Information Notice 1992-47, Intentional Bypassing of Automatic Actuation of Plant Protective Features
| ML031210746 | |
| Person / Time | |
|---|---|
| Issue date: | 06/29/1992 |
| From: | Rossi C Office of Nuclear Reactor Regulation |
| To: | |
| References | |
| IN-92-047, NUDOCS 9206230193 | |
| Download: ML031210746 (10) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C.
20555
June 29, 1992
INTENT
IONAL BYPASSING OF AUTOMATIC
ACTUATION OF PLANT PROTECTIVE FEATURES
Addressees
All holders of operating licenses or construction permits for nuclear power
reactors.
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert licensees to the importance of having formal criteria and
training regarding limitations on bypassing plant protective features. It is
expected that recipients will review the information for applicability to
their facilities and consider actions, as appropriate, to avoid similar
problems. However, suggestions contained in this information notice are not
NRC requirements; therefore, no specific action or written response is
required.
Description of Circumstances
On December 8, 1991, the Florida Power Corporation's Crystal River Nuclear
Station, Unit 3, experienced a slow loss of reactor coolant system (RCS)
pressure at 10 percent power during startup, because a pressurizer spray valve
failed in a partially open position. The operators did not promptly determine
the cause of the pressure decrease, in part, because they were misled by an
erroneous spray valve closed position indication. Believing the pressure
decrease to result from an increasing steam demand, the operators subsequently
withdrew control rods several times in an attempt to maintain RCS temperature
as steam flow was increased in preparation for loading the generator.
However, the RCS pressure continued to decrease, and the reactor tripped on
low pressure. Approximately 2 minutes later, the "ES A and B Not Bypassed"
alarms annunciated. These alarms indicate that the high pressure injection
(HPI) system and other engineered safeguards (ES) functions are not blocked, although they may be blocked during normal plant cooldown. Approximately 1 minute later, a control room operator inappropriately actuated the ES bypass
switches for the A and B HPI system. Approximately 6 minutes later, when a
sufficient number of actuation logic bistables tripped to actuate the system
if it had not been bypassed, the Acting Operations Superintendent questioned
the Shift Supervisor about the advisability of bypassing the ES, and the ES
was then unbypassed at which time the high pressure injection and other
systems activated. Operators then established manual control of the high
9206230193 z2r
IN 92-47 June 29, 1992 pressure injection system to maintain RCS pressure above 1500 psig.
The
operators did not determine the cause of the decrease in RCS pressure until
after the spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, (TMI-2)
accident was that the core damage resulted from operators manually terminating
safety injection based on an inaccurate diagnosis of plant conditions.
In
1979, the NRC issued a series of Bulletins requesting licensees to review
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions. After
the accident at TMI-2, licensees made many enhancements to emergency operating
procedures to improve the operator's control of safety functions and
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance delineating
limitations on bypassing the automatic actuation of engineered safeguards
functions.
This lack of guidance may have contributed to having high pressure
injection bypassed with the plant in a degraded condition for approximately
6 minutes without understanding the cause of the decrease in RCS pressure.
One of the licensee's corrective actions was to develop administrative
guidance on when it is appropriate to bypass the automatic actuation of
engineered safeguards functions.
This guidance has been
incorporated into
plant procedures.-
-_
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact:
Thomas Koshy, NRR
(301) 504-1176 Attachment:
List of Recently Issued NRC Information Notices
Attachment
June 29, 1992
Page 1 of I
LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information
Date of
Notice No.
Subject
Issuance
Issued to
92-46
92-45
92-44
92-43 Thermo-Lag Fire Barrier
Material Special Review
Team Final Report Findings,
Current Fire Endurance
Tests, and Ampacity Cal- culation Errors
Incorrect Relay Used in
Output Breaker Control
Circuitry
Problems with Westing- house DS-206 and DSL-206
Type Circuit Breakers
Defective Molded Phen- olic Armature Carriers
Found on Elmwood Con- tactors
Fraudulent Bolts in
Seismically Designed
Walls
Consideration of the
Stem Rejection Load in
Calculation of Required
Valve Thrust
Inadequate Testing of
Emergency Bus Under- voltage Logic Circuitry
Unplanned Return to
Criticality during
Reactor Shutdown
06/23/92
06/22/92
06/18/92
06/09/92
06/01/92
05/29/92
05/27/92
05/13/92
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
All holders of OLs or CPs
for nuclear power reactors.
92-42
92-41
92-40
92-39 OL = Operating License
CP = Construction Permit
IN 92-47 June 29, 1992 pressure injection system to maintain RCS pressure above 1500 psig.
The
operators did not determine the cause of the decrease in RCS pressure until
after the spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, (TMI-2)
accident was that the core damage resulted from operators manually terminating
safety injection based on an Inaccurate diagnosis of plant conditions. In
1979, the NRC issued a series of Bulletins requesting licensees to review
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions.
After
the accident at TMI-2, licensees made many enhancements to emergency operating
procedures to improve the operator's control of safety functions and
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance delineating
limitations on bypassing the automatic actuation of engineered safeguards
functions.
This lack of guidance may have contributed to having high pressure
injection bypassed with the plant in a degraded condition for approximately
6 minutes without understanding the cause of the decrease in RCS pressure.
One of the licensee's corrective actions was to develop administrative
guidance on when it is appropriate to bypass the automatic actuation of
engineered safeguards functions. This guidance has been
incorporated into
plant procedures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Original Signed by
OZ411 E. RoWd
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact:
Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992.
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR
ADM:RPB
SC/OEAB:DOEA:NRR
C/OEAB:DOEA:NRR
TKoshy*
JMaln*
DFischer*
AChaffee*
05/20/92
05/27/92
05/20/92
05/20/92 RII
D/DSP:AEOD
C/OGCB:DOEA:NRR
D
LReyes*
TNovak*
CBerlinger*
,CC~oriP*.
05/26/92
05/26/92
05/28/92
'-8 Document Name: 92-47.IN
I
I
IN 92-XX
May xx, 1992 then established manual control of the high pressure injection system to
maintain RCS pressure above 1500 psig.
The operators did not determine the
cause of the decrease in RCS pressure until after the spray line isolation
valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2 (TMI-2),
accident was that the core damage resulted from operators manually terminating
safety injection based on an inaccurate diagnosis of plant conditions. In
1979, the NRC issued a series of Bulletins to direct licensees to review
operating procedures and training to ensure that operators do not override
automatic ESF actuation without carefully reviewing plant conditions.
After
the accident at TMI-2, the licensees made many enhancements to emergency
operating procedures to improve the operator's control of safety functions and
engineered safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions
that permit bypassing the automatic actuation of engineered safeguards
functions.
This lack of guidance may have contributed to having high pressure
injection bypassed with the plant in a degraded condition for approximately 6 minutes without having specific procedural guidance or appropriate management
involvement.
One of the licensee's corrective actions was to develop
administrative guidance on when it is appropriate to bypass the automatic
actuation of engineered safeguards functions. This guidance has been
incorporated into plant procedures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact:
Thomas Koshy, NRR
(301) 504-1176 Attachment:
List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992.
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR
ADM:RPB
SC/OEAB:DOEA:NRR
C/OEAB:DOEA:NRR
TKoshy*
JMain*
DFischer*
AChaffee*
05/20/92
05/27/92
05/20 92
05/20/92 RII
D/DSP:AEOD
C/ECB:
A
D/DOEA
LReyes*
TNovak*
CBerlj9nger
CRossi
05/26/92
05/26/92
6/ /92
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IN 92-XX
May xx, 1992 injection system to maintain RCS pressure above 1500 psig.
decrease in RCS pressure remained unknown to the operators
spray line isolation valve was closed about an hour later.
The cause of the
until after the
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, accident was
that the core damage was a result of operators manually terminating safety
injection based on an inaccurate diagnosis of existing plant conditions. A
series of NRC Bulletins was issued in 1979, that directed licensees, in
general, to review operating procedures and training to ensure that operators
do not override automatic ESF actuation without careful review of plant
conditions. Many post-TMI enhancements were made to emergency operating
procedures to improve operator control of safety functions and engineered
safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions
that permit bypassing automatic actuation of engineered safeguards functions.
This lack of guidance may have contributed to having high pressure injection
bypassed with the plant in a degraded condition for approximately six minutes
without having specific procedural guidance or appropriate management
involvement.
One of the licensee's corrective actions was to develop
administrative guidance on when it is appropriate to bypass automatic
actuation of engineered safeguards functions. This guidance has been, or will
be, incorporated into plant procedures as appropriate.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact:
Thomas Koshy, NRR
(301) 504-1176 Attachment:
List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated
April 28, 1992.
t C.t
- SEE PREVIOUS CONCURRENCE
OEAB:DOEA:NRR
ADM:RPB
TKoshy*
JMain q
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5/27/92 D/DSP:AEOD
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05/20/92 C/OEAB:DOEA:NRR
AChaffee*
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D/DOEA
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C:\\BYPASS1 (ATB)
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IN 92-XX
May xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
One of the significant lessons of the Three Mile Island, Unit 2, accident was
that the core damage was a result of operators manually terminating safety
injection based on an inaccurate diagnosis of existing plant conditions. A
series of NRC Bulletins was issued in 1979, that directed licensees, in
general, to review operating procedures and training to ensure that operators
do not override automatic ESF actuation without careful review of plant
conditions. Many post-TMI enhancements were made to emergency operating
procedures to improve operator control of safety functions and engineered
safety features.
At Crystal River, the licensee's staff lacked formal guidance on conditions that
permit bypassing automatic actuation of engineered safeguards functions. This
lack of guidance may have contributed to having high pressure injection bypassed
with the plant in a degraded condition for approximately six minutes without
having specific procedural guidance or appropriate management involvement.
One
of the licensee's corrective actions was to develop administrative guidance on
when it is appropriate to bypass automatic actuation of engineered safeguards
functions. This guidance has, or will be, incorporated into plant procedures
as appropriate.
This information notice requires no specific action or written response.
If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
The designated personnel in the Human Factors Assessment Branch, Operator
Licensing Branch, and Reactor Systems Branch concurred in the draft attached
to the memorandum from William T. Russell to Edward L. Jordan dated April 28, 1992.
rN
Vo*. As L
OEAB:DOEA:NRR
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IN ECCS/KOSHY DUP 2
rrI
IN 92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
On April 20, 1992, Commonwealth Edison Company's LaSalle County Station, Unit
2, was shutting down the reactor water cleanup (RWCU) system to support
testing of isolation valves when a relief valve on the RWCU heat exchanger
opened causing high delta flow alarms and actuation of the isolation logic
(isolates the RWCU system after a 45 second time delay).
Assuming the alarms
to be spurious, a reactor operator bypassed automatic isolation of the RWCU
system before understanding the cause of the isolation signal.
The licensee's
corrective actions in response to this event are being developed.
Discussion
At Crystal River, the licensee's staff lacked formal guidance on conditions that
permit bypassing automatic actuation of engineered safeguards functions. This
lack of guidance may have contributed to having high pressure injection bypassed
with the plant in a degraded condition for approximately six minutes without
having specific procedural guidance or appropriate management involvement. One
of the licensee's corrective actions was to develop administrative guidance on
when it is appropriate to bypass automatic actuation of engineered safeguards
functions.
This guidance has, or will be, incorporated into plant procedures
as appropriate.
This information notice requires no specific action or written response.
If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92
- SEE PREVIOUS CONCURRENCE
OFC :DOEA:OEAB
- SC:DOEA:OEAB:C:DLPQ:LOLB :C:DLPQ:LHFB :C:DST:SRXB :C:DOEA:OEAB
____
____________
____________
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NAME :TKoshy*
- DFischer*
- RGallo*
- JWermiel*
- RJones*
- AChaffee*
DATE :04/23/92
- 04/23/92
- 04/24/92
- 04/23/92
- 04/24/92
- 04/23/92
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IN 92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
The licensee's staff lacked formal guidance on conditions that permit bypassing
automatic actuation of engineered safeguards functions. This lack of guidance
may have contributed to having high pressure injection bypassed with the plant
in a degraded condition for approximately six minutes without having specific
procedural guidance or appropriate management involvement. One of the licensee's
corrective actions was to develop administrative guidance on when it is appro- priate to bypass automatic actuation of engineered safeguards functions.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment: List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92
- SEE PREVIOUS CONCURRENCE
OFC :DOEA:OEAB
- SC:DOEA:OEAB:.C;LPQ:LOLB :C:DLPQ :LHFB :C:DST:SRXB :C:DOEA:OEAB
NAME :TKoshy*
- DFischer*
- Ruani'¶o
- JWermi 6
- RJones*
- AChaffee*
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_____
DATE :04/23/92
- 04/23/92
- t/./92
- ¶P/93/92
- 04/24/92
- 04/23/92
OFC
- C:DOEA:OGCB :D:DOEA
NAME :CBerlinger :CRossi
DATE: /
/92
- /
/92
OFFICIAL RECORD COPY
Document Name: IN ECCS/KOSHY DUP 2
--IN
92-XX
April xx, 1992 injection system to maintain RCS pressure above 1500 psig. The cause of the
decrease in RCS pressure remained unknown to the operators until after the
spray line isolation valve was closed about an hour later.
Discussion
The licensee's staff lacked formal guidance on conditions that permit bypassing
automatic actuation of engineered safeguards functions. This lack of guidance
led to having high pressure injection bypassed with the plant in a degraded
condition for approximately six minutes without having specific procedural
guidance or appropriate management involvement. One of the licensee's correc- tive actions was to develop administrative guidance on when it is appropriate
to bypass automatic actuation of engineered safeguards functions.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contact: Thomas Koshy, NRR
(301) 504-1176 Attachment:
List of Recently Issued NRC Information Notices
Reviewed by Technical Editor, J. Main, on 02/24/92 OFC
- DO A:OEAB
- SC:DOEA:OEAB:C:DLPQ:LOLB :C:DLPQ:LHFB :C:DST:SRXB :C:DOEA:OEAB :
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NAME :TKoshy
- DFischer
- RGallo
- JWermiel
- RJones
- AChaffee
DATE : ,/Is/92
- y/z/92
- /
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- /
/92
- A/a192
- 4/Y92
OFC
- C:DOEA:OGCB :D:DOEA
NAME :CBerlinger
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DATE: //92
- /
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OFFICIAL RECORD COPY
Document Name:
IN ECCS/KOSHY DUP 2