increase in internal risk (core damage

frequency) associated with the 2B EDG failure of February 18, 2010, was estimated at

6.DE-6. The dominant core damage sequence involves the loss of Facility B (13 kV

Service Bus No. 21), loss of steam generator cooling (main feedwater and auxiliary

feedwater), and the subsequent loss of once through cooling (feed and bleed. using the

charging system and a power operated relief valve).

Base!d upon the absence of an NRC external risk quantification tool, the SRA used

Constellation's ca[culated extemal risk values to approximate the external risk

contribution. Constel!ation's estimated external risk is based. upon a RISKMAN fire

modeling tool and was calculated at 1.1 E-6 for the T/2 exposure period. No appreciable

external risk contributions were identified for flooding or seismic events. The dominant

core damage external events include turbine building fires (involving the steam generator

main feedwater pump area) and high wind/hurricane events. The dominant turbine

building fire scenarios involve the failure of the available EDGs (2B and 1 B) and a

spurious initiation of the safety feature actuation system (SFAS). The dominant high

wind/hurricane event core damage scenarios involve the assumed failure of the OC

EDG. the subsequent failure of the remaining safety related EDGs, and a spurious

SFAS.

Based upon the SRA's calculated internal events risk estimate and Constellation's

estimated external events risk contribution, the total increase in Unit 2 core damage

frequency for this finding is approximately 7.1 E-6. Accordingly, this finding is of low to

modlarated safety significance (WHITE). This finding and the associated risk analysis

was reviewed by a Significance and Enforcement Review Panel (SERP) conducted on

June 1,2010. The SERP concluded that the stated Technical SpeCification violation and

associated risk characterization were appropriate. The violation does not represent an

immediate safety concern because the licensee took prompt corrective actions to

replace the Agastat relays in use beyond their service life for an three Fairbanks-Morris

EDGs and ensured the LO pressure sensing lines were properly backfilled. Subsequent

testing of all three EDGS verified operability, including a non-pre-Iubricated fast start of

the 2B EDG.

Enclosure

16

The Constellation PRA staff performed a risk assessment of the 2B EDG failure using

their CAFTA internal events model and RISKMAN external events model. Constellation

assumed the same exposure time as the Region I SRA of T/2 equal to 323 days.

Constellation's total risk estimate was 3.1 E-6 CDF. Based upon discussions with the

Constellation PRA staff, their risk estimate and dominant core damage sequences

compare favorably with the NRC results.

The cause of this finding is related to the crosscutting area of Human Performance,

I*

resources aspect because preventive maintenance procedures for the EDGs were not

properly established and implemented to maintain long term plant safety by maintenance

of design margins and minimization of long standing equipment issues (H.2(a).

Enforcement. Technical Specification 5.4.1 states, in part. that written procedures

I

specified in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, shall be

I*  !

established, implemented, and maintained. Section 9.b. of Appendix A to Regulatory

Guide 1.33 states, in part, that preventive maintenance schedules should be developed

to specify replacement of parts that have a specific service life. In March 2001

I

Constellation replaced their original10-year relay replacement preventive maintenance

with a proposed performance monitoring program, to ensure the continued reliability and

I

!

operability of Agastat relays installed in safety related applications beyond the vendor

recommended 10-year service life, via Engineering Change Package No. ES200100067.

Contrary to the above, the team identified that Constellation did not establish a

performance monitoring program, and aU Agastat relays installed in safety related

applications at Calvert Cliffs have been subject to "run to failure" preventive

maintenance/replacement interval. Constellation took prompt corrective action to

replace Agastat relays used in service, beyond their 10-year service life, in the 2B, 2A

and 1 B EDGs. The remaining Agastat relays, used in safety related applications beyond

their vendor recommended service life, are under evaluation by Constellation.

Constellation has initiated several CRs (see Attachment 1 to this report) associated with

this performance deficiency. Pending final significance determination, the finding is

identified as Apparent Violation (AV)05000318/2010006-02, Inadequate Preventive

Maintenance Results in the Failure of the 28 Emergency Diesel Generator.

2.3

Ground Fault Relay 251 G/B-22-2 Did Not Actuate on Ground Overcurrent to Trip Open

Breaker 252-2202

a.

Inspection Scope

The team reviewed design requirements, drawings, and maintenance history of the

251 GfB-22-2 relay. Failure of this relay to actuate and trip open the 252-2202 breaker

resulted in a loss of the P-13000-2 service transformer, which resulted in loss of power to

the Unit 2 RCPs and a Unit 2 trip with loss of normal decay heat removal. Unit 2

remained on atmospheric dump valves and auxiliary feedwater for heat removal for

approximately 68 hours7.87037e-4 days <br />0.0189 hours <br />1.124339e-4 weeks <br />2.5874e-5 months <br />. Constellation determined the most likely cause of the relay

failUre was premature coil aging due to the operating environment and the magnitude of

the current seen, which caused insulation breakdown and shorting of the magnetizing

coil. Even though Constellation could not conclusively identify the cause of the insulation

breakdown and magnitude of the signal that coincided with the breakdown, they did note

that the relay in this particular application is located in non-environmentally controlled

Enclosure

17

space which would impact aging mechanisms due to the temperature extremes.

Additionally, the 251 G/B-22-2 relay age was 39 years at the time of tlie event, which is

only 1 year within the 40-60 year service life.

The team reviewed Constellation's root cause analysis report (RCAR) for the 251 G/B-22

2 relay to determine the adequacy of the evaluation and the appropriateness of the

extent-of-condition review. Independent reviews of the design documentation, drawings,

maintenance history, and field walk-downs were performed to validate the cause of the

relay failure. The team reviewed the design requirement and the relay setting

information of the 13.8 kV fault protection relaying scheme to ensure proper equipment

protection during transient and steady state conditions. The team also reviewed the

history of the 251G/B-22-2 relay, along with other protective relays in the 13.S kV system

that were required during the event, to verify that the applicable test acceptance criteria

and maintenance frequency requirements were met.

b.

Findings

DefiGient Evaluation and Untimely Corrective Action Associated with Induction Disc

Bincling on CO-8 Type Relays

Introduction: The team identified a finding of very low safety significance (Green) that

involved a NCVof 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," because

Constellation did not thoroughly evaluate and correct a degraded condition of CO-S relay

disc sticking or binding issues which can adversely impact the function of the EDGs and

the electrical distribution protection scheme. Specifically, following the February 18,

2010, event Constellation did not identify and adequately evaluate the recent CO-S relay

failures due to sticking or binding of the induction discs in the safety related and non

safety related applications.

Description: The team reviewed Constellation's RCAR for the relay 2RY251 G/B-22-2 on

breaker 2BKR252-2202 which failed to trip open the breaker. The relay was a CO-S

ground fault over-current relay which had been in service for the life of the plant. The

relay consists of an electromagnet and an induction disc which rotates to close a moving

contact to a stationary contact to complete the breaker trip circuitry. The root cause

analYSis concluded that the magnetizing coil had shorted out the majority of the windings

in a manner that current would pass but the induction disc would not rotate.

The team reviewed Constellation's maintenance and corrective action history of the CO

S relay failures and noted that the induction disc type relays had a failure history

aSSOCiated with disc binding and sticking conditions. The team also noted that CO-S

relays and other induction disc type relays had a high failure rate for out of tolerance

conditions during the performance of relays calibration procedures. The team

determined that failures of the relay due to binding, sticking, and out of tolerance

conditions can potentially impact the breaker trip operation and affect breaker

coordination.

The failure history for binding, sticking, and out of tolerance conditions for the induction

type relays were reviewed since 2007. The team found 40 failures since 2007 and 5

failures of the CO-8 type relays. Constellation has a total of 68 CO-S type relays

installed in safety related and non-safety related applications, all of which have been

SChE~duled to be calibrated every 2 years since 2005. The team noted that from 1999 to

Enclosure

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2005 as-found testing and calibration of the relays were performed every 4 years. The

team reviewed the failure data of the CO-8 and other induction disc type relays prior to

2005 and concluded that the failure rate did not change significantly subsequent to the

increase in calibration frequency. The CO-8 relay failures were noted to be 10 percent

from 1999-2005.

Constellation replaced or cleaned the relays with sticking or binding conditions; however,

the licensee did not place the relays in any system or component monitoring program.

The relays were also not part of the system health tracking report. The team reviewed

the historical failures of the CO-8 relays and noted that for some of the testing

conditions, the induction disc needed to be mechanically agitated to free it from the

binding or sticking conditions. The team reviewed the vendor and Electric Power

Research Institute (EPRI) calibration and maintenance manual and determined that

Constellations' calibration and inspection procedure did not include all of the

recommended practices specified in the EPRI guideline related to inspection and

cleaning of the induction disc units. Constellation entered this issue into the corrective

action program (CRs 2010-004672 and 2010-004673).

Ana~ysis: The team reviewed Constellation's root cause evaluation, which concluded the

cause of the relay failure to be premature coil aging due to its operating environment and

the magnitude of the current seen by the relay. The team concluded that there was no

direct correlation between the coil failure and the historical binding and sticking

conditions of the C0-8 relay discs. However the team determined that Constellation's

failure histories ofthe CO-8 type relays were significant and the failure to evaluate the

degraded conditions and implement timely and effective action to correct this condition

adverse to quality was a performance deficiency. The CO-8 relays are used in multiple

safety related and non-safety related applications.

The finding was more than minor, in accordance with NRC IMC 0612, Appendix B,

"Issue Screening," (lMC 0612B) because, while it was not similar to any examples in IMC 0612, Appendix E, "Examples of Minor Issues" (IMC 0612E), it was aSSOCiated with the

equipment reliability attribute of the Mitigating Cornerstone and it adversely affected the

ass()ciated cornerstone objective of ensuring the availability, reliability. and capability of

systems that respond to initiating events to prevent undesirable consequences (I.e., core

damage). The team evaluated this finding using IMC 0612 Attachment 4, "Phase 1

Initial Screening and Characterization of Findings." The finding is of very low safety

significance (Green) because it is not a design or qualification deficiency, did not

repr<i;~sent a loss of a safety function of a system or a single train greater than its TS

allowed outage time, and did not screen as potentially risk significant due to external

events. The historical relay failures did not result in an actual loss of system safety

function.

The cause of the finding is related to the crosscutting area of Problem Identification and

Rest::Jlution, Corrective Action Program because Constellation did not thoroughly

evaluate the previous station operating experience of CO-8 relay induction disc sticking

and binding issues such that resolutions addressed the causes and extent-of-condition

(P.1(c>>.

Enfmcement: 10 CFR 50 Appendix B, Criterion XVI, "Corrective Action," requires. in

part, that measures shall be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to the above. Constellation did not

Enclosure

19

adequately evaluate and correct the degraded condition of CO-8 relays which can

potentially impact the function of multiple safety related systems or component. Because

the finding was* of very low safety significance and has been entered into Constellation's

corrective action program (CR 2010-004673), this violation is being treated as a NCV,

consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000317 &

3181:2010006-03, Failure to Evaluate Degraded Conditions Associated With CO-8

Relays and Implement Timely and Effe~ive Action to Correct the Condition

Adverse to Quality.

Deficient Offsite Power Distribution Tripping Scheme Design Control

Introduction: The team identified a finding having very low safety significance (Green)

for failure to translate design calculation setpoint standard listed in calculation E-90-058

and E-90-061 of phase overcurrent relay (250) on feeder breakers 252-1101, 1102,

1103,2101,2102, and 2103 into the actual relay settings.

Description: During the relay settings review, the team identified that the service

transformer 251G/ST-2 and service bus 251G/SB-21 ground overcurrent relays settings

specified in the relay setting sheets did not support the values listed in the relay setting

calculation E-90-61 for the 500/14 kV Service Transformer {P-13000-2}.* The value listed

in the calculations for the 251 G/ST-2 ground overcurrent relay tap settings was 2.5 amps

and the actual field setting, which is set in accordance with the relay setting sheets, was

found to be at 2 amps. For the service bus 251 G/SB-21 the calculation setting of the

time delay value was 4 seconds and the actual field settings was found to be at 3

seconds. Due to these discrepancies Constellation's engineering staff conducted an

evaluation to determine if the actual field settings as specified in the relay setting sheets

for the two overcurrent relays provided adequate coordination to ensure selective

tripping. The relays are designed to detect ground faults on the 13.8 kV system which

have not been cleared by the 500 kV transmission system relays and separate the

station service transformer P-13000-2 from the grid. The team reviewed Constellation's

evaluation and determined that there was no selective tripping coordination impact due

to the relay setting discrepancies on 251 G/ST-2 and 251G/S8-21. However. due to

these discrepanCies identified between the relay setting sheets and the design

calculations, Constellation conducted an extent-ot-condition review for the 13.8 kV

systems to determine it other similar relay settings discrepancies exist.

As a result of the extent-of-condition review, Constellation identified that the phase

overcurrent relay {250} pickup value for the six unit service transformers feeder breakers

252-1101, 1102, 1103, 2101, 2102, and 2103 were set at 1440 amps in accordance with

the relay setting sheets and the values specified in the calculations E-90-058 and E-90

061 were 1200 amps.

The normal system operation deSign when offsite power is available, is the 4.16 kV

system being supplied by the 13.8 kV system through six unit service transformers. The

unit service transformers have overcurrent protection to protect against transformer

faults in the primary or secondary side windings. This overcurrent protection per

calculations E-90-058 and E-90-061 was limited to be at 1200 amps due to the breaker

rating of all of the feeder breakers. Due to the as found relay setting of 1440 amps

exceeding the breaker ratings of 1200 amps, Constellation conducted an operability

analysis and performed a calculation which determined that the maximum load current

possible during the worst case electrical distribution line-up condition would be 982

Enclosure

20

amps. The calculation demonstrated that the maximum load current possible during the

worst case electrical distribution line-up would not challenge the feeder breaker ratings,

and therefore would not cause the breaker to fail prior to the trip operation (tripping).

Analysis: The team determined that the failure to translate the design calculation

setpoint standard values listed in the calculation E-90-058 and E-90-061 of phase

overcurrent relay (250) on feeder breakers 252-1101, 1102, 1103,2101,2102, and 2103

into the actual relay settings was a performance deficiency.

The team determined that this finding was more than minor because it affected the

Initiating Events Cornerstone attribute of equipment performance for ensuring the

availability and reliability of systems to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Also, this issue was similar to Example 3j of IMC 0612, Appendix E,

"Examples of Minor Issues," because the condition resulted in reasonable doubt of the

operability of the component, and additional analysis was necessary to verify operability.

The failure to translate adequate design calculation setpoint of phase overcurrent relays

on the feeder breakers resulted in an as-found relay setting that exceeded the rating of

the feeder breakers. The team determined that due to the as-found relay setting

exceeding the breaker ratings, certain phase overcurrent conditions could have

potentially caused the breaker to fail prior to the phase overcurrent relay sensing the

degraded condition. The team determined that this condition could affect the recovery of

the safety buses from the electrical grid. The team evaluated this finding using IMC 0612 Attachment 4, "'Phase i-Initial Screening and Characterization of Findings." This

finding was determined to be of very low safety significance (Green) because these

inadElquate relay settings did not result in an actual loss of system safety function and

Constellation also performed an evaluation and determined that the maximum load

current possible would not challenge the feeder breaker ratings. The finding did not

have a cross-cutting aspect because the most significant contributor to the performance

defiCiency was not reflective of current licensee performance.

Enforcement: This finding was not a violation of regulatory requirements because the

unit service transformers and the overcurrent protection relays are not a system or

component covered under 10 CFR Part 50, Appendix B. The issue has been entered

into the licensee's corrective action program (CR 2010-002123. Because this finding

does not involve a violation and has very low safety significance, it is identified as FIN

05000317 & 318/2010006-04: Failure to Translate Design Calculation Setpoint of

Phase Overcurrent Relay on Feeder Breakers.

2.4

Breaker 2BKR152-2501 (4 kV Bus 25 Normal Feed) Failed to Trip Open

a.

InSpElction Scope

The team reviewed design requirements, drawings, and maintenance history of the

2BKR152-2501 breaker. The breaker inspection reviewed the maintenance practice and

procedure of overhauling the 4 kV breakers to determine if adequate test acceptance

criteria were established and followed vendor recommendations. The team reviewed

Constellation's root cause analysis report for the 2BKR152-2501 to determine the

adequacy of the evaluation and the appropriateness of the extent-of-condition review.

Independent reviews of the design documentation, drawings, maintenance history, and

field walkdowns were performed to validate the cause of the breaker failure.

Enclosure

21

Additionally, operations, maintenance, and engineering staff were interviewed to confirm

the c,bservations and causes cited in Constellation's evaluation of this issue. The team

reviewed the adequacy of associated preventive maintenance, corrective actions, and

post maintenance testing performed on the 2BKR152-2501 breaker. Bus 25 supplies

power to three Unit 2 circulating water pumps.

No findings of significance were identified for this equipment issue. The team

determined that this failure of 2BKR 152-2501 to open had no adverse consequence

during this event.

2.5

Breaker 2BKR252-2201 (13 kV Unit 2 RCP Buses Normal Feed) Failed to Trip Open

a.

Inspection Scope

The team reviewed design requirements, drawings, and maintenance history of the

2BKR252-2201 breaker. The team reviewed the maintenance practice and procedure of

overhauling the 13.8 kV breakers to determine if adequate test acceptance criteria were

established and followed vendor recommendations. Constellation concluded the cause

of the breaker failing to open was infant mortality (Le., manufacturing defect). The team

reviewed Constellation's root cause analysis report for the 2BKR252-2201 to determine

the adequacy of the evaluation and the appropriateness of the extent-of-condition

review. Independent reviews of the design documentation, drawings, maintenance

history, and field walkdowns were performed to validate the cause of the breaker failure.

Additionally, operations, maintenance, and engineering staff were interviewed to confirm

the observations and causes cited in Constellation's evaluation of this issue. The team

reviewed the adequacy of associated preventive maintenance, corrective actions, and

post maintenance testing performed on the 2BRK252-2201 breaker.

b.

Findings

No findings of significance were identified.

3.

Human Performance

3.1

Event Diagnosis and Crew Performance

a.

Inspection Scope

The team interviewed the operations crew that responded to the February 18, 2010,

event, including three senior reactor operators, the shift manager, the control room

supervisor, the shift technical advisor, two reactor operators, and three equipment

operators to determine whether the operators performed in accordance with procedures

and training. The team also reviewed narrative logs, post-transient reports, condition

reports, PPC trend data, and procedures implemented by the crew.

b.

Findings/Observations

Deficient Procedure Guidance for CVCS Letdown Restoration

Enclosure

22

rntroduction: A self-revealing Green NCV of TS 5.4.1.a, "Procedures," was identified

because Constellation did not establish adequate procedures for restoration of CVCS

letdown flow. Deficient operating instructions prevented timely restoration of letdown

flow following letdown isolation, which ultimately led to exceeding the TS high limit for

pressurizer level.

Description: On February 18, 2010, Unit 1 was operating at 93% reactor power in

preparation for main steam safety valve testing with the 11 and 13 charging pumps

operating and increased letdown flow balanced with cparging flow. At 8:24 a.m., a

phase to ground overcurrent fault on 12B RCP switchgear resulted in an automatic reactor trip on Unit 1. Protective relaying isolated plant service transformer P-13000-2,

which de-energized Unit 1 4 kV bus 14. Instrument Bus 1Y10, which is normally fed

from 4 kV Bus 14, de-energized, isolating CVCS letdown by closing letdown isolation

valvI31-CVC-515. The 1B EDG automatically started on bus undervoltage and re

powered 4 kV Bus 14 about 8 seconds later.

Charging pump 13 stopped on loss of power when 14 Bus de-energized and charging

pump 11, powered from 4 kV Bus 11, continued running. At 8:31 a.m., operators re

started charging pump 13. Charging pumps remained running and pressurizer level

incrE~ased as expected. Operators performed makeup to the CVCS Volume Control

Tank (VCT) from 8:50 a.m. to 9:11 a.m. in order to maintain VCT inventory while the two

running charging pumps transferred VCT contents into the pressurizer. At 8:58 a.m., 34

minutes after the reactor trip, and with pressurizer level approaching the high end of the

EOP pressurizer level control band (180"), operators turned off charging pump 13.

Charging pump 11 continued to run in anticipation of restoring letdown. At 9:02 a.m.,

operators stopped charging pump 11 because pressurizer level was above the EOP high

level limit.

At 9:12 a.m., operators made their first attempt to restore letdown in accordance with 01

2A, "Chemical and Volume Control System", Section 6.7, "Starting Charging and

Letdown" by re-starting charging pump 11 and shortly thereafter opening letdown

isolation valves. They were not successful in restoring letdown. Subsequent post-event

analysis of system parameter data stored on the plant computer indicated that excess

flow check valve 1-CVC-343 was closed. Inadequate procedural guidance prevented

operators from re-opening the check valve to establish letdown flow. The procedure for

starting letdown consisted of setting letdown downstream control valves at 20% open in

manual, starting a charging pump to cool the letdown stream, then opening letdown

upstream isolations 1-CVC-515 and 1-CVC-5i6 to establish letdown flow. 01-2A did not

contain any information related to the possibility that excess flow check valve 1-CVC-343

might be closed and did not provide direction for opening the valve.

Operators were confused by indicated letdown flow remaining downscale and took about

7 minutes re-confirming the system lineup and monitoring their instrumentation before

stopping charging pump 11. They did not use 01-2A, Section 6.6, "Securing Charging

and Letdown" to stop charging and letdown because letdown was not yet established.

Initial conditions for using Section 6.6 were not met. Operators did not recognize a need

for simultaneously stopping charging and letdown in accordance with the general

methodology of Section 6.6. An additional 17 minutes elapsed from the time operators

stopped the charging pump 11 until they closed the upstream letdown isolation valves.

Enclosure

I

j.

23

Post-event data analysis showed the downstream letdown* piping temperature steadily

incre:ased into the 400

0 to 500°F range during the 17 minutes between stopping the

chan~ing pump and closing the upstream letdown isolation valves because of hot reactor

coolant flowing in the letdown line through the 10 gallons per minute (gpm) orifice which

bypasses around the excess flow check valve. Typically, reactor coolant is cooled by

charging flow through the letdown regenerative heat exchanger to about 220°F in the

letdown line. It is postulated that during letdown restoration attempts, the ReS which

was greater than 2000 psi pressure, re-pressurized the letdown line which rapidly

collapsed steam voids in the hot (400°F-500°F) letdown piping and re-closed the excess

flow check valve because of water hammer. A differential pressure was then established

across the check valve, maintaining it closed. The restoration method provided by

procedure OI-2A did not contain actions necessary for pressure equalization across this

spring-loaded check valve.

During the second letdown restoration attempt at 10:44 a.m., letdown continued to flow

through the bypass orifice for 21 minutes after stopping charging pump 11. This action

again heated the letdown line to near reactor coolant temperature. On the third attempt

at 11 :39 a.m., operators closed letdown isolation valves just 2 minutes after stopping the

char!Jing pump, which left the letdown line in a relatively cool state, such that the

transient conditions on the fourth and final attempt did not re-close the excess flow check

valve. Operators made a total of four attempts to restore letdown over 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> before

letdown was finally restored at 1 :17 p.m.

Pressurizer level remained above the specified limit in EOP-1 for all but a few minutes of

approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> following the reactor trip. Throughout this period, operators

attempted to control pressurizer level from the EOP high level limit of 180" to the normal

full power level of 215". This range was based on the constraints of contrOlling

pressurizer level below the TS high limit of 225" and high enough to prevent overfilling

the VCT. With letdown unavailable, operators were only able to lower pressurizer level

through the 6 gpm reactor coolant pump seal bleed off that returns to the VCT.

The team observed that unnecessarily conservative procedural requirements for

ensuring adequate shutdown margin in NEOP-301, "Operator Surveillance Procedure"

contributed to the operating crew's sense of urgency for letdown restoration. Operators

rec09nized that the 2400 gallon ReS boration required to satisfy the requirements of

NEOP-301 would cause pressurizer level to significantly exceed the TS high level limit if

performed with letdown isolated.

Other options existed for controlling VeT level such that bleed off could be allowed to

reduce pressurizer level to within the EOP band. These included intentionally draining

the VeT to the liquid waste system and aligning bleed off flow to return to the reactor

coolElnt drain tank instead of to the VeT. However, the station does not have an

abnormal operating procedure for responding to a sustained loss of letdown and

therefore no procedural guidance existed for using other methods to control veT level.

Around noon, shortly after the third attempt to restore letdown, operators became

involved in shifting main turbine gland sealing steam supply from main steam to auxiliary

steam and failed to control ReS temperature. Loop temperature rose approximately

5°F, causing pressurizer level, already high at 215", to rise and peak at 231."

Pressurizer level remained above the TS 3.4.9 high limit of 225" for apprOXimately 7

Enclosure

24

minutes until operator actions which were taken to lower RCS temperature succeeded in

reducing level to below the TS limit

The excess flow check valve did not re-close on the fourth restoration attempt. letdown

was successfu Ily re-established at 1317, approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after event initiation.

COnl:;tellation has established procedure guidance relating to letdown restoration

following closure of the excess flow check valve. The issue was entered into their CAP

for further evaluation as CR 2010-001378.

Analysis: The performance deficiency is that Constellation did not establish adequate

procedures for restoring letdown. Multiple factors contributed to pressurizer level

exceeding the TS high limit. These included time pressure from overly conservative

procedure requirements related to maintaining shutdown margin, filling the pressurizer

above the EOP band when RCS temperature was below its nominal no*load value,

makeup to the VCT to the high end of its control band when pressurizer level was

already high, the absence of proceduralized options for controlling VCT level, and

inattentiveness to reactor coolant temperature control. However, inadequate procedure

guidance for letdown restoration is the primary reason which led to operation outside of

EOP pressurizer level limits for an extended period of time and unnecessarily challenged

operators in their attempts to maintain pressurizer level control.

The team determined this finding is more than minor because it is associated with the

procedure quality attribute of the Mitigating Systems Cornerstone and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

The finding is of very low safety significance (Green) because it is not a design or

qualitfication defiCiency. did not represent a loss of a safety function of a system or a

single train greater than its TS allowed outage time, and did not screen as potentia!ly risk

significant due to external events. This finding has a crosscutting aspect in the area of

Human Performance, resources, because Constellation did not ensure that procedures

for restoring CVCS letdown were complete and accurate (H.2(c>>.

Enforcement: TS 5.4.1.a requires, in part, that written procedures be established,

implemented, and maintained for activities described in Appendix A of Regulatory Guide

(RG) 1.33, "Quality Assurance Program Requirements (Operation}." Specifically,

Section 3 of RG 1.33, Appendix A, "Instructions for energizing, filling, venting, draining,

startup, shutdown, and changing modes of operation should be prepared, as

appropriate, for the following systems," includes the Letdown/Purification System.

Contrary to the above, on February 18, 2010, the operators were unable to restore

charging and letdown using the existing instructions of OI-2A, "Chemical and Volume

Control System," due to inadequacy of the procedure. Because this issue is of very [ow

safety significance {Green) and Constellation entered this issue into their corrective

action program as CR 2010-001378, this finding is being treated as an NCV consistent

with Section VJ.A.1 of the NRC Enforcement Policy. (NCV 05000317/318/2010006-05,

Failed to Establish Adequate Procedures for Letdown Restoration).

3.2

Communications and Emergenqy Plan Applicability

a.

InsQ~:lction Scope

Enclosure

25

This event involved an automatic reactor trip of both units with multiple complicating

degraded equipment issues. Each unit lost one 500 kV offsite power supply (the Red

Bus). In addition, Unit 2 lost forced RCS circulation when all four RCPs tripped, the 28

EDG failed to reenergize the Unit 2 24 4 kVafety bus, and the Unit 2 normal heat

removal sink (main condenser) was unavailable for an extended time. Operators notified

the NRC of the event at 11 :47 a.m. on February 18 in accordance with 10 CFR 50.72.

Operators determined that emergency action level (EAL) entry criteria were not met and

accordingly did not declare an emergency event. The team reviewed operator logs,

emergency procedures, the Emergency Plan, plant operating data, and interviewed

station personnel to verify operators properly assessed the EAL entry criteria and

notified the NRC of the event.

b.

Findings

No findings of Significance were identified.

4.

Organizational Response

4.1

Immediate Response and Restart Readiness Assessment

a.

InSpE!ction Scope

The team interviewed personnel, reviewed various procedures and records, observed

plant operators and station meetings, and performed plant walkdowns to assess station

personnel's immediate response to the event and restart readiness assessment. The

licensee restart readiness assessment was performed in accordance with CNG-OP

1.01-1006, Post-Trip Reviews, Rev. 1.

No findings of Significance were identified.

Operators promptly announced the event, implemented the appropriate emergency

operating procedures, and correctly assessed EALs. However, human performance

deficiencies and/or procedure deficiencies led to Unit 1 exceeding the TS pressurizer

level limit (Section 3.1) and untimely verification of offsite power source availability.

Constellation augmented the on-shift staff promptly to support initial diagnosis and

corrective actions to address the numerous degraded equipment problems.

The post-trip review was sufficient to ensure operator performance issues and significant

equipment issues were identified and addressed. Notwithstanding, the team identified

several deficiencies which posed challenges to the effectiveness of the licensee restart

readiness assessment (CR 2010-004502). The team discussed each issue with licensee

management who entered the issues into the corrective action program, as applicable.

One notable issue was that station personnel did not quarantine several failed

components (breaker 152-2501, 2B EDG oil sensing line contents, relay 251 G/B-22-2).

This adversely limited the as-found information available to diagnose the failure

mechanisms.

4.2

Post-Event Root Cause Analysis and Actions

. Enclosure

26

a.

Inspection Scope

The team reviewed the RCAR for the 2010 Dual Unit Trip to determine whether the

causes of the event and associated human performance and equipment challenges

were properly identified. Additionally, the team assessed whether interim and planned

long term corrective actions were appropriate to address the cause(s).

No findings of significance were identified.

The RCAR properly evaluated causes and appropriate corrective actions for several

equipment challenges. For example, evaluation and corrective actions for the Unit 1 roof

leakage which initiated the ground fault event were comprehensive. In addition to the

root cause, the RCAR identified several contributing causes including deficient

maintenance rule implementation and performance monitoring, over reliance and

inadequate vendor oversight, incomplete incorporation of Quality Assurance findings,

and insufficient engineering involvement in roof construction. Interim corrective actions

were appropriate and long term actions were being developed through the corrective

action program.

In several other areas the team determined the RCAR lacked depth and technical rigor

in identifying and assessing potential causes. In each case the RCAR developed an

explanation for what may have caused the event or equipment response, but did not fully

develop other potential causes. Examples included:

RCAR did not identify the failure to implement an Agastat relay monitoring

program when the 10 year replacement PM was eliminated (2B EDG failure);

RCAR conclusion that loose diaphragm retaining ring screws on the Agastat relay

were caused by vibration and were the result of a manufacturing defect were not

well supported by the contracted failure analysis or data evaluation (2B EDG

failure);

Inforr:nation that the relay induction disc did not freely rotate back to the original

position during bench troubleshooting. was not incorporated into the RCAR (relay

2RY251G/B-22-2 failure);

RCAR did not thoroughly review previous internal OE regarding induction disc

failure on CO-8 type relays. Station personnel did not recognize the sensitivity of

the induction disc to sticking/binding (relay 251 G/B-22-2 failure);

RCAR did not include or address the 2008 as-found inspection results which

found the armature linkage misaligned and the trip coil loose. This was an

unexpected and infrequent occurrence (breaker 152-2501 failure); and

ReAR concluded the 152-2501 breaker failure was due to mechanical binding in

the trip linkage caused by human error during the October 2008 trip armature bolt

replacement. However, corrective actions did not investigate other breaker

maintenance performed by these technicians during that time period.

Enclosure

27

The team reviewed these issues and determined that none of these issues involved

violations of regulatory requirements or were already described as part of the previously

discussed violations in this report.

Enclosure

28

4.3.

Revi'9w of Operating Experience

a.

Inspection Scope

The team reviewed Constellation's use of pertinent industry and station operating

experience (OE), including evaluation of potential precursors to this event.

b.

Findings

No findings of significance were identified.

The team identified several instances where Constellation had not effectively evaluated

or initiated actions to address related station or industry operating experience issues.

Examples included:

  • Unit 1 and Unit 2 45 foot switchgear room roof leakage onto electrical switchgear

had been identified numerous times since 2002, but not corrected. Fifty-eight

open work orders for roof leaks, several> 24 months old, had not been

implemented (Section 2.1).

  • Industry OE has reported numerous problems with Agastat series 7000 relays;

several affecting reliability of the actuation setpoint. Yet engineers extended both

the service life and calibration periodicity of the EDG lube oil pressure trip time

delay relays beyond the vendor specified periods without adequate technical

basis (Section 2.2).

  • Technicians routinely did not consider relay actuation outside of the acceptance

band to be a test failure. Often no condition report was initiated and no

drift/performance trending was performed. Corrective action was often limited to

adjusting the as-left setpoint to within the acceptance band (e.g, agastat 7000

series time delay relays, CO-8 overcurrent protection relays) (CR 2010-004090).

The team reviewed these issues and determined that none of these issues involved

violations of regulatory requirements or were already described as part of the previously

discussed violations in this report.

5.

Risk Significance of the Event

a.

Initial Assessment

The initial risk assessment for this event is documented in the enclosed SIT charter.

b.

Final Assessment

Onsite follow-up and discussions with the Constellation PRA staff verified that there

were no additional plant conditions or operator performance issues that significantly alter

the initial event risk assessments performed for both units. The Unit 1 reactor trip

estimated conditional core damage probability (CCDP) was calculated to be 2.6 E-6 for

the February 18, 2010 reactor trip. The Unit 2 reactor trip CCDP, accounting for a loss

of reactor coolant forced Circulation (all RCPs tripped), loss of heat sink (main

Enclosure

.1

29

condenser}, and failure of the 28 EDG to run, was estimated to be 1.5 E-5 for the

February 18, 2010 event

40A3 Follow~up of Events

(Closed) Licensee Event Report (LER) 05000317/2010-001, Reactor Trip Due to Water

Intrusion into SWitchgear Protective Circuitry

On February 18, at 8:24 a.m., the Unit 1 reactor automatically tripped from 93 percent

reactor power in response to a RCS low flow condition. Water had leaked through the

auxiliary building roof into the 45' switchgear room, causing an electrical ground which

tripped the 128 RCP, thereby initiating the reactor protection system trip on RCS low

flow. Three of the four Unit 1 Reps continued operating. The electrical ground and

failure of a ground fault protection relay caused service transformer P-13000-2 to isolate,

thereby deenergizing the 144 kV safety bus and the 1Y1 a 120 volt instrument bus. The

1B EDG automatically started and reenergized the 14 bus as designed. The LER

accurately described operator response to the event. The team reviewed the LER and

idenlified no findings of significance beyond those previously documented in this report

(NRC Inspection Report No. 05000317/2010006). This LER stated a supplemental LER

will document a complete description of corrective actions after the event analysis and

cause determination is complete. This LER is closed .

. 2

(Cloe;ed) Licensee Event Report (LER) 05000318/2010-001, Reactor Trip Due to Partial

Loss of Offsite Power

On February 18, at 8:24 a.m., the Unit 2 reactor automatically tripped from 99.5 percent

reactor power due to a loss of power to all four Reps and the associated reactor

proteiCtion system RCS low flow trip. The event emanated from a ground fault on Unit 1

(see Section 2.1). A ground OIC relay failed to actuate as designed, permitting the Unit

1 ground OIC condition to reach Unit 2. Unit 2 electrical protection responded by

deenergizing the 500 kV"Red Bus" offsite power supply and multiple onsite electrical

buses including the 24 4 kV safety bus. The 28 EDG started as designed, but tripped on

low lube oil pressure (see Section 2.2). The LER accurately described operator

response to the event. The team reviewed the LER and identified no findings of

significance beyond those previously documented in this report (NRC Inspection Report

No.05000317/2010006}. This LER stated a supplemental LER will document a

complete description of corrective actions after the event analysis and cause

determination is complete. This LER is closed.

40A6 Meetings, Including Exit

Exit Meeting Summary

On April 30, 2010, the team presented their overall findings to members of Constellation

management led by Mr. G. Gellrich, Site Vice President, and other members of his staff

who l:lcknowledged the findings. The'team confirmed that proprietary information

reviewed during the inspection period was returned to Constellation.

Enclosure

Licensee Personnel

G. Gellrich

K. Allor

P. Amos

P. Darby

S. Dean

M. Draxton

D. Fitz

M. Flynn

D. Frye

M. Gahan

G. Gellrock

S. Henry

J. Koebel

D. Lauver

W. Mahaffee

J. McCullum

K. Mills

P. O'Malley

T. Riti

K. Roberson

A. Simpson

R. Stark

T. Trepanier

Others

S. Gray

M. Griffin

1-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Site Vice President

Senior Operations Instructor

Performance Improvement

Principal Assessor, Engineering Quality Performance Assessment

Manager, Maintenance

Manager, Nuclear Training

Communications

HR Director

Manager. Operations

GS, Design Engineering

Supervisor

Manager, Work Management

PRA

Director, Licensing

Supervisor, Chemistry Operation

Supervisor, Instrumentation and Controls

Assistant Operations Manager

Quality Performance Assessment

GS, System Engineering

Manager, NSS

Engineering/Licensing

Design Engineering

Plant General Manager

Power Plant Research Program Manager, Department of Natural

Resources, State of Maryland

Nuclear Emergency Preparedness Coordinator, Department of the

Environment, State of Maryland

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000317/318f2010006-01

05000317/318f2010006-02

05000317/318/2010006-03

NCV

Failure to Thoroughly Evaluate and Promptly

Correct Degraded Conditions Associated with

Auxiliary Building Roof Leakage {Section 2.1}

AV

Inadequate Preventive Maintenance Results in the

Failure of the 2B Emergency Diesel Generator

(Section 2.2)

NCV

Failure to Evaluate Degraded Conditions

Associated with CO-8 Relays and Implement

Attachment 1

1-2

Timely and Effective Action to Correct the Condition

05000317/318/201 0006-04

05000317/3'18/20 1 0006-05

Opened and Closed

05000317/201 0-001

05000318/2010-001

Drawings

Adverse to Quality (Section 2.3)

FIN

Failure to Translate Design Calculation Setpoint of

Phase Overcurrent Relay on Feeder Breakers

(Section 2.3)

NCV

Faifed to Establish Adequate Procedures for

Letdown Restoration (Section 3.1)

LER

Reactor Trip Due to Water Intrusion into Switchgear

Protective Circuitry (Section 40A3.1)

LER

Reactor Trip Due to Partial Loss of Offsite Power

(Section 40A3.2)

LIST OF DOCUMENTS REVIEWED

61004, Single Line Meter & Relay Diagram 13 kV System, Rev. 26

61001SH0001, Electrical Main Single Line Diagram FSAR Fig. No. 8-1, Rev. 42

63070SH0009, Schematic Diagram 13 KV Service Bus 22 RCP Bus Feeder Breaker 252-2201,

Rev. 11

63049, AC Schematic Diagram Service Bus 22 & Service Transformer P-13000-2, Rev. 17

Condition Reiports (CR)

IRE-000-433

CR 2009-008115

CR 2010-001707

2010-001779

2010-001780

2010-001781

2010-001782

2010-001783

2010-001784

2010-001787

2010-001813

2010-001888

2010-002875

2010-004411

2010-004493

2010-004502

2010-004613

2010-004652

2010-004672

2010-004673

2010-004674

2010-001699

2010-001700

IRE-004-399

CR 2009-008537

CR

IRE-004-400

CR 2009-008635

CR

IRE-011-621

CR 2010-001330

CR

IRE-011-769

CR 2010-001340

CR

I RE-020-768

CR 2010-001351

CR

I RE-020-769

CR 2010-001355

CR

IRE-020-776

CR 2010-001381

CR

IRE-022-227

CR 2010-001516

CR

IRE-026-951

CR 2010-001517

CR

IRE-D28-751

CR 201 0-001544

CR

IRE-031-691

CR 2010-001553

CR

IRE-032-766

CR 2010-001586

CR

CR 2008-001582

CR 201 0-001592

CR

CR 2008-002458

CR 201 0-001682

CR

CR 2009-004060

CR 201 0-001685

CR

CR 2009-004074

CR 2010-001690

CR

CR 2009-004606

CR 2010-001691

CR

CR 2009-005508

CR 2010-001671

CR

CR 2009-00:5629

CR

CR 2009-006187

CR

Attachment 1

1-3

Maintenance Orders

MO #1200801597, Replace Flex Hoses on the 18 EDG

MO #2199901416, Calibrate 2B EDG Lube Oil Pressure Gauge, 2-PI-4796

MO #2200000476, Perform E-19 on 2B EDG Agastat Relays

MO #2200201832, 2B EDG Engine Stop Relay

MO #2200401152, 2B EDG Engine Stop Relay

MO #2200501401, 2B EDG Engine Stop Relay

MO #2200700554, Replace Flex Hoses on the 2A EDG

MO #2200700555, Replace Flex Hoses on the 2B EDG

MO #2200700852, 2B EDG Engine Stop Relay

Operability Evaluation

OE-2009-003712

Procedures

Auxiliary Building Walkdown Results, MN-1-319 "Structure and System Walkdowns," Rev. 5

Auxiliary Building Walkdown Results, MN-1-319 "Structure and System WaIkdowns, "Rev. 7

1 0-02 uRain/Snow Water Intrusion Compensatory Measures,>> Rev. 1

CNG-AM-1.01-2000, "Scoping and Identification of Critical Components," Rev. 00200

CNG-CA-1.01-1000, "Corrective Action Program," Rev. 0200

CNG-OP-1.01-1006, "Post Trip Reviews," Rev. 00001

CNG-OP-1.01-2000, "Operations Logkeeping and Station Rounds," Rev. 00100

CNG-QL-1.01-1007, "Quality Performance Assessment Process," Rev. 00201

CNG-PR-1.01-1009, "Procedure Use and Adherence Requirements," Rev. 00400

FTE-87, "Powell 13.8 kVType PVDH Vacuum Circuit Breaker Inspection," Rev. 00101

FTE-51A, "General Electric Cubicle Inspection," Rev. 2

FTE-59, "Periodic Maintenance, Calibration and Functional Testing of Protective Relays," Rev. 5

MN-1-319 "Structure and System Walkdowns," Rev. 7

NO-1-200, "Control of Shift Activities, Rev. 04401

NO-1-201, "Calvert Cliffs Operating Manual," Rev. 02000

OI-2A, "Chemical and Volume Control System," Rev. 55/Unit 1

Miscellaneous

Control Room Operations NarratiVe Logs

Operations Administrative Policy 90-7, Guidelines, System Expert and Shift Crew Ownership

Program Guidelines and Expectations, January 27,2010, Change 15

Plant Areas System 102 Walkdowns, 1- Unit 1 performed January 5.2010, & March 31, 2010

System 102 "Plant Areas," Maintenance Rule Scoping Document, Rev. 30

Site Roof Leakage Condition Report Scoping Document

U-1 Alarm History Printout for February 18, 2010

U-2 Alarm History Printout for February 18, 2010

U-1 Sequence of Events Recorder Printout for February 18,2010

U-2 Sequence of Events Recorder Printout for February 18, 2010

Engineering Service Package ES200100067, Revision 1, Delete Requirement in E-406

Sec 234.0.1 to Change Out Agastat Prior to Ten Years and Remove Testing

Recommendations to VTM 15-167-001

Procedure E-406, Rev. 0, Installation and Replacement for Agastat Relays

R001617, Revision 4, Guideline for Testing Agastat Relay Models

Constellation Nuclear Generation Fleet Administrative Procedure CNG-CA-1.01-1 004

Root Cause Analysis, Revision 00301

Attachment 1

1-4

Procedure FTI-328, Revision 1, Calibration Check/Calibration of Allen-Bradley Pressure

Switches

Rover Maintenance Approval and Closeout Form, MN-1-101, Revision 03601, 2A EDG

Oil Sensing Line Flush

Calvert Cliffs SUrveillance Test Procedure, STP 0-8B-2, Revision 26, Test of 2B DG and

4 kV Bus 24 LOCI Sequencer

Calvert Cliffs Surveillance Test Procedure, STP 0-8A-2, Revision 26, Test of 2A DG and

4 kV Bus 24 LOCI Sequencer

Operating Experience OE13852 - Inadequate Venting of the Emergency Diesel

Generator Lubricating Oil System

Sch(:)matic Diagram Diesel Generator 1\\10. 2B Engine Control, No. 63086SH0010,

Revision 39

Work Order C90791765, 2B Diesel Generator Failed to Start and Load on the 24 4 kV

Bus on an ESFAS UV Signal

Operating Experience, ACE 013617, Surry EDG Agastat Relay Failure

Constellation Nuclear Generation Fleet Administrative Procedure CNG-AM-1.01-1 018

Preventive Maintenance Program, Revision 00400

Vendor Manual 15167-001-1001, Agastat Timing Relays 7000 Series

Vendor Manual 15167-001-1005, Tyco Electronics

Herguth Labratories Crankcase Oil Sample Data

Troubleshooting Data Sheet to Determine Cause of 2B EDG Trip after Closing onto 24 4

kVBus

CCNPP Procurement Engineering Specification, PES - 25180. Revision 17, Agastat

Relays and Associated Hardware

Maintenance Strategy 2RY2DG2BAlT3A Relay

2-PS-4798 Master Calibration Data Package, 2/19/10

Root Cause Analysis

CNG-CA-1.01-1004 "Root Cause Analysis" Dual Unit Trip, Rev 00301

Apparent C~luse Evaluation

IRE-007-70S

Calculations/Engineering Evaluation Reports

E-90-058, Blreaker 252-1101, 1102, 1103, Rev. 2

E-90-061, Breaker 252-2101, 2102, 2103, Rev. 2

E-90-062, BI'eaker 252-2201, Rev. 2

RCS Letdown Line Evaluation for Potential Water Hammer dated 3/16/10

Completed Tests/Surveillances

E-30, 4.16 kV Magne-Blast Circuit Breaker Overhaul Procedure, Performed 10/04/04

FTE-51 , 4 kV General Electric Magne-Blast Circuit Breaker Inspection, Performed 11/18/08,

4114105

FTE-59. Periodic Maintenance, Calibration and Functional Testing of Protective Relays,

Performed 04/06/00,03126/03,05/03/04, 10/01/05,05/08/07, 10/10/07,03/08/08,

11120108, 02128109

FTE-87, Powell 13.8 kV Type PVDH Vacuum Circuit Breaker Inspection, Performed 3/15/07

STP-O-90-1 and STP-0-90-2, TrAC Sources and Onsite Power Distribution Systems 7 Day

Operability Verification, Rev. 22

Attachment 1

CC

1-5

AV

LlCDF

CFR

CR

eves

DRP

DRS

EAL

EDG

EOP

ESDP

gpm

IMC

kV

LlLERF

LER

LO

NCV

NRC

OC

OE

PM

PORC

PPC

PRA

RCAR

RCP

RCS

RG

RPS

SOP

SM

SPM-A

SRA

SIT

SPAR

ST

TD

TS

UV

VCT

LIST OF ACRONYMS

Apparent Violation

Calvert Cliffs

Increase in Core Damage Frequency

Code of Federal Regulations

Condition Report

Chemical and Volume Control System

Division of Reactor Projects

Division of Reactor Safety

Emergency Action Level

Emergency Diesel Generator

Emergency Operating Procedure

Emergency Shutdown Panel

Gallons per Minute

Inspection Manual Chapter

Kilovolt

Increase in Large Early Release Frequency

Licensee Event Report

Lube Oil

Non-cited Violation

Nuclear Regulatory Commission

Overcurrent

Operating Experience

Preventive Maintenance

Plant Onsite Review Committee

Plant Process Computer

Probabilistic Risk Assessment

Root Cause Analyses Report

Reactor Coolant Pump

Reactor Coolant System

Regulatory Guide

Reactor Protection System

Significance Determination Process

Shift Manager

Woodward SPM-A Synchronizer

Senior Reactor Analyst

Special Inspection Team

Standardized Plant Analysis Risk

Surveillance Test

Time Delay

Technical Specification

Under-Voltage

Volume Control Tank

Attachment 1

2-1

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

SPECIAL INSPECTION TEAM CHARTER

February 22,2010

MEMORANDUM TO:

Glenn Dentel, Manager

Special Inspection Team

David Kern. Leader

Special Inspection Team

FROM:

David C. Lew, Director

IRA!

Division of Reactor Projects

Darrell J. Roberts, Director

IRA!

Division of Reactor Safety

SUBJECT:

SPECIAL INSPECTION TEAM CHARTER

CALVERT CLIFFS PARTIAL LOSS OF OFFSITE POWER AND

DUAL UNIT TRIP WITH COMPLICATIONS ON

FEBRUARY 18, 2010

In accordance with Inspection Manual Chapter (IMC) 0309, "Reactive Inspection Decision

Basis for Reactors," a Special Inspection Team (SIT) is being chartered to evaluate a Calvert

Cliffs dual unit trip with complications which occurred on February 18,2010. The decision to

conduct this special inspection was based on meeting multiple deterministic criteria (multiple

failures in equipment needed to mitigate an actual plant event, significant unexpected system

interactions, and events involving safety related equipment deficiencies) specified in Enclosure

1 of IMC 0309 and the event representing a preliminary conditional core damage probability in

the low E-6 range for Unit 1 and low E-5 range for Unit 2.

The SIT will E:lxpand on the inspection activities started by the resident team immediately after

the event. The team will review Constellation's organizational and operator response to the

event, equipment and design deficiencies, and the causes for the event and subsequent issues.

The team will collect data, as necessary, to refine the existing risk analysis. The team will also

assess whether the SIT should be upgraded to an Augmented Inspection team.

The inspection will be conducted in accordance with the guidance contained in NRC Inspection

Attachment 2

G. Dentel, D. Kern

2-2

Procedure 93812, "Special Inspection," and the inspection report will be issued within 45 days

following the, final exit meeting for the inspection.

The special inspection will commence on February 22,2010. The following personnel have

been assigned to this effort:

Manager:

Glenn Dentel, Branch Chief,

Projects Branch 1, Division of Reactor Projects (DRP). Region I

Team Leader:

David Kern, Senior Resident Inspector

DRP, Region I

Full Time Members:

Peter Presby. Operations Inspector

Division of Reactor Safety (DRS). Region I

Manan Patel, Electrical Inspector

DRS, Region I

Brian Smith, Resident Inspector

DRP, Region I

Part Time Member:

William Cook, Senior Reactor Analyst

DRS, Region I

Enclosure: Special Inspection Charter

Attachment 2

G. Dentel, D. Kern

2-3

The special inspection will commence on February 22, 2010.

been assigned to this effort:

The following personnel have

Manager:

Glenn Dentel, Branch Chief,

Projects Branch 1. Division of Reactor Projects (DRP). Region 1

Team Leader:

David Kern, Senior Resident Inspector

DRP, Region [

Full Time Members:

Peter Presby, Operations Inspector

Division of Reactor Safety (DRS), Region I

Manan Patel, Electrical Inspector

DRS, Region I

Brian Smith, Resident Inspector

DRP, Region I

Part Time Member:

William Cook, Senior Reactor Analyst

DRS, Region I

Enclosure: Special Inspection Charter

ccw/encl:

B. Borchardt, EDO (RidsEDOMailCenter)

B. Mallett, DEDO (RidsEDOMaHCenter)

E. Leeds, NRR

B. Boger, NRR

J. Wiggins, NSIR

S. CoHins, RA (R10RAMAIL RESOURCE)

M. Dapas, ORA (R1 ORAMAIL RESOURCE)

D. Lew, DRP (1~10RPMAIL RESOURCE)

J. Clifford, DR? (R1DRPMAIL RESOURCE)

D. Roberts, DRS(R1DRSMail Resource)

P. Wilson, DRS (R1DRSMaii Resource)

L. Trocine, RI OEDO

G. Dentel, DR?

N. Perry, DRP

J. Hawkins, DRP

S. Sloan, DRP

S. Kennedy. DRP, SRI

M. Davis, DRP, RI

C. Newgent, DRP, Resident OA

RidsNrrPMCalvertCliffs Resource

RidsNrrDorlLpl1-1 Resource

D. Screnci, PAO

N. Sheehan, PAO

R. Barkley, ORA

N. McNamara, SLO

D. Tifft, SLO

I

!

!

SUNSI Review Complete:

NP

(Reviewer's Initials)

Non-Public Designation Category: MD 3.4 Non-Public

B.1

(A.3 - A.7 or B.1)

DOCUMENT NAME: G:\\ORP\\BRANCH1\\CC-SIT CHARTER Final.doc

ML - will be obtained when ADAMS is available

After declaring this document "An Official Agency Record"'t will not be released to tI:le Public.

OFFICE

NAME

DATE

To receive a copy of this document, indicate in the box: ~c* =Copy without attachment/enclosure "E" =Copy with

h

fJ

"N" N

attac men enclosure

= o COP'

RIIDRP

I

RI/DRP

I

RI/DRS

I

RIIDRP

I

NPerry/NP

DKern/NP via

GDentel/GTD

DLew/JWC for

teleconf

02/22/10

02/22110

02122/10

02/22/10

RI/DRS I

DRoberts/PW

for

02/22/10

OFFICIAL RECORD COpy

Attachment 2

2-4

Special Inspection Team Charter

Calvert Cliffs Nuclear Power Plant

Dual Unit Trip with Complications due to a Partial Loss of Offsite Power

on February 18. 2010

. Backgrounl~:

At 8:24 a.m. on February 18, 2010, Calvert CUffs Unit 1 experienced an unexpected loss of the

12B reactor coolant pump (RCP). The loss of the RCP trip resulted in a valid reactor protection

system (RPS) actuation on low reactor coolant system flow and a Unit 1 trip.

At approximately the same time, Unit 2 experienced a loss of the 500 kV to 13.8 kV transformer

for the "Red Bus" (500 kV). The Red Bus is the feeder for offsite power for the Unit 1 "14" and

Unit 2 "24" 4 kV safety buses. Unit 2 experienced the following system/component responses

based on the loss of the Red Bus: loss of the non-safety related buses, a loss of load RPS trip

signal, a loss of all RCPs, and a Unit 2 trip. The loss of the non-safety related buses resulted in

the loss of the circulating water pumps, the main feedwater pumps, and condensate pumps, and

the subsequent loss of the normal heat sink. Bus 21 , the other Unit 2 safety 4 kV bus, normally

aligned to the Black Bus, remained energized.

The los$ of power to the "'14" and "24" 4 kV safety buses resulted in a valid start signal for the

1B and 28 EDGs, respectively. The 1B EDG started and re-powered the "14" safety bus;

however, thE! 2B EDG tripped during loading resulting in the loss of the "24" safety bus. This

resulted in the unavailability of the "B" safety train. Calvert Cliffs subsequently restored power

to the "24" safety bus via the Black Bus alternate power supply.

Unit 1 was c()oled down and entered a refueling outage that was originally scheduled to begin

on February 20,2010. Unit 2 was stabilized on natural circulation, and normal decay heat

removal was subsequently restored; the plant has entered a forced outage.

At the time of the event, the resident team responded to the control room and monitored

licensee actions to stabilize the plant and restore offsite power. An NRC regional inspector was

also deployed to the site to supplement the resident staff.

Basis for the Formation of the SIT:

The IMC 0309 review concluded that three deterministic criteria were met. The deterministic

criteria met included: 1) multiple failures of plant equipment in systems used to mitigate an

event; 2) Significant unexpected system interactions; and 3) events involving safety related

equipment deficiencies. These criteria were met based on the partial loss of offsite power due

to the transformer loss, and the subsequent failure of the 28 EDG to start and restore a safety

bus. In addition, the system interactions between the 12B RCP trip and the transient, which

resulted in the opposite 500 kV transformer loss, were unexpected. The Unit 2 transformer loss

also resulted in a complete loss of forced flow to Unit 2 due to the expected loss of all four

Reps, and the loss of the Unit 2 main condenser as a heat sin.k.

The event was also evaluated for risk significance because the IMC 0309 review concluded that

at least one deterministic criteria was met. Based upon best available information, the Region I

Senior Risk Analyst (SRA) conducted a preliminary risk estimate for each unit on February 18.

Using the Gn:lphical Evaluation Module initiating event quantification tool and the Calvert Cliffs

Unit 1 and Unit 2 Standardized Plant Analysis Risk (SPAR) models, the conditional core

Attachment 2

2-5

damage probability (CCDP) for Unit 1 was estimated to be in the low E-6 range, and the Unit 2

estimated CCDP was in the low E-5 range. On February 19, 2010, the SRA discussed these

results with the Constellation PRA staff and determined that the risk estimates (CCDP)

performed by Constellation favorably compared to the NRC SPAR model generated values.

Based upon the preliminary CCDP estimates, and in accordance with IMC 0309, the Unit 1 and

Unit 2 events fall within the overlap ranges of No Additional Inspection and Special Inspection

Team (SIT) for Unit 1, and SIT and Augmented Inspection Team (AIT) for Unit 2. After

consultation with NRC headquarters personnel, an SIT was initiated.

Objectives <of the Special Inspection:

The SIT will review Constellation's organizational and operator response to the event,

equipment and design deficiencies, and the causes for the event and subsequent issues. The

team will collect data, as necessary, to refine the existing risk analysis. The team will also

assess whether the SIT should be upgraded to an Augmented Inspection Team. Additionally,

the team leader will review lessons learned identified during this special inspection and, if

appropriate, prepare a feedback form on recommendations for revising the Reactor Oversight

Process (ROP) baseline inspection procedures.

To accomplish these objectives, the team will:

1. Develop a complete sequence of events including follow-up actions taken by

Constellation.

2. Review and assess the equipment response to the event. This assessment should

include an evaluation of the consistency of the equipment response with the plant's

d,esign and regulatory requirements. In addition, review and assess the adequacy of

any operability assessments, corrective and preventive maintenance, and post

maintenance testing.

3. Review and assess operator performance including procedures, logs,

communications (internal and external), and emergency plan implementation.

4. Review and assess the effectiveness of Constellation's response to this event. This

includes overall organizational response, failure modes and effect analysis

dl~veloped for the equipment challenges, causal analyses conducted, and interim

and proposed longer term corrective actions taken.

5. Evaluate Constellation's application of pertinent industry operating experience and

evaluation of potential precursors, including the effectiveness of any actions taken in

response to the operating experience or precursors; and

6. Collect any data necessary to refine the existing risk analysis and document the final

risk analysis in the SIT report.

Attachment 2

2-6

Guidance:

Inspection Procedure 93812, "Special Inspection", provides additional guidance to be used by

the Special Inspection Team. Team duties will be as described in Inspection Procedure 93812.

The inspection should emphasize fact-finding in its review of the circumstances surrounding the

event. It is not the responsibility of the team to examine the regulatory process. Safety

concerns identified that are not directly related to the event should be reported to the Region I

office for appropriate action.

The team will conduct an entrance meeting and begin the inspection on February 22, 2010.

While on site, the team Leader will provide daily briefings to Region I management, who will

coordinate with the Office of Nuclear Reactor Regulation, to ensure that all other parties are

kept informed. A report documenting the results of the inspection will be issued within 45 days

following the final exit meeting for the inspection.

This Charter may be modified should the team develop significant new information that warrants

review.

Attachment 2

3-1

DETAILED SEQUENCE OF EVENTS

February 18, 2010 Dual Unit Trip with Complications

The sequence of events was constructed by the team from review of Control Room Narrative

Logs, correc:tive action program condition reports, post transient review report, process plant

computer (FPC) data (alarm message file and plant parameter graphs) and plant personnel

interviews. The sequence of events is listed separately by Unit 1 and Unit 2.

UNIT 1 EVENT '"IMELINE

Clock Time IEvent Time

Description

0211812010

A phase to ground fault occurs on the 13 kV supply line to Unit 1

Reactor Coolant Pump (RCP) 12B Motor, upstream of 12B RCP

08:24:25:225 0.000 sec Breaker 252-14P02, which is already open (normal lineup).

Rep 12B Breaker 252-14P01 trips open on differential overcurrent

08:24:25:225 0.000 sec relay actuation, stopping 12B RCP.

Feeder Breaker 252-2104 to 13 kV Service Bus 21 trjps open, de-

energizing Unit 2 Non-vital balance of plant, Unit 2 Vital 4 kV Bus 24

08:24:27 :251 2.026 sec

and Unit 1 Vital 4 kV Bus 14.

208/120 VlAC Bus 12 de-energizes, resulting in isolation of the Unit

1 RCS letdown f10wpath in the Chemical and Volume Control

08:24:27:421 2.196 sec

System (CVCS).

13 kV Service Bus 22 Supply Breaker 252-2202 to Unir1 RCPs trips

open. Unit 1 RCPs are not affected as they are aligned to their

normal power supply from 13 kV Station Service Transformer P

08:24:28:803 3.578 sec

13000-1 through 13 kV Service Bus 12.

08:24:28:781 3.556 sec 500 kV Switchyard Red Bus Isolation Breaker 552-41 trips open.

500 kV SWitchyard Red Bus Isolation Breakers 552-21 and 552-61

trip open, completing the high side isolation 13 kV Station Service

08:24:28:783 3.558 sec

ransformer P-13000-2.

init 1 automatic reactor trip on reactor coolant low flow signal from

3% initial reactor power level. 3 of 4 Unit 1 reactor coolant pumps

08:24:29:110 3.885 sec

are still operating.

08:24:29:146 3.921 sec

Unit 1 reactor trip breakers open.

08:24:29:417 4.192 sec

Unit 1 turbine trip.

Undervoltage signal actuates on Unit 1 4 kV Vital Bus 14, initiating

08:24:29:423 4.198 sec the 1 B Emergency Diesel Generator start sequence.

Unit 14 kVVital Bus 14 Normal Feeder Breaker 152-1414 trips

.08:24:29:948 4.723 sec

open.

13 kV Service Bus 21 Supply Breaker 252-2103 to Transformer U

08:24:33:818 18.593 sec

4000-22 opens.

13 kV Service Bus 21 Supply Breaker 252-2102 to Transformer U

08:24:33:818 8.593 sec

4000-21 opens.

13 kV Service Bus 21 Supply Breaker 252-2101 to Transformer U

08:24:33:819 8.594 sec

4000-23 opens.

08:24:36:101 10.876 sec Emergency Diesel Generator 1 Breaches 810 rpm.

Emergency Diesel Generator 1 B Output Breaker 152-1403 to 4 kV

08:24:37:255 12.030 sec Vital Bus 14 closes.

IShutdown Sequencer on 4 kV Vital Bus 14 actuates, to re-start bus

08:24:37:26712.042 sec Iloads.

Attachment 3

3-2

UNIT 1 EVENT TIMELINE

Clock Time

Event Time

Description

08:24:37:748 12.523 sec 208/120 V/AC Bus 12 re-energizes.

08:24:37:774 12.549 sec Undervoltage signal clears on Unit 1 4 kV Vital Bus 14.

Reactor Operator backs up the automatic reactor trip signal by

08:24:42:015 16.790 sec depressing manual reactor trip pushbuttons.

08:24:55

30 sec

Crew enters EOP-O, Post-Trip Immediate Actions

Component Cooling Pump 11 is manually started. Component

08:26:35

2.17 min

Cooling system pressure and flow are restored.

08:31

7min

Charging Pump 13 re-started.

08:40

16 min

Crew exits EOP-O and enters EOP-1, Reactor Trip.

09:00

36 min

Pressurizer level out of EOP control band high, >180 inches.

09:02

38 min

Charging Pump 11 stopped.

Operators attempt to restore CVCS letdown (1 st attempt). Charging

09:12

48 min

Pum p 11 started. Letdown Isolations CVC-515 and 516 opened.

09:20

56 min

Charging Pump 11 sto~ed.

09:37

73 min

Letdown Isolation Valves CVC-515 and 516 closed.

10:41

2.28 hrs

Pressurizer level returns within EOP control band, <180 inches.

Operators attempt to restore CVCS letdown (2nd attempt).

Charging Pump 11 started. Letdown Isolations CVC-515 and 516

10:44

2.33 hrs

opened.

10:47

2.38 hrs

Pressurizer level out of EOP control band high, >180 inches.

11:07

2.72 hrs

Charging Pum p 11 stopped.

11:28

3.07 hrs

Letdown Isolation Valves CVC-515 and 516 closed.

Operators attempt to restore CVCS letdown (3rd attempt). Charging

11:39

3.25 hrs

Pump 11 started. Letdown Isolations CVC-515 and 516 opened.

11:47

3.38 hrs

Completed 4 hr report to NRC, as required per 10CFR50.72.

11 :50

3.43 hrs

Charging Pump 11 stopped.

11:52

3.47 hrs

Letdown Isolation Valves CVC-515 and 516 closed.

12:02

3.63 hrs

Pressurizer level above Tech Spec limit, >225 inches.

12:07

3.72 hrs

Pressurizer level returns within Tech Spec limit, <225 inches.

Completed STP-O-90-1, AC Sources and Onsite Power Distribution

12:07

3.72 hrs

Systems 7 Day Operability Verification.

12:11

3.78 hrs

Disconnects for 500 kV Switchyard Breaker 552-21 are opened.

12:14

3.83 hrs

Disconnects for 500 kV Switchyard Breaker 552-61 are opened.

12:15

3.85 hrs

Disconnects for 500 kV Switchyard Breaker 552-23 are opened.

12:17

3.88 hrs

Disconnects for 500 kV Switchyard Breaker 552-22 are opened.

12:18

3.90 hrs

Disconnects for 500 kV Switchyard Breaker 552-63 are opened.

13:06

4.70 hrs

Pressurizer level returns within EOP control band, <180 inches.

Operators attempt to restore CVCS letdown (4th attempt). Charging

Pump 11 started. Commenced ReS boration from 11 Boric Acid

13:09

4.75 hrs

Tank.

13:11

4.77 hrs

Pressurizer level out of EOP control band high, >180 inches.

Letdown Isolations CVC-515 and 516 opened. CVCS letdown

restored. Letdown Excess Flow Check Valve 1-CVC-343-CV

13:17

4.88 hrs

opened on 4th letdown restoration attempt.

13:30

5.10 hrs

Pressurizer level returns within EOP control band, <180 inches.

Attachment 3

3-3

UNIT 1 EVENT TIMELINE

Clock Time

Event Time

Description

Crew exits EOP-1 and enters OP-5, Plant Shutdown From Hot

13:38

5.23 hrs

Standby to Cold Shutdown.

13:46

5.37 hrs

Boratlon stopped, charging suction from VCT to lower VCT level.

13:58

5.57 hrs

Boration re-commenced from 11 Boric Acid Tank.

14:07

5.72 hrs

4 kV Vital Bus 14 Alternate Feeder Breaker 152-1401 closed.

Emergency Diesel Generator 1B Output Breaker 152-1403 to 4 kV

14:13

5.82 hrs

Vital Bus 14 opened.

14:15

5.85 hrs

Emergency Diesel Generator 1 B shutdown.

Boratlon completed. Approximately 2420 gaHons of boric acid

14:16

5.87 hrs

injected.

14:37

6.22 hrs

RCS sampled for boron. Concentration at 529 ppm.

16:00

7.6 hrs

RCS sampled for boron. Concentration at 622 ppm.

21:50

13.4 hrs

ts for 500 kV Switchyard Breaker 552-22 closed.

22:00

13.6 hrs

500 kV Switch yard Breaker 552-22 closed.

22:01

13.6 hrs

Disconnects for 500 kV SWitchyard Breaker 552-23 closed.

22:07

13.7 hrs

500 kV Switchyard Breaker 552-23 Closed.

02119/2010

12:01

27.6 hrs

SMECO now credited to 4 kV Bus 24.

02120/2010

17:05

Started 12B RCP.

19:20

~ Commenced RCS cooldown to MODE 5 per OP-5.

02121/2010

05:38

69 hrs

Unit 1 in MODE 5, RCS temperature < 200°F.

05:50

69.5 hrs

Divorced from SMECO, re-energized 500 kV Red Bus.

UNIT 2 EVENT TIMELINE

Clock Time

Event Time

Description

02118/2010

A phase to ground fault occurs on the 13 kV supply line to Unit 1

Reactor Coolant Pump (RCP) 12B Motor, upstream of 12B RCP

08:24:25:225 0.000 sec Breaker 252-14P02, which is already open (normal lineup}.

RCP 12B Breaker 252-14P01 trips open on differential overcurrent

08:24:25:225 0.000 sec relay actuation, stopping 12B RCP.

Feeder Breaker 252-2104 to 13 kV Service Bus 21 trips open, de-

energizing Unit 2 Non-vital balance of plant, Unit 2 Vital 4 kV Bus 24

i08:24:27:251 2.026 sec

and Unit 1 Vital 4 kV Bus 14.

208/120 VJAC Bus 22 de-energizes, resulting in isolation of the Unit

2 RCS letdown flowpath in the Chemical and Volume Control

08:24:27:478 2.253 sec

System (CVCS).

13 kV Service Bus 22 Supply Breaker 252-2202 to Unit 1 Reps trips

open. Unit 1 RCPs are not affected as they are aligned to their

normal power supply from 13 kV Station SerVice Transformer P

08:24;28:803 13.578 sec

13000-1 through 13 kV Service Bus 12.

108:24;28:781 :13.556 sec 500 kV Switchyard Red Bus Isolation Breaker 552-41 trips open.

Attachment 3

3-4

UNIT 2 EVENT TIMELINE

I

Clock Time

Event Time

Description

500 kV SWitchyard Red Bus Isolation Breakers 552-21 and 552-61

trip open, completing the high side isolation 13 kV Station Service

08:24:28:783 3.558 sec Transformer P-13000-2.

Undervoltage signal actuates on Unit 2 4 kV Vital Bus 24, initiating

08:24:29:451 4.226 sec

the 2B Emergency Diesel Generator start sequence.

Unit 2 4 kV Vital Bus 24 Normal Feeder Breaker 152-2401 trips

08:24:29:511 4.286 sec open.

Unit 2 automatic reactor trip on reactor coolant low flow signal from

100% initial reactor power level. All Unit 2 reactor coolant pumps

08:24:29:788 4.563 sec have stopped.

08:24:29 :827 4.602 sec Unit 2 reactor trip breakers open.

08:24:30:019 4.794 sec

Unit 2 turbine trip.

~Ta:897sec Emergency Diesel Generator 2B reaches 250 rpm.

13 kV Service Bus 21 Supply Breaker 252-2103 to Transformer U

108:24;33:818 8.593 sec 4000-22 opens.

13 kV Service Bus 21 Supply Breaker 252-2102 to Transformer U

08:24;33:818 8.593 sec

~OOO-21 opens.

13 kV Service Bus 21 Supply Breaker 252-2101 to Transformer U

08:24:33:819 8.594 sec 4000-23 opens.

08:24:33:889 8.664 sec 4 kV Non-Vital Bus 22 Feeder Breaker 152-2201 opens.

08:24:33:909 8.684 sec 4 kV Non-Vital Bus 23 Feeder Breaker 152-2311 opens.

08:24:35:988 10.763 sec Emergencv Diesel Generator 2B reaches 810-rpm.

Emergency Diesel Generator 2B Output Breaker 152-2403 to 4 kV

08:24:37:306 12.081 sec Vital Bus 24 closes.

08:24:37:785 12.560 sec 208/120 V/AC Bus 22 re-energizes.

08:24:37:887 12.662 sec Undervoltage signal clears on Unit 2 4 kV Vital Bus 24.

08:24:45:155 19.930 sec Emergency Diesel Generator 2B trips.

Emergency Diesel Generator 2B Output Breaker 152-2403 to 4 kV

08;24:45:185 19.960 sec Vital Bus 24 opens.

08:24:45:320 20.095 sec 208/120 V/AC Bus 22 de-energizes.

08:24:47:315 22.090 sec Undervoltage signal actuates on Unit 2 4 kV Vital Bus 24.

. 908 sec 21 and 22 Steam Generator Feed Pumps low suction pressure trip .

Reactor Operator backs up the automatic reactor trip signal by

1.110 sec depressing manual reactor trip pushbuttons.

08:24:55

30 sec

Crew enters EOP-O, Post-Trip Immediate Actions

Commenced boration because of loss of power to rod position

indication. Aligned gravity feed flowpath from boric acid storage

tanks to charging pump suction through 2-MOV-508 and 2-MOV

08:26

2min

509.

Manually closed 2-MS-343, Main Steam (MS) Isolation to 22

'Moisture Separator Reheater (MSR) as altemate action because 2

08:32

8 min

iMS-4019-CV, MS to 22 MSR 2nd Stage failed to close.

Steam-driven AFW Pump 21 started to maintain SG heat sink,

08:33

9min

feeding approximately 150 gpm to each steam generator.

08:34

10min

2Y10 tied to 2Y09. Power restored to 2Y10.

Crew exits EOP-O and enters EOP-2, Loss of Offsile Power I Loss of

08:38

14 min

Forced Circulation

08:47

23 min

Report of smoke and acrid odor, vicinity of MCC-207

Attachment 3

3-5

UNIT 2 EVENT TIMELINE

Clock Time

Event Time

Description

08:53

29 min

Unit 2 main steam isolation valves closed.

4 kV Vital Bus 24 Alternate Feeder Breaker 152-2414 closed.

Shutdown sequencer is manually initiated per EOP Attachment 16.

08:57

33 min

The undervoltage signal clears on Unit 2 4 kV Vital Bus 24.

09:00

36 min

Restored Unit 2 CVCS letdown.

09:08

44 min

Low condenser vacuum.

.vCT Outlet MOV-501 opened. Boration stopped. Approximately

09:10

46 min

1936 gallons of boric acid injected.

!

Electricians report acrid odor coming from closed 4 kV Non-vital Bus

23 Supply Breaker 152-2501 (cause later diagnosed as a burnt

09:20

56 min

breaker trip coil).

10:46

2.37 hrs

Chemistry samples RCS for boron concentration.

Completed verification of required shutdown margin per NEOP-301 '

11:00

2.60 hrs

Attachment 3. Required concentration determined to be 1297_ppm.

Started 23 AFW Pump (motor-driven) and stopped 21 AFW Pump

111 :17

2.88 hrs

Ilturbine-driven).

Crew exits EOP-2 and enters OP-5, Plant Shutdown From Hot

11 :18

2.90 hrs

Standby to Cold Shutdown.

Chemistry reports RCS boron 1479 ppm. Initial concentration was

11:30

3.10 hrs

1129 ppm prior to the event.

11 :47

3.38 hrs

Completed 4 hr report to NRC, as required per 10CFR50.72.

,

12:11

3.78 hrs

Disconnects for 500 kV Switch yard Breaker 552-21 are opened.

i12:14

3.83 hrs

Disconnects for 500 kV Switchyard Breaker 552-61 are opened.

~.

3.85 hrs

Disconnects for 500 kV Switchyard Breaker 552-23 are opened.

12:17

3.88 hrs

Disconnects for 500 kV Switchyard Breaker 552-22 are opened.

12:18

3.90 hrs

Disconnects for 500 kV Switchyard Breaker 552-63 are opened.

Completed STP-O-90-2, AC Sources and Onsite Power Distribution

Systems 7 Day Operability Verification. This was a missed action

requirement of TS 3.8.1, required to be completed within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of

12:55

4.52 hrs

the event.

Commenced RCS CooJdown # 87 using Natural Circulation to target i

113:30

5.10 hrs

temperature of 445°F per OP-5 to protect RCP seals.

IStopped RCS Cool down # 87 based on decision to start two RCPs

14:45

6.35 hrs

land gO on forced circulation. RCS temperature at 505°F.

17:13

8.82 hrs

Started 21 Band 22A RCPs. Forced RCS circulation restored.

21:50

13.43 hrs Disconnects for 500 kV Switchyard Breaker 552-22 closed.

22:00

13.60 hrs 500 kV Switchyard Breaker 552-22 closed.

22:01

13.62 hrs Disconnects for 500 kV Switchyard Breaker 552-23 closed.

22:07

13.72 hrs 500 kV Switchyard Breaker 552-23 closed.

02/19/2010

00:29

Started 21 Condensate Pump

02:56

Started 21 CirculatinQ Water Pump

Restored Gland Sealing Steam

Performed fast speed start test of EDG 2A

EDG 2A paralleled to 4 kV Bus 21.

07:49

A at full load on 4 kV Bus 21.

l10:08

ed SMECO to 13 kV Bus 21.

Attachment 3

i

UNIT 2 EVENT TIMELINE

Clock Time

Event Time

Description

11 :01

Energized U-4000-21 from 13 kV Bus 21 (SMECO feeding).

11 :02

Energized U-4000-22 from 13 kV Bus 21 (SMECO feeding).

Two offsite power sources verified OPERABLE with SMECO

12:05

27.6 hrs

supplying 13 kV Bus 21 and available to Unit 2 4 kV buses.

12:28

Unloaded EDG 2A.

12:32

Shutdown EDG 2A. Completed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> loade'd test run.

Restored normal power supply alignment for 208/120 Instrument

13:52

Bus 22 (2Y10). 2Y09 and 2Y10 are un-tied.

02120/2010

17:19

57 hrs

Performed fast speed start test of EDG 2B.

17:36

EDG 2B paralleled to 4 kV Bus 24.

17:46

EDG 2B at full load on 4 kV Bus 24.

21:57

Unloaded EDG 2B.

22:02

Shutdown EDG 2B. Completed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> loaded test run.

22:31

62 hrs

EDG 2B declared OPERABLE.

02/21/2010

04:24

Commenced drawing main condenser vacuum.

05:50

69.5 hrs

Divorced from SMECO, re-energized 500 kV Red Bus.

09:24

Opened 21 and 22 Main Steam Isolation Valves

09:25

73 hrs

Recommenced RCS Cooldown # 87 to MODE 5 per OP-5.

17:16

81 hrs

Unit 2 in MODE 4, RCS temperature < 350°F.

20:12

84 hrs

Stopped RCS cooldown to degas RCS.

02/2212010

01:30

89 hrs

Recommenced RCS cooldown.

05:00

92.6 hrs

Unit 2 in MODE 5, RCS temperature < 200°F.

Attachment 3