IR 05000461/2019004

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000461/2019004
ML20044D295
Person / Time
Site: Clinton Constellation icon.png
Issue date: 02/12/2020
From: Dave Hills
NRC/RGN-III/DRP/B1
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2019004
Download: ML20044D295 (27)


Text

February 12, 2020

SUBJECT:

CLINTON POWER STATION - INTEGRATED INSPECTION REPORT 05000461/2019004

Dear Mr. Hanson:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Clinton Power Station. On January 16, 2020, the NRC inspectors discussed the results of this inspection with Mr. T. Chalmers, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Clinton Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

David E. Hills, Chief Branch 1 Division of Reactor Projects

Docket No. 05000461 License No. NPF-62

Enclosure:

As stated

Inspection Report

Docket Number:

05000461

License Number:

NPF-62

Report Number:

05000461/2019004

Enterprise Identifier: I-2019-004-0066

Licensee:

Exelon Generation Company, LLC

Facility:

Clinton Power Station

Location:

Clinton, IL

Inspection Dates:

October 01, 2019 to December 31, 2019

Inspectors:

B. Bartlett, Senior Operations Engineer

J. Beavers, Senior Resident Inspector

S. Bell, Health Physicist

M. Domke, Reactor Inspector

M. Holmberg, Senior Reactor Inspector

C. Mathews, Illinois Emergency Management Agency

D. Sargis, Resident Inspector

W. Schaup, Senior Resident Inspector

J. Seymour, Reactor Ops Engineer

D. Szwarc, Senior Reactor Inspector

L. Torres, Illinois Emergency Management Agency

Approved By:

David E. Hills, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Clinton Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Establish Adequate Breaker Maintenance Frequency Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000461/2019004-01 Open/Closed None (NPP)71153 A self-revealed Green finding and associated non-cited violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion III, "Design Control," was identified when the licensee failed to review for suitability of application of materials that were essential to the safety-related functions of the 4160 V breakers. Specifically, the licensee extended the maintenance frequency for 4160 V breakers without reviewing the suitability of the lubricant for the extended time frame, which caused the failure of the Division 1 main feed breaker.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000461/2019003-01 Unresolved Item Regarding the Primary Calibration of the Heating, Ventilation, and Air Conditioning Effluent Monitor Noble Gas Channel 71124.06 Closed URI 05000461/2019010-01 Fuses Subject to Part 21 Potentially Installed in Safety-Related Circuits 71152 Closed LER 05000461/2019-001-00 LER 2019-001-00 for Clinton Power Station, Unit 1, Main Feed Breaker Failed to Close During Bus Shift 71153 Closed LER 05000461/2019-001-01 LER 2019-001-01 for Clinton Power Station, Unit 1, Main Feed Breaker Failed to Close During Bus Shift 71153 Closed LER 05000461/2019-003-00 LER 2019-003-00 for Clinton Power Station, Unit 1,

Reactor Water Cleanup System Differential Flow Instrumentation Inoperable 71153 Closed

LER 05000461/2019-002-00 LER 2019-002-00 For Clinton Power Station, Unit 1, Turbine Driven Reactor Feed Pump Hydraulic Control Failure Results in Automatic SCRAM 71153 Closed

PLANT STATUS

The unit began the inspection period shut down for Refueling Outage C1R19. Startup was commenced on October 15, 2019, and the unit was synchronized to the grid on October 17, 2019. The unit reached full rated thermal power (approximately 99 percent power)and approximately 1120 MWe on October 21, 2019. The unit remained at full rated thermal power through the end of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

Winter Readiness

The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures for the following systems:

  • cycled condensate
  • fire protection

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)

'B' control room ventilation on November 19, 2019 (2)high pressure core spray system on November 20, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (2 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire Zone A-3a, RHR 'B' pump and heat exchanger room, elevation 702' on October 3, 2019
(2) Fire Zone C-2, containment, elevation 755' on October 31, 2019

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from September 23, 2019 to October 17, 2019:

03.01.a - Nondestructive Examination and Welding Activities. (The first part of this inspection sample is listed in NRC Inspection Report 05000461/2019003)

1. Visual examination (VT-1 and VT-3) of fuel cooling system components

1FC14008A-WA and 1FC14008A, weld attachment and anchor, ASME category D-A and F-A located in the fuel building

2. Visual examination (VT-1 and VT-3) of essential service water components

1SX19008R-WA and 1SX19008R, weld attachment and rigid support, ASME category D-A and F-A located in the control building

3. Visual examination (VT-1) of reactor head upper vessel penetration

component 1-NB-1-1-2Q1-FB, flange bolting, ASME category B-G-2 located in the containment building

4. Surface magnetic particle examination of residual heat removal heat

exchanger "A" component HEA-3, nozzle-to-head weld, ASME category C-B located in the A/B residual heat removal room

5. Volumetric ultrasonic examination (UT-1) of residual heat removal heat

exchanger "A" component HEA-3, nozzle-to-head weld, ASME category C-B located in the A/B residual heat removal room

6. Volumetric ultrasonic examination (UT-1) of high pressure core spray

component 1-HP-5-1, valve-to-pipe weld, ASME category R-A located in the fuels building

7. Field welds FW1 and FW2 and FW3 and FW4 and 4R1 for residual heat

removal bravo train minimum flow line gate valve 1E12-F018B and check valve 1E12-F046B repairs described by ASME Section XI repair/replacement plan in work order 01230601 task 39

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam administered from November 6, 2019 through December 12, 2019.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered on November 8, 2019.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during reactor startup on October 15, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification simulator exam ESG-LOR-19 on November 13, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (4 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1)main steam system safety relief valve replacement during refueling outage on October 29, 2019 (2)containment isolation valve local leak rate failures during refueling outage on December 20, 2019 (3)

'A' residual heat removal suppression pool suction valve failure during refueling outage on November 21, 2019 (4)

'A' switch gear heat removal condensing unit hydramotor failure on November 19, 2019

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Part 21 for emergency diesel generator fuel injectors issued on October 24, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (2 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Action Request 4281606, "MCR [main control room] Alarm: 5060-3E, Ground 125 Vdc MCC [motor control center] 1A" on October 3, 2019
(2) Action Request 4296225, "RHR [residual heat removal] 'C' Room Cooler South Cooling Coil Leakage" on November 14, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors reviewed the 50.59 and modification package for the accident tolerant fuel lead test assemblies that were installed during the 2019 refueling outage. The inspectors reviewed the composition of the limited number of lead test assemblies, placement of lead test assemblies in non-limiting core locations, and Technical Specification (TS) 5.6.5, Core Operating Limits Report, including the analytical methods that were previously reviewed and approved by the NRC.

(1) Engineering Change 627786, "Accident Tolerant Fuel (ATF) at Clinton (IronClad and ARMOR)"

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post-maintenance tests:

(1)

'B' reserve auxiliary transformer following maintenance on October 8, 2019 (2)

'A' residual heat removal suppression pool suction valve following valve repair on October 10, 2019

(3) Division 1 solenoids for safety relief valves B21-F041B and B221-F051B following wiring corrections on October 17, 2019
(4) Division 1 diesel generator run following governor replacements on October 29, 2019 (5)

'C' residual heat removal cooler south cooling coil after replacement on November 22, 2019 (6)

'A' plant service water to shutdown service water valve test following valve replacement on December 3, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Refueling Outage C1R19 activities from October 1-17, 2019.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Inservice Testing (IP Section 03.01)

(1) Division 1 shutdown service water pump inservice test on November 20, 2019

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) reactor coolant system leakage testing on October 11, 2019

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) The inspectors observed the annual licensed operator requalification drill with drill and exercise program opportunity on November 20,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Partial)

The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests:

(1)

(Partial)0RIX-PR001/2; station heating, ventilation, and air conditioning exhaust effluent monitor (HVAC).

This inspection activity augments the inspection results contained within NRC inspection report 05000461/2019003.

OTHER ACTIVITIES - BASELINE

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in control of measurement and test equipment that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) The inspectors reviewed the licensees implementation of its corrective action program related to emergency core cooling system sump in leakage.

71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000461/2019-001-00 and LER 05000461/2019-001-01, Main Feed Breaker Failed to Close During Bus Shift (ADAMS Accession: ML19322A109)

The circumstances surrounding this LER are documented in the Results section.

(2) LER 05000461/2019-002-00, Turbine Driven Reactor Feed Pump Hydraulic Control Failure Results in Automatic SCRAM (ADAMS Accession: ML19277E367)

The circumstances surrounding this LER are documented in the Results section.

(3) LER 05000461/2019-003-00, Reactor Water Cleanup System Differential Flow Instrumentation Inoperable (ADAMS Accession: ML19333B814)

The circumstances surrounding this LER are documented in the Results section.

INSPECTION RESULTS

Unresolved Item (Closed)

Unresolved Item Regarding the Primary Calibration of the Heating, Ventilation, and Air Conditioning Effluent Monitor Noble Gas Channel URI 05000461/2019003-01 71124.06

Description:

The licensee was unable at the time of the inspection (NRC inspection report 05000461/2019003) to provide records of its primary calibration of the station heating, ventilation, and air conditioning exhaust effluent monitor 0RIX-PR001/2 for the high range noble gas channel. Following that inspection, the licensee then located and provided the primary calibration for this monitor to the inspectors for review. The inspectors reviewed the provided documentation and did not identify any performance deficiency or compliance issues.

Corrective Action Reference(s): Action Request 4282015

Unresolved Item (Closed)

Fuses Subject to Part 21 Potentially Installed in Safety-Related Circuits URI 05000461/2019010-01 71152

Description:

The NRC issued an unresolved item (URI) when the inspectors identified that the licensee did not evaluate the impact of a Part 21 for Gould Shawmut TR30R fuses. The inspectors noted that the licensee was susceptible to the same failure mechanism described in Part 21. At the time, it was not known if any fuses from the affected lot number were installed in safety-related circuits. The licensee identified all of the circuits in the plant that used TR30R fuses, and they determined how potential fuse failures would impact the safety functions of plant equipment. The licensee performed inspections to determine if fuses from the affected lot were installed in the plant, and they determined that they were not installed in the plant. The inspectors reviewed the licensee's determinations and verified that the work tasks associated with the fuse replacements were completed. The inspectors also observed the fuse replacements for a safety-related circuit and reviewed the licensee's risk mitigation plan associated with the work.

None of the licensee's fuses were from the affected lot number. Therefore, there was no impact on any electrical circuits. The inspectors did not identify any violations of NRC requirements.

Corrective Action Reference(s): Action Request 4250520, "NRC Question: P21 Fuse" and Action Request 4251536, "Part 21 Assessment Results for TR30R Fuses"

Observation: Control of Measurement and Test Equipment 71152 The inspectors reviewed recent corrective action documents regarding measurement and test equipment that failed post-use calibration and that were reported damaged. During the inspection period, the licensee issued three issue reports that documented adverse trends in control of measurement and test equipment. The inspectors noted that two of the issue reports were placed in the non-corrective action program. Control of measurement and test equipment is a requirement for quality assurance programs. Therefore, the inspectors determined that the trends identified should not have been placed in the non-corrective action program, but should have been placed in the licensee's corrective action program. The licensee revised the issue reports to place them in the corrective action program. The inspectors determined that this issue was of minor significance.

Observation: Emergency Core Cooling System Sump in Leakage 71152 The inspectors reviewed the licensee's problem identification and resolution activities associated with emergency core cooling system sump in leakage. Sump alarm issues and cooling water leakage items were reviewed, the cooling water leakage ultimately led to the inoperability of the high pressure core spray system. Although the inspectors determined there were earlier opportunities to resolve this issue, neither deviations from the corrective action program standards nor previous system operability issues were identified.

Failure to Establish Adequate Breaker Maintenance Frequency Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000461/2019004-01 Open/Closed None (NPP)71153 A self-revealed Green finding and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified when the licensee failed to review for suitability of application of materials that were essential to the safety-related functions of the 4160 V breakers. Specifically, the licensee extended the maintenance frequency for 4160 V breakers without reviewing the suitability of the lubricant for the extended time frame, which caused the failure of the Division 1 main feed breaker.

Description:

On May 22, 2019, the licensee was establishing initial conditions to perform a Division 1 emergency diesel generator surveillance test. The Division 1 4160 V bus had three available power sources. The offsite sources were the reserve auxiliary transformer 'B' (RAT B) and the emergency reserve auxiliary transformer (ERAT), which were powered from separate offsite electrical sources. The onsite power source was the Division 1 emergency diesel generator. The licensee attempted to shift the power source to the Division 1 bus from the ERAT to the RAT B. When the licensee attempted to close the feed breaker from RAT B to the Division 1 bus, the feed breaker failed to close. The licensee declared the RAT B feed to the Division 1 bus inoperable and unavailable, and restored the electrical configuration so that the ERAT was supplying power to the bus. The licensee removed and replaced the breaker, verified proper operation of the new breaker, and declared the RAT B feed to the Division 1 bus operable.

The licensee reported this event to the NRC in LER 2019-001-00 and in LER 2019-001-01.

The licensee noted that the last time the breaker was successfully operated was April 17, 2019. The licensee determined that the breaker was inoperable from that date until the breaker was replaced and tested on May 22, 2019. This exceeded the allowed outage time in TS 3.8.1, Condition A.2, which required restoring an inoperable offsite circuit to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The licensee performed a causal evaluation. As part of the evaluation, the licensee sent the breaker to its vendor for a failure analysis. The failure analysis identified that the lubricant in the breaker was dry and tacky. The tacky lubricant was found throughout the breaker, indicating that it was an age-related degradation. The analysis determined that the dried lubricant prevented free movement of the internal mechanisms in the breaker, which caused it to fail to close. The licensee reviewed the preventive maintenance frequency and identified that it was changed in 2015. The breaker maintenance that cleans and lubricates the breaker had its frequency changed from every 4 years to every 8 years. The breaker that failed was last cleaned and lubricated 7 years before the failure.

The inspectors reviewed the licensee's causal evaluation and the paperwork associated with changing the maintenance frequency from 4 years to 8 years. Service Request 90522 documents the licensee's justification for changing the maintenance frequency. The maintenance template for the breaker stated, "The condition of the lubricant is essential to proper operation. Inadequate lubrication is by far the dominant cause of breaker failures...

The lubricant can be expected to harden if a breaker is cycled scarcely at all in a period approaching six years." The feed breakers to the safety buses are cycled approximately once per month for emergency diesel generator testing. Service Request 90522 did not address how the lubricant would be affected by remaining in service for the extended period of time.

The inspectors determined that the maintenance frequency extension to 8 years did not ensure the circuit breaker could perform its safety function. The inspectors also identified that when the licensee changed the maintenance frequency, they did not review the materials, parts, or equipment inside the breaker to determine if they were suitable to perform their safety-related function for the period between maintenance.

Corrective Actions: The licensee replaced the failed breaker, changed the breaker preventive maintenance frequency, and revised the maintenance procedure to incorporate a different grease.

Corrective Action References: Action Request 4250932, "1AP07EK Main Feed Breaker Failed to Close During Bus Shift"

Performance Assessment:

Performance Deficiency: The failure to establish a maintenance frequency that ensured medium voltage circuit breakers would perform their safety function was a performance deficiency. Specifically, the licensee extended the maintenance frequency for circuit breakers without reviewing the suitability of the lubricant for the extended time frame, as required by 10 CFR Part 50, Appendix B, Criterion III, "Design Control."

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency caused the Division I main feed breaker to fail to close, which rendered a required source of offsite power inoperable and unavailable.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors used Inspection Manual Chapter 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," to determine significance. The inspectors answered "Yes" to question 3 because the failure created a loss of function for a required source of offsite power for greater than its TS-allowed outage time. Therefore, the NRC performed a detailed risk evaluation.

A regional senior reactor analyst evaluated the significance of the finding using the Clinton Standardized Plant Analysis Risk model, version 8.59. The model was first modified by the Idaho National Laboratory because the plants normal offsite power alignment during the exposure period was different from the current version of the model. The 'A' and 'C' 4 kV Divisions were normally fed from the ERAT, while the 'B' Division was normally fed from the RAT.

The senior reactor analyst modeled the degraded condition as a failure of the 'A' breaker from the RAT to the bus. The failure mode of the breaker was a failure to close. The exposure time was approximately 31 days. The change in risk was less than 1E-6/yr. because each 4 kV division has three sources of power - RAT, ERAT, and a diesel generator, and the finding affected only one source to one of the buses for a limited period of time.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance. The change to the breaker maintenance frequency occurred greater than three years ago.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that measures shall be established for the selection and review for suitability of application of materials that are essential to the safety-related functions of the structures, systems, and components.

Contrary to the above, from December 2015 to May 22, 2019, the licensee failed to review for suitability of application of materials that were essential to the safety-related functions of the components. Specifically, the licensee extended the maintenance frequency for 4160 V breakers without reviewing the suitability of the lubricant for the extended time frame, which caused the failure of the Division 1 main feed breaker.

Additionally, because the licensee was not aware of the Division 1 main feed breaker inoperability, the licensee failed to take the actions required by TS 3.8.1, Condition A.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Minor Violation 71153 Minor Violation: On August 3, 2019, the initial NRC event notification for an automatic low reactor level SCRAM did not include all reportable conditions for the event. On August 4, 2019, securing high pressure core spray injection was added per 10 CFR 50.72(b)(3)(v)(D). On August 6, 2019, an unanalyzed condition that could have prevented the fulfillment of the primary containment function due to being outside the initial conditions to ensure that drywell and containment pressures remain within design values during a loss of coolant accident, 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(C).

The latter two notifications were late.

Screening: The inspectors determined the performance deficiency was minor. The inspectors determined the initial, on time notification triggered the appropriate Agency event response. Additionally, all necessary notifications were eventually made with those on August 4, 2019, and August 6, 2019, beyond the time requirements of NRC regulations.

Enforcement:

This failure to comply with 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(C) constitute a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Observation: Reactor Water Cleanup System Differential Flow Instrumentation Inoperable 71153 The inspectors determined that it was not reasonable to foresee or correct the cause discussed in LER 05000461/2019-003-00; therefore, no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 16, 2020, the inspectors presented the integrated inspection results to Mr. T. Chalmers, Site Vice President, and other members of the licensee staff.
  • On October 17, 2019, the inspectors presented the Inservice Inspection Exit inspection results to Mr. D. Shelton, Regulatory Assurance Manager, and other members of the licensee staff.
  • On November 8, 2019, the inspectors presented the Biennial inspection of the licensed operator requalification program inspection results to Mr. J. Kowalski, Plant Manager, and other members of the licensee staff.
  • On December 13, 2019, the inspectors presented the Biennial inspection of the requalification examination security portion of the licensed operator requalification program inspection results to Mr. T. Dean, Training Director, and other members of the licensee staff.
  • On December 17, 2019, the inspectors presented the radiation protection baseline inspection results to Mr. D. Shelton, Regulatory Assurance Manager, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

CPS 1860.01

Cold Weather Operation

9d

71111.04Q Drawings

Drawing

M05-1074

P&ID High Pressure Core Spray (HP)

AH

Procedures

CPS

3309.01E001

High Pressure Core Spray Electrical Lineup

8b

CPS

3309.01V001

High Pressure Core Spray Valve Lineup

11b

CPS

3309.01V002

High Pressure Core Spray Instrument Valve Lineup

CPS

3402.01E001

Control Room HVAC Electrical Lineup

10e

CPS

3402.01V001

Control Room HVAC Valve Lineup

17a

CPS

3402.01V002

Control Room HVAC Instrument Valve Lineup

6a

71111.05Q Corrective Action

Documents

AR 4269365

1FP052 - PCIV Will Not Operate - Breaker Trips

08/03/2019

AR 4271550

Motor Tests Bad for 1FP052

08/03/2019

Procedures

CPS 1893.01

Fire Protection Impairment Reporting

20f

CPS

1893.04M104

707 Auxiliary: RHR 'B' Pump and Heat Exchanger Room

Prefire Plan

5a

CPS

1893.04M220

755 Containment: Prefire Plan

FSI Log Number:

001-08-2019

"Sample" Manual Fire System Impairment (FSI) Permit

Work Orders

WO 4948721

1FP052 - PCIV will not Operate - Breaker Trips

08/30/2019

71111.08G Corrective Action

Documents

4135343

Erosion on 1E12F018B Valve Internals

05/07/2018

283694

C1R19 Pitting Identified on RHR-B Min Flow Line Elbow

09/30/2019

Corrective Action

Documents

Resulting from

Inspection

288995

NRC ISI Exit Meeting -Minor Violations

10/18/2019

289811

NRC ID'd ASME Code Requirements used in EC 629521

10/21/2019

Engineering

24182

Evaluation of 1E12F046B and 1E12F018B Valve Body

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Evaluations

Degradation

Procedures

CC-AA-501-1021

Exelon Nuclear Welding Program Repair of Welds and Base

Metal

Work Orders

230601

When Required, Replace Eroded RHR B Pump Minimum

Flow Line

05/13/2018

71111.11A

Corrective Action

Documents

04189731

Reactor Water Level Controller Challenges

10/31/2018

04190336

4.0 Critique Reactor SCRAM on High IRM Flux

11/01/2018

238238

White Finding for Division 2 Diesel Generator Event

04/10/2019

269480

4.0 Critique Reactor SCRAM

08/04/2019

272315

4.0 Critique for 4010.02 Plant Chemistry Off-Normal Entry

08/15/2019

Miscellaneous

ESG-LOR-01

Loss of Coolant Accident - Simulator Exercise Guide

004

ESG-LOR-092

Loss of RPS Solenoid Inverter - Restoration of High

Pressure Feed

003

ESG-LOR-106

RR Pump High Vibrations - RHR C Suction Leak (Simulator

Exercise Guide)

000

N-08NASIM

Simulator Based NRC Annual Operating Exam after Crew

Remediation

2/01/2017

N-08NASIM

Simulator Based NRC Annual Operating Exam - Crew

Failure

11/30/2017

PRCDS for an

Individual

Operator

NRC Written Exam Failure Review

11/06/2017

Procedures

OP-AA-102-106

Operator Response Time Program

OP-CL-102-106-

1001

Operator Response Time Master List at Clinton Power

Station

8c

Self-Assessments 04219981

Pre-NRC 71111.11 Inspection Licensed Operator

Requalification Training Assessment

06/06/2019

71111.11B

Corrective Action

Documents

AR 4183901

File Transfer Not in Compliance With TQ-AA-201

10/15/2018

AR 4188538

Reactor Scram on High IRM Flux

10/28/2018

AR 4288756

Single Data Point Not Retained for Test-Simulator

10/17/2019

Corrective Action

Documents

Resulting from

Inspection

AR 4295512

NRC ID: Steady State Test Does Not Include CRD Flow and

Temp

11/07/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

10-28-2018 IRM

Scram

Post Event Simulator Test

04/08/2019

2017 LORT

Written Exam

Question Usage

Biennial Written Exam Data

11/07/2019

2018 LORT

Annual Exam

Information

Tables

Annual Operating Exam Data

2/05/2019

2018 LORT

Annual Exam

Lineups

Annual Operating Exam Data

2/05/2019

2019 LORT Exam

JPM Distribution

Annual Operating Exam Data

2/05/2019

2019 NRC

Biennial Exam

Validation Matrix

Exam Validation Plan

2/05/2019

2019 Written

Exam Sample

Plan

Biennial Written Exam Data

2/05/2019

Crew and

Individual

Evaluation Forms

Various

11/06/2019

Crew E/S1 (RO

Exam)

2019 Comprehensive Biennial Written Exam

10/27/2019

Crew E/S1 (SRO

Exam)

2019 Comprehensive Biennial Written Exam

10/27/2019

ESG-LOR-10

Simulator Exercise Guide

ESG-LOR-16

Simulator Exercise Guide

ESG-LOR-21

Simulator Exercise Guide

ESG-LOR-92

Simulator Exercise Guide

Guide 1.02

Simulator Stability Test

08/27/2018

Guide 5.01

Manual Scram Transient Test

08/27/2018

Guide 5.04

Simultaneous Trip of All Recirculation Pumps

08/27/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Guide 5.08

Design Basis Accident with Loss of All Offsite Power

08/27/2018

ILT 17-1 NRC

Exam S-1

Scenario-Based Training Report

08/17/2018

ILT 17-1 NRC

Exam S-3

Scenario-Based Training Report

08/18/2018

JPM 007

Job Performance Measure

JPM 205

Job Performance Measure

JPM 215

Job Performance Measure

JPM 223

Job Performance Measure

JPM 225

Job Performance Measure

JPM 273

Job Performance Measure

JPM 277

Job Performance Measure

JPM 289

Job Performance Measure

JPM 455

Job Performance Measure

JPM 524

Job Performance Measure

Medical Records

Licensed Operator Medical Records, Various

N/A

OP-AA-105-102

Reactivation of License Log

03/26/2018

OP-AA-105-102

Reactivation of License Log

04/26/2018

OP-AA-105-102

Reactivation of License Log

09/20/2019

OP-AA-105-102

Reactivation of License Log

03/21/2018

OP-AA-105-102

Reactivation of License Log

08/21/2019

OP-AA-105-102

Reactivation of License Log

03/19/2018

OP-AA-105-102

Reactivation of License Log

09/03/2019

Simulator Work Request 133464

EC 401727 - Power Supply 1IA005 and 1IA008 (Div I) and

1IA006 and IA007 (Div 2)

08/14/2017

Simulator Work Request 133576

Loss of Div 3 Power - E22F015, E22F011 & F036 Did Not

Lose Power

09/21/2017

Simulator Work Request 133593

3D Monicore Values Do Not Match the Plant

09/26/2017

Simulator Work Request 133595

Evaluate Simulator Response to the Loss of DC MCC 1F

09/27/2019

Simulator Work Request 133598

RHR SDC Warming the RHR Loop Does Not Work Properly

09/28/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Simulator Work Request 133615

Defeating LPCS Injection Valve Seal-in Remote Does Not

Work Properly

10/05/2017

Simulator Work Request 133632

Review/Evaluate EC 402156 Turbine Testing Switch Mod for

Simulator Impacts

10/12/2017

Simulator Work Request 133661

EC 405760 - VF Mod

07/10/2018

Simulator Work Request 133690

Verify RAT B to ERAT 4160v 1B1 Bus Transfer Indications

11/02/2017

Simulator Work Request 134422

Simulator Model/Coding Leading to Some Inconsistent ANSI

Test Results

07/05/2018

Simulator Work Request 134864

RCIC Overspeed Trip

2/13/2018

Simulator Work Request 134933

OPEX: RCIC Will Not Trip on Overspeed

01/15/2019

Simulator Work Request 135258

CRD Pump Run Out After Scram Reset

05/15/2019

Simulator Work Request 135348

DFW FW003B Valve Would Not Operate in Manual

06/26/2019

Simulator Work Request 135607

Collect and Establish Baseline for Suppression Pool

Temperature

10/17/2019

Simulator Work Request 135649

Post Event Analysis of 8/3/19 Reactor Scram

11/05/2019

TQ-AA-201

Examination Security and Administration

TQ-AA-224-F-100 Remedial Training Notification and Action on Failure

10/25/2018

TQ-AA-224-F-100 Remedial Training Notification and Action on Failure

05/17/2019

TQ-AA-306-F-06

BWR Critical Conditions for Cold Startup

05/16/2018

TQ-AA-306-F-07

BWR Power Coefficient of Reactivity and Control Rod Worth

05/16/2018

TQ-AA-306-F-08

BWR Xenon Worth

05/16/2018

TQ-AA-306-F-09

BWR Site Specific Shutdown Margin and Reactivity Anomaly

Tests

05/16/2018

Training

Attendance

Records

Various

2017-2019

Procedures

TQ-AA-150

Operator Training Programs

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-306

7, Simulator SWR Prioritization

TQ-AA-306

20, Operability Testing Parameters and Criteria

Self-Assessments AR 04219981

Pre-NRC 71111.11 Inspection Licensed Operator Training

Assessment

06/05/2019

71111.11Q Procedures

CPS 3001.01

Preparations for Startup and Approach to Critical

29b

CPS 3002.01

Heatup and Pressurization

33b

71111.12

Corrective Action

Documents

AR 4083820

1VX04CA Tripped Breaker Twice

2/13/2017

AR 4263973

5050-3E Trip of Div 1 VX Cond Unit 1VX06CA

07/14/2019

AR 4283464

1E12-F004A Failed to Stroke Closed

09/30/2019

AR 4284084

Hydramotor Improperly Quarantined Prior to Failure Analysis

10/01/2019

AR 4291198

Part 21 - EMD Fuel Injectors Seized Plunger and Bushing

10/25/2019

AR 4302112

Trend IR for Appendix J failures in C1R19

2/06/2019

Miscellaneous

Failure

Classification

Form

Issue Processed in Engage Health Under ER-AA-320

Maintenance Rule 2.0 Process as per IR 4263973

09/12/2019

Failure

Classification

Form

Failure of Breaker 1AP27E3E as per IR 4083820

2/09/2018

MR Function

Evaluation

VX-00, RPC Switchgear Heat Removal System

08/07/2019

Project: CPS-

91701

Failure Analysis of Actuator, Hydramotor Model NH91 Pull

Type-Spring

10/29/2019

Procedures

CPS

1305.01F001

Type "B" Local Leak Rate Summary Sheet

Work Orders

WO 4964974

1E12F004A Failed to Stroke Closed

WR 1439180

5050-3E Trip of Div 1 VX Cond Unit 1VX06CA

71111.15

Corrective Action

Documents

AR 4281606

MCR Alarm: 5060-3E, Ground 125 Vdc MCC 1A

09/24/2019

Drawings

Drawing

E02-1DG99

Diesel Generator Sys (DG), Diesel Generator 1, Governor

Control

R

Procedures

CPS 3503.01

Battery and DC Distribution (DC)

19b

CPS

3503.01P001

Battery and DC Distribution (DC) Ground Isolation

1b

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.18

Calculations

NEDC-33903P

GNF IronClad ATF Lead Test Assembly for Clinton Unit 1

NEDC-33904P

GNF ARMOR ATF Lead Test Assembly for Clinton Unit 1

NEDO-33903

GNF IronClad ATF Lead Test Assembly for Clinton Unit 1

NEDO-33904

GNF ARMOR ATF Lead Test Assembly for Clinton Unit 1

Engineering

Changes

EC 627786

Accident Tolerant Fuel (ATF) at Clinton (IronClad and

ARMOR)

Miscellaneous

CL-2019-E-007

Use of GNF ARMOR and IronClad Lead Test Assemblies in

Clinton Cycles 20 through 22

71111.19

Corrective Action

Documents

AR 4280422

1SX014A LLRT Failure

09/18/2019

AR 4281606

MCR Alarm: 5060-3E, Ground 125 Vdc MCC 1A

09/24/2019

AR 4284526

EOID SRV 51B Actuates Instead of 41B

10/02/2019

Procedures

CPS

3506.01P001

Division 1 Diesel Generator Operations

5d

Work Orders

WO 4711141-13

Perform Valve Inspection/Replacement if Necessary of 1SX0 09/23/2019

WO 4711141-14

Perform Valve Inspection/Replacement if Necessary of 1SX0 09/22/2019

WO 4713433-01

9861.09H20 LRT SX Boundary Valve Leak Testing

(1SX014A)

09/18/2019

WO 4713433-02

9861.09H20 LRT SX Boundary Valve Leak Testing

(1SX014A)

09/18/2019

WO 4713433-03

9861.09H20 LRT SX Boundary Valve Leak Testing

(1SX014A)

09/19/2019

WO 4963565

MCR Alarm: 5060-3E, Ground 125 Vdc MCC 1A

09/26/2019

WO 4966208-02

EOID SRV 51B Actuates Instead of 41B

10/04/2019

71111.22

Drawings

Drawing

M05-1052

P&ID Shutdown Service Water (SX)

BC

Procedures

CPS 9059.01

Reactor Coolant System Leakage Test

2a

WO 4955706-01

9069.01A20 OP SX Pump Oper Test (SX Pump A)

11/20/2019

71124.06

Calibration

Records

PR-033

Primary Calibration of Station Heating, Ventilation and Air

Conditioning Exhaust Monitor

01/28/1986

Corrective Action

Documents

Resulting from

Inspection

282015

NRC ID: Discrepancy with Primary Calibration

09/25/2019

71152

Corrective Action

Documents

AR 4286915

Adverse Trend - Torque Wrenches Damaged By Excessive

Torque

10/11/2019

AR 4289680

Trend ID: Torque Wrench Damaged By Excessive Torque

10/21/2019

AR 4298901

1SX149 LPCS Pump Room Cooler Relief Valve

AR 4304484

Adverse Trend - Torque Wrench Damaged By Excessive

Torque

2/17/2019

Work Orders

WO 4925835

NRC Question: P21 Fuse

11/09/2019

71153

Corrective Action

Documents

AR 4250932

1AP07EK Main Feed Breaker Failed to Close During Bus

Shift

05/22/2019

AR 4279730

Both Division of RT Differential Flow Failed Downscale

AR 4369353

TDRFP B Turbine LVDT Failure Results in an Automatic

RPS SCRAM on RPV Level 3

Corrective Action

Program

Evaluation Report

1AP07EK Main Feed Breaker Failed to Close During Bus

Transfer

08/29/2019

Miscellaneous

PMCR Number:

90490

PM Change Review Form

PMCR Number:

90522

PM Change Review Form

Procedures

CPS 8410.12

Westinghouse Cubicle Inspection

6a

CPS

8410.21C001

Westinghouse DHP Circuit Breaker Checklist

CPS 8501.60

Bus 1A1 Main Feed Breaker Protective Relays Logic System

Functional Testing

0b

Work Orders

WO 4923911-04

1AP07EK Main Feed Breaker Failed to Close During Bus

Shift

05/23/2019

WO 4923911-05

1AP07EK Main Feed Breaker Failed to Close During Bus

Shift

05/23/2019

WO 4923911-06

1AP07EK Main Feed Breaker Failed to Close During Bus

Shift

05/23/2019