IR 05000461/2019010

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Biennial Problem Identification and Resolution Inspection Report 05000461/2019010
ML19184A105
Person / Time
Site: Clinton Constellation icon.png
Issue date: 07/02/2019
From: Kenneth Riemer
Reactor Projects Branch 1
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2019010
Download: ML19184A105 (21)


Text

July 2, 2019

SUBJECT:

CLINTON POWER STATION, UNIT 1BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000461/2019010

Dear Mr. Hanson:

On May 24, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution inspection at your Clinton Power Station, Unit 1 and discussed the results of this inspection with Mr. T. Stoner and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth Riemer, Chief Branch 1 Division of Reactor Projects

Docket No.: 05000461 License No.: NPF-62

Enclosure:

Inspection Report 05000461/2019010

Inspection Report

Docket Number:

05000461

License Number:

NPF-62

Report Number:

05000461/2019010

Enterprise Identifier: I-2019-010-0044

Licensee:

Exelon Generation Company, LLC

Facility:

Clinton Power Station, Unit 1

Location:

Clinton, IL

Inspection Dates:

May 06, 2019 to May 24, 2019

Inspectors:

J. Bozga, Senior Reactor Inspector

J. Neurauter, Senior Reactor Inspector

C. Phillips, Project Engineer

D. Sargis, Resident Inspector

Approved By:

Kenneth Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Clinton Power Station, Unit 1 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000461/2019010-01 Fuses Subject to Part 21 Potentially Installed in Safety-Related Circuits 71152B Open

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Corrective Action Program Effectiveness: Based on the samples reviewed, the team determined that the licensees performance in each of these areas adequately supported nuclear safety.

Effectiveness of Problem Identification: Overall, the stations effectiveness at identifying issues at a low threshold and properly entering them into the Corrective Action Program (CAP) as required by station procedures was inconsistent. There were several items that were not identified or were not entered into the CAP when identified. For example, non-cited violation (NCV) 2018050-02 described how between May 11 and May 17, 2018, equipment operators repeatedly failed to identify that the isolation valves from the Division 2 emergency diesel generator (EDG) air start receivers to the air start motors were locked closed and failed to identify that this made the Division 2 EDG inoperable.

In addition, NCV 2018004-02 described how the station failed to recognize the conditions present for steam voiding in the B residual heat removal (RHR) shutdown cooling return line.

After the inspectors brought this to the licensee's attention, the licensee wrote Action Request (AR) 4166749, NRC Question on Potential Voiding of Piping Near 1E12F053B, in response to the inspectors questions. The station evaluated the condition in EC 625392, Evaluation of Potential Voiding of RHR [residual heat removal] B Shutdown Cooling Injection Line, and determined that a void would be present if the body-to-bonnet leak worsened or if the system depressurized as it would during shutdown and cooldown.

Also, NCV 2019011-01 described how station procedures Clinton Power Station (CPS) 4402.01 and CPS 4407.01 did not ensure the high pressure core spray system and the suppression pool would remain available for decay heat removal for the duration of a station blackout event. This was identified by an NRC engineering team and was communicated to the licensee who then had to be prompted by the NRC team on more than one occasion before it was finally entered into the CAP.

Finally, AR 4172856, NRC Observation, dated September 13, 2018, documented an NRC observation that a ladder was tied off to safety-related service water piping that was under 4 inches in diameter with no evaluation. This was not allowed without an evaluation per CPS 1019.05, Appendix C. The inspectors identified this as a concern and it took additional questions and prompting before the licensee identified this as a problem that needed to addressed through CAP. This issue was not documented in a previous NRC inspection report because it was considered a minor performance deficiency when a further evaluation determined it was acceptable to tie off the ladder to the pipe.

Effectiveness of Prioritization and Evaluation of lssues: ln-depth reviews of a risk-informed sampling of ARs, work orders (WOs), and cause evaluations were completed, including a 5-year time period for the Division 1 EDG. The team determined that the issues were generally being appropriately prioritized and evaluated for resolution. There were, however, examples of where the NRC identified flaws in the licensee's methods of evaluation. On September 13, 2018, the licensee performed a water hammer evaluation to determine whether voiding in the RHR shutdown cooling injection line would impact operability. The evaluation was documented in Engineering Change (EC) 625522, Evaluation of Water Hammer Forces From Potential Voiding in RHR Shutdown Cooling Injection Line. Based on the evaluation the licensee concluded the resulting water hammer event would be 10 pound-force (lbf), which was within the capability of the piping and support structures. Therefore, the licensee concluded there was no impact to operability, and operations removed the item from the potential limiting condition for operation list. The inspectors reviewed the calculation and identified multiple deficiencies that significantly impacted the conclusion reached by the licensee. Subsequently the licensee performed a more detailed evaluation that concluded the resulting water hammer event would be approximately 4600 lbf. Though the calculated margin from the initial evaluation was significantly reduced, the conclusion of the second evaluation was still within the capability of the system. The inspectors reviewed the updated calculation and did not identify any additional deficiencies. This performance deficiency was also described in NCV 2018004-02.

The inspectors reviewed the licensees evaluation of low pipe wall thickness readings on the A minimum flow line of the RHR system documented in AR 04133436, Low Thickness Readings Discovered On A RHR Minimum Flow Line, dated May 2, 2018. Specifically, the licensee performed EC 624133, Evaluate RHR A Minimum Flow Line Wall Thinning, Revision 1, to demonstrate operability of this piping and concluded that the piping met the design basis and American Society of Mechanical Engineers (ASME) code requirements. However, the inspectors identified that in EC 624133 the licensee calculated an average pipe section modulus around the pipe circumference at the location of low pipe wall thickness readings used to further calculate pipe stress. In addition, the inspectors did not identify specification of an average section modulus to calculate pipe stress in the ASME code. The licensee entered the concern into the CAP as AR 04250898, PI&R Inadequate Methodology in EC 624113, dated May 22, 2019, that indicated using an average section modulus to calculate pipe stress was not a methodology recognized by the ASME code. In addition, AR 04250898 documented reasonable assurance that the A minimum flow line of RHR system was operable by using pipe stress acceptance criteria in Appendix F of Section III of the ASME code in comparison to pipe stress conservatively factored to account for wall thinning. Section C.11 of NRC Inspection Manual Chapter 0326, Operability Determinations & Functionality Assessments for Conditions Adverse to Quality or Safety, issued November 20, 2017, documents the licensee may use criteria in Appendix F for piping and piping support operability determinations. This was considered a minor performance deficiency.

The inspectors reviewed the licensees evaluation associated with snubber 1RT01003S failed function test documented in AR 04011410, Mechanical Snubber 1RT01003S Failed Function Test, dated May 16, 2017. Specifically, snubber 1RT01003S failed its drag test and was found locked in the hot setting position. The licensee performed EC 619714 to evaluate the effect of this additional restraint to ensure the piping system was not overstressed. The inspectors noted that EC 619714 did not consider the effect of thermal binding during system cooldown on pipe stress and support loads as the as found snubber did not return to its cold setting. The licensee entered the concern into the CAP as AR 04251430, Failed Snubber Evaluation Inadequate, dated May 23, 2019, that documented immediate corrective action that evaluated the condition and concluded no stress limit was exceeded. Since failed snubber 1RT01003S was replaced, the inspectors also reviewed the licensees associated VT-3 visual examination reports and verified no relevant / recordable indications were identified for the restraint. This was considered a minor performance deficiency.

Effectiveness of Corrective Actions: The team concluded that the corrective actions that were implemented were neither consistently robust nor consistently completed. For example, in 2017 and early 2018 the licensee took actions to address a declining trend in human performance errors. The inspectors reviewed those corrective actions and documented the results in NRC inspection report 2018003. In May 2018 at least six separate procedure errors resulted in the Division 2 EDG remaining unavailable when it was being depended upon for plant safety. This was documented in NCV 2018050-01 which became a White finding. Predominately because of this event the inspectors found the licensees previous corrective actions regarding human performance to be ineffective. Since that event the licensee has taken more robust corrective actions in regard to human performance. There have been fewer human performance events since the implementation of these new corrective actions.

The inspectors reviewed AR 04073056, Identified USFAR [updated final safety analysis report]

Chapter 10 Discrepancies Still in USAR [updated safety analysis report], dated November 9, 2017. This AR documented that actions to prepare a change package to Chapter 10 of the UFSAR had twice been generated and twice closed out without actually being performed. The change to Chapter 10 of the UFSAR was in the review process but was not implemented as of May 9, 2019. This was considered a minor performance deficiency.

The inspectors reviewed AR 04168460, DAC [derived air concentration] Value Discrepancy Discovered in Countroom Software, dated August 30, 2018. The licensee identified that the DAC values in countroom software, used to determine if a potentially airborne work area should be posted or not, did not match the inhalation DAC table values in accordance with Title 10 of the Code of Federal Regulations (CFR), Part 20, for two radio-nuclides. The licensee performed hand calculations to verify that the room was not required to have been posted as an airborne area. A follow-up action was to go and verify that the other values in the software matched 10 CFR Part 20 values. The licensee found about 35 more radio-nuclides whose software value did not match 10 CFR Part 20 but did not go and do hand calculations for previous samples to determine if they had required posting. The licensee has since performed those hand calculations with no issues identified. Questions regarding this issue resulted in finding a similar issue in AR 02620909, 10CFR20 Inhalation DAC Value For KR-85M Found Incorrect, dated February 2, 2016. An action that came from AR 02620909 was to validate the entire library for additional errors. This was marked as complete in March 2016 but was never actually accomplished. This was documented in AR 04247547 and was considered a minor performance deficiency.

The inspectors reviewed AR 4017613, Welding Cables Through Both RT [reactor water clean up] Pump Room B Doors, dated June 2, 2017, which documented that welding cables were running through both secondary containment doors while in mode 2 ( NCV 2017003-05). The corrective actions were assignments -34 and -35 which were to complete a read and sign for all schedulers and planners on the plant barrier impairments (PBI) procedure and its interaction with the work process. The effectiveness was measured with action -42. The corrective actions (CAs) failed the first effectiveness review (EFR) as documented in AR 4062608, EFR for CAPE [corrective action program evaluation] 4017613, dated October 13, 2017. This AR documents that the EFR was done in the same month the corrective action was closed.

Therefore, the licensee should have given it more run time, and the licensee re-performed the EFR two months after the CA was closed. Action request 4073308, Effectiveness Review Results For AR 4062608, dated November 10, 2017, documented that the second EFR determined that the CA was ineffective. This time the licensee created a new CA that evaluated the PBI process and implemented actions to resolve the need for emergent PBI requests. The EFR was completed SAT for this CA. The original actions (-34 and -35) were not robust and only addressed the work planners. The later CAs took a larger view of the PBI process and addressed the issue at the shop level and maintenance planner level.

Operating Experience (OpE) and Self-Assessments and Audits: The team concluded that the licensee was generally effective in the use of OpE in the CAP, self-assessments and audits.

The team determined that when performing causal analysis and determining CAs that OpE was routinely utilized. ln addition, the team sampled OpE from NRC, industry, vendors, and third party groups and determined that for the samples selected that appropriate assessments for applicability to the licensee were performed.

Safety Conscious Work Environment: The team found evidence that the licensee's safety conscious work environment (SCWE) was appropriate. The licensee's employees appeared willing to raise nuclear safety concerns through at least one of several means available. The team observed various station meetings, including those in which new CAP items were reviewed, and interviewed a representative cross-section of station personnel, both individually and small groups. Additionally, the team assessed the overall health of the Employee Concerns Program. Specifically, the team interviewed the Employee Concerns Coordinator, reviewed recent case logs and case files and considered statement received during interviews with station personnel.

Unresolved Item (Open)

Fuses Subject to Part 21 Potentially Installed in Safety-Related Circuits05000461/2019010-01 71152B

Description:

On August 23, 2018, the NRC received a 10 CFR Part 21 notification (Part 21) under LER 05000440/2018-002-00 (ML18236A294). The Part 21 report described a manufacturing defect of Gould Shawmut TR30R fuses. The Part 21 described that the fuse internals had separated from one another indicating that they were under tension. The tension was likely placed on the fuse during manufacturing when the ferrule ends of the fuse were crimped onto the fuse barrel. The Part 21 identified that the fuse had failed even though it was never exposed to an electrical current large enough to have failed the fuse.

The licensee initiated an action under AR 04061497-77, 10 CFR Part 21 Applicability Determination, dated September 25, 2018, to perform a Part 21 applicability determination for Clinton Power Station because Clinton was not specifically named in the Part 21. The licensee identified that they had purchased Gould Shawmut TR30R fuses, commercially dedicated them, and installed them in the plant. The licensee believed that the Part 21 would not affect the plant because the fuses purchased were commercially dedicated, checked for ferrule tightness, and checked for resistance. The licensee failed to generate a site specific AR with actions for supply and engineering to evaluate the impact to the station. As a result, the licensee failed to evaluate fuses installed during initial construction, failed to evaluate the impact on operability, and failed to determine if the commercial grade dedication process was adequate to identify this failure mechanism. The above failures were self-imposed standards, not regulatory requirements, and were of minor significance.

The inspectors questioned the adequacy of the licensee's determination that the Part 21 does not affect the site and identified that the licensee did not generate a site specific AR as required by their operating experience procedure. The licensee placed the issue in the corrective action program and evaluated the impact of the fuses. The licensee determined that the fuses identified in the Part 21 were from Lot number E-64. The fuses the licensee has installed in the plant were not from this lot, but the licensee did not know if the fuses originally installed in the plant were from lot E-64. The licensee identified that there were five locations in which a failure of the fuse would result in a partial loss of safety function.

This is an unresolved item. In order to resolve this issue, the inspectors need to know whether fuses from lot E-64 were installed in safety-related circuits.

Planned Closure Actions: The inspectors need to know if any of the fuses from lot E-64 are installed in safety-related circuits. The licensee plans to visually inspect each circuit that could contain the affected fuses. The inspectors will evaluate the results of the inspection and determine if a violation existed.

Licensee Actions: The licensee plans to determine if the affected lot of fuses were installed in the plant. The licensee plans to visually inspect each location that this type of fuse is installed.

If any fuses from the affected lot are identified, the licensee plans to replace those with fuses that were not from the affected lot.

Corrective Action References: AR 04250520, NRC Question: P21 Fuse, dated May 5, 2019 AR 04251536, Part 21 Assessment Results for TR30R Fuses, dated May 24,

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On May 24, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Mr. T. Stoner and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Calculations

IP-M-0513

Division I, II and III SX Pipe Wall Thinning Analysis Including

RHR Piping

0W

Corrective Action

Documents

04034973

Oil Leak From 1SX01PA

07/24/2017

AR 02385999

1DG005A Relief Valve Lifting Repeatedly

09/25/2014

AR 02490408

Reactor SCRAM from Trip of 1AP07EJ

2/09/2017

AR 02592592

1DG005A: Relief Valve Lifting Repeatedly

11/25/2015

AR 02595942

NCV 2015003-03, Failure to Obtain Lic Amend on Sec Cnmt

Mod

2/04/2015

AR 02596437

Upper Bearing Oil Cooler Leak

2/06/2015

AR 02598117

1WS01PB, WS 'B' Lower Bearing Oil Level Sightglass Full

2/09/2015

AR 02620909

10CFR20 Inhalation DAV Value for KR-85M Found Incorrect

2/02/2016

AR 02644384

OPEX Evaluation: IER L3-16-6, Control Rod Drive Vent Plug

Leakage Concern

03/23/2016

AR 02649780

RAT 4538 Failure: Numerous Unexpected Alarms 5010-1A,

1C, 8A

04/02/2016

AR 02654953

1FW01PB (TDRFP B) Vibration has Continued to Degrade

04/13/2016

AR 02667822

Unexpected Alarms 5050-1F/2F and 1VH01CA Trip

05/10/2016

AR 02675486

1WS01PB, WS Pump B Leaking from Upper Bearing

05/30/2016

AR 02704548-04

NRC Information Notice 2016-11: Potential for Material

Handling Events to Cause Internal Flooding

11/14/2016

AR 02742442

CDBI: Inappropriate Calculation Method for CR Habitability

11/17/2016

AR 03950913

WS Requires Maintenance Rule (A)(1) Evaluation

01/09/2017

AR 03962443-97

CFR Part 21 Applicability Determination

10/12/2017

AR 03978324

Lost 138KV Feed Causing ERAT Transient

2/24/2017

AR 04006988

OPEX Evaluation: NRC IN 2017-01, Reactor Coolant System

Leakage from a Control Rod Drive Threaded Connection

05/05/2017

AR 04007861

Entered 4008.01 and 4002.01 Due to FCV Runback

05/07/2017

AR 04009845

PSU: C1R17 MSIV LLRT [local leak rate test] Tech Spec 3.6.1.3 Limit Exceeded

05/12/2017

AR 04011410

Mechanical Snubber 1RT01003S Failed Function Test

05/16/2017

AR 04015342

NRC Identified Two Issues Regarding Snubber Testing

05/26/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 04016563

Automatic Reactor Scram

05/30/2017

AR 04017613

Welding Cables Through Both RT Pump Room 'B' Doors

06/02/2017

AR 04022757-02

NRC Information Notice 2017-03 Anchor Darling Double Disc

Gate Valve Wedge Pin and Stem-Disc Separation Failures

08/19/2017

AR 04044082

OPEX Review: NRC IN 2017-04, High Energy Arcing Faults in

Electrical Equipment Containing Aluminum Components

08/21/2017

AR 04049063

OPEX Evaluation: IN 2-17-05, Potential Binding of Schneider

Electic/Square-D Master Pact 480-VAC Circuit Breaker Anti-

Pump Feature

09/05/2017

AR 04052455

CFR Part 21 Update Regarding Grayboot Socket Contacts

09/15/2017

AR 04052639

Gothic V8.1 and V8.2 Computer Code Errors Potential Part 21

08/22/2017

AR 04054180

Follow Up on Overall Strategy for 1CC103 Leak

09/20/2017

AR 04055133

Valve 1IA128B Failed Seat Leakage Test

09/23/2017

AR 04056394

2017PIR 4410.00C001 Needs 50.59 Screening

09/27/2017

AR 04061340

Part 21 For HMA Relay Potentially Applicable

10/10/2017

AR 04061497-77

CFR Part 21 Applicability Determination

09/25/2018

AR 04062608

EFR for CAPE 4017613

10/13/2017

AR 04066250

OPEX Level 3 Review - NRC IN 2017-06, Battery and Battery

Charger Short-Circuit Current Contributions to a Fault on the

Direct Current Distribution System

10/24/2017

AR 04069750

BRE [bullet resistant enclosure] Energized Power Plug

11/01/2017

AR 04069935

MCR [main control room] Unexpected Alarm 5067-3F MS

[main steam] Line Radiation High

11/02/2017

AR 04071277

ERAT SVC [static variable compensator] Tripped Due to

Substation Breaker Cycling

11/05/2017

AR 04072627

Shephard Calibrator Interlocks not Functioning as Designed

11/08/2017

AR 04073308

Effectiveness Review Results for AR 4062608

11/10/2017

AR 04075431

NCV 2017007-01 Fail to Eval Defeating RCIC Interlocks/Trips

11/16/2017

AR 04075432

NCV 2017003-05 Entered Mode 2 While Secondary

Containment Inop

11/16/2017

AR 04075433

NCV 2017003-01 Condition Based Maint Approach On MSIV

[main steam isolation valve] Leakage

11/16/2017

AR 04075433

NCV 2017003-01 Condition Based Maint Approach on MSIV

Leakage

11/07/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 04075435

NCV 2017-003-03, Fail to Perform Engineering Evaluation for

Snubber Failure

11/16/2017

AR 04075436

NCV 2017003-04 RR Pump Runback Due to FCVs not Locked

Out

11/16/2017

AR 04075581

IP 92723 - Inadequate Extent of Condition on NCV 2016002-

11/16/2017

AR 04075779

RHR A & B Min Flow Piping Removed From C1R18 Scope

11/17/2017

AR 04080756

SEC ID-Camera 37 Loss of Coverage

2/04/2017

AR 04081583

Potential NRC SL IV Violation for Time to Boil 72.48 Screen

2/06/2017

AR 04084004

SEC ID: EVD#2 Failed Testing

2/14/2017

AR 04089480

Failure to Implement CAPR [corrective action to prevent

recurrence] At First Available Opportunity

01/02/2018

AR 04096509

RCIC PCIV 1E51-F064 Isolated During 9030.01 Surveillance

01/24/2018

AR 04099250

NRC FIN 2017012-02 Fail to Prop Classify NSR Aux

Transformer

01/30/2018

AR 04102073

CFR Part 21 - NRC Log 2017-55 - SOR

2/08/2018

AR 04105979

NRC NCV 2017004-02 Failure to Assess and Manage Risk

2/20/2018

AR 04105980

NRC NCV 2017004-003, Failure to Perform an Extent of

Condition

2/20/2018

AR 04105981

NRC SL IV NCV 2017004-04, URI 72.48 Time-to-Boil

Calculation Closed

2/20/2018

AR 04107258

NRC Information Notice: IN 2018-01, ISFSI Noble Gas

Releases

2/23/2018

AR 04108860-02

NRC 2018-002 Target Rock 3-Stage SRV Model 0867F

Degredation

07/13/2018

AR 04111775-05

Information Notice (IN) 2018-04: Operating Regarding Failure

of Operators to Trip the Plant when Experiencing Unstable

Conditions

06/27/2018

AR 04125651

Part 21 - Potential Failure of Reverse Power Relays

04/11/2018

AR 04128705

1VT02A Cooling Coil has Cracked Tube

04/19/2018

AR 04130828

NRC Question on Last Performance of 9861.09D006

04/25/2018

AR 04131749

NRC NCV 2018001-01 Failure to Follow Procedure Isolates

RCIC

04/27/2018

AR 04133436

Low Thickness Readings Discovered on A RHR Minimum

05/02/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Flow Line

AR 04134393

1VH01CA SX Pump Room A Area Cooler Tripped

05/04/2018

AR 04134785

Low Thickness Readings Discovered on B RHR Minimum

Flow Piping

05/05/2018

AR 04137003

Rejected Weld Indication During Radiography B RHR Piping

05/12/2018

AR 04137330

9861.02D017, Leakage Needs Evaluated, RCIC Steam Supply

05/14/2018

AR 04139396

9861.09 and Data Sheets - SX Boundary Leak Test Procedure

Changes

05/20/2018

AR 04140601

Steam Leak in 6 Pipe Elbow on 1GS15B

05/23/2018

AR 04143037

Piping Upstream of 1CC103 Still Leaking after Maintenance

05/31/2018

AR 04151429

L3 OPEX Evaluation Results - Battery Charger Fault

Contribution

06/28/2018

AR 04156632

NRC IN 2018-07: Pump/Turbine Bearing Oil Sightglass

Problems

07/18/2018

AR 04160873

RPID: TSP 2017-67 Needs to Remain in Place Permanently

08/01/2018

AR 04161074

RPID: Increased Dose Rates On WZ Piping

08/02/2108

AR 04162483

NRC NCV 2018002-02, Fail to Establish Adequate Leak Test

Procedure

08/07/2018

AR 04163523

NRC IN 2018-09: Electric Arc Flash Caused by Foreign

Material Damages Fire Door

08/11/2018

AR 04164644

UT Pipe Wall Thinning at 4 Elbow of Pipe of 1SX21AB

08/15/2018

AR 04164975

UT Indicates Pipe Wall Tinning at 24 Pipe of 1WS14A

08/16/2018

AR 04166724

Leak Identified on 1DG155 Flanged Joint

08/23/2018

AR 04166725

Leak Identified on 1DG04TA Threaded Joint

08/23/2018

AR 04166730

Packing Leak on 1DG011A

08/23/2018

AR 04166731

Two Threaded Joint Leaks Found on 1DG169

08/23/2018

AR 04168460

DAC Value Discrepancy Discovered in Countroom Software

08/30/2018

AR 04172921

UT Pipe Wall Thinning at 4 Elbow of Pipe 1SX21AA

09/13/2018

AR 04173375

UT Pipe Wall Thinning on 2-1/2 Pipe 1WSB9W

09/14/2018

AR 04177094

NRC Information Notice: IN 2018-11, Kobe Steel Quality

Assurance Falsification

09/26/2018

AR 04177203

Interruption In 138 KV Line Service to CPS ERAT [emergency

reserve auxiliary transformer]

09/26/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 04179395

NRC NCV 2018412-01 Fail to Search All Areas of a Vehicle

10/02/2018

AR 04180603

NRC IN 2018-03 - Failure to Meet TSs for Changing Plant

Conditions

10/05/2018

AR 04188313

Evaluate RHR A SDC Temperature Transient

10/27/2018

AR 04188538

Reactor Scram on High IRM Flux

10/28/2018

AR 04194966

Part 21 - Notification of Dry Type Transformer S/N 24-26458

11/14/2018

AR 04199126

NRC NCV 2018041-02, Fail to Establish Acceptance Criteria

for Component Performance Monitoring

11/30/2018

AR 04202559

Division 2 Diesel Generator 1DG01KC Oil Cooler Leak (Oil)

2/12/2018

AR 04203045

Improve Rounds Point for Division 3 EDG

2/14/2018

AR 04206548

Small Oil Leak on Division 3 DG AC Circ LO Pump 1DG616PA

2/29/2018

AR 04208699

Division 2 DG Governor Oil Leak

01/07/2019

AR 04208701

Division 2 DG 26 Cyl AC Circ Oil Pump Leak

01/07/2019

AR 04208708

Oil Leak from Casing of 1DG16A

01/07/2019

AR 04208712

1DG628PA Oil Leak from Fitting

01/07/2019

AR 04208720

Oil Leaking from Fitting on 1DG605PA

01/07/2019

AR 04209422

Division 1 DG 12 Cyl LO Filter Leak

01/09/2019

AR 04209427

Division 1 DG 16 Cyl Crankcase Seal Leak

01/09/2019

AR 04211426

Oil Leaking from Division 1 DG Oil Cooler Flanges

01/16/2019

AR 04212873

SEC ID: Contingency Weapon Left Unattended in the OCA

[owner controlled area]

01/22/2019

AR 04216769

1DG622PA Has Small Oil Leak

2/03/2019

AR 04218343

SEC ID: Security Fencing Needs Repair

2/08/2019

AR 04220198

NRC NCV 2018004-04 Fail Follow Proc. Resulting CRD Pump

Trip

2/14/2019

AR 04220199

NRC NCV 2018004-03, Fail to Include Acceptance Criteria for

Division 3 EDG

2/14/2019

AR 04220200

NRC NCV 2018004-02-Fail to ID a Degraded Cond. in RHR B

2/14/2019

AR 04220201

NRC NCV 2018004-01 Fail to Prevent Instal of Non-Conf.

Parts

2/14/2019

AR 04220251

NOS ID: Combustible Material Less than 3 Feet from a SWGR 02/14/2019

AR 04220260

NOS ID: Wrong PIDS Methodologies Used for Testing

2/14/2019

AR 04221273

Several Throughwall Pinhole Leaks Downstream of 1SX013D

2/18/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 04225272

Request for Decon of the Spent Resin Pump Room

03/01/2019

AR 04227872

UT Pipe Wall Thinning of 3 Pipe of 1SX29BB

03/08/2019

AR 04229909

UT Indicates Pipe Wall Thinning at 8 Pipe of 1SX04AC

03/15/2019

AR 04231145

SX Piping Mitigation Strategy Review

03/20/2019

CAPE 04012075

Workers Enter Incorrect Elevation of the Drywell Bioshield

06/22/2017

CAPE 04181437

October Trip of Reserve Auxiliary Transformer (RAT) Static

VAR Compensator (SVC)

2/05/2018

CAPE 4017613

Secondary Containment ITS Violation

06/28/2017

CAPE 4096509

RCIC PCIV 1E51-F064 Isolated During 9030.01 Surveillance

2/28/2018

CAPR 03982792-

Modify VC Load Shedding Wiring 0AP06E (EC 625821)

2/13/2018

CAPR 03982792-

Modify VC Load Shedding Wiring 0AP05E (EC 625820)

2/26/2019

ECAP 02667822

Unexpected Alarms 5050-1F/2F and 1VH01CA Trip

06/01/2016

ECAPE 04148838 High Pressure Core Spray (HPCS) 1E22-F004 Valve Found

Open

09/21/2018

RCR 04016563

Automatic Reactor Scram

07/20/2017

RCR 04082490

Transformer Failure Results in Trip of 4160V 1A1 Breaker

1AP07EJ and Loss of Power to 480V Unit Substation A

(0AP05E) and 480V Unit Substation 1A (1AP11E)

10/04/2018

RCR 4188538

IRM Scram

2/14/2018

Corrective Action

Documents

Resulting from

Inspection

AR 04247254

NRC ID: Gaps Associated with Actions Under 4073308

05/08/2019

AR 04247547

NRC ID: Ineffective Action Closure

05/08/2019

AR 04247831

NRC PI&R RHR Area Walkdown Issues

05/09/2019

AR 04248044

PI&R Identified Min Wall Reading on 1SX21AB Below

Allowable

05/10/2019

AR 04248056

PI&R WO Acceptance Criteria Not Per Calc

05/10/2019

AR 04248079

PI&R 1SX21AB-4 Replacement Not Scheduled

05/10/2019

AR 04249310

NRC ID: Root Cause Report 401653 Process Weakness

05/15/2019

AR 04249310

NRC ID: Root Cause Report 4016563 Process Weakness

05/15/2019

AR 04249610

NRC ID: IR 4180203 Should be Sig Level 3D

05/16/2019

AR 04250520

NRC Question: P21 Fuse

05/20/2019

AR 04250898

PI&R Inadequate Methodology in EC 624113

05/22/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 04251096

Tracability of Fuses Issued to Ops and IMD

05/22/2019

AR 04251113

PI&R Identified Violation Actions Inadequate

05/22/2019

AR 04251114

NRC ID: Min Wall Calcs Extent of Condition

05/22/2019

AR 04251430

Failed Snubber Evaluation Inadequate

05/23/2019

AR 04251536

Part 21 Assessment Results for TR30R Fuses

05/24/2019

Engineering

Changes

EC 350224

Evaluation of Proposed Heatup/Startup of RHR in Shutdown

Cooling

Revision 1

EC 438722

1SX01PC Pump Acceptance Criteria, Motors Amps and

Coastdown Time

2/05/2019

EC 619936

Endorsement and Application of GE Analysis for OPRM

Setpoint Change

03/07/2018

EC 621828

Replace Springs with Temporary Struts on RT Lines in the

Drywell (1RT01004C and 1RT01014C)

EC 625392

Evaluation Of Potential Voiding In RHR B Shutdown Cooling

Injection Line

Revision 0

Engineering

Evaluations

EC 619714

Snubber (1RT01003S) Failure Evaluation of Snubber

Inspection Program

EC 624113

Evaluate RHR A Minimum Flow Line Wall Thinning

Miscellaneous

AR 04005206-02

RP OE: Loss of Radiation Monitoring Equipment Due to Loss

of 23kV Station Service

06/21/2017

AR 04009125-02

  1. 407927 OE - Equipment Misoperation - Event Final Complete

Last Updated: 2017-05-05 Sequoyah

06/26/2017

AR 04111775-05

Information Notice 2018-04: Operating Regarding Failure of

Operators to Trip the Plant When Experiencing Unstable

Conditions

06/27/2018

AR 04138790

Root Cause Report for Division 2 Emergency Diesel Generator

Air Receivers Found Isolated During Rounds

06/26/2018

AR 4008122-02

Exelon Nuclear Event Report (NER) AC-17-001, Reactor

Protection System B Half SCRAM (Blown Fuse Investigation)

06/21/2017

AR 4053493-35

ICES # 431701 Indian Point Unit 3 Automatic Trip Due to A

Loss of Main Generator Excitation

06/13/2019

AR 4117076

  1. 432283 Loss of Instrument Air Due to Dryer Valve Failure

07/16/2018

C1R17-419

VT-3 NDE Report, Component 1RT01003S

05/11/2017

C1R17-529

VT-3 NDE Report, Component 1RT01003S

05/15/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Event Number:

2736

Part 21 - Interim Notification of a Potential Defect on a Printed

Circuit Board

06/23/2017

LER

05000440/2018-

2-00

Part 21 - Failed Fuse Leads to Loss of Safety Function

08/23/2018

LER

05000461/2017-

009-00

Trip of Emergency Reserve Auxiliary Transformer Static VAR

Compensator Causes Positive Secondary Containment

Pressure Following Voltage Transient on 138kV Offsite Source

01/04/2018

LER

05000461/2018-

001-00

Degraded Personnel Airlock Interlock Results in Loss of

Primary Containment

05/29/2018

LER

05000461/2018-

003-01

Load Driver Card Failure Resulting in High Pressure Core

Spray Inoperability

06/20/2018

LER

05000461/2018-

005-02

Unplanned Reactor Scram During Maintenance Outage Due to

High Intermediate Range Monitor Flux

04/24/2019

M-1RT01003S

Support/Hanger Drawing

F

N/A

CFR Part 21 Curtiss-Wright Grayboot Socket Contacts

06/21/2017

NSED Review

95012

Commercial Grade Dedication Summary

Revision 1

Operability

Evaluations

EC 620644

Oil Leak From Div 1 SX Motor

Revision 2

Procedures

CPS 9431.26

OPRM Channel Calibrations

Revision 39c

CPS 9861.09

Shutdown Service Water Boundary Valve Leak Testing

08/29/2018

ER-AA-335-016

VT-3 Visual Examination of Component Supports,

Attachments, and Interiors of Reactor Vessels

ER-CL-300

Clinton Power Station Snubber Program

LS-AA-107

UFSAR/FPR [fire protection report] Update Procedure

Revision 12

MA-CL-0001

Fuse Program Guidance

Revision 3

NES-MS-03.1

Piping Minimum Wall Thickness Calculation

NES-MS-03.2

Evaluation of Discrepant Piping and Support Systems

NO-AA-10

Quality Assurance Topical Report (QATR)

Revision 94

OP-AA-108-115

Operability Determinations

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PI-AA-115-1003

Processing of Level 3 OPEX Evaluations

Revision 5

PI-AA-120

Issue Identification and Screening Process

Revision 8

PI-AA-125

Corrective Action Program (CAP) Procedure

Revision 6

PI-AA-125-1001

Root Cause Analysis Manual

Revision 3

PI-AA-125-1003

Corrective Action Program Evaluation Manual

PI-AA-125-1006

Investigation Techniques Manual

Revision 4

Self-Assessments

AR 04047344

Perform Self-Assessment Operational Decision Making

(ODMs) Closed Prior Year (Last 12 Months)

2/07/2017

AR 3950645-02

Maintenance Role In Work Management

01/26/2017

AR 4014949

Nuclear Oversight Audit Report - Engineering Design Control

08/01/2017

AR 4030936

FIN Team Process Compliance Self-Assessment

10/12/2017

AR 4099631

Control of Quality Parts

2/28/2019

AR 4103467

MP Use of Work Package Quality Verification Checklist

09/12/2018

AR 4106025

2018 Clinton Clearance and Tagging Self-Assessment

01/18/2018

AR 4108988

Clinton Reactivity Management

08/31/2018

AR 4114268

Nuclear Oversight Audit Report - Engineering Programs and

Station Blackout

04/11/2018

AR 4209487

Nuclear Oversight Audit Report - Materials Management and

Procurement Engineering

2/06/2019

NOSA-CPS-17-06

(AR 4014520)

Radiation Protection Audit Report

07/18/2017

NOSA-CPS-17-08

(AR 04039870)

Clinton Operations Audit

08/07/2017

NOSA-CPS-19-02

(AR 4209506)

Security Programs Audit Report

2/20/2019

Work Orders

WO 01136842-02

Replace 1SX29BB-3 Piping

04/14/2009

WO 01136842-07

Coat Inside of Pipe 1SX29BB

04/13/2009

WO 01230598-02

1E12D001A, Fabricate New Orifice Plate

09/17/2013

WO 01230598-13

1RH198BA, Coat Prefabricated Piping Spools

04/16/2015

WO 01230598-30

1E12D001A, Fabricate New Orifice Plate

04/20/2015

WO 01865591-01

NDE Ultrasonic Examination, 1SX29BA-3 Piping Downstream

of 1SX23M Division 1 Orifice

03/24/2017

WO 01872658-19

Install New Upper Motor Oil Cooler

04/06/2016

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO 01898016

Model Work Order, Measure Motor Amps and Coastdown

Time

WO 01923407-02

Replace Overload Relays

05/03/2016

WO 01923407-03

Operations Post Modification Test Run 1VH01CA IAW 3405.01 05/11/2016

WO 04646520

Update OPRM Setpoints Per EC 619936

10/19/2017

WO 04680029-89

T-MOD, Install Rigid Strut on 1RT01004C

05/01/2018

WO 04680029-90

Remove Temporary Rigid Strut / Restore Support 1RT01004C

05/12/2018

WO 04680029-97

T-MOD, Install Rigid Strut on 1RT01014C

05/01/2018

WO 04680029-98

Remove Temporary Rigid Strut / Restore Support 1RT01014C

05/12/2018

WO 04766924

Containment 828 Personnel Airlock Interlock Failure

03/30/2018

WO 04772358

1PL12JA GGP Relay Holding Coil Potential Deficiency

05/24/2018

WO 04798571-11

Replace High Pressure Core Spray Load Driver 1H13-P663-

A16-A123

06/21/2018

WO 04798571-16

Replace High Pressure Core Spray Driver 1H13-P663-A16-

A121

06/22/2018

WO 04838315-01

Modify VC Load Shedding Wiring, 0AP05E (EC625820)

2/22/2019

WO 04838315-02

Post Modification Testing, DC Control Circuit Ground

Verification, 0AP05E (EC 625820)

2/23/2019

WO 04838315-03

Post Modification Testing, Test of 480V Bus A Sequencing,

0AP05E (EC 625820)

2/23/2019

WO 04838315-06

Operations Post Modification Testing, 0AP05E (EC 625820)

2/23/2019

WO 04846440

1WSB9A: Trend in UT Results Indicate Pipe Replacement

Needed

05/19/2019

WO 04847239-01

Modify VC Load Shedding Wiring, 0AP06E (EC 625821)

2/07/2018

WO 04847239-02

Post Modification Testing, DC Control Circuit Ground

Verification, 0AP06E (EC 625821)

2/08/2018

WO 04847239-03

Post Modification Testing, Test of 480V Bus A Sequencing,

0AP06E (EC 625821)

2/08/2018

WO 04847239-06

Operations Post Modification Testing, 0AP06E (EC 625821)

2/10/2018

WO 04864828-01

0AP117E, Inspect/Clean ERAT SVC Fans and Filter

03/26/2019

WO 04866066-01

Measure Motors Amps and Coastdown Time

03/16/2019