IR 05000346/1977014

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IE Insp Rept 50-346/77-14 on 770216-18 & 0301-03,08 & 14-16. No Noncompliance Noted.Major Areas Inspected:Damage to Vessel Internals from Hot Functional Test or Core Support Assembly Removal & Review of Diagnostic Noise Monitoring
ML19329B588
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 05/29/1977
From: Cook R, Little W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19329B432 List:
References
50-346-77-14, NUDOCS 8002050723
Download: ML19329B588 (7)


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UNITED STATES NUCLEAR REGULATORY COMMISSION

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0FFICE OF lilSPECT1011 AND ENFORCEMENT

REGION III

Report of Operations Inspection

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IE Inspection Report No. 50-346/77-14 Licensee:

Toledo Edison Company Edison Plaza 300 Madison Avenue Toledo, OH 43652 Davis-Besse Nuclear Power Station License No. CPPR-80 s

Unit 1 Category:

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Oak Harbor, OH

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Type of Licensee:

PWR (B&W) MWe Type of Inspection:

Special, Announced

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Dates of Inspection:

February 16-18, March 1-3, 8, 14-16, 1977 Principal Inspector:

R. J. Cook

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Accompanying Inspectors:

None

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Other Accompanying Personnel:

V. Noonan, D0R (March 1, 1977, only)

J. Rajan, DSS (March 1, 1977,only)

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Y(ill/A W.S). Little, Chief 85h7

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l Reviewed By:

Nuclear Support Branch

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-~s SUM 1MRY OF FINDINGS

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Inspection Summary An inspection was performed on February 16-18, March 1-3, 8, 14-16, 1977, (77-14):

regarding exanination of damage to vessel internals as a result of the hot functional test (HFT) and/or the core support assembly (CSA) removal, review of possible causes for the damage,

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review of diagnostic noise monitoring capabilities, and the review of applicable fc2111ty records.

Enforcement Items None.

Licensee Action on Previously Identified Enforcement Items

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None inspected.

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.Other Significant Items A.

Systems and Components None.

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B.

Facility Items (Plans and Procedures)

None.

C.

Managerial Items None.

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D.

Deviations

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None.

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E.

Status of Previously Reported Unresolved Items.

None inspected.

Management Interview A management interview was conducted with Mr. Evans, Station Superin-tendent at the completion of the inspection on March 16, 1977.

Mr. Tambling, RIII was in attendance. The following items were discussed.

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A.

The inability to determine the sensitivity of the installed Loose

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i Parts Monitor (LPM) for known energy impact phenomenon was dis-

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cussed. The licensee agreed to perform additional preassembly testing to establish the response of the LPM to remotely initiated signals.

(Paragraph 6, Report Details)

B.

The lack of existing LPM baseline data, data analysis and data correlation were discussed.

The licensee agreed to develop a test-ing program for acquiring LPM baseline data at various power plateaus and to investigate for internal assembly anomalies.

(Para-graph 6, Report Details)

C.

The inspector stated that another RIII inspector would follow the details of the vessel internals repairs.

The licensee acknowledged the comment.

(Paragraphs 3 and 4, Report Details)

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N REPORT UCTAILS l

1.

Persons Contacted J. Evans, Station Superintendent B. Beyer, Maintenance Engineer J. Hartigan, Assistant Engineer R. Brown, Assistant Engineer G. Meyer, Assistant Engineer D. Bolfa, Maintenance Machinist J. Buck, Operations Quality Assurance Supervisor J. Huges, QC (TECo/Bechtel)

A. Casalena, QC Inspector - TECo C. Wills, B&W Supervisory Engineer C. Hillings, B&W QC Supervisor

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B. Donavan, B&W Nuclear Services Engineer 2.

General

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During the removal of the vessel internals, galling occurred where

the core support assembly (CSA) mates with the vessel keys located at the vessel flange and at the outlet nozzle contact surfaces.

Further examination of the CSA revealed that gauling had occurred on at least one guide block associated with each of the 12 pairs of blocks used to ensure lower CSA alignment. A bolt used in the

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block attachment to the CSA was found broken in one guide block.

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Gauling was also found on some of the lugs attached to the vessel inside wall which engage the CSA guide blocks.

An inspection was conducted to examine the extent of damage incur-red by the vessel internals, review of possible causes for the gauling, and to review vibration monitoring capabilities.

3.

Vessel Condition During the inspection, the inside of the vessel was physically examined. This examination revealed by evidence of galling that at least 5 of the alignment lugs attached to the vessel wall had been in contact with the CSA guide blocks during hot functional t

i testing (HFT).

Ideally, a 20 mil clearance would exist on either side between the guide lug and the CSA guide block.

Die penetrant i

testing of the guide lug attachment did not disclose any surface cracking.

The licensee had dressed the " mating" lug surfaces I

with light grinding.

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TECo QA noted that a nominal 1/2" - 15 chamfer at the top of the vessel guide lugs had not ieen formed during the original manu-facture. This 15 chamfer was formed in place by grinding.

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e chamfers were shaped to conform with the originnl design using

'N B&W Construction Field Procedure No. 318.

These chamfers were g

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examined and compared to the construction prints and appeared to agree with the original design.

The vessel outlet nozzle mating surfaces were found galled.

This galling is attributed to removal of the CSA in a nonplumb align-ment with the vessel. At the time of the inspection the galled surfaces had been relieved by hand grinding to an intended width /

depth ratio of 3/1. The gauge depths are nominally 1/16 to 1/8 inch deep with the nozzle oriented towards the west being the most severely galled. Die penetrant testing after relieving dis-closed no signs of surface cracking.

The vessel support ledge for the CSA was examined over the entire contact surface. No indications of CSA " rocking" or deformed metal which might indicate gross CSA motion were noted.

c During HFT, the inner 0-ring seal between the closure head and the reactor vessel flange leaked. This leakage damaged the vessel

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flange seating surface.

Patch weld was added to the vessel flange

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at the damaged surface locations and machined to the original seal-

ing surface.

B&W Weld Control Records, Welding Instruction Sheets, General Procedure and personnel qualifications were reviewed.

No discrepancies were noted.

Vessel keys (4 keys) were examined and found to be galied on the sides. The gall marks are vertically oriented and essentially run the full length of the key.

It appears that these gall marks were formed during CSA removal. Upset metal was removed by hand grinding. The key geometry was not damaged enough to require further action.

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4.

Core Support Assembly (CSA) Condition The CSA has 12 pairs of guide blocks evenly spaced around the peri-phery of the lower extremities. At least one block of each pair of blocks showed signs of being in contact with the mating vessel guide lug either during hot functional testing (HFT) or CSA removal.

One of the blocks located at a designated Y-axis position was found with cracked capture welds on a bolt head used to maintain block attachraent to the CSA.

Further investigation revealed that the bolt was hr lan flash with the CSA as a result of cyclic fatigue. This failure is attributed to loading of the bolt as a result of a dowel pin not being fitted to specifications and therefore, unable to assume the design dowel pin loading.

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i Measurements of the CSA guide block horizontal opening were taken (_s and compared to the thickness of each mating vessel guide lug.

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It was found that these openings were nominally 100 to 230 mils s

in excess of the guide lug thickness. The original design is for a nominal 40 mil clearance with 20 mils existing on either side of the guide lug. The CSA guide blocks were subsequently repositioned to establish nominal design clearances and welded in place.

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While the CSA was located on the support stand it was noted that

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stand support pads had come in contact with locking clips for core barrel-thermal shield bolts.

This caused a deflection on the contacted locking clips of about 1/8 inch.

These deflected clips were located between the designated X and Y-axes.

Ideally, the CSA support stand would make contact only with the heads of the core barrel-thermal shield bolts when the CSA is supported upright.

It was determined by the licensee that the CSA support stand is

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elliptical which causes some of the support pads to engage the locking clips.

The licensee subsequently placed metal sheathing between the core barrel-thermal shield bolts and the support pads.

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The licensee ultimately plans to remove interfering metal from

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the contact pads.

The CSA outlet nozzles were found galled with the marks running in a prefered vertical direction. The gall marks on either side of a vertical axis through the centerline of the nozzle appear to

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('~'N match those marks found on the reactor vessel outlet nozzles. At the time of the inspection the upset metal had been relieved by g'

grinding. The galling is attributed to removal of the CSA in a nonplumb configuration with the reactor vessel.

Essentially all the contact surface between the CSA and reactor vessel was examined on the CSA. No indications of plastic deforma-tion or upset metal were noted.

The CSA keyways were examined and found galled. These gall marks were in a predominantly vertical orientation and appear to match

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the gall marks in the reactor vessel keys. The galling is believed to have occurred during CSA removal. The upset metal was removed by light grinding on 3 of the 4 keyways. The remaining keyway was heavily ground and the ficup tolerance was destroyed.

This keyway was subsequently brought within design tolerance by weld buildup and machining. The key / keyway design calls for a clearance of 10 to 16 mils.

The clearances were found to be 15, 18, 23 and 44 mils on a nominal average across the engaged surface. The licensee indica-ted the repairs restored the keyways such that the function has not been impaired.

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Inspection of Internals Adapter Assembly (\\s)

During investigations to determine the loss of plumb when the CSA was removed, a lifting nut on one of the internals handling adapter trusses (Part No. 258, B0W Drawing No. 181369E) was found to be loose and not in the previously set position.

During the disas-sembly, it was noted that a staking allen screw in the lifting nut could not be removed. After removal of the nut from the lifting bar (Part No. 257 B&W Drawing No. 181309E), it was noted that the last four threads were damaged. An end cap disc plate was also found damaged. The licensee procured an identical internals hand-ling adapter truss from another plant for use during subsequent CSA handlings.

6.

Noise Monitoring Capability The capability of the ir. stalled Loose Parts Monitor (LPM) to detect

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indications of gross cote barrel motion and derive quantitative information were reviewed. The licensee had not instituted a rig-erous program for procuring baseli.ne data using the installed LPM during hot functional testing (HFT). However, enough data was taken

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which could show a comparison between spectra taken at a reactor coolant system (RCS) temperatures and pressures of 385 F and 1500 psig with data at 530 F and 2170 psig. These traces indicate that

a low frequency (9H_) spike may have existed at 385 F which appears much less pronounce 8 at 530 F.

The first mode b>am model frequency

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notbecorrelatedcoanyknown$nergyimpactforces.

Correlations

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for the core barrel is about 9U. The amplitude of the signal could with noise data taken by B&W during HFT was not available at the site. The data taken during HFT with the installed LPM was on a 0 to 512 H full scale which is ackward for gross motion monitoring.

g However, clie LPM has the capability of changing the full scala to O to 25H for examing low frequency spectrum.

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