IR 05000346/2020003
| ML20318A039 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 11/12/2020 |
| From: | Billy Dickson NRC/RGN-II/DRP/RPB2 |
| To: | Tony Brown Energy Harbor Nuclear Corp |
| References | |
| IR 2020003 | |
| Download: ML20318A039 (16) | |
Text
November 12, 2020
SUBJECT:
DAVIS-BESSE NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000346/2020003
Dear Mr. Brown:
On September 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Davis-Besse Nuclear Power Station. On October 23, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding did not involve a violation of NRC requirements.
If you disagree with a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Davis-Besse Nuclear Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Billy C. Dickson, Jr, Chief Branch 2 Division of Reactor Projects
Docket No. 05000346 License No. NPF-3
Enclosure:
As stated
Inspection Report
Docket Number:
05000346
License Number:
Report Number:
Enterprise Identifier: I-2020-003-0025
Licensee:
Energy Harbor Nuclear Corp.
Facility:
Davis-Besse Nuclear Power Station
Location:
Oak Harbor, OH
Inspection Dates:
July 01, 2020 to September 30, 2020
Inspectors:
J. Harvey, Resident Inspector
D. Mills, Senior Resident Inspector
R. Ruiz, Project Engineer
Approved By:
Billy C. Dickson, Jr, Chief
Branch 2
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Davis-Besse Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Failure to Install Adequate Fuses Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000346/2020003-01 Open/Closed None (NPP)71153 A finding of very low safety significance (Green) was self-revealed when the licensee was required to manually trip the reactor after a loss of two reactor coolant pumps (RCP) due to a failed fuse. Specifically, the licensee failed to adequately evaluate a replacement fuse in 2014, which led to a spurious failure resulting in a loss of the RCPs.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000346/2020-002-00 LER 2020-002-00 for Davis-Besse Nuclear Power Station, Unit 1, Manual Reactor Trip on Trip of Reactor Coolant Pumps due to loss of 13.8 kV Bus Potential Transformer Fuse 71153 Closed
PLANT STATUS
The unit operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities, and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) High pressure injection (HPI) train 1 during HPI train 2 planned testing during the week ending July 11, 2020
- (2) Station blackout diesel during emergency diesel generator train 2 planned testing during the week ending July 11, 2020
- (3) Containment spray (CS) train 1 while CS train 2 was inoperable during planned safety features actuation channel 4 maintenance during the week ending August 8, 2020
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Station blackout diesel building during the week ending September 25, 2020
- (2) Auxiliary feed pump 2 (room 238): Fire area F during the week ending September 12, 2020
- (3) A/C equipment room (room 603): Fire area HH during the week ending August 22, 2020
- (4) Electrical penetration 1 (room 402): Fire area DG during the week ending August 29, 2020
71111.06 - Flood Protection Measures
Cable Degradation (IP Section 03.02) (1 Sample)
The inspectors evaluated cable submergence protection in:
- (1) Manholes MHSA1, MHSA2, MHSB1, and MHSB2 during the week ending September 25, 2020
71111.07A - Heat Sink Performance
Annual Review (IP Section 03.01) (1 Sample)
The inspectors evaluated readiness and performance of:
- (1) Component cooling water heat exchanger 1
===71111.07T - Heat Sink Performance
Triennial Review (IP Section 03.02)===
- (1) Emergency core cooling system room cooler 1, cooled by service water
- (2) Ultimate Heat Sink, section 02.02d, specifically, sections 02.02d.4 and 02.02d.5 were completed
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during planned downpower to 95 percent for control rod exercising and turbine valve testing during the week ending September 5, 2020
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated crew performance during three emergency plan training simulator scenarios on September 24, 2020
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Partial)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function. At the end of the inspection period, the inspectors were awaiting the receipt of follow-up information from the licensee in order to complete Section 03.01 of this procedure:
(1)
(Partial)
Repeat failure of containment air cooler 2 service water outlet, SW1357 [Condition Report 2020-06619]
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Shield building crane lift during the week ending July 4, 2020
- (2) Component cooling water pump 1 inoperable due to high bearing vibrations, 72-hour LCO during the week ending July 15, 2020
- (3) Pilot operated relief valve (PORV) block valve planned maintenance during the week ending August 22, 2020
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) CR 2020-06093: Emergency diesel generator 2 intake silencer throughwall leak
- (2) CR 2020-05316: Control rod 7-3 absolute position indication issues
- (3) CR 2020-04512: Auxiliary feed pump 1, PSL106D failed to close MS106 and MS106A
- (4) CR 2020-02524: 1R21 Unapproved material found in containment during mode 3
- (5) CR 2020-05002: Hole discovered during shield building crane anchor drilling
- (6) CR 2020-06389: Component cooling water pump 1 elevated bearing vibration past operability
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated the following post maintenance test activities to verify system operability and functionality:
- (1) Safety features actuation system channel 4 power supply after planned replacement during the week ending August 8, 2020
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) Tabletop emergency preparedness drill scenario during the week ending August 15, 2020
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors evaluated:
- (1) Tabletop emergency response scenario during the week ending August 8,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS06: Emergency AC Power Systems (IP Section 02.05)===
- (1) Unit 1 (April 1, 2019 - June 30, 2020)
MS07: High Pressure Injection Systems (IP Section 02.06) (1 Sample)
- (1) Unit 1 (April 1, 2019 - June 30, 2020)
MS08: Heat Removal Systems (IP Section 02.07) (1 Sample)
- (1) Unit 1 (July 1, 2019 - June 30, 2020)
===71153 - Followup of Events and Notices of Enforcement Discretion
Event Report (IP Section 03.02)===
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000346/2020-002-00, Manual reactor trip following trip of reactor coolant pumps due to loss of 13.8 kV bus potential transformer fuse, ADAMS Accession No.
ML20157A121. The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71153. This LER is closed.
INSPECTION RESULTS
Failure to Install Adequate Fuses Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events
Green FIN 05000346/2020003-01 Open/Closed
None (NPP)71153 A finding of very low safety significance (Green) was self-revealed when the licensee was required to manually trip the reactor after a loss of two reactor coolant pumps (RCP) due to a failed fuse. Specifically, the licensee failed to adequately evaluate a replacement fuse in 2014, which led to a spurious failure resulting in a loss of the RCPs.
Description:
On March 25, 2020, operators manually tripped the reactor while in mode 2 during startup following refueling outage 21. The operators initiated the reactor trip after reactor coolant pumps 1-2 and 2-1 tripped, circulating water pump 4 tripped, and the 13.8 kilovolts (kV) B-bus indicated low voltage. Following the reactor trip, operators appropriately entered the post-trip procedure to stabilize the plant.
The licensee generated condition report (CR) 2020-02620 to document the event. Upon investigation, the licensee determined that the B-phase fuse for the B-bus potential transformer (PT) 1 failed, resulting in low bus voltage and pump trips. Additionally, the licensee submitted event notification EN 54611, "Manual Trip due to Loss of Reactor Coolant Pumps," per 10 CFR 50.72(b)(2)(iv)(B), and subsequent licensee event report (LER)2020-002-00, "Manual Reactor Trip on Trip of Reactor Coolant Pumps due to loss of 13.8 kV Bus Potential Transformer Fuse," per 10 CFR 50.73(a)(2)(iv)(A).
The licensee performed a causal evaluation to determine the primary cause of the failed fuse.
As a result of the causal evaluation, the licensee concluded that an inadequate part/component equivalent replacement package, PERP 000833, (performed in 2014) was the primary cause. Specifically, PERP 000833 resulted in the licensee replacing obsolete Cooper Bussmann JCT 1/2 E fuses with Cooper Bussmann 15.5CAV0.5E fuses. The PERP noted that the fuse clearing times were different but stated the difference was acceptable without a full evaluation of the shorter clearing time of the replacement fuses. The licensee determined that the shorter clearing time caused the 15.5CAV0.5E fuse to blow in response to expected inrush current. As documented in CR 2020-02620, following the trip, the licensee evaluated alternative replacement fuses and identified that a currently available fuse with similar clearing times to the original specification was more appropriate to the application than the 15.5CAV0.5E fuses. The licensee reviewed the extent of condition to identify other locations where the 15.5CAV0.5E fuses were used and generated corrective actions to replace all affected fuses by the next refueling outage.
The inspectors referenced NOP-CC-2007, "Part/Component Equivalent Replacement Packages," revision 03 while performing the inspection. Step 8.c of NOP-CC-2007 requires that the licensee evaluate the impact of the differences and/or operating experience identified and provide the basis for the acceptability of the differences or impact of the operating experience information. The inspectors determined the licensee failed to adequately evaluate the impact of the differences between the two fuse models.
Corrective Actions: Immediate corrective actions included replacing the failed fuses.
Additionally, the licensee performed an evaluation to determine the appropriate fuse for the application and generated corrective actions to track the replacement of all currently installed subject Cooper Bussmann 15.5CAV0.5E fuses.
Corrective Action References: Condition report 2020-02620
Performance Assessment:
Performance Deficiency: The licensee failed to evaluate the impact of the differences of the 13.8 kV fuse replacement as required by NOP-CC-2007. This contributed to a spurious blown fuse which resulted in a loss of two RCPs, a circulating water pump and a subsequent manual reactor trip.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee failed to adequately evaluate a modification associated with the high voltage fuses. This resulted in a fuse failure, causing a loss of reactor coolant pumps and a manual reactor trip.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power.
Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.
Enforcement:
Inspectors did not identify a violation of regulatory requirements associated with this finding.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 23, 2020, the inspectors presented the integrated inspection results to Mr. T. Brown, Site Vice President and other members of the licensee staff.
- On October 2, 2020, the inspectors presented the triennial heat sink inspection results to Mr. G. Michael, Director, Site Engineering and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
20-04965
Immersion Heater to SBODG Auto Function not Working
06/10/2020
20-05467
BACC CS32 Pipe Cap
07/04/2020
Corrective Action
Documents
Resulting from
Inspection
20-06171
Blowout Panels 6C/6B Missing 1 Bolt
08/04/2020
20-06172
ECCS Room# 1 Pedestal Corner is Broken
08/04/2020
Drawings
M-017D
Station Blackout Diesel Generator
M-033A
High Pressure Injection
M-034
Emergency Core Cooling System CTMT [Containment]
Spray and Core Flooding Systems
Procedures
DB-OP-06011
HPI Train 1
DB-OP-06011
High Pressure Injection System
DB-OP-06013
Containment Spray System
DB-OP-06334
Station Blackout Diesel Generator Operating Procedure
Corrective Action
Documents
Resulting from
Inspection
20-07050
Oil Leak on Snubber SNT310 for AFW Train 2
09/09/2020
Fire Plans
FHAR
Fire Hazards Analysis Report
Auxiliary Feed Pump 2 Room
A/C Equipment Room and Records and Storage Area, Fire
Area HH
Service Building 6, Laydown Area, Station Black-Out Diesel
Procedures
DB-FP-00007
Control of Transient Combustibles
EN-DP-01141
FHAR Updating
NG-DB-00302
Number 1 Electrical Penetration Room
71111.07A Corrective Action
Documents
2016-05172
Less than Minimum Wall Thickness Measured on CCW #1
Shell per Order 200486506
04/12/2016
20-05972
QC ID Work Order 200643129 Minimum Wall Thickness not
Met for E22-1, CCW [Component Cooling Water] Heat
Exchanger 1-1
07/27/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
Resulting from
Inspection
20-06135
FME Cover not on
08/03/2020
20-07564
Error in EER 600724048, CCW HX Tube Evaluation
09/29/2020
Miscellaneous
EPRI NP-7552
Heat Exchanger Performance Monitoring Guidelines
2/1991
M-023-00020-03
Operating and Maintenance Instructions for Component
Cooling Heat Exchangers
03/14/2005
MRPM
Maintenance Rule Program Manual
Procedures
NOP-ER-2006
Service Water Reliability Management Program
Work Orders
200643129
PM 0076 E22-1 Cln-Insp CCW HX #1
08/12/2020
200764549
07/23/2020
71111.07T Calculations
2501-703 (H&H-
1)
Thermal Performance Analysis for Ultimate Heat (UHS) Sink
Pond
C-ICE-009.01-
001
Ultimate Heat Sink Temperature Indications
C-NSA-009.05-
001
Ultimate Heat Sink Volumes and Surface Areas
C-NSA-009.05-
003
UHS Thermal Performance Analysis for Maximum
Evaporation Meteorological Conditions
C-NSA-032.02-
006 R03 PN09
C-NSA-032.02-009 Was Prepared as Alternate Evaluation of
ECCS Room Cooler Performance
09/19/2017
C-NSA-032.02-
009
ECCS Room Cooling Heat Exchangers Performance During
Post-LOCA
09/27/2017
Corrective Action
Documents
2017-03328
NRC 2017 UHS Inspection: Issues with ECCS Room Cooler
Clean/Inspection Strategy
03/23/2017
2017-03953
Historical Inspection Data for ECCS Room Coolers
04/06/2017
2017-06335
Tube Blockage Identified in DB-E42-2, ECCS Room Cooler 1 06/07/2017
CR-2019-02869
Results of Ultimate Heat Sink Bathymetric Survey
03/27/2019
CR-2019-02950
Issues with 2016 Ultimate Heat Sink Silt Depth Calculation
03/29/2019
CR-2019-10336
Results of Ultimate Heat Sink Silt Depth Survey
2/12/2019
Corrective Action
Documents
Resulting from
Inspection
CR-2020-07638
Incorrect Value Reported in UFSAR 9.2.5
10/01/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Drawings
C-39
Circulating Water Intake System On-Shore Plan Profile &
Sections
M-041A
Service Water Pumps and Secondary Service Water System
M-041B
Primary Service Water System
M-041C
Service Water System for Containment Air Coolers
OS-020 SH1
Operational Schematic Service Water System
103
Engineering
Evaluations
Notification
600773046
ECCS Room Cooler Plugging Criteria Along with Maximum
Tube Plugging Limits
10/02/2017
Miscellaneous
M-410-00681
Vendor Manual Trane Co. Installation and Maintenance
Instructions for Air-Cooled Condensers Ca Series
11/19/2014
M-411 Q
Specification for Replacement Coils for ECCS Room Cooling
Units
11/26/2003
M-411Q-00001
Vendor Manual for Aerofin Type "WR" Coils for ECCS Room
Cooling Units
SD-018
System Description for Service Water System
Operability
Evaluations
POD for CR
2017-03953
POD for CR 2017-03953 for E42-1 and 2 and Closure
06/10/2017
Procedures
DB-OP-03007
Miscellaneous Instrument Daily Checks
DB-OP-06261
Service Water System Operating Procedure
Self-Assessments SA-BN-2020-
1935
Assess Davis-Besse's Compliance with Respect to the
Requirements Outlined in NRC Inspection Procedure 71111.07.
08/14/2020
Work Orders
200632106
PF4736-001 ECCS Room Cooler Monitoring Test
2/26/2017
200640589
PF4736-001 05.000 E42-1,2,3 TRN2 Coolers Monitoring
Test
06/13/2017
200665125
SP3006-001 05.000 SW TRN2 Cold Forebay Service Water
Train 2 Cold Forebay Design Flow
2/25/2019
200699715
Clean and Inspect DB-E42-1 ECCS Room Cooler
05/03/2018
200731883
E42-1 Inspection Completed
05/02/2018
200735477
SP3005-001 05.000 SW TRN1 Cold Forebay Service Water
TRN1 Cold Forebay Design Flow
2/17/2020
200741937
PF3023-001 05.000 P3-2 SW PMP 2 QTRLY SW Pump 2
Quarterly Test Service Water Pump 2 QTRLY Test
2/14/2020
200747409
PF3226-001 05.1+2 P3-2 SW Online Compreh P3-2 SW
07/29/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Online Comprehensive Test
200749494
PF3020-008 05.1+3 SW1424 Stroke SW1424 Stroke Time-
TS Applicable in Modes 1 Thru 4 Only
05/01/2020
200749496
PF3023-001 05.000 P3-2 SW PMP 2 QTRLY SW Pump 2
Quarterly Test Service Water Pump 2 QTRY Test
05/08/2020
200759098
PF3027-007 05.100 SW1395 Stroke SW1395 Stroke Time
FA Norm TS Applicable in Modes 1 Thru 4 Only SW1395
SYSE, SFAS TIME
07/10/2020
200760910
PP3020-007 05.100 SW1399 Stroke SW1399 Stroke Time
FA Norm-TS Applicable in Modes 1 Through 4 Only
SW1399 SYSE, SFAS TIME
07/23/2020
Corrective Action
Documents
2017-10018
SW1357 Failed to Close During Air Drop Test due to
SV1357B Continuously Venting
10/31/2017
2018-02603
SW1357, CAC [Containment Air Cooler] SW [Service Water]
Outlet, would not Stroke Closed during Test
03/18/2018
20-06619
SW1357 would not Stroke Closed
08/23/2020
Procedures
DBBP-OPS-003
Online Risk Management Process
NOP-OP-1007
Risk Management Plan
NOP-OP-1007-01 Risk Management Plan
Corrective Action
Documents
2016-07315
CRD Abnormal Procedure Entry due to Rod 7-3 Degraded
API/RPI Indication
06/29/2016
2018-05792
Aux Feed Pump 1, PSL106C Failed to Close MS106,
MS106A
06/24/2018
20-02524
1R21 - Unapproved Material Found in CTMT during Mode 3
03/23/2020
20-04512
Aux Feed Pump 1, PSL106D Failed to Close MS106,
MS106A
05/24/2020
20-05002
Hole Discovered during Shield Building Crane Anchor Drilling 07/27/2020
20-06093
Small Hole Identified in Outer Skin of EDG-2 Intake Silencer
07/27/2020
20-06224
First Half IPA Site Gap Identified for Equipment Reliability
08/03/2020
20-06389
P43-1 Outboard Pump Bearing Axial Vibrations are
Increasing
08/13/2020
CR 2020-05316
Control rod 7-3 Absolute Position Indication Issues
06/27/2020
CR 2020-05355
Control Rod 7-3 Erratic
06/28/2020
CR 2020-05973
System Monitoring: Rod 7-3 API Indication Momentarily
07/25/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Affected during CAC #3 Testing
CR 2020-06837
Heat Related Degradation of PI Tubes Identified by Vendor
Inspections Performed Under CA 2016-07315
08/31/2020
CR 2020-07068
Rod 7-3 API Indication Erratic
09/16/2020
Work Orders
200756758
AFW Train 1 Level Control, Interlock and Flow Transmitter
Test
05/24/2020
Procedures
DB-SC-03113
SFAS [Safety Features Actuation System] Channel 4
Functional Test
DB-SC-03113
SFAS Channel 4 Functional Test
Work Orders
200688175
SFAS Ch 4 Power Supplies
08/05/2020
200761396
SFAS Ch 4 Functional
08/04/2020
Miscellaneous
Emergency Preparedness 3rd Quarter 2020 Emergency
Response Organization Scenario
07/29/2020
Procedures
NOP-LP-5011
Emergency Response Drill and Exercise Program
71151
Corrective Action
Documents
20-04930
Missed MSPI Failure Report in the First Quarter 2020
06/09/2020
Miscellaneous
Reactor Oversight Program Mitigating System Performance
Index Basis Document
Procedures
NG-DB-00001
On-Line Risk Management
Corrective Action
Documents
2014-07743
Sizzling Coming from HB05 PT-2 X02 Transformer
04/28/2014
2018-10428
EI6210, SU [Startup] XFRM [Transformer] 02 to Bus B
Voltmeter Indicates 6 kV
11/24/2018
20-02620
Reactor Trip due to Loss of B Bus PT Fuse
03/25/2020
Engineering
Evaluations
PERP 000883
PT Fuses JCT 1/2E are no Longer Available, Replacement
Requires Configuration Update
Miscellaneous
50-346/2020-002-
Manual Reactor Trip on Trip of Reactor Coolant Pumps due
to Loss of 13.8 kV Bus Potential Transformer Fuse
05/26/2020
Procedures
NOP-CC-2007
Part/Component Equivalent Replacement Packages
NOP-LP-2001
Corrective Action Program
48