|
---|
Category:EXAMINATION REPORT
MONTHYEARIR 05000412/19993011999-04-20020 April 1999 NRC Operator Licensing Exam Rept 50-412/99-301(including Completed & Graded Tests) for Tests Administered on 990322- 25.All Applicants Passed All Portions of Exams IR 05000334/19983011998-08-21021 August 1998 Exam Repts 50-334/98-301OL & 50-412/98-301OL Conducted During Wks of 980803-07 & 17-21.Exam Results:Four Unit 2 SRO Candidates Passed All Portions of Initial Exam.Good Performance Noted During Exam in Area of Crew Communication IR 05000334/19983001998-06-0303 June 1998 Exam Rept 50-334/98-300OL Conducted on 980420-24 & 0518.Exam Results:Three SRO Instant Candidates Passed All Portions of Initial License Exam IR 05000334/19970101998-01-0909 January 1998 NRC Operator Licensing Exam Rept 50-334/97-10OL (Including Completed & Graded Tests) for Tests Administered on 971215- 18 ML20140C1581997-05-30030 May 1997 NRC Operator Licensing Exam Repts 50-334/97-03OL & 50-412/97-03OL for Tests Administered on 970317-21 & 0428-0502.Exam Results:All Candidates Passed All Portions of License Exam IR 05000334/19930191993-09-0202 September 1993 Exam Rept 50-334/93-19 OL-RQ on 930902.Exam Results:Six SRO fill-ins Were Examined & Five Evaluated Satisfactory & One Was Found Unsatisfactory Based on nonsafety-related Performance Deficiencies IR 05000334/19900141990-08-23023 August 1990 Requalification Program Evaluation Rept 50-334/90-14OL-RQ on 900709-19.Exam Results:Nine Senior Reactor Operators & Seven Reactor Operators Passed All Portions of Exam.One Crew Failed IR 05000412/19900111990-08-0909 August 1990 Requalification Program Evaluation Rept 50-412/90-11OL-RQ on 900529-0607.Evaluation results:15 of 16 Operators Passed All Portions of Exam & 3 of 4 Crews Evaluated as Satisfactory IR 05000334/19890161989-08-16016 August 1989 Requalification Program Evaluation Rept 50-334/89-16 on 890727-28.Rept Results:One Reactor Operator Successfully Completed Two Simulator Scenarios & Written Exam IR 05000334/19880241988-09-27027 September 1988 Exam Rept 50-334/88-24OL on 880817-18.Exam Results:One of Two Senior Reactor Operators Passed Exams ML20154B2261988-03-30030 March 1988 Exam Rept 50-412/88-06OL on 880223-24.Exam Results:One Senior Reactor Operator Candidate Passed Both Written & Operating Exams IR 05000412/19870651988-02-26026 February 1988 Exam Rept 50-412/87-65OL on 881202-03.Exam Results:Three Reactor Operator & Four Senior Reactor Operator Candidates Passed ML20236E7861987-07-20020 July 1987 Exam Rept 50-334/87-08OL on 870520-22.Exam Results:Two Operators Failed Operating Exam & Nine Operators Failed Written Exam.Operator Weaknesses Extensive & Individualized. Requalification Program Found Unsatisfactory IR 05000412/19870421987-07-0202 July 1987 Exam Rept 50-412/87-42OL on 870518-22.Of Eight Reactor Operator (RO) & 14 Senior Reactor Operator (SRO) Candidates, Four RO Candidates & Eight SRO Candidates Passed All Portions,Written & Oral,Of Exams ML20210R2761986-09-15015 September 1986 Exam Rept 50-334/OL-86-16 on 860722-31.Exam Results:Seven Reactor Operators,Two Senior Reactor Operator (SRO) Retake Candidates & One SRO Candidate Passed All Portions of Exam IR 05000334/19860021986-04-15015 April 1986 Exam Rept 50-334/86-02 on 860204-14.Exam Results:All 5 Reactor Operator Candidates Passed & 1 of 11 Senior Reactor Operator Candidates Passed IR 05000334/19850101985-06-21021 June 1985 Exam Rept 50-334/85-10 on 850430-0503.Exam Results:All Candidates Passed Exams 1999-04-20
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-I-99-048, on 991022,operators Initiated Plant Shutdown from 100% Reactor Power,Due to Continued RCS Leakage Through B Pressurizer Code Safety Valve to Primary Relief Tank. Operators Are Reducing Reactor Power at 12% Per H1999-10-22022 October 1999 PNO-I-99-048:on 991022,operators Initiated Plant Shutdown from 100% Reactor Power,Due to Continued RCS Leakage Through B Pressurizer Code Safety Valve to Primary Relief Tank. Operators Are Reducing Reactor Power at 12% Per H ML20217N1491999-10-21021 October 1999 Notice of Violation from Insp on 990720-29.Violation Noted: as of July 1999,licensee Did Not Take Adequate Measures to Assure That Condition Adverse to Quality Involving Macro Biological Fouling of Service Water System Corrected IR 05000334/19990061999-10-0707 October 1999 Insp Repts 50-334/99-06 & 50-412/99-06 on 990809-13 & 990823-27.Violations Noted.Major Areas Inspected:Licensee Corrective Action Program Implementation IR 05000334/19990051999-09-30030 September 1999 Insp Repts 50-334/99-05 & 50-412/99-05 on 990725-0904.Two Violations Noted & Being Treated as Nvcs.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support ML20211Q5791999-09-0707 September 1999 Insp Rept 50-412/99-07 on 990720-29.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000334/19990041999-08-24024 August 1999 Insp Repts 50-334/99-04 & 50-412/99-04 on 990613-0724. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support PNO-I-99-036, on 990718,update to Beaver Valley,Unit 2 Forced Outage Made.Licensee Replaced Suspected Voltage Regulator Control Relays & Satisfactorily Retested EDG 2-2.Resident Inspectors Continue to Monitor Licensee Corrective Action1999-07-26026 July 1999 PNO-I-99-036:on 990718,update to Beaver Valley,Unit 2 Forced Outage Made.Licensee Replaced Suspected Voltage Regulator Control Relays & Satisfactorily Retested EDG 2-2.Resident Inspectors Continue to Monitor Licensee Corrective Action PNO-I-99-033, on 990716,apparent Electrical Fault Occurred During EDG Full Load Test,Which Opened Supply Breaker Between Emergency & Normal 4 Kilovolt Busses.Station Personnel Intend to Resolve & Correct Electrical Fault1999-07-19019 July 1999 PNO-I-99-033:on 990716,apparent Electrical Fault Occurred During EDG Full Load Test,Which Opened Supply Breaker Between Emergency & Normal 4 Kilovolt Busses.Station Personnel Intend to Resolve & Correct Electrical Fault IR 05000334/19990031999-07-0707 July 1999 Insp Repts 50-334/99-03 & 50-412/99-03 on 990502-0612.No Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support.Results of Y2K Readiness Assessment Also Included IR 05000334/19990021999-05-21021 May 1999 Insp Repts 50-334/99-02 & 50-412/99-02 on 990321-0501.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000334/19990011999-04-22022 April 1999 Insp Rept 50-334/99-01 & 50-412/99-01 on 990207-0320. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support.Also Results of Insp by Regional Security & Inservice Insp Specialists IR 05000412/19993011999-04-20020 April 1999 NRC Operator Licensing Exam Rept 50-412/99-301(including Completed & Graded Tests) for Tests Administered on 990322- 25.All Applicants Passed All Portions of Exams IR 05000334/19980111999-02-25025 February 1999 Insp Repts 50-334/98-11 & 50-412/98-11 on 981227-990206. Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support ML20207E0761999-02-25025 February 1999 Notice of Violation from Insp on 981227-990206.Violation Noted:Licensee Failed to Promptly Identify & Correct Condition Adverse to Quality in That Investigation of Improperly Calibr Channnels Was Incompleted ML20206U3141999-02-0505 February 1999 Notice of Violation from Insp on 981116-1217.Violation Noted:On or Before 981217,design Control Measures Were Not Established to Ensure That Design Basis Closing Voltage Requirements of Circuit Breakers Were Met & Verified IR 05000334/19980091999-02-0505 February 1999 Insp Repts 50-334/98-09 & 50-412/98-09 on 981115-1217. Violations Noted.Major Areas Inspected:Engineering IR 05000334/19980101999-01-13013 January 1999 Insp Repts 50-334/98-10 & 50-412/98-10 on 981115-1226.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support.Matl Condition of Fire Protection Equipment Installed in Plant Was Excellent IR 05000334/19980061998-12-0404 December 1998 Corrected Pages 17 & 18 to Insp Repts 50-334/98-06 & 50-412/98-06,correcting Errors on Subj Pages ML20196H2951998-12-0202 December 1998 Insp Repts 50-334/98-08 & 50-412/98-08 on 981026-30.No Violations Noted.Major Areas Inspected:Operations & Maint ML20196H3231998-12-0202 December 1998 Insp Repts 50-334/98-06 & 50-412/98-06 on 981004-1114.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000334/19980071998-11-0505 November 1998 Insp Repts 50-334/98-07 & 50-412/98-07 on 981006-07.No Violations Noted.Major Areas Inspected:Performance of Emergency Response Organization IR 05000334/19980051998-10-23023 October 1998 Insp Repts 50-334/98-05 & 50-412/98-05 on 980816-1003. Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations, Engineering,Maint & Plant Support ML20151Z3231998-09-15015 September 1998 Insp Repts 50-334/98-04 & 50-412/98-04 on 980628-0815. Violation Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20151Z3181998-09-15015 September 1998 Notice of Violation from Insp on 980628-0815.Violation Noted:On 980808,inspectors Observed Maint Supervisor Manipulate Outboard Pump Packing Supply Valve & Perform Maint by Adjusting Outboard Packing Gland Nuts IR 05000334/19983011998-08-21021 August 1998 Exam Repts 50-334/98-301OL & 50-412/98-301OL Conducted During Wks of 980803-07 & 17-21.Exam Results:Four Unit 2 SRO Candidates Passed All Portions of Initial Exam.Good Performance Noted During Exam in Area of Crew Communication ML20236X8661998-08-0505 August 1998 Notice of Violation from Insp on 980426-0627.Violation Noted:From 1988 to Sept 1997,licensee Routinely Vented Units 1 & 2 HHSI Piping Prior to Surveillance Testing W/O Proper Controls to Evaluate Amount of Gas.No Response Required IR 05000334/19980031998-08-0505 August 1998 Insp Repts 50-334/98-03 & 50-412/98-03 on 980426-0627. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support ML20236X8631998-08-0505 August 1998 Notice of Violation from Insp on 980426-0627.Violation Noted:During Period of 980428-0608,licensee Failed to Implement Procedures as Evidenced by Listed Examples IR 05000334/19983001998-06-0303 June 1998 Exam Rept 50-334/98-300OL Conducted on 980420-24 & 0518.Exam Results:Three SRO Instant Candidates Passed All Portions of Initial License Exam ML20217F5881998-04-22022 April 1998 Notice of Violations from Insp on 980208-0321.Violations Noted:Conditions Adverse to Quality Were Not Promptly Corrected from Nov 1993 to March 1998,util Failed to Correct Known Unit 1 & 2 TS Deficiency in Timely Manner ML20217F5951998-04-22022 April 1998 Insp Repts 50-334/98-01 & 50-412/98-01 on 980208-0321. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support ML20217B9771998-03-17017 March 1998 Notice of Violation from Insp on 971228-980207.Violations Noted:Repair Activities for 2-1 Station Battery Were Not Properly pre-planned & Implemented ML20217B9851998-03-17017 March 1998 Insp Repts 50-334/97-11 & 50-412/97-11 on 971228-980207. Violations Noted.Major Areas Inspected:License Operations, Engineering,Maint & Plant Support.Security Program Was Also Inspected ML20216E8071998-03-0909 March 1998 Notice of Violation from Insp on 980105-0212.Violations Noted:On 971218 Dl Implemented Change to Temporary Operating Procedure to Allow Operators to Control Cooldown & Heatup Rate of Reactor Coolant by Mean Other than by Regulating ML20216E8191998-03-0909 March 1998 Insp Repts 50-334/98-80 & 50-412/98-80 on 980105-0212. Violations Noted.Major Areas Inspected:Evaluation of Implementation of 10CFR50.59 SE Program Relating to Changes, Tests or Experiments at Plant ML20202A9691998-02-0404 February 1998 Insp Repts 50-334/97-09 & 50-412/97-09 on 971116-1227. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support.Rept Also Includes Results of Announced Insp in Areas of Emergency Preparedness IR 07100116/20120271998-02-0404 February 1998 Notice of Violation from Insp on 971116-1227.Violation Noted:Licensee Had Not Tested 20 of 27 Direct Lines at Alternate EOF in Coraopolis,Pa PNO-I-98-002, on 980130,operators Declared Both Trains of Component Cooling Reactor & Reactor Plant River Water Sys Inoperable Due to Failure to Meet TS Surveillance Testing Requirements.Entered TS 3.0.3 & 4.0.31998-02-0202 February 1998 PNO-I-98-002:on 980130,operators Declared Both Trains of Component Cooling Reactor & Reactor Plant River Water Sys Inoperable Due to Failure to Meet TS Surveillance Testing Requirements.Entered TS 3.0.3 & 4.0.3 IR 05000334/19970101998-01-0909 January 1998 NRC Operator Licensing Exam Rept 50-334/97-10OL (Including Completed & Graded Tests) for Tests Administered on 971215- 18 ML20198K4761998-01-0606 January 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Between 1988 & 970912, Condition Adverse to Quality Existed at Unit 1 & 2,when Excessive Gas Accumulated in HHSI Pumps Suction Lines ML20199A1711997-12-31031 December 1997 EN-97-119:on 980106,notice of Proposed Imposition of Civil Penalty in Amount of $55,000 Issued to Licensee.Action Based on Violation Involving Failure to Take Adequate Action to Correct Significant Condition Adverse to Quality PNO-I-97-077, on 971216,Duquesne Light Co Initiated Unit 2 Reactor Shutdown in Accordance W/Ts 3.0.3.Licensee Plans to Address Unit 2 Design Deficiency for CR Emergency Air Cleanup & Pressurization,During Shutdown1997-12-17017 December 1997 PNO-I-97-077:on 971216,Duquesne Light Co Initiated Unit 2 Reactor Shutdown in Accordance W/Ts 3.0.3.Licensee Plans to Address Unit 2 Design Deficiency for CR Emergency Air Cleanup & Pressurization,During Shutdown ML20203D7421997-11-26026 November 1997 Insp Repts 50-334/97-08 & 50-412/97-08 on 971005-1115. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 07100005/20110151997-11-26026 November 1997 Notice of Violation from Insp on 971005-1115.Violations Noted:Workers,Found in Radiology Controlled Areas,Not Aware of Radiological Conditions in Work or Travel Areas IR 05000334/19970071997-11-0707 November 1997 Insp Repts 50-334/97-07 & 50-412/97-07 on 970831-1004. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20198S6351997-11-0707 November 1997 Notice of Violation from Insp on 970830-1004.Violation Noted:Licensee Changed QA Program Resulting in Reduction in Commitments in QA Program Description Previously Accepted by NRC W/O Prior NRC Approval IR 05000334/19970061997-09-18018 September 1997 Insp Repts 50-334/97-06 & 50-412/97-06 on 970720-0830.No Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support & Licensed Operator Requalification Training Program ML20217P7731997-08-18018 August 1997 Notice of Violation from Insp on 970608-0719.Violation Noted:Previous Corrective Actions Inadequate in That on 970701,unplanned Engineered Safety Feature Actuation, Occurred During Troubleshooting Activities on Unit 1 IR 05000334/19970051997-08-18018 August 1997 Insp Repts 50-334/97-05 & 50-412/97-05 on 970608-0719. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support ML20141G9971997-07-0303 July 1997 Notice of Violation from Insp on 970209-0426.Violation Noted:During EDG Surveillance Tests,Load Test Values Used Were Inadequate to Ensure That EDGs Achieved 2750 Kw Due to Inaccuracies in Kilowatt Meter Instrument Loop 1999-09-07
[Table view] |
Text
.
. .
,
'
.'.
.
U.S. NUCLEAR REGULATORY COMMISSION REGION I OPERATOR LICENSING EXAMINATION REPORT EXAMINATION REPORT NO. 50-334/88-24(0L)
FACILITY DOCKET N0. 50-334 FACILITY LICENSE NO. OPR-66 LICENSEE: Duquesne Light Company Post Office Box 4 Shippingport, Pennsylvania 15077 FACILITY: Beaver Valley Power Station Unit 1 EXAMINATION DATES: August 17 and 18, 193 CHIEF EXAMINER La
[ J '?/ '_ h27'88 Date yE.Brigpf,SeniorOperationsEngineer f? '
ll i APPROVED BY: o fM1 Peter Eselgr' th, Chief, PWR Section 9'27'fff Date Operations / ranch, Division of Reactor Safety
,
SUMMARY: Written examinations and operating tests were administered to two
, (2) senior reactor operator (SRO) candidates. One SR0 passed the examinations.
<
l l
I I
'
l
.i
-
v
.
l
._ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ _ . _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ . _ . . . _ . . _ , _ _ _ _ _ _ . _
_ _ , _ . . _ . , _ _ _ , _
.
-
,
.
.
'
,.
OETAILS
.
TYPE OF EXAMINAI!ON: Replacement EXAMINATION RESULTS:
l R0 l SR0 l l Pass /Fafl l Pass / Fail l I l l I I I I l Written 1 0/0 l 1/1 l I ._ l l l l l 1 I I Operating l 0/0 l 2/0 I I I I I I I I I l Overall l 0/0 1 1/1 l 1 I I I CHIEF EXAMINER AT SITE: Larry E. Briggs, Senior Operations Engineer OTHER EXAMINERS: James Prell, Senior Operations Engineer PERSONNEL PRESENT AT THE EXIT INTERVIEW:
Tom Burns, Director Operations - Training James Crum, Nuclear Operations and Maintenance Instructor Larry Freeland, Nuclear Operations Supervisor
.
l
!
L
'
...
.-.* .
1
.
-3- SUMMARY OF NRC AND LICENSEE COMMENTS MADE AT THE EXIT MEETING a. The NRC expressed appreciation to the Training and Operations Departments for providing a sistance in expediting the examination process, b. The NRC reviewed the number and type of examinations conducted curing the week and observations made, c. There were no generic strengths or weaknesses observed during the examinations due to the limited number of caicidate '
d. The following is a sumary of NRC coments concerning reference material supplied by the facility for exam preparation, The ?xaminer noted that some Operating Manuals (CM) did not n.ppear to support the Enabling Objective and should be reviewed to determine applicabilit In particular the ON for the Reactor Coolant Pump appeared to be deficien . The examiner noted that although OM's and other reference material had an index in the front of the manual there were no tabs provided for easy access to each desired section. This caused a protracted period for exam preparatio . The examiner noted that the anr.unciator response procedures contained in the, CM's were not in any logical sequence and almost unusable in the provided forma Those in the control room are contained in separate binders divide:1 by annunciator section.
! The examiner stated that the P&lDs provided were reduced in size to the point of poor quality and were aften unreadable even with a magnifying glass.
'
The license's response to comments 1 through 4 was that an effort would be made to upgrade the reference material that would be supplied for future exam preparation.
l The NRC stated that during the plant walkthrough portion of the
operating test, it was observed that the remote shutdown panel 1 did not incorporate any physical restrictions to prevent control and operation transfer between the control room and the shutdown panel. The licenste said that this concern would be :
evaluated to determine acceptability, l
'
Attachments:
- NRC response to facility coment . Facility coments on written examination Written Examination and Answer Key (SRO) ;
!
._ - .-
_ ______ _ _ _ _ _
. .' .
i
.,. .
. l ATTACHMENT 1 ilRC RESPONSE TO FACILITY COMMENTS
The following statements address the NRC's disposition of comments submitted by the facility (see attachment 2) on the written SRO examination and changes .
made to the answer key during the grading proces .0 THEORY OF NUCLEAR POWER PLANT OPERATION, FLUIDS AND THERMODYNAMICS 5.07.a.1&2 Coment noted. Credit was given if candidate specified assumed plant conditions in answe . 5.0 Answer key revised during grading to delete "Early extrapolation of the 1/M plot results in a late prediction of criticality" since the question would not elicit that part of the answer. Question point value was reduced by 0.5 point .0 PLANT SYSTEMS DESIGN, CONTPOL AND INSTRUMENTATION 6.03.e & f Comment accepte As stated, the reference material was in erro The answer key was changed in part e. to reflect the correct valve number. Part f. was changed to denote that the valve did not receive an ESF signa .0 Answer key revised during grading to include OT delta T and P11 as acceptable answer .06 Coment accepted. Answer key was changed to indicate that final steady state SG 1evel would be at normal program leve .09 Coment accepted. Answer key changed to "Trip of all running main feed pumps".
6.09. Coment accepted. Answer key changed to "Steam driven AFW start signal not follo ed by discharge pressure".
6.0 Answer key revised during grading to accept "breaker racked out" as an acceptable answer.
[
6.0 Coment accepte Valve position changed from not fully open to
"not fully closed".
- _. - - .-. ._ . _-____ . _ _ - _ _ _ _ _ - .- -
.
a . . .
'
.",
.
.
.
I PROCEDURES-NORMAL, ABNORMAL, EMERGENCY AND RADIOLOGICAL CONTROL l
'
7.0 Answer key revised during grading to accept "Local manual trip of the turbine" as an acceptable part of the answer.
i j 7.0 Coment accepted. Answer key revised to include "RCS subcooling
- less than attachment' and "Pressurizer level less than 5 percent" i as acceptable answers.
7.07 Coment accepte "Lifetime exposure is more limiting" was !
' deleted from the answer key and the question point value was !
]
reduced by 0.25 points. Although not specifically asked for in i
.
the question it was necessary for the candidate to determine which '
t exposure limit was the cost restrictive in order to answer the ,
I quastion.
i
- ADMINISTRATIVE PROCEDURLS, CONDITIONS AND LIMITATIONS 8.01 Coment accepte Credit was giveri if the candidate stated the '
assumption that the primary to secondary leakage was in only one l
- steam generator. Due to the wording of the RCP seal leakage statenent of the question it would be possible for the candidate to consider the 4.2 GPM as either controlled leakage or identitied >
'
leakag The answer key was revised to include Identified Leakage as ene of the acceptable answers,
'
t J 8.0 Coment accepted in part. Sufficient information was given for i the candidate to recognize th?t a fire in the diesel generator
- breaker had disabled the diesel generator for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Tab 26 of EPP/I-1 definition of an Alert states "Fire which POTENTIALLY ,
affects safety systems". Loss of an Emergency Diesel Generator
due to a fire definately has the potential to affect safety l systems.
,
The answer key was changed as follows: Classification level to i "Alert" and Justification to "Fire which potentially affects
safety systems", i j 8.04 Coment not accepted. SRO's are required to be able to recognize that they have exceeded an LCO and entered an action statemen >
They must also know that they cannot change modes (toward mode 1) !
{ while relying on a action statement, if 3.0.4 is applicabl If ,
i the candidata does not know if 3.0.4 does or does not apply then ,
) he can state action for both case ;
} l
j i
i
'
i
!
l i
,
. . .
,
.,. .
,
l .
i j 8.0 Comment accepted. Answer key revised to incorporate new personnel j titles.
.
! 8.0 Answer key revised during grading to reflect that Tab 1 of EPP/1-1 I would require an unusual event to be declared for an unplanned I release. This would require a "One hour notification" and a "30
'
day LER" IAW SAP 3B No. 31.
l 8.1 Coppent noted. The question asks for two things, what j notifications must be made and to indicate which of those j notification (s) must be made in one hour.
I
I
1 t
!
l
$
!
!
!
!
l l
\ l i
i
!
)
?
i l
i i
l
1 i
_ _ - _ . _ _ _ _ . _ _ _ .