Potential Common-Mode Post-Accident Failure of Containment CoolersML031060112 |
Person / Time |
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Site: |
Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant ![Entergy icon.png](/w/images/7/79/Entergy_icon.png) |
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Issue date: |
08/12/1996 |
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From: |
Grimes B Office of Nuclear Reactor Regulation |
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To: |
|
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References |
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IN-96-045, NUDOCS 9608090031 |
Download: ML031060112 (10) |
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Similar Documents at Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination 2020-09-03 The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>.
[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>. |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, DC 20555-0001 August 12, 1996 NRC INFORMATION NOTICE 96-45: POTENTIAL COMMON-MODE POST-ACCIDENT FAILURE OF
CONTAINMENT COOLERS
Addressees
All holders of operating licenses or construction permits for nuclear power
reactors.
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to a potential common-mode post-accident failure of
containment coolers. It is expected that recipients will review the
information for applicability to their facilities and consider actions, as
appropriate, to avoid similar problems. However, suggestions contained in
this information notice are not NRC requirements; therefore, no specific
action or written response is required.
Description of Circumstances
On February 13, 1996, the licensee for Diablo Canyon determined that the
containment fan coolers were susceptible to component cooling water flashing
in the cooler unit cooling coils during a design-basis loss-of-coolant
accident (LOCA) with a concurrent loss of offsite power or with a delayed
sequencing of safety-related equipment. Diablo Canyon has five fan coolers
per unit. The containment fan coolers are designed to remove heat from the
containment atmosphere during normal operation. The fan coolers are also
automatically initiated engineered safety features, which help maintain
containment integrity by reducing post-accident containment pressure by the
condensation of steam and the removal of heat in conjunction with operation of
the containment spray system. The fan coolers are cooled by component cooling
water under both normal and accident conditions.
During a postulated design-basis LOCA with a concurrent loss of offsite power, the component cooling water pumps and the fan cooler fans would lose power.
The component cooling water flow stops almost immediately, while the fans
coast down over a period of minutes. The first fan cooler will restart on
slow speed approximately 22 seconds after the loss of offsite power. The
component cc'ling water pumps will restart 26 to 30 seconds after the
accident. In this scenario, the high temperature containment atmosphere would
be forced across the cooling coils for several seconds with no component
cooling water flow. This process may cause the stagnant component cooling
water to boil, thereby creating steam voids in the cooling coils and the
9608090031 I-i5- V4 At- Iu 9 i moos
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IN 96-45 August 12, 1996 component cooling water piping. When the component cooling water pumps
restart, the pumped liquid would collapse the steam voids and may create
significant hydrodynamic loads (waterhammer). The hydrodynamic loads may
adversely affect the integrity of the fan coolers or the associated component
cooling water piping. This problem may cause the fan cooler pipes to rupture
and could cause a significant loss of component cooling water inventory, which
could threaten cooling to emergency core cooling system components. The
licensee for Diablo Canyon evaluated this potential failure mechanism and has
installed a nitrogen pressurization system on the component cooling water head
tank to increase the margin to boiling.
On July 22, 1996, the licensee for Haddam Neck declared all four of its
containment air recirculation fans inoperable and initiated a plant shutdown
The air recirculation fans are the only credited heat removal system for post- accident containment heat loads, and the associated cooling coils are cooled
by the station service water system. The fans were declared inoperable after
the licensee review of the consequences of two-phase service water flow
following a LOCA concurrent with a loss of normal power. The licensee
analysis predicted hydrodynamic loads that exceeded the service water piping
and support structural limits.
Discussion
At many plants, containment fan coolers provide a significant safety function
in reducing containment pressure and removing heat from the containment
building. The postulated failure scenario could cause a common failure of all
the containment coolers, thereby potentially challenging the integrity of the
containment building. In certain cases, failure of the cooling water system
piping could cause a potential containment bypass flow path and may jeopardize
cooling to other safety-related loads.
An individual plant vulnerability to these postulated failures is dependent on
a number of factors. The coastdown rates of the cooling water flow and the
cooler fans, the operating pressure and pressure decay rate of the cooling
water system, the timing of cooling water pump restart, the containment
temperature profile during the design-basis accident, and other site-specific
parameters have an effect on facility vulnerability to this potential failure
mode. This failure mode would also be applicable to the design-basis main
steam line break in containment.
Westinghouse issued Nuclear Safety Advisory Letter NSAL-96-003, "Containment
Fan Cooler Operation During a Design Basis Accident," to alert their customers
to this concern. NSAL-96-003 is provided as an attachment to this information
notice.
I--1 IN 96-45 August 12, 1996 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical Contacts: James Tatum, NRR John Tappert, NRR
(301) 415-2805 (301) 415-1167 Internet: jetl@nrc.gov Internet: jrt@nrc.gov
Alan Levin, NRR Howard Wong, Region IV
(301) 415-2890 (510) 975-0296 Internet: ael@nrc.gov Internet: hjw@nrc.gov
William Raymond, Region I
(203) 267-2571 Internet: wjr~nrc.gov
Attachments:
1. Nuclear Safety Advisory Letter NSAL-96-003, dated 06/20/96
2. List of Recently Issued NRC Information Notices
- 4-11,gC-411 'LJ 41-1 k-0 t
Westinghouse
Energy NUCLEAR SAFETY ADVISORY LETTER
Systs
-a Business
Usk
TIS [S A NOTIFICATION OF A RECENTLY IDENTIFIED POTENTIAL SAFEY ISSUE PERTANrNG TO BASIC
COMPONENU SUPPLIED BY WESTINGHOUSE THIS INFORMATION 1S BEING PROVIDED TO YOU SO THAT A
REVIEW OF THIS ISSUE CAN BE CONDUCTED BY YOU TO DETERMINE IF ANY ACTION IS REQUIRED.
P.O. Box 335. Pkubuqgb. PA 152304355 Subject: Containet Fan Cooler Operation During a .Dosipn Basis Accidl?{ umber. NSAL-96-003 Basic Coponent: Coota-eat Fan Coole Date: 6/20/96 Plaits: Westinghouse and MHI NSSS Plants
, - n r y i* * S .5 % `,
__.-_ _ _ , .. _ - _.. . . - - -r- ..-. . - .- _. -.,. . Ye &su 5-
. Transfer of ormation Pursuant to 10 CFR 21.21(b) Yes O
- 'Advisory Eformaion Pursuant to 10 CFR 21.21(cX2) Yes M
.Refcreace:
The purposc of this loe is to provide Westintouse NSSS Ownens information regarding the potential
paformace of some containment fan cooler units (CFCUs) during accidenit conditions which may
compromise the containment cooling system capability.
This Westinghouse Nuclear Safety Advisory Letter deals with the potential susceptibility for the cooling
water of cain CFCUs to flash to steam during a desin basis Lou of Coolant Accident (LOCA) with
ether a cocurrent LOSS of Offsite Power (LOOP) or a delayed sequencing of safety-related equipment.
The applicability of this issue to a given nuclear unit depends on plant specific aspects of the containment
cooling sysem desip and its heat removal system. The Nuclear Regulatory Commission has been
Rotified by _ LER (Reference 1).
Additional iafornation, if required, may be obtained from the originator. Telephone 412-374-5750.
Originator(s):
J. T. Crane W. R. Ricc. Interim Manager
Regulatoiy & Licensing Initiatives Regulatory & Licensing Initiatives
AlTACHMM 1 Ul *sWrW Pff Sheet I of 3
\ -,A
ISSUE DESCRIPTION
The potenial for this condition wu discovered during an %vestivgeto into Component Cooling Water
(CCW) system design issues by a Westinghouse NSSS Owners The CCW System provides cooling
water directly to the CFCUs in that plant's design. Depending on the specific design conditions, it
may be applicable to plants that utilize cooling waler systems other thin the CCW for their CFCUs
This issue concerns a type of containment cooling deaig that has a single set of CFCUs for heat
removal during both nonmal operating conditions and accident conditis. In the Licensee's design the
CFCUs arc equipped with a swo-speed blower that operates at about 1200 rpm for normal operation
and about 600 rpm for accident conditions. Cooling water to the heat exchanger coils for both normal
and accident operation is supplied by the CCW sytem. The License's containmcn analysis ausumas
the fan coolers operate during postulated accidents, removing beat so as to maintain containment
pressure within design bais limits.
During a postulated LOOP coincident with a design basis LOCA, power is lost to bpth the CCW
pumps and the CFCU blowan. The CCW pumps aem calculated to coast down to 0 rpm within 1-2 seconds while the CFCUI blowers ar calculated to coast down firm a aomiasl speed of 1200 rpm to
600 rpm in approximately 30 seconds and then to 0 rpm an estimated 700 second laser. Accountiig
for diesel-generator start time'seand emergency buss loading sequence, the CFCU blowers are rc-
- energized approximiaeij 20 seconds afler the initiation of the LOOP, and the CCW pumps at re- energized about 30 seconds after the initiation of the LOOP. This timing of events provides for hot, steam-laden cont ent ai to be drawn over the heat exchanger coils at a elatively high velocity for
30 seconds before cooling liquid flow is reestablished to the coils.
The high heat content of containment atmosph=r under accident conditions being drawn over the
CFCU heat exchanger coil with no pumped liquid flow kw been calculated to resit in steaming of the
stationary liquid inventory of the coils. When the CCW pups are re-nergizod, the pumped liquid
flow acts to collapse the steam void in Oe CFCU piping. Collapsing &a steam void is predicted to
mrIlt iG.a wzasAsmer with nfficient energy and force that may impact the integrity of either the
beat exchanger coil or its associated piping, resulting in a lost of inteWy of the CCWs rystm.
To prevent flashing of the CFCU cooling woter, the Licensee has instafled a nitrogen pressurization
system on the CCW system.
TECHNICAL EVALUATION
The following discussion provides several items to consider in evaluating your CFCUs.
In general a plant u has CFCUs with a 2 speed blower motor and a diesel loading sequence that
results in water flow through the cooler coil later than 15 seconds after a design basis large break
LOCA, may have a similar situation. However, there arn other plant specific aspects that can impact
CFCU functioning. The containment cooling design in this issue has a singk set of fan coolens that
are used for containment cooling during both normal and accident conditions. Flashing and
subsequent void collapse may not apply if a plant has separate sets of equipment where the accident
CFCUs arc not operating prior to a design basis accident. These accident related fan coolers would be
at containment ambient conditions with no forced convective et transfer at the beginning of the
13i7AMWFWIN
Sheet 2 of 3
I
accident. Since their fmns would not be operating u the beginning of the Postulated accident (as
compated to a single set f fa cooles which would be coasting down) the heat release from a design
basis accacent wouia be ttisfurred to the coil cooling water ju a much slower rate.
Flashing of the CFCU cooling water may not occur in a specific plant design because of factors such
as hea transfer capability, saturation pressure of the cooling systcm. coutdown time of the fan
blower, and coutdown time of the cooling water pump(s). Also, the timing of when ECCS eQuipment
will start in a design basis accident can determine if the CFCUs do or do not have stagnant cooling
water.
In summary, the issue is wbether safety related CFCUs will function as intended during a design basis
event, if they am postulated to experience flshing of the water in the cooling coils. If Rubing can be
postulated, then the issue of whether the CFCUs will maiuntan euctrl integrity during subsequent
void collapse should be addrssod.
ASSESSMENT OF SAFETY SIGNMCANCE .
Westinghouse canot deteaine the potential for flashing in the CFCUr on a generic basis because of
the various plant specific designs for the containment cooling system and situation specific heat
umnsfer conditions. Thus &* mott effective action that can be taken is a notification to all
Westinghouse plants.
REEORTABILrY
The NRC is awarm of this imue via an LER (Reference 1).
RECOMENDEDACTINS
Licensees should review d* containment cooling system to determine if their safety related
contaL-=e-t fan ccolerv am nsceptible to cooling water void formation and subsequent void collapse
and waterhammer during a design bais accident.
REFERENCE
1. Pacific Gas A Etcic letter. PO&E DCL-96-097, April 26, 1996 to U. S. Nuclear Regulatory
Commission, 'Licec Evet Report 1.96-005-00 (Voluntary) Potential for Flushing in
Containment Fin Cooer Units
Sheet 3 of 3
I
Attachment
IN 96-45 August 12, 1996 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date of
Notice No. Subject Issuance Issued to
%_
s41TOr.ASDPAP
A c -crssq
.UeiUFU WTA_ Urn
n aa, raMLAr.__^__ Z/U?/vb All holders of Ls or CPs
irip breaker trom Lracking for nuclear power reactors
of Phenolic Material in
secondary contact assembly
96-43 Failures of General 08/02/96 All holders of OLs or CPs
Electric Magne-Blast for nuclear power reactors
Circuit Breakers
96-42 Unexpected Opening of 08/05/96 All holders of OLs or CPs
Multiple Safety Relief for nuclear power reactors
Valves
96-41 Effects of a Decrease in 07/26/96 All holders of OLs or CPs
Feedwater Temperature on for pressurized water
Nuclear Instrumentation reactors
96-40 Deficiencies in Material 07/25/96 All holders of OLs or CPs
Dedication and Procurement for nuclear power reactors
Practices and in Audits of
Vendors
96-09, Damage in Foreign Steam 07/10/96 All holders of OLs or CPs
Supp. 1 Generator Internals for pressurized-water
reactors
96-39 Estimates of Decay Heat 07/05/96 All holders of OLs or CPs
Using ANS 5.1 Decay Heat for nuclear power reactors
Standard May Vary Signi- ficantly
96-38 Results of Steam Generator 06/21/96 All holders of OLs or CPs
Tube Examinations for pressurized water
reactors
96-37 Inaccurate Reactor Water 06/18/96 All pressurized water
Level Indikation and Inad- reactor facilities holding
vertent Draindown During an operating license or a
Shutdown construction permit
96-36 Degradation of Cooling 06/12/96 All holders of OLs or CPs
Water Systems Due to Icing for nuclear power reactors
OL - Operating License
CP - Construction Permit
IN 96-45 August 12, 1996 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
/s/ Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical Contacts: James Tatum, NRR John Tappert, NRR
(301) 415-2805 (301) 415-1167 Internet: jetlnrc.gov Internet: jrt~nrc.gov
Alan Levin, NRR Howard Wong, Region IV
(301) 415-2890 (510) 975-0296 Internet: ael nrc.gov Internet: hjw~nrc.gov
William Raymond, Region I
(203) 267-2571 Internet: wjr~nrc.gov
Attachments:
1. Nuclear Safety Advisory Letter NSAL-96-003, dated 06/20/96
2. List of Recently Issued NRC Information Notices
... .. ..-.. , An,% ........... t P^ P. ^ ,
AS ^ .
UUIUMM NAME: U:\JdK\LUN1LLK.IN
OFFICE Contacts* C/SPLB:DSSA C/PECB:DRPM D/DRPM
KA ALevin LMarsh* AChaffee* BGri
HWong
JTatum
JTappert
WRaymond
DATE 08/08/96 08/08/96 08/08/96 Official Record Copy
s ;
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IN 96-XX
August XX, 1996 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical Contacts: James Tatum, NRR John Tappert, NRR
(301) 415-2805 (301) 415-1167 Internet: jetl nrc.gov Internet: jrt@nrc.gov
Alan Levin, NRR Howard Wong, Region IV
(301) 415-2890 (510) 975-0296 Internet: ael nrc.gov Internet: hjw~nrc.gov
William Raymond, Region I
(203) 267-2571 Internet: wjr~nrc.gov
Attachments:
1. Nuclear Safety Advisory Letter NSAL-96-003, dated 06/20/96
2. List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\JRT\CONTCLR.IN
OFFICE Contacts C/SPLB:DSSA C/PECB:DRPM D/DRPM
Km ALevin LMarsh-'i AChaffep BGrimes
JTatdm'
JTappertJf 7 A
WRa ondM U _ _U
DATE I / t/96 / 96 / t'/96 / /96 arts
- - ...
j If.
uTTIcial Kecora Gopy
IN 96-XX
August XX, 1996 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical Contacts: James Tatum, NRR John Tappert, NRR
(301) 415-2805 (301) 415-1167 Internet: Jetlnrc.gov Internet: Jrt@nrc.gov
Alan Levin, NRR Howard Wong, Region IV
(301) 415-2890 (510) 975-0296 Internet: ael~nrc.gov Internet: hjw~nrc.gov
Attachment: List OT' Recently Issued NRC Information Notices
DOCUMENT NAME E: :\JRT\4 NCR.IN
OFFIM Contacts C/SPLB:DSSA C/PECB:DRPM D/DRPM
K"E ALevin 0 + LMars AChaffee BGrimes
HWong p r>
JTatum
JTappe
V-I
14r
C
rAx
DATE I / /96 4/196 / /96 / /96 Official Record Copy
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list | - Information Notice 1996-01, Potential For High Post-Accident Closed-Cycle Cooling Water Temperatures to Disable Equipment Important to Safety (3 January 1996)
- Information Notice 1996-01, Potential for High Post-Accident Closed-Cycle Cooling Water Temperatures to Disable Equipment Important to Safety (3 January 1996)
- Information Notice 1996-02, Inoperability of Power-Operated Relief Valves Masked by Downstream Indications During Testing (5 January 1996, Topic: Stroke time)
- Information Notice 1996-03, Main Steam Safety Valve Setpoint Variation as a Result of Thermal Effects (5 January 1996)
- Information Notice 1996-03, Main Steam Safety Valve Setpoint Variation As a Result of Thermal Effects (5 January 1996)
- Information Notice 1996-04, Incident Reporting Requirements for Radiography Licensees (10 January 1996, Topic: Brachytherapy)
- Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel (18 January 1996, Topic: Reactor Vessel Water Level)
- Information Notice 1996-06, Design & Testing Deficiencies of Tornado Dampers at Nuclear Power Plants (25 January 1996)
- Information Notice 1996-07, Slow Five Percent Scram Insertion Times Caused by Viton Diaphragms in Scram Solenoid Pilot Valves (26 January 1996)
- Information Notice 1996-08, Thermally Induced Pressure Locking of a High Pressure Coolant Injection Gate Valve (5 February 1996, Topic: Anchor Darling, Cold shutdown justification)
- Information Notice 1996-09, Damage in Foreign Steam Generator Internals (12 February 1996, Topic: Earthquake)
- Information Notice 1996-10, Potential Blockage by Debris of Safety System Piping Which Is Not Used During Normal Operation or Tested During Surveillances (13 February 1996)
- Information Notice 1996-10, Potential Blockage by Debris of Safety System Piping Which is Not Used During Normal Operation or Tested During Surveillances (13 February 1996)
- Information Notice 1996-11, Ingress of Demineralizer Resins Increases Potential For Stress Corrosion Cracking of Control Rod Drive Mechanism Penetrations (14 February 1996)
- Information Notice 1996-11, Ingress of Demineralizer Resins Increases Potential for Stress Corrosion Cracking of Control Rod Drive Mechanism Penetrations (14 February 1996)
- Information Notice 1996-12, Control Rod Insertion Problems (15 February 1996)
- Information Notice 1996-13, Potential Containment Leak Paths Through Hydrogen Analysis (26 February 1996)
- Information Notice 1996-14, Degradation of Radwaste Facility Equipment at Millstone Nuclear Power Station, Unit 1 (1 March 1996)
- Information Notice 1996-15, Unexpected Plant Performance During Performance of New Surveillance (8 March 1996)
- Information Notice 1996-16, BWR Operation with Indicated Flow Less than Natural Circulation (14 March 1996)
- Information Notice 1996-17, Reactor Operation Inconsistent with the Updated Final Safety Analysis Report (18 March 1996)
- Information Notice 1996-18, Compliance with 10 CFR Part 20 for Airborne Thorium (25 March 1996, Topic: Brachytherapy)
- Information Notice 1996-19, Failure of Tone Alert Radios to Activate When Receiving a Shortened Activation Signal (2 April 1996)
- Information Notice 1996-20, Demonstration of Associated Equipment Compliance with 10 CFR 34.20 (4 April 1996, Topic: Brachytherapy)
- Information Notice 1996-21, Safety Concerns Related to the Design of the Door Interlock Circuit on Nucletron High-Dose Rate and Pulsed Dose Rate Remote Afterloading Brachytherapy Devices (10 April 1996, Topic: Brachytherapy)
- Information Notice 1996-22, Improper Equipment Settings Due to Use of Nontemperature-Compensated Test Equipment (11 April 1996, Topic: Brachytherapy)
- Information Notice 1996-23, Fires in Emergency Diesel Generator Exciters During Operation Following Undetected Fuse Blowing (22 April 1996, Topic: Brachytherapy)
- Information Notice 1996-24, Preconditioning of Molded-Case Circuit Breakers Before Surveillance Testing (25 April 1996, Topic: Brachytherapy)
- Information Notice 1996-25, Traversing In-Core Probe Overwithdrawn at Lasalle County Station, Unit 1 (30 April 1996, Topic: Brachytherapy)
- Information Notice 1996-26, Recent Problems with Overhead Cranes (30 April 1996, Topic: Brachytherapy)
- Information Notice 1996-26, Recent Problems With Overhead Cranes (30 April 1996)
- Information Notice 1996-27, Potential Clogging of High Pressure Safety Injection Throttle Valves During Recirculation (1 May 1996, Topic: Brachytherapy)
- Information Notice 1996-28, Suggested Guidance Relating to Development and Implementation of Corrective Action (1 May 1996, Topic: Brachytherapy)
- Information Notice 1996-29, Requirements in 10 CFR Part 21 for Reporting and Evaluating Software Errors (20 May 1996, Topic: Brachytherapy)
- Information Notice 1996-30, Inaccuracy of Diagnostic Equipment for Motor-Operated Butterfly Valves (21 May 1996)
- Information Notice 1996-31, Cross-Tied Safety Injection Accumulators (22 May 1996)
- Information Notice 1996-32, Implementation of 10 CFR 50.55a(g) (6) (II) (A), Augmented Examination of Reactor Vessel (5 June 1996, Topic: Non-Destructive Examination)
- Information Notice 1996-32, Implementation of 10 CFR 50.55a(g) (6) (ii) (A), Augmented Examination of Reactor Vessel (5 June 1996, Topic: Nondestructive Examination)
- Information Notice 1996-33, Erroneous Data From Defective Thermocouple Results in a Fire (24 May 1996, Topic: Reverse polarity)
- Information Notice 1996-33, Erroneous Data from Defective Thermocouple Results in a Fire (24 May 1996, Topic: Reverse polarity)
- Information Notice 1996-34, Hydrogen Gas Ignition During Closure Welding of a VSC-24 Multi-Assembly Sealed Basket (31 May 1996)
- Information Notice 1996-35, Failure of Safety Systems on Self-Shielded Irradiators Because of Inadequate Maintenance and Training (11 June 1996)
- Information Notice 1996-36, Degradation of Cooling Water Systems Due to Icing (12 June 1996, Topic: High winds, Ultimate heat sink, Frazil ice)
- Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown (18 June 1996, Topic: Reactor Vessel Water Level)
- Information Notice 1996-38, Results of Steam Generator Tube Examinations (21 June 1996)
- Information Notice 1996-39, Estimates of Decay Heat Using ANS 5.1 Decay Heat Standard May Vary Significantly (5 July 1996)
- Information Notice 1996-40, Defciencies in Material Dedication and Procurement Practices and in Audits of Vendors (7 October 1996, Topic: Coatings, Troxler Moisture Density Gauge)
- Information Notice 1996-41, Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation (26 July 1996)
- Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves (5 August 1996, Topic: Reactor Vessel Water Level)
- Information Notice 1996-43, Failures of General Electric Magne-Blast Circuit Breakers (2 August 1996)
... further results |
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