ML043100605

From kanterella
Jump to navigation Jump to search
IR 05000397-04-004; 6/24/2004 - 9/23/2004; Columbia Generating Station. Surveillance Testing and Event Followup
ML043100605
Person / Time
Site: Columbia 
Issue date: 11/05/2004
From: William Jones
NRC/RGN-IV/DRP
To: Parrish J
Energy Northwest
References
EA-04-0192 IR-04-004
Download: ML043100605 (46)


See also: IR 05000397/2004004

Text

November 5, 2004

EA-04-0192

J. V. Parrish (Mail Drop 1023)

Chief Executive Officer

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

SUBJECT:

COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION

REPORT 05000397/2004004

Dear Mr. Parrish:

On September 23, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Columbia Generating Station. The enclosed inspection report documents the

inspection findings which were discussed on September 30, 2004, with Mr. Webring and other

members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one NRC identified finding, three self-revealing findings, and a finding

with both an NRC and a self-revealing examples that were of very low safety significance

(Green). Three of these findings were determined to involve violations of NRC requirements.

However, because of the very low safety significance and because they are entered into your

corrective action program, the NRC is treating these three findings as non-cited violations

(NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest these

NCVs, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control

Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV, 611

Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

inspector at the Columbia Generating Station.

Energy Northwest

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

William B. Jones, Chief

Project Branch E

Division of Reactor Projects

Docket: 50-397

License: NPF-21

Enclosure:

NRC Inspection Report 05000397/2004004

cc w/enclosure:

W. Scott Oxenford (Mail Drop PE04)

Vice President, Nuclear Generation

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

Albert E. Mouncer (Mail Drop PE01)

Vice President, Corporate Services/

General Counsel/CFO

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

Chairman

Energy Facility Site Evaluation Council

P.O. Box 43172

Olympia, WA 98504-3172

Douglas W. Coleman (Mail Drop PE20)

Manager, Regulatory Programs

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

Energy Northwest

-3-

Gregory V. Cullen (Mail Drop PE20)

Supervisor, Licensing

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

Chairman

Benton County Board of Commissioners

P.O. Box 190

Prosser, WA 99350-0190

Dale K. Atkinson (Mail Drop PE08)

Vice President, Technical Services

Energy Northwest

P.O. Box 968

Richland, WA 99352-0968

Thomas C. Poindexter, Esq.

Winston & Strawn

1400 L Street, N.W.

Washington, DC 20005-3502

Bob Nichols

Executive Policy Division

Office of the Governor

P.O. Box 43113

Olympia, WA 98504-3113

Lynn Albin, Radiation Physicist

Washington State Department of Health

P.O. Box 7827

Olympia, WA 98504-7827

Technical Services Branch Chief

FEMA Region X

Federal Regional Center

130 228th Street, S.W.

Bothell, WA 98021-9796

Energy Northwest

-4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS STA (DAP)

Senior Resident Inspector (ZKD)

Resident Inspector (RBC1)

Branch Chief, DRP/E (WBJ)

Senior Project Engineer, DRP/E (VGG)

Acting Team Leader, DRP/TSS (RVA)

RITS Coordinator (KEG)

Matt Mitchell, OEDO RIV Coordinator (MAM4)

Columbia Site Secretary (LEF1)

Dale Thatcher (DFT)

W. A. Maier, RSLO (WAM)

NSIR/EPPO (JDA1)

ADAMS: W Yes

G No Initials: _WBJ__

W Publicly Available G Non-Publicly Available

G Sensitive W Non-Sensitive

R:\\_COL\\2004\\COL2004-04RP-ZKD.wpd

RIV:SRI:DRP/E

RIV:SRI:DRP/E

RIV:SPE:DRP/E

C:DRS/EB

ZK Dunham

RBCohen

VGGaddy

JAClark

T-WBJ

T-WBJ

E-WBJ

LEE For

11/4/04

11/4/04

11/4/04

11/4/04

C:DRS/OB

C:DRS/PSB

C:DRS/PEB

C:DRP/E

TGody

MShannon

LJSmith

WBJones

/RA/

/RA/

E-WBJ

/RA/

11/5/04

11/4/04

11/4/04

11/5/04

OFFICIAL RECORD COPY D=Discussed T=Telephone E=E-mail F=Fax

Enclosure

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-397

License:

NPF-21

Report:

05000397/2004004

Licensee:

Energy Northwest

Facility:

Columbia Generating Station

Location:

Richland, Washington

Dates:

June 24 through September 23, 2004

Inspectors:

Z. Dunham, Senior Resident Inspector, Project Branch E, DRP

G. Replogle, Senior Resident Inspector, Project Branch E, DRP

R. Cohen, Resident Inspector, Project Branch E, DRP

G. Larkin, Resident Inspector, Project Branch E, DRP

R. Lantz, Senior Emergency Preparedness Inspector

M. Sitek, Resident Inspector, Project Branch C, DRP

T. McKernon, Senior Operations Engineer, Operations Branch

D. Stearns, Project Engineer, Project Branch E, DRP

P. Elkmann, Emergency Preparedness Inspector

L. Ricketson, Senior Health Physicist, Plant Support Branch

L. Ellershaw, Senior Engineering Inspector, Engineering Branch

Approved By:

W. B. Jones, Chief, Project Branch E, Division of Reactor Projects

ATTACHMENT:

Supplemental Information

Enclosure

CONTENTS

PAGE

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REACTOR SAFETY

1R04

Equipment Alignments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05

Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R07

Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R11

Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R13

Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . . 6

1R15

Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R16

Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R19

Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R20

Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R22

Surveillance Testing

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R23

Temporary Plant Modifications

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1EP1 Exercise Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

OTHER ACTIVITIES

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

4OA4 Crosscutting Aspects of Findings

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA5 Other . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA7 Licensee Identified Vioations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

ATTACHMENT: SUPPLEMENTAL INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

Items Opened and Closed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

Partial List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

Enclosure

SUMMARY OF FINDINGS

IR05000397/2004004; 6/24/2004 - 9/23/2004; Columbia Generating Station. Surveillance

Testing and Event Followup.

The report covered a 13-week period of inspection by the resident inspectors, emergency

preparedness inspectors, a health physicist inspector, an operations inspector, and an

engineering inspector. Three Green noncited violations, two Green findings, and two

unresolved item were identified. The significance of most findings is indicated by their color

(Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance

Determination Process. Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing finding associated with control room operators failure to

adequately monitor condenser hotwell level occurred when hotwell level was

established high in the indicating range and above the hotwell level high level

alarm. This condition resulted in the associated hotwell level high level

annunciator being locked in and was effectively out of service. A manual reactor trip was initiated when the hotwell level excursion resulted in the loss of the only

operating reactor feedwater pump.

This finding is greater than minor because it was a human performance issue

which impacted the initiating events cornerstone objective. Specifically,

adequate compensatory actions were not put in place to address the hotwell

level high level annunciator. This finding had crosscutting aspects in the area of

human performance in that adequate monitoring of hotwell level was not

implemented which contributed to the reactor scram. A Phase 2 evaluation was

performed in accordance with Manual Chapter 0609, Significance Determination

Process, based on the finding contributing to both the likelihood of a reactor trip

and that mitigation functions would not be available. The Phase 2 review was

performed using the Columbia Generating Station site specific worksheets. A

senior reactor analyst reviewed the Phase 2 results and performed a limited

Phase 3 review. The senior reactor analyst considered the limited time the plant

was at a low power level and adjusted the time in power operations to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

The finding was determined to be of low safety significance. Corrective actions

included revising hotwell alarm response and operating procedures to preclude

operation of the hotwell at levels above the high level alarm (Section 4OA3.2)

Green. A self-revealing finding occurred when an equipment operator failed to

follow a clearance order instruction when filling and venting a condensate heat

exchanger. This action resulted in a low suction trip of a reactor feedwater

pump, the loss of reactor feedwater and a subsequent manual reactor scram.

-2-

Enclosure

This finding is greater than minor because it was a human performance issue

which impacted the initiating events cornerstone objective to limit the likelihood

of those events that upset plant stability and challenge critical safety functions.

This finding had crosscutting aspects in the area of human performance in that

adequate pretask briefings were not performed for the the operator placing the

feedheater back into service. A Phase 2 evaluation was performed in

accordance with Manual Chapter 0609, Significance Determination Process,

based on the finding contributing to both the likelihood of a reactor trip and that

mitigation functions would not be available. The Phase 2 review was performed

using the Columbia Generating Station site specific worksheets. A senior

reactor analyst reviewed the Phase 2 results and performed a limited Phase 3

review. The senior reactor analyst considered the limited time the plant was at a

low power level and adjusted the time in power operations to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The

finding was determined to be of low safety significance. Corrective actions

included temporary senior reactor operator oversight of all pretask briefings and

remedial training for the individuals involved (Section 4OA3.3).

Cornerstone: Mitigating Systems

Green. A self-revealing noncited violation of Technical Specification 5.4.1.a

occurred when operators failed to return a nuclear power range instrument to

service after bypassing the instrument for a gain adjustment in accordance with

a surveillance procedure. This resulted in the instrument being left out of service

for an additional seven hours after it was available for use. There were

indications readily available to the control room staff to identify the out of service

component earlier than when it was finally identified. This finding had cross

cutting aspects in the area of human performance in that the nuclear power

range instrument was not appropriately returned to service and several

opportunities were available, including a shift turnover to identify the condition.

Corrective actions included returning the instrument to service and revising the

frequency of panel walkdowns in the control room to ensure a more thorough

examination of plant indications.

This finding is greater than minor because it involved a configuration control

issue which impacted the mitigating systems cornerstone objective to ensure the

reliability of systems that respond to initiating events to prevent undesirable

consequences. The issue was of very low safety significance (Green) because

the finding did not result in the loss of function of a safety system or represent an

actual loss of a safety function of a single train for greater than its Technical

Specification allowed outage time (Section 1R22).

Cornerstone: Emergency Preparedness

-3-

Enclosure

Green. The inspectors identified a noncited violation for Energy Northwests

failure to activate the Emergency Response Data System within 60 minutes in

accordance with 10 CFR 50.72(a)(4) after declaring an Alert on July 30, 2004.

This finding had cross cutting aspects in the area of human performance in that

Emergency Response Data System was not initiated as required within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

The finding is greater than minor because it was associated with an actual event

response performance deficiency that affected the emergency preparedness

cornerstone objective to ensure that Energy Northwest is capable of

implementing adequate measures to protect the health and safety of the public in

the event of a radiological emergency. By not activating Emergency Response

Data System within the required time, Energy Northwest hindered the NRCs

ability to verify plant conditions to ensure the appropriateness of any licensee

recommended emergency response actions. The finding was of very low safety

significance because although the finding was associated with an

implementation problem during an actual Alert declaration, the failure to comply

with the requirements of 10 CFR 50.72(a)(4) did not constitute a failure to

implement a risk significant planning standard. Corrective actions included

assigning additional on-shift personnel the responsibility of activating Emergency

Response Data System to ensure that time requirements are met

(Section 4OA3.1)

Cornerstone: Occupational Radiation Safety

Green. The inspector reviewed two examples of a noncited violation of

10 CFR 20.1501(a) because Energy Northwest failed to evaluate radiological

conditions. One example was self-revealing; one was NRC-identified. In the first

example, Energy Northwest failed to evaluate the changing radiological

conditions during gasket replacement on Reactor Water Clean Up Pump 1B. As

a result, four workers were internally and externally contaminated. In the second

example, also involving the reactor water clean up system, Energy Northwest

failed to survey airborne radioactivity before or during work activities on a system

pump despite the potential for steam leaks. The findings were entered into

Energy Northwests corrective action program as Condition Reports 2-04-01975

(PER 20400759) and 2-04-04966.

The finding was more than minor because it was associated with one of the

cornerstone attributes (exposure control) and affected the associated

cornerstone objective because it resulted in decreased licensee awareness of

possible radiological hazards. The occurrence involved individual workers

unplanned, unintended doses or potential of such a dose resulting from actions

contrary to NRC regulations that could have been significantly greater as a result

of a single minor, reasonable alteration of the circumstances. Using the

Occupational Radiation Safety Significance Determination Process, the inspector

determined the finding was of very low safety significance because it was not (1)

-4-

Enclosure

an ALARA finding, (2) an overexposure, (3) a significant potential for

overexposure, or (4) a loss of ability to assess dose. This finding also had

crosscutting aspects associated with human performance (Section 2OS2).

B.

Licensee Identified Violations

Violations of very low safety significance which were identified by Energy Northwest

have been reviewed by the inspectors. Corrective actions taken or planned by Energy

Northwest have been entered into their corrective action program. These violations and

corrective action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status:

The inspection period began with Columbia Generating Station at 100 percent power. The

plant was maintained at essentially 100 percent power for the entire inspection period with the

following exceptions: July 30, 2004, the plant automatically tripped on high reactor pressure

vessel pressure due to a failed main turbine governor valve control circuit card. The plant

remained shutdown and entered Forced Outage 04-01 to perform repairs on two main steam

isolation valves; August 14, 2004, the plant was started up and entered the power range;

August 15, 2004, the plant was manually tripped due to a loss of feedwater which occurred

when the main condenser hotwell overflowed; August 16, 2004, the plant was started up and

entered the power range; August 17, 2004, the plant was manually tripped due to a loss of

feedwater which occurred when an equipment operator failed to properly fill and vent a

condensate heater; August 20, 2004, the plant was started up and entered the power range

and exited Forced Outage 04-01; August 24, 2004, the plant achieved 100 percent power. The

plant was maintained at essentially 100 percent power for the rest of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04

Equipment Alignments (71111.04)

.1

Quarterly Partial Equipment Alignments

a.

Inspection Scope

The inspectors completed three partial system walkdowns of safety-related systems

during the inspection period. The inspectors reviewed system drawings, the Final

Safety Analysis Report, Technical Specifications, and operating procedures to establish

the proper equipment alignment to ensure system operability.

Residual Heat Removal (RHR) System Train A: On August 12, 2004, the

inspectors walked down the mechanical and electrical alignment of the RHR

system Train A while Train B was inservice providing decay heat removal during

a forced outage. The inspectors reviewed the alignment of critical system

components using Procedure SOP-RHR-SDC, RHR Shutdown Cooling,

Revision 4.

Emergency Diesel Generator (EDG) Train B: On September 8, 2004, the

inspector walked down the mechanical and electrical alignments of the EDG

Train B while the EDG Train A was out of service for planned surveillance

testing. The inspectors reviewed the alignment of critical system components

using Procedure SOP-DG2-STBY, Emergency Diesel Generator (Div 2) Standby

Lineup, Revision 3, as criteria for this inspection.

-2-

Enclosure

Reactor Core Isolation Cooling (RCIC): On September 13, 2004, the inspectors

performed one partial walk down of accessible portions of the RCIC system to

evaluate the correct alignment of mechanical components. The inspectors

utilized facility drawings, procedures and alignment checklists to verify the

correct system alignment. The inspectors then compared the as-found condition

of the system to verify that it could perform it safety function. The inspectors

also evaluated the material condition of the system.

b.

Findings

No findings of significance were identified.

.2

Complete System Walkdown (Semiannual)

a.

Inspection Scope

On August 31, 2004, the inspectors performed a walkdown of accessible portions of the

Standby Service Water (SW) System Train A, while the system was in service to verify

operational status and material condition of the system and its components. The

inspectors reviewed system drawing M-524, "Flow Diagram Standby Service Water

System," Revision 104, to verified proper electrical and mechanical system lineup. The

inspectors also reviewed outstanding maintenance work orders and assessed

operability and conformance with licensing requirements and commitments. The

inspectors evaluated Energy Northwests corrective measures to address related

conditions adverse to quality to verify that corrective measures were timely and

adequate. The inspectors reviewed the following documents during the inspection:

Final Safety Analysis Report Chapter 9.2, Water Systems

Technical Specification 3.7.1, SW System and Ultimate Heat Sink (UHS),

Amendment No. 169

Drawing M-524, "Flow Diagram Standby Service Water System" Revision 104

PER [Proble Evaluation Request] Resolution 203-0234, potential adverse trend

on SW flow indicators.

PER Resolution 203-0589, SW-PI-40 (HPCS [High Pressure Core Stray] SW

PAM instrumentation) is inoperable for greater than 30 days.

PER Resolution 203-1202, UT inspection reveals two areas of small wall loss in

the SW piping downstream of SW-RO-2B.

PER Resolution 203-1616, several deficiencies noted on 18" SW (22)-2 SW A

return Line between SWPH A and the SW B Spray Pond.

PER Resolution 203-1348, UT inspection revealed several small areas with

thickness below ASME Code requirements in an area where a pin hole leak was

discovered, downstream of SW-RO-2A.

PER Resolution 203-2983, during a check of SW flows per the values of OSP-

SW-M 102, less than the minimum required flow was identified.

-3-

Enclosure

PER Resolution 203-2989, current practice of aligning SW to CCH-CR-1B after

performing OSP-SW-M 102 seems to affect SW B system flow balance more

than previously thought.

PER Resolution 203-3123, recent low flow PERS pose a question regarding SW

system reliability.

PER Resolution 203-3180, scheduled UT measurement of piping downstream of

SW shows continued cavitation-induced wall loss.

PER Resolution 203-3294, identified SW flow below the minimum for operability

to CAC-HR-1B.

PER Resolution 203-3427, SW-LI-1B and SW-LI-1BR are indicating

approximately 1.5 feet higher than actual spray pond level.

PER Resolution 203-4101, unplanned Technical Specification action statement

entry due to low service water flow on CAC MCC room cooler.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

.1

Quarterly Walkdowns

a.

Inspection Scope

The inspectors performed walkdowns of eight fire protection areas to verify operational

status and material condition of fire detection and mitigation systems, passive fire

barriers and fire suppression equipment. The inspectors reviewed Energy Northwests

implementation of controls for combustible materials and ignition sources in selected fire

protection zones. The inspectors compared observed plant conditions against

descriptions and commitments described in the Final Safety Analysis Report,

Section 9.5.1, Fire Protection System, and Appendix F, Fire Protection Evaluation.

The fire areas inspected were:

Fire Area RC-10; Main Control Room; July 15, 2004

Remote Shutdown Room; July 15, 2004

Fire Area DG-1; High Pressure Core Spray Diesel Generator; August 11, 2004

Fire Area DG-2; Diesel Generator 1A; August 10, 2004

Fire Area DG-3; Diesel Generator 1B; August 10, 2004

Fire Area R-4; Residual Heat Removal Pump 2B Room; August 18, 2004

Fire Area R-5; Residual Heat Removal Pump 2A Room; August 18, 2004

Fire Area R-7; Residual Heat Removal Pump 2C Room; August 18, 2004

b.

Findings

No findings of significance were identified.

-4-

Enclosure

1R07

Heat Sink Performance (71111.07)

a.

Inspection Scope

On July 16, 2004, the inspectors analyzed one evaluation associated with the HPCS

EDG cooling water heat exchanger thermal performance which was tested on June 23,

2004. The inspectors reviewed the test data to ensure that test acceptance criteria were

appropriate and considered differences between test conditions and design conditions.

The inspectors also considered Energy Northwests incorporation of instrument

inaccuracies into the test program. Lastly, the inspectors performed checks of selected

test results through independent calculation to ensure that the heat exchanger was

capable of removing its design heat load. The inspectors referenced Procedure PPM

8.4.63, Thermal Performance Monitoring of DCW-HX-1C, dated June 23, 2004.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification (71111.11)

a.

Inspection Scope

On July 19, 2004, the inspectors observed one licensed operator requalification training

exam as operators participated in an evaluated scenario on the plant simulator. The

inspectors evaluated the crews performance in terms of command, control, and

communications and procedure usage. The inspectors also observed Energy

Northwests evaluation of crew performance to ensure that performance deficiencies

were appropriately discussed and evaluated. Simulator fidelity was also reviewed by the

inspectors.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12)

.1

Routine Maintenance Effectiveness Evaluations

a.

Inspection Scope

The inspectors performed one in-office review of maintenance rule related issues and/or

safety related systems to evaluate Energy Northwests assessment of availability and

reliability of risk-significant structures, systems and components.

-5-

Enclosure

Performance Evaluation Report (PER) 204-0628; E-IN-3A was running, for

testing, in parallel with E-IN-3B which could cause an overload condition of the

Division 1 125 VDC system; March 10, 2004

The inspectors utilized the following documents for this inspection:

TI 4.22, Maintenance Rule Program, June 19, 2001

Columbia Generating Station Maintenance Rule Scoping Matrix,

October 30, 2003

NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants, Revision 2

Procedure 1.5.11; Maintenance Rule Program, Revision 6

b.

Findings

No findings of significance were identified.

.2

Biennial Maintenance Rule Implementation Inspection

a.

Inspection Scope

Periodic Evaluation Reviews

The inspectors reviewed Energy Northwest's last four biannual periodic assessments,

Maintenance Rule Program Biannual Period Status Report, each covering a 6-month

period beginning with the July through December 2002 report, and ending with the

January through June 2004 report. These reports documented the results of Energy

Northwests assessment of the Maintenance Rule Program based on performance

monitoring, condition monitoring, and preventive maintenance. In addition, the

inspectors reviewed Energy Northwests overall implementation of the Maintenance

Rule, including their Maintenance Rule Scope, (a)(1) determinations, performance

criteria, program definitions, use of industry operating experience, and Maintenance

Rule related self assessments. With respect to those structures, systems, or

components identified as being in an (a)(1) status, the inspectors verified the

establishment of appropriate goals, corrective actions and the impact of risk monitoring.

The inspectors reviewed the conclusions reached by Energy Northwest with regard to

the balance of reliability and unavailability for specific maintenance rule functions. The

inspectors selected the following systems that had either been placed in (a)(1) status, or

had recently been returned to (a)(2) status for a detailed review:

SW-SYS-A and -B [both in (a)(1)]

DG-SYS-A [returned to (a)(2) from (a)(1)]

RPS-MG-1 [returned to (a)(2) from (a)(1)]

RHR-SYS-A [in (a)(1)]

RCIC-SYS-1 [in (a)(1)]

-6-

Enclosure

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors selected four samples of planned and emergent maintenance tasks for

evaluation. The evaluation consisted of reviewing Energy Northwests assessment of

plant risk for the activity, risk management and review of compensatory measures,

where appropriate, and reviewing plant status to ensure that other equipment

deficiencies did not adversely impact the planned risk assessment. The inspectors

sample included:

Main steam leakage control Train A out of service coincident with EDG Train B

diesel generator and Train B RHR system; June 30, 2004

Main steam isolation Valve MS-V-28D and MS-V-22D repairs; August 9, 2004

Feedwater containment isolation Valve RFW-V-65A emergent work;

August 27, 2004

RCIC maintenance outage coincident with standby gas treatment Train A

maintenance; September 1, 2004

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed three operability evaluations to evaluate Energy Northwests

assessment of operability for degraded or nonconforming equipment performance. The

inspectors reviewed the Final Safety Analysis Report, Technical Specifications,

applicable system drawings and design specifications, and associated corrective action

documents to determine if Energy Northwest had appropriately evaluated operability.

PER 204-0935, Several discrepancies noted on the positions of D/G room

ventilation dampers; July 19, 2004

CR 2-04-04511, Pressurization of Train B RHR Low Pressure Piping During

Reactor Heat-up; August 16, 2004

-7-

Enclosure

CR 2-04-01508, In 1995 an incorrect stem diameter was applied during

diagnostic testing of Valve MSLC-V-1D. Actual thrust/torque is greater than

recorded; identified by licensee on April 15, 2004; reviewed on

September 21, 2004

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

The inspectors reviewed operator workarounds to ascertain the cumulative effects on

reliability, availability, and potential for misoperation of a system. The review also

included an assessment of the cumulative operator workarounds, operator burdens, and

whether they could affect multiple mitigating systems and whether operators were able

to respond in a correct and timely manner to accidents and plant transients.

b.

Findings

No findings of significance were identified.

1R19

Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors observed or completed an in-office review of six postmaintenance tests.

The inspectors evaluated the scope of the maintenance activity, reviewed design basis

information, and reviewed technical specifications to verify that each test adequately

demonstrated equipment operability. The inspection samples included:

Work Order 01082365; RHR-FIS-10B Replacement; June 30, 2004

Work Order 01084406; MS-V-67D Valve Replacement; August 12, 2004;

reviewed on August 16, 2004

Work Order 01077279; MS-V-28D Disassemble and Reassemble;

August 12, 2004

Work Order 01060822; MS-V-22D Disassemble and Reassemble;

August 13, 2004

Work Order 01062381; Replace IRM-DET-2F; August 18, 2004

-8-

Enclosure

Work Order 01079061; RCIC-P-1 Change Bearing Housing Oil;

August 31, 2004

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities (71111.20)

a.

Inspection Scope

Forced Outage 04-01 began on July 30, 2004, and ended on August 24, 2004. During

the outage, the inspectors observed reactor scram recovery, cooldown, startup, and

maintenance activities to verify that Energy Northwest maintained the plant capabilities

within the applicable Technical Specification requirements and within the scope of the

outage risk plan. Specific activities evaluated included:

Reactor Water Inventory Controls - verified that flow paths, equipment

configurations, and alternative means for inventory addition were appropriate to

prevent inventory loss.

Reactivity Controls - ensured compliance with Technical Specifications and

verified that activities, which could affect reactivity, were reviewed for proper

control within the outage risk plan.

Monitored Shutdown Cooling System - verified that operating parameters were

established and maintained within the required range.

Reactor Coolant System Instrumentation Indication - verified that reactor coolant

system pressure, level, and temperature instrumentation were installed and

configured to provide accurate indication.

Heatup and Startup Activities - ensured that Technical Specifications and

administrative procedure prerequisites for mode changes were met prior to

changing modes or plant configurations. Included an inspection of the drywell

prior to drywell closeout.

Electrical Power - verified that electrical power systems were available to ensure

compliance with Technical Specifications and the outage risk plan.

b.

Findings

No findings of significance were identified.

-9-

Enclosure

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors observed the performance and/or reviewed the results of the five

surveillance tests listed below. Of the five surveillance tests, two were in-service tests of

risk significant components. The inspectors reviewed Technical Specification, Final

Safety Analysis Report, and applicable Energy Northwest procedures to determine if the

surveillance tests demonstrated that the tested components were capable of performing

their intended design functions. Additionally, the inspectors evaluated significant test

attributes such as potential preconditioning, clear acceptance criteria, accuracy and

range of test equipment, procedure adherence, and completion and acceptability of test

data.

Procedure OSP-RHR/IST-Q704; Emergency Core Cooling Systems;

Revision 14; July 28, 2004

Procedure TSP-MSIV-B801; Train D MSIV Leak Rate Testing; Revision 1;

August 13, 2004

Procedure ISP-LPCS/RHR-Q901; RHR A & LPCS Discharge Pressure - ADS

Trip System A Permissive (By K10A Relay) - CFT/CC; Revision 7; July 28, 2004

Procedure TSP-APRM-C301; APRM and Core Thermal Power Channel

Calibration Check; Revision 4; August 24, 2004

Procedure OSP-LPCS/IST-Q702; LPCS System Operability Test; Revision 12;

August 29, 2004

b.

Findings

Introduction. A Green self revealing NCV occurred as a result of Energy Northwests

failure to follow a surveillance test procedure and return Average Power Range

Monitor (APRM) B to service. This was identified as a violation of Technical Specification 5.4.1.a.

Description. On August 24, 2004, control room operators performed Procedure TSP-

APRM-C301, APRM and Core Thermal Power Channel Calibration Check, Revision 4,

to perform a gain adjustment on APRM B. The APRM was bypassed at 1600 per TSP-

APRM-C301, Attachment 9.1, Step 3, to facilitate the gain adjustment. Following the

gain adjustment, the operators failed to return APRM B to service by unbypassing the

instrument per Step 8 of Attachment 9.1. Procedure TSP-APRM-C301 was

subsequently reviewed by a senior reactor operator and was closed out at 1751. At

0100 the next day, during a control board walkdown in preparation for a gain adjustment

on a different channel APRM, the reactor operator noted that APRM B was bypassed.

APRM B was then returned to service. During the time that APRM B was inadvertently

-10-

Enclosure

bypassed, APRM D and APRM F were operable and would have performed the required

Reactor Protection System (RPS) B trip functions associated with those instruments.

The inspectors noted the following two performance issues which had human

performance crosscutting aspects:

1.

Operators failed to identify the APRM was in bypass following the conduct of the

surveillance activity and during the shift turnover. Specifically, while APRM B

was out of service, Energy Northwest underwent a control room shift change at

6:00 p.m. PDT. None of the control room staff noted that APRM B was

bypassed during the shift turnover. At 1:00 a.m. PDT (7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> following the shift

turnover) the bypassed instrument was identified. Means of having identified the

APRM was bypassed were: an APRM Bypass control board indicator, an

APRM Bypass indicator on the APRM B instrument drawer located in the

control room, and the control board APRM bypass control switch out of its

normal position.

2.

A senior reactor operator signed Procedure TSP-APRM-C301 for closure

indicating that he had reviewed the procedure. However, the initial block in

Attachment 9.1, indicating return to service of APRM B, was not initialed for the

period of time in question.

Analysis. Energy Northwests failure to return APRM B to service following the gain

adjustment was determined to be a performance deficiency and was more than minor

because it was a configuration control issue which impacted the mitigating systems

cornerstone objective to ensure the reliability of systems that respond to initiating events

to prevent undesirable consequences. The issue was of very low safety significance

(Green) because the finding did not result in the loss of function of a safety system and

did not represent an actual loss of a safety function of a single train for greater than its

Technical Specification allowed outage time.

Enforcement. Technical Specification 5.4.1.a required, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation),

Appendix A, Section 8.b, required, in part, that specific procedures for calibrations

should be written to include incore flux monitor calibrations. Contrary to this

requirement on August 24, 2004, from 4:00 p.m. PDT, to August 25, 2004, at 1:00 a.m.

PDT, the control room operators failed to return APRM B to service in accordance with

Procedure TSP-APRM-C301, Attachment 9.1, Step 8, which required that the operator

be requested to unbypass the APRM. This violation is being treated as a noncited

violation, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 50-

397/04-04-01, Failure to Identify and Return to Service APRM B in a Timely Manner).

Energy Northwest documented this issue in their corrective action program in PER 204-

1056. Immediate corrective actions taken by Energy Northwest included verifying that

APRM B was in fact operable and returning the instrument to service. Other corrective

actions included changing the frequency of panel walkdowns in the control room to

ensure a more thorough examination of plant indications.

-11-

Enclosure

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

On August 18 and 19, 2004, the inspectors evaluated Energy Northwests use of

temporary lead shielding in the residual heat removal pump rooms. The inspectors

reviewed Energy Northwests technical and licensing basis impact evaluations for the

temporary shielding requests to ensure that the safety functions of the RHR system

remained unaffected. The inspectors also reviewed Procedure GEN-RPP-14, Control

of Temporary Shielding, Revision 3, to ensure that the use of the temporary shielding

was in accordance with Energy Northwests procedural requirements.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a.

Inspection Scope

The inspectors reviewed the objectives and scenario for the 2004 Biennial Emergency

Preparedness Exercise to determine if the exercise would acceptably test major

elements of the emergency plan. The scenario included seismic activity, which resulted

in steam leaks, valve malfunctions, and other broken equipment. Additional seismic

activity caused increased steam leakage and fuel damage, failure of isolation valves,

and a subsequent release of radioactivity to the environment. Energy Northwest

activated all of their emergency facilities to demonstrate their capability to implement the

emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of classification, notification, protective action recommendations, and

assessment of offsite dose consequences in the simulator control room and the

following emergency response facilities:

Technical Support Center

Operations Support Center

Emergency Operations Facility

The inspectors also assessed personnel recognition of abnormal plant conditions, the

transfer of emergency responsibilities between facilities, communications, protection of

emergency workers, emergency repair capabilities, and the overall implementation of

the emergency plan to verify compliance with the requirements of 10 CFR 50.47(b),

10 CFR 50.54(q), and Appendix E to 10 CFR Part 50.

-12-

Enclosure

The inspectors attended the post-exercise critiques in each of the above emergency

response facilities to evaluate the initial licensee self-assessment of exercise

performance. The inspectors also attended the formal presentation of critique items to

plant management. The inspectors completed one sample during the inspection.

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

The inspectors observed one Energy Northwest simulator evaluation on

August 16, 2004, in which the control room staff were required to make and report

emergency classifications in response to a simulated accident. The inspectors reviewed

the facility emergency plan implementing procedures (EPIPs) and Emergency Plan to

establish the criteria for the simulated emergency classifications. Additionally, the

inspectors reviewed the completed emergency action level declaration and notification

forms to verify the accuracy of the forms. Lastly, the inspectors reviewed Energy

Northwests evaluation of the drill to ensure that any performance deficiencies

associated with classification, notification, and PAR development were accurately

characterized.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety [OS]

2OS2 ALARA Planning and Controls (71121.02)

a.

Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual

and collective radiation exposures as low as is reasonably achievable (ALARA). The

inspectors used the requirements in 10 CFR Part 20 and Energy Northwests

procedures required by Technical Specifications as criteria for determining compliance.

The inspector interviewed licensee personnel and reviewed:

Current 3-year rolling average collective exposure

An on-line maintenance work activity scheduled during the inspection period and

associated work activity exposure estimates that were likely to result in the

highest personnel collective exposures

-13-

Enclosure

Three work activities from previous work history data that resulted in the highest

personnel collective exposures

Site specific trends in collective exposures, plant historical data, and source-term

measurements

Site specific ALARA procedures.

ALARA work activity evaluations, exposure estimates, and exposure mitigation

requirements

Intended versus actual work activity doses and the reasons for any

inconsistencies

Assumptions and basis for the current annual collective exposure estimate, the

methodology for estimating work activity exposures, the intended dose outcome,

and the accuracy of dose rate and man-hour estimates

Method for adjusting exposure estimates, or replanning work, when unexpected

changes in scope or emergent work were encountered

Source-term control strategy or justifications for not pursuing such exposure

reduction initiatives

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

Self-assessments and audits related to the ALARA program since the last

inspection

Corrective action documents related to the ALARA program and follow-up

activities such as initial problem identification, characterization, and tracking

The inspector completed 10 of the required 15 samples and 2 of the optional samples.

b.

Findings

Introduction. The inspectors reviewed two examples of a noncited, Green violation of

10 CFR 20.1501(a) resulting from Energy Northwests failure to evaluate radiological

conditions in work areas. One example was self-revealing; the other was

NRC-identified.

Description. On May 4, 2004, four individuals alarmed personnel contamination

monitors after performing a gasket replacement on reactor water clean up Pump 1B.

The workers were found to be internally and externally contaminated. Air samples

analyzed after the occurrence indicated 3 derived air concentrations of Cobalt-60.

Energy Northwests review of the occurrence stated that the airborne radioactivity was

likely caused by the drying of the upper pump cavity. It also stated that airborne

precautions were not adequately reconsidered and that the use of an airborne

-14-

Enclosure

radioactivity monitor may have provided an early indication that airborne conditions

existed. The inspector concluded that Energy Northwest had not adequately surveyed

or evaluated the changing radiological conditions and potential hazards.

On September 1, 2004, Energy Northwest again worked on reactor water clean up

Pump 1B. This time the tasks included postmaintenance testing and hot torquing. In

addition, one worker was assigned to look for steam leaks in the pump room. The

individual used a mirror to aid in the detection of a steam leak. At one point,

unexpectedly high dose rates were encountered in the pump room, and the job was

stopped by radiation protection personnel until further planning was completed. While

reviewing the work documents, the inspector determined that no airborne radioactivity

survey was conducted prior to or during the tasks conducted in the pump room.

The inspector concluded that this constituted a second example of a failure to survey

based on the following items: Energy Northwests search for steam leaks meant Energy

Northwest believed there was a potential for leaks to exist. Steam leaks from the

reactor water clean up system had the potential to cause unsafe airborne radioactivity

levels. Energy Northwests use of a mirror to find steam leaks meant that the leaks

were hard to see, unaided. Therefore, high airborne activity could have existed without

Energy Northwest knowing until a worker with a mirror identified a steam leak.

Analysis. A failure to survey was a performance deficiency. The finding was more than

minor because it was associated with one of the cornerstone attributes (exposure

control) and affected the associated cornerstone objective because it resulted in

decreased licensee awareness of possible radiological hazards. The occurrence

involved individual workers unplanned, unintended doses or potential of such a dose

resulting from actions contrary to NRC regulations that could have been significantly

greater as a result of a single minor, reasonable alteration of the circumstances, such as

higher airborne radioactivity concentrations. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined the finding was of very

low safety significance because it was not (1) an ALARA finding, (2) an overexposure,

(3) a significant potential for overexposure, or (4) a loss of ability to assess dose. This

finding also had crosscutting aspects associated with human performance in that

licensee personnel failed to implement the established survey requirements designed to

prevent excess occupational radiation exposure.

Enforcement. Pursuant to 10 CFR 20.1003, survey means an evaluation of the

radiological conditions and potential hazards incident to the production, use, transfer,

release, disposal, or presence of radioactive material or other sources of radiation.

10 CFR 20.1501 requires that each licensee make or cause to be made surveys that

may be necessary for Energy Northwest to comply with the regulations in

10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent

of radiation levels, concentrations or quantities of radioactive materials, and the potential

radiological hazards that could be present. Energy Northwest violated this requirement

when it did not perform a survey to comply with the requirements of 10 CFR 20.1201.

Because the failures to survey were determined to be of very low safety significance and

have been entered into Energy Northwests corrective action program as Condition

Reports 2-04-01975 (PER 20400759) and 2-04-04966, this violation is being treated as

a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement Policy:

-15-

Enclosure

NCV 05000397/2004004-02, Two Examples of Failure to survey.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Mitigating Systems Cornerstone

a.

Inspection Scope

The inspectors assessed the accuracy of the two performance indicators listed below.

The inspectors compared the data with operator logs, equipment out of service logs,

and corrective action documents for the last four quarters. The inspectors verified that

Energy Northwest calculated performance indicators in accordance with NEI 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 2.

Safety System Unavailability - BWR High Pressure Coolant Injection System

(High Pressure Core Spray)

Safety System Unavailability - Residual Heat Removal System

b.

Findings

No findings of significance were identified.

.2

Emergency Preparedness Cornerstone:

a.

Inspection Scope

The inspectors sampled submittals for the performance indicators listed below for the

period from October 1, 2003, through June 30, 2004. The definitions and guidance of

Nuclear Engineering Institute NEI 99-02, Regulatory Assessment Indicator Guideline,

Revision 2, were used to verify Energy Northwests basis for reporting each data

element in order to verify the accuracy of performance indicator data reported during the

assessment period.

Drill and exercise performance

Emergency response organization participation

Alert and notification system reliability

The inspectors reviewed a 100 percent sample of drill and exercise scenarios, licensed

operator simulator training sessions, notification forms, and attendance and critique

records associated with training sessions, drills, and exercises conducted during the

verification period. The inspectors reviewed the qualification, training, and drill

participation records for a sample of 12 emergency responders. The inspectors

reviewed alert and notification system maintenance records and procedures, and a

100 percent sample of siren test results. The inspectors also interviewed licensee

personnel that were responsible for collecting and evaluating the performance indicator

data. The inspectors completed three samples during this inspection.

-16-

Enclosure

b.

Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

.1

Annual Sample Review

a.

Inspection Scope

The inspectors selected 6 condition records (corrective action program inputs) and

13 problem evaluation requests for detailed review based on their linkage with event

classification, notification of offsite authorities, and processes for providing protective

action recommendations. The records were reviewed to ensure that the full extent of

the issues were identified, an appropriate evaluation was performed, and appropriate

corrective actions were specified and prioritized.

b.

Findings

No findings of significance were identified.

.2

Biennial Maintenance Rule Identification and Resolution of Problems

The inspectors reviewed selected corrective action documents associated with

Maintenance Rule related findings. With one exception, the inspectors verified that

Energy Northwest took, or planned, appropriate corrective measures for identified

issues.

On December 10, 2002, Energy Northwest personnel initiated Problem Evaluation

Request (PER) 202-3461. The PER, categorized as nonsignificant, was dispositioned

and closed on February 4, 2003, based on actions to be taken as identified on the PER

resolution form. There were three specific actions identified, all associated with some

aspect of Maintenance Rule scoping review. Energy Northwest personnel closed the

PER when they initiated an individual plant tracking log (PTL) for each of the three

actions. The PTL was an additional corrective action document used to cause a review,

evaluation, and implementation of specified actions.

The inspectors initiated a review of the three PTLs to verify that a resolution to each of

the conditions had been effected since it was noted that all three PTLs had been closed.

PTL H 194829 was appropriately closed on March 20, 2003. PTLs H 196658 and

H 196664 were shown to be closed on April 15, 2003, and August 28, 2003,

respectively. Closer review by the inspectors, however, revealed that the identified

actions needed to resolve the individual conditions had been transferred to the Mrule

Open Scoping Issue list. This list is a non-proceduralized and uncontrolled document

created as an aide to the Maintenance Rule Coordinator in an attempt to keep track of

Maintenance Rule scoping questions requiring resolution. Therefore, the conditions

originally documented as deficiencies on a PER have still not been corrected, yet all of

the associated corrective action documents have been closed out. This is a minor

violation of Criterion XVI in Appendix B to 10 CFR Part 50.

-17-

Enclosure

Additionally, the Mrule Open Scoping Issue list contained 56 scoping issues, only 2 of

which had been closed. Review of several of the open issues revealed that some had

resolutions which appeared to close the item, but they were still shown as being open.

The majority of the issues appeared to deal with the question of whether certain

structures or components, or their functions, should be included in the scope of the

Maintenance Rule. The inspectors were able to ascertain that the list contained open

scoping issues that dated back to at least July 2002.

Energy Northwest personnel initiated on September 23, 2004, Condition Report (CR)

CR 2-04-05341 to review and evaluate the two conditions discussed above.

.3

Cross-References to Problem Identification and Resolution Findings Documented

Elsewhere

A problem identification and resolution crosscutting aspect was identified for actions

needed to resolve individual conditions had been transferred to the Mrule Open

Scoping Issue list. This list is a non-proceduralized and uncontrolled document created

as an aide to the Maintenance Rule Coordinator in an attempt to keep track of

Maintenance Rule scoping questions requiring resolution (1R12).

A problem identification and resolution crosscutting aspect was identified for the

effectiveness of Energy Northwest's problem identification and resolution processes

regarding exposure tracking, higher than planned exposure levels, and radiation worker

practices (Section 2OS2).

4OA3 Event Followup (71153)

.1

July 30, 2004, Automatic Reactor Scram and Alert Declaration

a.

Inspection Scope

On July 30, 2004, the inspectors observed and evaluated Energy Northwests response

to an automatic reactor scram and Alert declaration which was made at 10:00 p.m. PDT.

The inspectors responded to the control room and verified the status of plant conditions

by observing key plant parameters, annunciator status, and observing the current status

of safety related mitigating equipment. The inspectors also observed reactor operator

actions in response to the plant scram and senior reactor operators evaluation of plant

conditions and oversight of the reactor operators. Following the declaration of the Alert,

the inspectors relocated to the technical support center to observe Energy Northwests

response to the event to ensure that actions taken were commensurate with established

emergency implementing procedures and that technical support center staffs evaluation

and assessment of plant conditions and emergency response was adequate. Energy

Northwest subsequently terminated the Alert at 11:57 a.m. PDT after verifying that plant

conditions were stable and that the initial criteria for which the Alert had been declared

no longer were met. During a post event review, the inspectors reviewed operator logs,

plant computer data, condition reports, and conducted interviews with plant employees

to evaluate the appropriateness of operator actions and to verify plant response.

-18-

Enclosure

b.

Findings

Operator Response to Automatic Scram and Alert Declaration

Introduction. An Unresolved Item was identified pending the NRCs determination of the

regulatory aspects and evaluation of the safety significance of the performance issues

associated with Energy Northwests Alert declaration.

Description. On July 30, 2004, at 9:23 a.m. PDT, an automatic reactor scram occurred

due to a high pressure condition. The high pressure condition occurred when the No. 1

Main Turbine Governor Valve drifted closed as a result of the associated control circuit

card failure. Following the automatic scram, the reactor operators actuated alternate

rod insertion (ARI) after noting that two control rods did not indicate fully inserted.

Operators had been trained that with more that one control rod not fully inserted

following a reactor scram that a control rod pattern did not exist which alone always

assured a shutdown reactor under all conditions. Approximately two minutes after ARI

was activated all control rods indicated fully inserted.

A prompt determination whether the reactor scram occurred because of a valid reactor

protection system (RPS) actuation was not made. Energy Northwest noted that at

08:13 a.m. PDT a surveillance activity, Procedure, ISP-MS-Q909, ATWS/ARI/RPT Trip

Reactor Pressure, had been approved for performance. Conduct of this procedure had

the potential for causing a reactor scram if not properly performed. The shift manager

initially considered that the RPS trip may have been caused by the conduct of the

surveillance activity and therefore the RPS trip may not have been valid. In fact,

although procedure ISP-MS-Q909 had been approved for performance, it had not

actually been started at the time of the scram. The shift managers review of one of the

reactor pressure chart recorders did not identify any increase in pressure which

preceded the automatic scram. At 9:53 a.m. PDT, the shift manager determined that a

valid RPS trip had occurred because of high reactor coolant system pressure. This

determination was made following the review of plant computer data which indicated a

reactor system pressure increase preceding the automatic scram.

The Emergency Plan Implementing Procedure (EPIP) 13.1.1, Classifying the

Emergency, Revision 32, described in Emergency Action Level 2.2.A.1 the following

criteria for declaring an Alert: 1) any RPS setpoint (including manual) has been

exceeded per Technical Specification 3.3.1.1; 2) RPS actuation failed to result in a

control rod pattern which alone always assures reactor shutdown under all conditions,

and; 3) manual actions (mode switch in shutdown, manual push buttons and ARI) result

in reactor power less than or equal to five percent. After reviewing the EPIP and

considering the initial rod indications and subsequent determination that a valid RPS

actuation had occurred, the shift manager declared an Alert at 10:00 a.m. PDT.

Following the Alert declaration, Energy Northwest notified offsite local and state

authorities, and activated its emergency response organization including activation of

the technical support center, emergency operating facility, and joint information center.

Additionally, Energy Northwest officially notified the NRC Headquarters Operations

-19-

Enclosure

Officer at 10:58 a.m. PDT, of the Alert declaration and activated the Emergency

Response Data System (ERDS) at 11:03 a.m PDT. After determining that the plant

conditions were stable and that the conditions for declaring the Alert no longer existed,

Energy Northwest terminated the Alert at 11:57 a.m. PDT.

A subsequent review of plant computer data by Energy Northwest determined that all

rods had fully inserted during the initial plant scram and that the position indications for

the two indeterminate control rods had not registered the rods where fully inserted until

approximately 2 minutes following the scram. Energy Northwest retracted the Alert

declaration on July 31, 2004.

Energy Northwest determined that the operators had indications available at the time the

scram occurred for determining that conditions for declaring an Alert had not been

satisfied. Specifically, Energy Northwest determined that the operators had multiple

indications available to demonstrate that all control rods had inserted during the scram.

For the 185 total control rods in the core, 183 of the control rods initially indicated fully

inserted (prior to ARI manual initiation). ARI causes a redundant scram by relieving the

scram air header independent of an RPS actuation. Energy Northwest concluded that

the operators should have realized that with 183 control rods indicating full in that the

scram air header was already depressurized and that actuation of ARI did not result in

any additional rod movement. Energy Northwest later determined that the two control

rods had only experienced indication problems. The inspectors reviewed Energy

Northwests assessment and concluded that although information was available to

determine that all rods had inserted, that at the time of the event the control room staff

made the correct and prudent decision to initiate ARI given the training they had

received to check the rod worth minimizer for all rods inserted indication.

The inspectors noted the following performance issues:

1. Immediately following the reactor scram, the reactor operator acknowledged and

reset the alarming annunciators. This reset and cleared the annunciators which would

have provided information to the shift manager in establishing the validity of the RPS

trip. In addition, the operators failed to identify those annunciators which provide entry

conditions into the emergency operating procedures. Operating Instruction OI-9,

Operations Expectations and Standards, Revision Z, Section 13.0, Annunciator

Response, provides that during transient/EOP [emergency operating procedure]

implementation that alarms are promptly evaluated and operationally significant alarms

communicated by the operator to the control room supervisor. Those annunciators

flagged as potential EOP entries are assessed by the operator and communicated to the

control room supervisor as EOP entry conditions including parameter, value, units, and

trends.

2. Prompt measures were not initiated to determine the cause of the reactor scram

including review of the computer alarm logs and each of the reactor pressure chart

recordings. The shift manager indicated that he had reviewed one of the reactor

pressure chart recordings which did not indicate a pressure increase prior to the scram.

However, the post event review clearly indicated a pressure increase on the three chart

-20-

Enclosure

recorders. Additionally, immediately prior to the scram, the control room received

average power range monitor upscale alarms. These alarms provided indication of a

plant anomaly which could include a reactor pressure increase.

3. The shift manager did not contact the personnel responsible for performing

surveillance Procedure ISP-MS-Q909 and therefore was unable to rule out the potential

for conduct of the surveillance procedure being the cause of the reactor scram.

4. The declaration of the Alert was not initiated until 37 minutes after the reactor scram.

At the time of the event, the shift manager concluded that ARI was responsible for final

insertion of the two control rods. The inspectors noted that the information needed for

the shift manager to make the Alert declaration (based on the actions taken) was

available within 15 minutes of the reactor scram.

5. At the time that the Alert declaration was made at 10:00 a.m. PDT, the conditions for

declaring the Alert no longer existed since all rods indicated full in. Emergency Plan

Implementing Procedure EPIP 13.1.1, step 3.7, Transitory Event Classification,

provided that a transitory event classification be made whenever it is discovered that a

condition had existed which met the emergency classification criteria, but where no

emergency had been declared and the basis for which no longer exists.

An Unresolved Item (URI) 50-397/04-04-03, was opened for the NRC review of the

performance issues associated with the operators response to the reactor scram and

the declaration of the Alert. The inspectors noted that Energy Northwest initiated

immediate actions to provide control room staff training and briefings on evaluating plant

conditions to verify full rod insertion and expectations of verifying all available plant

indications when verifying the validity of RPS trips

Analysis. The issues associated with the reactor scram and declaration of the Alert

classification are under review by the NRC staff. A determination of the safety

significance associated with any performance deficiencies will be addressed in the

resolution to the unresolved item.

Enforcement. The issues associated with the reactor scram and declaration of the Alert

classification are under review by the NRC staff. A determination of the enforcement

aspects associated with any performance deficiencies will be addressed in the

resolution to the unresolved item.

Emergency Response Data System (ERDS)

Introduction. An NRC identified Green NCV was identified for Energy Northwests

failure to activate ERDS within one hour. This was identified as a violation of 10 CFR 50.72(a)(4).

Description

Energy Northwest activated ERDS 63 minutes after the Alert declaration. The NRC

questioned the status of ERDS following the Alert declaration and noted that the system

was not activated within one hour after declaring an Alert.

-21-

Enclosure

Analysis.

Energy Northwests failure to activate ERDS within one hour as required by 10 CFR 50.72(a)(4) was determined to be a performance deficiency. The inspectors determined

that the failure to activate ERDS within the prescribed time limit was of more than minor

risk significance because it was associated with an actual event response performance

deficiency that affected the emergency preparedness cornerstone objective to ensure

that Energy Northwest is capable of implementing adequate measures to protect the

health and safety of the public in the event of a radiological emergency. By not

activating ERDS within the required time, Energy Northwest hindered the NRCs ability

to verify plant conditions to ensure the appropriateness of any licensee recommended

emergency response actions. Manual Chapter 0609, Appendix B, Emergency

Preparedness Significance Determination Process (EP SDP), section 2.2(e), states that

a failure to activate ERDS constitutes a failure to comply with the requirements of

10 CFR 50.72(a)(4) and should be considered a failure to implement under the EP SDP.

Utilizing Sheet 2, Actual Event Implementation Problem, of the EP SDP, the inspectors

determined that the finding was of very low safety significance (Green). Although the

finding was associated with an implementation problem during an actual Alert

declaration, the failure to comply with the requirements of 10 CFR 50.72(a)(4) did not

constitute a failure to implement a risk significant planning standard.

Enforcement.

10 CFR 50.72(a)(4) required, in part, that a licensee shall activate ERDS as soon as

possible but not later than one hour after declaring an Alert. Contrary to this

requirement, on July 30, 2004, Energy Northwest declared an Alert at 1000 but did not

activate ERDS until 1103. This violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy (NCV 50-397/04-04-04, Failure to

Activate the Emergency Response Data System Within One Hour). Energy Northwest

documented this issue in their corrective action program in Condition Report 2-04-

04103. Corrective actions included assigning additional on-shift personnel the duty of

activating ERDS to ensure timely activation.

.2

Reactor Scram due to Loss of Reactor Feedwater, August 15, 2004

a.

Inspection Scope

On August 15, 2004, the reactor plant was manually scrammed due to lowering reactor

vessel water level when the Reactor Feedwater Pump A (RFW-P-1A) unexpectedly

tripped. RFW-P-1A was the only feedwater pump in service at the time. The inspectors

observed plant conditions and operator response following the plant trip to ensure that

the reactor plant was stable and that operators were adhering to plant procedures. The

inspectors also verified alarm printouts and the status of mitigating equipment to

determine if there was any unusual plant response to the loss of feedwater and

subsequent plant scram.

-22-

Enclosure

b.

Findings

Introduction. A Green self-revealing finding was identified for Energy Northwests failure

to adequately monitor condenser hotwell level after raising hotwell level above a high

hotwell level alarm setpoint. This contributed to the operators not identifying a hotwell

excursion in a timely manner which resulted in a loss of reactor feedwater and a

subsequent manual reactor scram. No violations of NRC requirements were identified.

Description. On August 9, 2004, in anticipation of a reactor startup following a forced

outage, reactor operators raised the in-service hotwell level controller COND-LIC-1

setpoint from its nominal setpoint of zero inches to a higher control setpoint of +5.5

inches (the upper end of the control band and indicating range for COND-LIC-1 was

+6.0 inches). The operators raised the setpoint to support a plant forced outage water

management plan to accommodate additional water storage in the condenser hotwell

during the reactor startup. As a consequence of operating the hotwell at a level of +5.5

inches, the hotwell high level annunciator which had a setpoint of +3 inches was locked

in. The operators recognized this condition and implemented hourly logs of hotwell level

while the high level annunciator was locked in. The reactor was subsequently brought

critical on August 14, 2004. On August 15, 2004, while at 18 percent reactor power,

operators raised reactor power which resulted in an increase in feedwater flow from the

hotwell to the reactor and a subsequent lowering of hotwell inventory. Controller COND-

LIC-1 responded per design to the lowering hotwell level and directed water from the

condensate storage tanks to the hotwell via the make-up line and then the surge line.

However, as hotwell level increased, controller COND-LIC-1 did not respond to close the

make-up and surge line isolation valves. Level in the hotwell continued to rise above the

indicating range and eventually overflowed to Main Drain Tank No. 1 (MD-TK-1). RFW-

P-1A automatically tripped on a high level condition in MD-TK-1. With RFW-P-1A

tripped, reactor vessel level lowered in response to the loss of feedwater. Operators

manually scrammed the reactor prior to receiving an automatic scram on low reactor

vessel level (level 3).

A post event review conducted by Energy Northwest determined that Controller COND-

LIC-1 operated per design during the event and had not failed. It was determined that

the cause of failure of the hotwell level control system to restore and maintain hotwell

level at the automatic setpoint of +5.5 inches was due to operators selecting an

automatic setpoint which was too close to the upper operating range of the controller.

Once hotwell level increased beyond the top of the indicating and controlling range for

Controller COND-LIC-1, the controller failed to detect any further increase in hotwell

level as the detected level was fixed at +6.0 inches. The controller design was such that

given enough time it would have detected the +0.5 inches difference between the

sensed hotwell level of +6.0 inches and the setpoint of +5.5 inches and closed the

make-up and surge line isolation valves. However, the hotwell overflowed causing the

trip of the reactor feedwater pump and the plant was manually scrammed prior to this

occurring.

The inspectors noted the following performance issues:

1. Hourly logs by the operators to monitor hotwell level while the high level alarm was

locked in was not sufficient to monitor level in the event of a level transient. By

-23-

Enclosure

operating the Controller COND-LIC-1 at +5.5 inches, there was only a +0.5 inch margin

to hotwell level being high out of sight. In the event of a failure of the controller, hotwell

level would have exceeded the top of the indicating range in a matter of minutes.

2. At the time that the operators raised hotwell level to +5.5 inches and placed the

automatic control setpoint of Controller COND-LIC-1 at +5.5 inches, the back-up

Controller COND-LIC-2 was above the indicating range. This was due to differences in

location of the two controllers which resulted in an approximate +0.5 inch difference in

indicated level. The consequence of which was that the back-up controller was not

available for use since its indicated level was already above the indicating range.

3. Operating with the hotwell level above the hotwell level high alarm rendered that

alarm out-of-service as it was locked in and provided no information on level change.

Procedure PPM 1.3.1, Operating Policies, Programs and Practices, Revision 66,

Step 4.18.6.b, required, in part, that each out-of-service alarm should be reviewed by

the control room supervisor to evaluate the need for compensatory measures and

ensure adequate monitoring of the unavailable parameter. Contrary to this procedure,

Energy Northwests compensatory measure of logging condenser hotwell level on an

hourly basis was not adequate to monitor hotwell level with hotwell level maintained at

the top of the hotwell level controller indicating range.

Analysis. The inspectors determined that Energy Northwests failure to adequately

monitor condenser hotwell level in accordance with PPM 1.3.1 while operating with level

high in the indicating range was a performance deficiency and was reasonably within

Energy Northwests ability to foresee and correct and could have been prevented. The

finding was of more than minor safety significance because it was a human

performance issue which impacted the initiating events cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety functions.

A Phase 2 evaluation was performed in accordance with Manual Chapter 0609,

Significance Determination Process, based on the finding contributing to both the

likelihood of a reactor trip and that mitigation functions would not be available. The

Phase 2 review was performed using the Columbia Generating Station site specific

worksheets. A senior reactor analyst reviewed the Phase 2 results and performed a

limited Phase 3 review. The senior reactor analyst considered the limited time the plant

was at a low power level and adjusted the time in power operations to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The

condition existed from criticality on August 14, 2004, at 2:56 p.m. PDT until the scram on

August 15, 2004, at 1:03 p.m. PDT. Therefore, the exposure time window used was < 3

days. The initiating event likelihood credit for a transient loss of service water system

was increased from four to three by the senior reactor analyst in accordance with Usage

Rule 1.2 in Manual Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-

Informed Inspection Notebook Usage Rules. This change reflects the fact that the

finding increased the likelihood of the transient with loss of power conversion system,

but the exact magnitude of the increase was not known. The configuration of the

hotwell ensured that the feedwater system function would be lost following any transient.

Therefore, the power conversion system was not given any mitigation system credit in

the worksheets analyzed. Because the system was recoverable by two different means,

the senior reactor analyst gave credit of 1 for the mitigating system function of the power

conversion system. The finding was determined to be of low safety significance.

-24-

Enclosure

Enforcement. While Energy Northwests failure to adequately maintain and monitor

hotwell level contributed to the initiating event, the finding was not subject to

enforcement actions. The condensate system was not safety related and no violations

of regulatory requirements were identified. (FIN 50-397/04-04-05, Inadequate

Monitoring of Hotwell Level Contributes to Loss of Reactor Feedwater). Energy

Northwest documented this finding in their corrective action program in CR 2-04-04547.

Corrective actions included revising an annunciator response and operating procedure

to preclude operation of the condenser hotwell above the high hotwell level setpoint.

.3

Reactor Scram due to Loss of Reactor Feedwater, August 17, 2004

a.

Inspection Scope

On August 17, 2004, the reactor plant was manually scrammed due to lowering reactor

vessel water level when the Reactor Feedwater Pump A (RFW-P-1A) unexpectedly

tripped due to low suction pressure. RFW-P-1A was the only feedwater pump in service

at the time. The inspectors observed plant conditions and operator response following

the plant trip to ensure that the reactor plant was stable and that operators were

adhering to plant procedures. The inspectors also verified alarm printouts and the

status of mitigating equipment to determine if there was any unusual plant response to

the loss of feedwater and subsequent plant scram.

b.

Findings

Introduction. A Green self-revealing finding was identified for Energy Northwests failure

to follow a clearance order instruction which resulted in a low suction trip of a reactor

feedwater pump and a subsequent reactor scram. No violations of NRC requirements

were identified.

Description. On August 17, 2004, an equipment operator failed to follow clearance

order instruction D-COND-RV-177A which was used to isolate and then restore

condensate heat exchangers 1A and 2A from service to facilitate replacement of relief

valve COND-RV-177A. The equipment operator was to jog open COND-V-123A in

order to slowly backfill and vent the heat exchangers following the maintenance activity.

Contrary to the clearance order instruction, the equipment operator fully opened COND-

V-123A which rapidly filled condensate heat exchangers 1A and 2A which resulted in a

low suction trip of RFW-P-1A.

Analysis. The inspectors determined that the equipment operators failure to fill and

vent condensate heat exchangers 1A and 2A in accordance with clearance order

D-COND-RV-177A was a performance deficiency and was reasonably within Energy

Northwests ability to foresee and correct and could have been prevented. The finding

was of more than minor safety significance because it was a human performance issue

which impacted the initiating events cornerstone objective to limit the likelihood of those

events that upset plant stability and challenge critical safety functions. A Phase 2

evaluation was performed in accordance with Manual Chapter 0609, Significance

Determination Process, based on the finding contributing to both the likelihood of a

reactor trip and that mitigation functions would not be available. The Phase 2 review

was performed using the Columbia Generating Station site specific worksheets. A

-25-

Enclosure

senior reactor analyst reviewed the Phase 2 results and performed a limited Phase 3

review. The senior reactor analyst considered the limited time the plant was at a low

power level and adjusted the time in power operations to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The condition existed

from criticality on August 14, 2004, at 2:56 p.m. PDT until the scram on August 15,

2004, at 1:03 p.m. PDT. Therefore, the exposure time window used was < 3 days. The

initiating event likelihood credit for a transient loss of service water system was

increased from four to threee by the senior reactor analyst in accordance with Usage

Rule 1.2 in Manual Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-

Informed Inspection Notebook Usage Rules. This change reflects the fact that the

finding increased the likelihood of the transient with loss of power conversion system,

but the exact magnitude of the increase was not known. The configuration of the

hotwell ensured that the feedwater system function would be lost following any transient.

Therefore, the power conversion system was not given any mitigation system credit in

the worksheets analyzed. Because the system was recoverable by two different means,

the senior reactor analyst gave credit of 1 for the mitigating system function of the power

conversion system. The finding was determined to be of low safety significance.

Enforcement. While the equipment operators failure to properly fill and vent

condensate heat exchangers 1A and 2A in accordance with clearance order D-COND-

RV-177A was the cause of the initiating event, the finding was not subject to

enforcement actions. Operation of the condensate system was not a safety related

activity and no violations of regulatory requirements were identified (FIN 50-397/04-04-

06, Failure to Follow Clearance Order Instruction Results in Loss of Reactor Feedwater).

Energy Northwest documented this finding in their corrective action program PER 204-

1042. Corrective actions included temporary senior reactor operator oversight of all

pretask briefings and remedial training for the individuals involved.

.4

Reactor Water Cleanup Relief Valve Failure

a.

Inspection Scope

On September 10, 2004, control room operators received alarms and indications in the

control room indicative of a Reactor Water Cleanup (RWCU) leak. Indications included

a RWCU system differential flow alarm, heat exchanger room high temperature

indications, reports from personnel in the reactor building that steam was issuing from

floor drains outside of the RWCU heat exchanger room, and increased radioactive

particulate concentration in the reactor building recirculation ventilation system. The

leak was caused by RWCU heat exchanger relief valve RWCU-RV-3 inadvertently lifting

and failing to close. The inspectors, who were present in the control room when the

event occurred, observed operator response to the abnormal condition to verify that

plant abnormal procedures were followed and to assess the adequacy of operator

actions to isolate the leak. The inspectors also reviewed operator logs, applicable

drawings, and corrective action documents to determine the history of previous similar

relief valve failures. Energy Northwest repaired the relief valve and returned the RWCU

system to service.

b.

Findings

No findings of significance were identified.

-26-

Enclosure

.5

(Closed) LER 05000397/2002005-00: Main Steam Leakage Control Fan potentially

inoperable during a design basis accident due to undersized thermal overloads.

The inspectors reviewed LER 2002005-00 to determine if there were any identified

violations or aspects of human performance associated with the LER. See

Section 4OA7.1 for an associated Energy Northwest identified violation.

.6

(Closed) LER 05000397/2003009-00: Reactor Core Isolation Cooling Rendered

Inoperable due to a 250VDC Battery Cell not meeting TS Requirements.

The inspectors reviewed LER 2003009-00 to determine if there were any identified

violations or aspects of human performance associated with the LER. See

Section 4OA7.2 for an associated Energy Northwest identified violation.

.7

(Closed) LER 05000397/2003010-00: Unanticipated inoperability of the high pressure

core spray system due to isolation valve leakage while the system was isolated.

The inspectors reviewed LER 2003010-00 to determine if there were any identified

violations or aspects of human performance associated with the LER. This event did

not constitute a violation of NRC requirements. Energy Northwest entered this condition

into the corrective action program as Problem Evaluation Request 203-3684.

4OA4 Crosscutting Aspects of Findings

A human performance cross cutting aspect was identified when the control room staff

failed to identify that APRM B was bypassed and out of service during a shift turnover

and did not identify the condition until several hours later even though there were control

board indications which clearly indicated the bypassed condition. Additionally, a senior

reactor operator signed an associated surveillance procedure for closure when he failed

to recognize that an initial block indicating the return to service of APRM B was not

initialed (Section 1R22).

Two examples with human performance cross-cutting aspects were identified which

involved failures to survey (Section 2OS2 ).

A human performance aspect was identified when reactor operators failed to adequately

monitor hotwell level after raising hotwell level above the hotwell high alarm setpoint

(Section 4OA3.2).

A human performance aspect was identified when an equipment operator failed to follow

a clearance order which resulted in a low suction trip of the running reactor feedwater

pump and a subsequent loss of reactor feedwater and manual trip of the reactor

(Section 4OA3.3).

-27-

Enclosure

4OA5 OTHER

.1

Temporary Instruction (TI) 2515/154, Spent Fuel Material Control and Accounting

at Nuclear Power Plants

The inspectors collected the data specified in Phases I and II of the TI. The data was

forwarded to the individuals identified in the TI, for consolidation and assessment.

.2

Retraction of Two Safety System Functional Failure Performance Indicators

On May 26, 2004, Energy Northwest informed the NRC that the reporting basis for two

LERs (LER 50-397/2003-003-00 and LER 50-397/2003-005-00) had been changed from

reportable per 10 CFR 50.73(a)(2)(v) to voluntary. Both LERs involved the interruption

of flow in the residual heat removal system while in the shutdown cooling mode of

operation. Additionally, both events were reported in 3rd quarter 2003 as mitigating

systems performance indicator safety system function failures. 10 CFR 50.72(a)(2)(v)(B) required to report any event or condition that could have prevented the

fulfillment of the safety function of structures or systems that are needed to remove

residual heat. Following the reclassification of the LERs to voluntary, Energy

Northwest retracted both issues from the safety system functional failure performance

indicator in the 3rd quarter, 2004. The NRC is evaluating the acceptability of Energy

Northwest not reporting both loss of shutdown cooling events as failures to fulfill a safety

function per 50.72(a)(V)(B) and the subsequent retraction of both events from the safety

system function failure performance indicator. Pending completion of the NRCs

evaluation, this issue will be characterized as an Unresolved Item (URI 50-397/04-04-

07, Retraction of Two Loss of Shutdown Cooling Events from SSFF Performance

Indicator).

4OA6 Meetings, Including Exit

Resident Inspector Routine Exit Summary

The inspectors presented the emergency preparedness exercise inspection results to

Mr. V. Parrish, Chief Executive Officer, and members of his staff at the conclusion of the

inspection on September 3, 2004. Energy Northwest acknowledged the findings

presented.

On September 30, 2004, the resident inspectors presented the inspection results to

Mr. D. K. Atkinson, Vice President, Technical Services, and other members of his staff

who acknowledged the findings.

On October 2, 2004, the inspectors presented the inspection results to Mr. V. Parrish,

Chief Executive Officer, and other members of his staff who acknowledged the findings.

A subsequent discussion was conducted on October 4, 2004, by telephone with

Mr. D. Coleman, Manager, Performance Assessment and Regulatory Programs and

other members of the staff.

-28-

Enclosure

The inspectors telephonically presented the inspection results to Mr. Doug Coleman,

Manager, Regulatory Programs, and other members of licensee staff on

October 8, 2004.

The inspectors verified no proprietary information was discussed during any of the

inspection exits.

4OA7 Energy Northwest Identified Violations

The following violations of very low risk significance (Green) were identified by Energy

Northwest and are violations of NRC requirements which meet the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as noncited

violations.

Cornerstone: Mitigating Systems

.1

Energy Northwest identified a violation of Technical Specifications 3.6.1.8, Main Steam

Isolation Valve Leakage Control System (MSLC), which required that one MSLC

subsystem may be inoperable for 30 days. If the MSLC train is not returned to service

within that time, then to be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Energy Northwest reported the

problem to the NRC via Licensee Event Report 50-397/2002-005, Revision 0.

Undersized thermal overload relays had been installed in the Train A main steam

isolation valve leakage control fan motor. As a result of not installing the properly sized

thermal overload relays for the fan, the motor was considered inoperable from May 1991

until December 29, 2002, when the properly sized relays were installed. Corrective

actions included verifying the sizing of relays on other fan motors related to the system

and revised appropriate program procedures and electrical drawings to preclude

recurrence. This finding was of very low risk significance because although it did impact

the barrier cornerstone objective, it did not represent a degradation of the radiological

barrier function provided for the control room, auxiliary building, SFP, or SGT system,

the finding did not represent a degradation of the barrier function of the control room

against smoke or a toxic atmosphere, and the finding did not represent an actual open

pathway in the physical integrity of reactor containment or an actual reduction of the

atmospheric pressure control function of the reactor containment. Energy Northwest

captured this issue in their corrective action program as Problem Evaluation Request

202-3581.

.2

Technical Specification 5.4.1.a required, in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation).

Regulatory Guide 1.33, Appendix A, Section 8.b, required, in part, that specific

procedures for surveillance tests be written for emergency power tests. During a review

of LER 2003-009, which documented an inoperable condition of battery E-B2-1 which

affected battery operability, the inspectors noted that Energy Northwest identified a

violation of Technical Specification 5.4.1.a for inadequate acceptance criteria for battery

cell specific gravity in procedure ESP-B21-Q101. Procedure ESP-B21-Q101, Quarterly

Battery Testing 250 VDC E-B2-1, Revision 5, step 8.14.1, stated that the acceptance

-29-

Enclosure

criteria for the difference in specific gravity for an individual battery cell and the average

of all the connected cells specific gravity be less than or equal to 0.20. However,

Technical Specification 3.8.6, Battery Cell Parameters, required that specific gravity

for an individual cell be not more than 0.020 below the average of all connected cells.

Procedure ESP-B21-Q101 was performed on August 20, 2003. On August 20, 2003,

cell No. 166 specific gravity was measured as greater than 0.020 above the average cell

specific gravity. However, because of the inaccurate acceptance criteria, the out of

specification was not identified until August 22, 2003, during a subsequent review of the

test data. Although the finding affected the mitigating systems cornerstone, it was of

very low safety significance (Green) because the finding: (1) did not result in the loss of

function of a safety system; (2) did not represent an actual loss of a safety function of a

single train for greater than its technical specification allowed outage time; and (3) did

not represent an actual loss of safety function of one or more non-technical specification

trains of equipment designated as risk significant per 10 CFR 50.65 for greater than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Energy Northwest documented this issue in their corrective action program in

PER 203-3125. Corrective actions included revising Procedure ESP-B21-Q101 to

include the correct acceptance criteria and a review of other battery surveillance

procedures to correct any other identified discrepencies.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Energy Northwest

D. Atkinson, Vice President, Technical Services

I. Borland, Manager, Radiation Protection

D. Coleman, Manager, Performance Assessment and Regulatory Programs

D. Dinger, Radiation Protection Manager (Acting)

D. Feldman, System Engineering Manager

B. Gardes, Performance Manager

S. Grundhauser, Maintenance Training Supervisor

M. Humphries, Manager, Engineering

T. Lynch, Manager, Operations

C. Moore, Supervisor, Emergency Preparedness

S. Oxenford, Plant General Manager

V. Parrish, Chief Executive Officer

R. Webring, Vice President Nuclear Generation

NRC Personnel

L. Carson II, Senior Health Physicist

R. Cohen, Resident Inspector

Z. Dunham, Senior Resident Inspector

W. Jones, Chief, Project Branch E

M. Shannon, Chief, Plant Support Branch

ITEMS OPENED AND CLOSED

Items Opened, Closed, and Discussed During this Inspection

Opened

50-397/04-04-03

URI

NRC Review of Performance Issues Associated with the July 30,

2004, Reactor Scram and the Declaration of Alert

(Section 4OA3.1)

50-397/04-04-07

URI

Retraction of Two Loss of Shutdown Cooling Events from SSFF

Performance Indicator (Section 4OA5.2)

Opened and Closed

50-397/04-04-01

NCV

Failure to Identify and Return to Service APRM B in a Timely

Manner (Section 1R22)

50-397/04-04-02

NCV

Two Examples of Failure to Survey (Section 2OS2)

50-397/04-04-04

NCV

Failure to Activate the Emergency Response Data System Within

One Hour (Section 4OA3.1)

A-2

Enclosure

50-397/04-04-05

FIN

Inadequate Monitoring of Hotwell Level Contributes to Loss of

Reactor Feedwater (Section 4OA3.2)

50-397/04-04-06

FIN

Failure to Follow Clearance Order Instruction Results in Loss of

Reactor Feedwater (Section 4OA3.3)

Closed

50-397/2002005-00

LER

Main Steam Leakage Control Fan potentially inoperable during a

design basis accident due to undersized thermal overloads.

(Section 4OA3.5)

50-397/2003009-00

LER

Reactor Core Isolation Cooling Rendered Inoperable due to a

250VDC Battery Cell not meeting TS Requirements. (Section

4OA3.6)

50-397/2003010-00

LER

Unanticipated inoperability of the high pressure core spray system

due to isolation valve leakage while the system was isolated.

(Section 4OA3.7)

Discussed

None

PARTIAL LIST OF DOCUMENTS REVIEWED

Procedures

PPM 8.4.63; Thermal Performance Monitoring of DCW-HX-1C; June 23, 2004

PPM 1.5.14; Risk Assessment and Management for Maintenance/Surveillance Activities;

Revision 13

ISP-RHR-X304; ECCS-LPCI (B&C) Pump Discharge Low (Min Flow) - CC; Revision 0

PPM 10.24.234; I&C Removal/Reinstallation of IRM/SRM Detectors

ISP-IRM-X306; Intermediate Range Monitor Channel F Calibration; Revision 8

ISP-IRM-W402; Intermediate Range Monitors - Channels B, D, F & H - CFT; Revision 8

OSP-RCIC/IST-Q701; RCIC Operability Test; Revision 28

ISP-LPCS/RHR-Q901; RHR A & LPCS Discharge Pressure - ADS Trip System A Permissive

(By K10A Relay) - CFT/CC; Revision 7

TSP-APRM-C301; APRM and Core Thermal Power Channel Calibration Check; Revision 4

OSP-LPCS/IST-Q702; LPCS System Operability Test; Revision 12

ESP-MSIV-B301; MSIV Closure Limit Switches - CC; Revision 0

-3-

A-3

Enclosure

General Operating Procedure 3.1.1, "Plant Startup," Revision 32

Site-Wide Procedure SWP-OPS-05, Restart Evaluation Process, Revision 1

Operating Instruction OI-004-000, Operation Shift Logs, Revision 28

Administrative Procedure 1.5.14, Risk Assessment and Management for

Maintenance/Surveillance Activities, Revision 13

Administrative Procedure 1.3.5, Reactor Trip Report, Revision 17

OSP-RHR/IST-Q704, RHR Loop C Operability Test, Revision 14

Calculations

Calculation 216-92-057; Weaklink Analysis for Valve No. MS-V-146 and RFW-V-65A,B (Velan

24" 900# Gate Valves); Revision 1

Drawing M551; Flow Diagram HVAC Circ. & M/U Water, S.W. & Diesel Generator Bldg.;

Revision 55

Drawings

ME-02-02-43; Room Temperature Calculation for DG Building, Reactor Building, Radwaste

Building and Service Water Pumphouse Under Design Basis Accident Conditions; Revision 7

Drawing M-519, "Flow Diagram Reactor Core Isolation Cooling System" Revision 86

Other

Technical Specification 3.5, ECCS and RCIC, Revision No. 38

Final Safety Analysis Report Chapter 5.4, Component and Subsystem Design

WO 0108554; RFW-V-65A Electrically Backseat Per System Engineers Direction; August 27,

2004

WO 01082365; RHR-FIS-10B Replacement; June 30, 2004

WO 01062381; Replace IRM-DET-2F; August 18, 2004

WO 01060822; MS-V-22D Disassemble and Reassemble

WO 01077279; MS-V-28D Disassemble and Reassemble

WO 01079061; RCIC-P-1 Change Bearing Housing Oil

FO-04-01 Shutdown Safety Plan

PMR-02-86-0305, Rod Position Information System

-4-

A-4

Enclosure

General Electric Services Information Letter Number 532, Full in Control Rod Position

Indication, dated March 27,1991

Work Request 29032502

Work Order 01077952

PERs / Condition Reports

PER 204-0628; E-IN-3A was running, for testing, in parallel with E-IN-3B which could cause an

overload condition o the Div 1 125 VDC system; March 10, 2004

PER 204-0935; During the performance of PPM 2.10.4 in response to high temps in the DG

rooms, several discrepancies were found on the position of dampers; July 19, 2004

CR 2-04-01508; In 1995 an incorrect stem diameter was applied during diagnostic testing of

MSLC-V-1D. Actual thrust/torque is greater than recorded; April 15, 2004

PER 204-1056; During Panel Walkdown to Perform TSP-APRM-C301 Discovered the APRM-

CH-B Bypass Switch in Bypass; August 25, 2004

PER 202-3056

PER 204-0972

PER 203-3111

PER 202-3581

PER 203-3125

Condition Reports

CR-2-04-03321

CR-2-04-00739

CR-2-04-00783

CR-2-04-02214

CR-2-04-03884

CR-2-04-05341

Problem Evaluation Requests

202-3461

203-2370

203-3782

203-0316

203-4200

203-4174

203-4176

203-0950

-5-

A-5

Enclosure

203-3872

Plant Tracking Log

A 207409

A 206232

A 206370

H 194829

A 207162

A 206234

A 206371

H 196658

A 207166

A 206237

A 206372

H 196663

A 216273

A 206369

A 205042

H 196664

Procedures

PPM 1.5.11, Maintenance Rule Program, Revision 6

SWP-CAP-03, Operating Experience Program, Revision 12

PPM 10.25.105, Motor Control Center and Switch Gear Maintenance, Revision 21

TI 4.22, Maintenance Rule Program, Revision 8

Miscellaneous

SA-2003-0044, Maintenance Rule 2003 Self-Assessment, November 25, 2003

Maintenance Rule (a)(1) Systems, as of September 20, 2004

Maintenance Rule Biannual Period Report July-December 2002

Maintenance Rule Biannual Period Report January-June 2003

Maintenance Rule Biannual Period Report July-December 2003

Maintenance Rule Biannual Period Report January-June 2004

Maintenance Rule Open Scoping Issue List

1EP1 Exercise Evaluation (71114.01)

Columbia Generating Station Emergency Plan, Revision 38

Emergency Plan Implementing Procedures (EPIPs):

13.1.1, Classifying the Emergency, Revision 33

13.2.2, Determining Protective Action Recommendations, Revision 15

13.4.1, Emergency Notifications, Revision 30

13.10.2, TSC Manager Duties, Revision 25

13.10.4, Radiological Protection Manager Duties, Revision 28

13.10.9, OSC Manager and Staff Duties, Revision 35

13.11.1, EOF Manger Duties, Revision 33

13.11.7, Radiological Emergency Manager Duties, Revision 28

13.11.10, Security Manager Duties, Revision 25

13.12.19, Joint Information Center Management, Revision 10

August 4, 2004 Drill Report

ERO Team D 2004 Exercise Summary, August 31, 2004, Management Critique

4OA1 Performance Indicators Verification (71151)

-6-

A-6

Enclosure

Emergency Plan Implementing Procedures (EPIPs):

13.14.8, Drill and Exercise Program, Revision 16

13.14.9, Emergency Program Maintenance, Revision 24

Emergency Preparedness Group Instructions (EPIs):

EPI-11, ERO Administration Program, Revision 6

EPI-18, EP NRC Performance Indicators, Revision 8

EPI-21, Drill and Exercise Performance, Revision 6

Section 2OS2: ALARA Planning and Controls (71121.02)

Procedures

GEN-RPP-01

ALARA Program Description, Revision 4

GEN-RPP-02

ALARA Planning and Radiation Work Permits, Revision 8

GEN-RPP-13

ALARA Committee, Revision 3

SWP-RPP-01

Radiation Protection Program, Revision 5

Corrective Action Documents

CR# 2-04-00205, CR# 2-04-01183, CR# 2-04-01941, CR# 2-04-01942, CR# 2-04-02413,

CR# 2-04-02995, CR# 2-04-03190, CR# 2-04-03283, CR# 2-04-03928, PER-203-2908,

PER 203-2913

Audits and Self-Assessments

Qualitys Integrated Performance Assessment Report (July 1, 2003 through October 31, 2003)

SA-2003-0015 Annual Assessment of the Radiation Protection Program (2003)

Continuous Monitoring Reports - December 2003 through January 2004, February 2004,

April 2004

ALARA Work Packages

30001231, 30001216, 30001227

4OA2 Problem Identification and Resolution

Condition Records:

CR 2-04-02187, Timely and accurate notification to the NRC via ENS may be challenged...

CR 2-04-04103, ... ERDS was activated three minutes beyond the one hour requirement ...

CR 2-04-04292, The ALERT declared during the scram event of July 30, 2004 was determined

to be a failed NRC DEP PI...

CR 2-04-04111, An Alert was declared at 1000 on 30 Jul 04."

CR 2-04-04896, SAE declaration untimely

-7-

A-7

Enclosure

CR 2-04-04920, Control Room failed to timely recognize entry conditions for SAE.

Problem Evaluation Requests:

203-3712, 3786, 3921, 3922, 3926, 3971, 3983, 4424

204-0175, 0429, 0645, 0977, 0993