Information Notice 1992-47, Intentional Bypassing of Automatic Actuation of Plant Protective Features
ML031210746 | |
Person / Time | |
---|---|
Issue date: | 06/29/1992 |
From: | Rossi C Office of Nuclear Reactor Regulation |
To: | |
References | |
IN-92-047, NUDOCS 9206230193 | |
Download: ML031210746 (10) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555 June 29, 1992 NRC INFORMATION NOTICE 92-47:
INTENT
IONAL BYPASSING OF AUTOMATIC
ACTUATION OF PLANT PROTECTIVE FEATURES
Addressees
power
All holders of operating licenses or construction permits for nuclear
reactors.
Purpose
information
The U.S. Nuclear Regulatory Commission (NRC) is issuing this criteria and
notice to alert licensees to the importance of having formal
features. It is
training regarding limitations on bypassing plant protective to
expected that recipients will review the information for applicability
to avoid similar
their facilities and consider actions, as appropriate, notice are not
problems. However, suggestions contained in this information is
NRC requirements; therefore, no specific action or written response
required.
Description of Circumstances
River Nuclear
On December 8, 1991, the Florida Power Corporation's Crystal system (RCS)
Station, Unit 3, experienced a slow loss of reactor coolant
spray valve
pressure at 10 percent power during startup, because a pressurizer determine
did not promptly
failed in a partially open position. The operators misled by an
the cause of the pressure decrease, in part, because they were
Believing the pressure
erroneous spray valve closed position indication. subsequently
decrease to result from an increasing steam demand, the operators RCS temperature
withdrew control rods several times in an attempt to maintain
as steam flow was increased in preparation for loading the generator.
tripped on
However, the RCS pressure continued to decrease, and the reactor B Not Bypassed"
low pressure. Approximately 2 minutes later, the "ES A and
that the high pressure injection
alarms annunciated. These alarms indicate are not blocked, (HPI) system and other engineered safeguards (ES) functions
plant cooldown. Approximately 1 although they may be blocked during normal the ES bypass
minute later, a control room operator inappropriately actuated
later, when a
switches for the A and B HPI system. Approximately 6 minutes the system
sufficient number of actuation logic bistables tripped to actuate
Operations Superintendent questioned
if it had not been bypassed, the Acting and the ES
of bypassing the ES,
the Shift Supervisor about the advisability and other
was then unbypassed at which time the high pressure injection
of the high
systems activated. Operators then established manual control
9206230193 z2r
IN 92-47 June 29, 1992 pressure injection system to maintain RCS pressure above 1500 psig.
operators did not determine the cause of the decrease in RCS pressure The
after the spray line isolation valve was closed about an hour later. until
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, (TMI-2)
accident was that the core damage resulted from operators manually terminating
safety injection based on an inaccurate diagnosis of plant conditions.
1979, the NRC issued a series of Bulletins requesting licensees to reviewIn
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions.
the accident at TMI-2, licensees made many enhancements to emergency After
procedures to improve the operator's control of safety functions and operating
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance delineating
limitations on bypassing the automatic actuation of engineered safeguards
functions. This lack of guidance may have contributed to having high
pressure
injection bypassed with the plant in a degraded condition for approximately
6 minutes without understanding the cause of the decrease in RCS pressure.
One of the licensee's corrective actions was to develop administrative
guidance on when it is appropriate to bypass the automatic actuation
engineered safeguards functions. This guidance has been incorporatedof
plant procedures.- into
-_
This information notice requires no specific action or written response.
you have any questions about the information in this notice, please If
the technical contact listed below or the appropriate Office of Nuclearcontact
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Attachment
IN 92-47 June 29, 1992 Page 1 of I
LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date of
Notice No. Subject Issuance Issued to
92-46 Thermo-Lag Fire Barrier 06/23/92 All holders of OLs or CPs
Material Special Review for nuclear power reactors.
Team Final Report Findings, Current Fire Endurance
Tests, and Ampacity Cal- culation Errors
92-45 Incorrect Relay Used in 06/22/92 All holders of OLs or CPs
Emergency Diesel Generator for nuclear power reactors.
Output Breaker Control
Circuitry
92-44 Problems with Westing- 06/18/92 All holders of OLs or CPs
house DS-206 and DSL-206 for nuclear power reactors.
Type Circuit Breakers
92-43 Defective Molded Phen- 06/09/92 All holders of OLs or CPs
olic Armature Carriers for nuclear power reactors.
Found on Elmwood Con- tactors
92-42 Fraudulent Bolts in 06/01/92 All holders of OLs or CPs
Seismically Designed for nuclear power reactors.
Walls
92-41 Consideration of the 05/29/92 All holders of OLs or CPs
Stem Rejection Load in for nuclear power reactors.
Calculation of Required
Valve Thrust
92-40 Inadequate Testing of 05/27/92 All holders of OLs or CPs
Emergency Bus Under- for nuclear power reactors.
voltage Logic Circuitry
92-39 Unplanned Return to 05/13/92 All holders of OLs or CPs
Criticality during for nuclear power reactors.
Reactor Shutdown
OL = Operating License
CP = Construction Permit
IN 92-47 June 29, 1992 pressure injection system to maintain RCS pressure above 1500 psig. The
operators did not determine the cause of the decrease in RCS pressure until
after the spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, (TMI-2)
accident was that the core damage resulted from operators manually terminating
safety injection based on an Inaccurate diagnosis of plant conditions. In
1979, the NRC issued a series of Bulletins requesting licensees to review
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions. After
the accident at TMI-2, licensees made many enhancements to emergency operating
procedures to improve the operator's control of safety functions and
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance delineating
limitations on bypassing the automatic actuation of engineered safeguards
functions. This lack of guidance may have contributed to having high pressure
injection bypassed with the plant in a degraded condition for approximately
6 minutes without understanding the cause of the decrease in RCS pressure.
One of the licensee's corrective actions was to develop administrative
guidance on when it is appropriate to bypass the automatic actuation of
engineered safeguards functions. This guidance has been incorporated into
plant procedures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager. Original Signed by
OZ411 E.RoWd
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992.
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR ADM:RPB SC/OEAB:DOEA:NRR C/OEAB:DOEA:NRR
TKoshy* JMaln* DFischer* AChaffee*
05/20/92 05/27/92 05/20/92 05/20/92 RII D/DSP:AEOD C/OGCB:DOEA:NRR D
LReyes* TNovak* CBerlinger* ,CC~oriP*.
05/26/92 05/26/92 05/28/92 '-8 Document Name: 92-47.IN
I I
IN 92-XX
May xx, 1992 then established manual control of the high pressure injection system to
maintain RCS pressure above 1500 psig. The operators did not determine the
cause of the decrease in RCS pressure until after the spray line isolation
valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2 (TMI-2),
accident was that the core damage resulted from operators manually terminating
safety injection based on an inaccurate diagnosis of plant conditions. In
1979, the NRC issued a series of Bulletins to direct licensees to review
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions. After
the accident at TMI-2, the licensees made many enhancements to emergency
operating procedures to improve the operator's control of safety functions and
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions
that permit bypassing the automatic actuation of engineered safeguards
functions. This lack of guidance may have contributed to having high pressure
injection bypassed with the plant in a degraded condition for approximately 6 minutes without having specific procedural guidance or appropriate management
involvement. One of the licensee's corrective actions was to develop
administrative guidance on when it is appropriate to bypass the automatic
actuation of engineered safeguards functions. This guidance has been
incorporated into plant procedures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992.
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR ADM:RPB SC/OEAB:DOEA:NRR C/OEAB:DOEA:NRR
TKoshy* JMain* DFischer* AChaffee*
05/20/92 05/27/92 05/20 92 05/20/92 RII D/DSP:AEOD C/ECB: A D/DOEA
LReyes* TNovak* CBerlj9nger CRossi
05/26/92 05/26/92 6/ /92 / /92 Document Name: C:\BYPASS1 (ATB)
r I ,
IN 92-XX
May xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, accident was
that the core damage was a result of operators manually terminating safety
injection based on an inaccurate diagnosis of existing plant conditions. A
series of NRC Bulletins was issued in 1979, that directed licensees, in
general, to review operating procedures and training to ensure that operators
do not override automatic ESF actuation without careful review of plant
conditions. Many post-TMI enhancements were made to emergency operating
procedures to improve operator control of safety functions and engineered
safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions
that permit bypassing automatic actuation of engineered safeguards functions.
This lack of guidance may have contributed to having high pressure injection
bypassed with the plant in a degraded condition for approximately six minutes
without having specific procedural guidance or appropriate management
involvement. One of the licensee's corrective actions was to develop
administrative guidance on when it is appropriate to bypass automatic
actuation of engineered safeguards functions. This guidance has been, or will
be, incorporated into plant procedures as appropriate.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992. t C.t
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR ADM:RPB SC/OEAB:DOEA:NRR C/OEAB:DOEA:NRR RII
TKoshy* JMain q DFischer* AChaffee* LReyes
O , 5/27/92 05/20/92 05/20/92 5/2L/92 D/DSP:AEOD C/OGCB:DG EA:NRR D/DOEA
TNovak CBerlingeer CRossi
5/x6 /92 / /92 / /92 Document Name: C:\BYPASS1 (ATB)
I
- IN 92-XX
May xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, accident was
that the core damage was a result of operators manually terminating safety
injection based on an inaccurate diagnosis of existing plant conditions. A
series of NRC Bulletins was issued in 1979, that directed licensees, in
general, to review operating procedures and training to ensure that operators
do not override automatic ESF actuation without careful review of plant
conditions. Many post-TMI enhancements were made to emergency operating
procedures to improve operator control of safety functions and engineered
safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions that
permit bypassing automatic actuation of engineered safeguards functions. This
lack of guidance may have contributed to having high pressure injection bypassed
with the plant in a degraded condition for approximately six minutes without
having specific procedural guidance or appropriate management involvement. One
of the licensee's corrective actions was to develop administrative guidance on
when it is appropriate to bypass automatic actuation of engineered safeguards
functions. This guidance has, or will be, incorporated into plant procedures
as appropriate.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated April 28, 1992.
rN Vo*. AsL
OEAB:DOEA:NRR SCItVAB:DOEA:NRR C B:DOEA:NRR RII
TKoshy g DFischer AChaffee LReyes
5T Ao/92 K' /z/92 S/zVo/92 / /92 D/DSP:AEOD C/OGCB:DOEA:NRR D/DOEA
TNovak CBerlinger CRossi
/ /92 / /92 / /92 Document Name: IN ECCS/KOSHY DUP 2
rrI
IN 92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
On April 20, 1992, Commonwealth Edison Company's LaSalle County Station, Unit
2, was shutting down the reactor water cleanup (RWCU) system to support
testing of isolation valves when a relief valve on the RWCU heat exchanger
opened causing high delta flow alarms and actuation of the isolation logic
(isolates the RWCU system after a 45 second time delay). Assuming the alarms
to be spurious, a reactor operator bypassed automatic isolation of the RWCU
system before understanding the cause of the isolation signal. The licensee's
corrective actions in response to this event are being developed.
Discussion
At Crystal River, the licensee's staff lacked formal guidance on conditions that
permit bypassing automatic actuation of engineered safeguards functions. This
lack of guidance may have contributed to having high pressure injection bypassed
with the plant in a degraded condition for approximately six minutes without
having specific procedural guidance or appropriate management involvement. One
of the licensee's corrective actions was to develop administrative guidance on
when it is appropriate to bypass automatic actuation of engineered safeguards
functions. This guidance has, or will be, incorporated into plant procedures
as appropriate.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92
- SEE PREVIOUS CONCURRENCE
OFC :DOEA:OEAB :SC:DOEA:OEAB:C:DLPQ:LOLB :C:DLPQ:LHFB :C:DST:SRXB :C:DOEA:OEAB
____
____________ ____________ ____________ ---------
NAME :TKoshy* :DFischer* :RGallo* :JWermiel* :RJones* :AChaffee* :
DATE :04/23/92 :04/23/92 :04/24/92 :04/23/92 :04/24/92 :04/23/92 :
OFC :C:DOEA:OGCB :D:DOEA
NAME :CBerlinger :CRossi : :
DATE: / /92 : / /92 : : : :
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OFFL~LAL Ducument Name: IN EUUZ/OSHT Dur 2
IN 92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
The licensee's staff lacked formal guidance on conditions that permit bypassing
automatic actuation of engineered safeguards functions. This lack of guidance
may have contributed to having high pressure injection bypassed with the plant
in a degraded condition for approximately six minutes without having specific
procedural guidance or appropriate management involvement. One of the licensee's
corrective actions was to develop administrative guidance on when it is appro- priate to bypass automatic actuation of engineered safeguards functions.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92
- SEE PREVIOUS CONCURRENCE
OFC :DOEA:OEAB :SC:DOEA:OEAB:.C;LPQ:LOLB :C:DLPQ :LHFB :C:DST:SRXB :C:DOEA:OEAB
NAME :TKoshy* :DFischer* :Ruani'¶o :JWermi 6 :RJones* :AChaffee*
_ - _ - --_ ___- - _____
- - - -- - - - - ---------
DATE :04/23/92 :04/23/92 : t/./92 :¶P/93/92 :04/24/92 :04/23/92 :
OFC :C:DOEA:OGCB :D:DOEA :
NAME :CBerlinger :CRossi : :
DATE: / /92 : / /92 : : :
OFFICIAL RECORD COPY
Document Name: IN ECCS/KOSHY DUP 2
--IN 92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
The licensee's staff lacked formal guidance on conditions that permit bypassing
automatic actuation of engineered safeguards functions. This lack of guidance
led to having high pressure injection bypassed with the plant in a degraded
condition for approximately six minutes without having specific procedural
guidance or appropriate management involvement. One of the licensee's correc- tive actions was to develop administrative guidance on when it is appropriate
to bypass automatic actuation of engineered safeguards functions.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92 OFC :DO A:OEAB
NAME :TKoshy :DFischer :RGallo
-:------------
- SC:DOEA:OEAB:C:DLPQ:LOLB :C:DLPQ:LHFB :C:DST:SRXB
- JWermiel :RJones
- C:DOEA:OEAB :
LA ---: _ A L-
- AChaffee
--- -- ---
DATE : ,/Is/92 : y/z/92 : / /92 : / /92 : A/a192 :4/Y92 :
OFC :C:DOEA:OGCB :D:DOEA
NAME :CBerlinger :CRossi : :
DATE: //92 :/ /92 : :
OFFICIAL RECORD COPY
Document Name: IN ECCS/KOSHY DUP 2