IR 05000324/2017004

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NRC Integrated Inspection Report 05000325/2017004 and 05000324/2017004
ML18029A003
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 01/29/2018
From: Steven Rose
NRC/RGN-II/DRP/RPB4
To: William Gideon
Duke Energy Progress
References
IR 2017004
Download: ML18029A003 (23)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ary 29, 2018

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT 05000325/2017004 AND 05000324/2017004

Dear Mr. Gideon:

On December 31, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Steam Electric Plant, Units 1 and 2 facilities. On January 23, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy. Further, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest these violations or the significance of the violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the NRC Resident Inspector at the Brunswick Steam Electric Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC resident inspector at the Brunswick Steam Electric Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62

Enclosure:

IR 05000325, 324/2017004 w/Attachment: Supplemental Information

REGION II==

Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62 Report No.: 05000325/2017004, 05000324/2017004 Licensee: Duke Energy Progress, LLC Facility: Brunswick Steam Electric Plant, Units 1 and 2 Location: Southport, NC Dates: October 1, 2017 through December 31, 2017 Inspectors: G. Smith, Senior Resident Inspector J. Steward, Resident Inspector M. Schwieg, Resident Inspector M. Bates, Senior Operations Engineer Approved by: Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

Integrated Inspection Report 05000325/2017004, 05000324/2017004; October 1, 2017, through

December 31, 2017; Brunswick Steam Electric Plant, Units 1 and 2; Follow-up of Events.

The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There was one self-revealing violation and one licensee identified violation documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, (SDP) dated April 29, 2015.

The cross-cutting aspects are determined using IMC 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated November 1, 2016. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.

Cornerstone: Initiating Events

Green.

A self-revealing non-cited violation (NCV) was identified for the licensees failure to properly transfer power to the E-4 4160 volt emergency bus from the E-4 emergency diesel generator (EDG), to the normal switchgear bus 2C, as required by procedure 0OP-50.1 Diesel Generator Emergency Power System Operating Procedure. This resulted in a momentary under voltage condition followed by a re-energization of the E-4 emergency bus by EDG-4. This was entered into the licensees corrective action program (CAP) as nuclear condition report (NCR) 2151329.

The licensees failure to parallel across (i.e., reclose) the normal feeder breakers prior to unloading the EDG-4 and opening the EDG-4 output breaker, which resulted in a valid and automatic actuation of the EDG-4, was a performance deficiency. The finding was determined to be greater than minor because it was associated with the human performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Using IMC 0609.04, Initial Characterization of Findings, Exhibit 1, the issue was classified as a transient initiator contributor because it was associated with a loss of offsite power (LOOP). Finally, using Appendix A of IMC 0609, SDP for Findings at-Power, the finding was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating systems would not be available. Using Manual Chapter 0310, Aspects Within the Cross-Cutting Areas, the inspectors identified a cross-cutting aspect in the procedural adherence of the human performance area, because the operators failed to properly utilize an existing procedure pertinent to their particular situation and this directly resulted in the momentary loss of an emergency 4160 volt bus. [H.8] (Section 4OA3)

A violation of very low safety significance which was identified by the licensee was reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program (CAP). That violation and corrective action tracking number are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at essentially 100 percent rated thermal power (RTP) throughout the period.

However there were numerous instances where reactor power was limited by the power to flow maps described in the core operating limits report. There were also numerous minor down powers during the period in order to perform control rod adjustments. These adjustments provided adequate margin to increase recirculation flow in order to compensate for fuel burnup.

The elevated number of rod pattern adjustments was caused by an ongoing flux suppression activity as a result of a minor fuel cladding leak on one fuel assembly.

Unit 2 operated at essentially 100 percent RTP throughout the period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Seasonal Extreme Weather Conditions The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme low temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of and during seasonal extreme weather conditions. Documents reviewed are listed in the Attachment. The inspectors evaluated the following risk-significant systems:

  • Diesel Generating Building

b. Findings

No findings were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial Walkdown The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment.

The inspectors selected the following systems or trains to inspect:

  • EDG-2 while EDG-1 was OOS for planned maintenance

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection The inspectors evaluated the adequacy of selected pre-fire plans by comparing the pre-fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the pre-fire plans, the inspectors assessed the following items:

  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees corrective action program The inspectors toured the following four fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the attachment.
  • Unit 2 reactor building
  • EDG building cells 1 through 4
  • Control building elevation 24

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flooding The inspectors reviewed related flood analysis documents and walked down the area listed below containing risk-significant structures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for flood mitigation were consistent with design requirements and internal flooding analysis assumptions. The inspectors also assessed the condition of flood protection barriers and drain systems. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the corrective action program. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

a. Inspection Scope

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

On November 15, 2017, the inspectors observed a simulator scenario conducted for training of an operating crew during a routine requalification cycle. This evaluated scenario involved a high press coolant injection (HPCI) line leak resulting in a steam leak in the reactor building. This was followed by a leak in the circulating water (CW) system which resulted in internal flooding in the turbine building. Subsequently, the CW pumps were tripped and the reactor was scrammed, however the rods failed to insert into the core. Eventually, the scenario evolved to a line rupture in the suction of the recirculation pumps and with the failure of the HPCI system, an emergency depressurization was required.

The inspectors assessed the following:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance Documents reviewed are listed in the Attachment.

.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual

Plant/Main Control Room On December 13, 2017, the inspectors observed licensed operator performance in the main control room during a Unit 1 power reduction from 95 percent RTP to 87 percent RTP as a prerequisite to a control rod improvement evolution.

The inspectors assessed the following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision

.3 Annual Review of Licensee Requalification Examination Results

On September 29, 2017, the licensee completed the comprehensive biennial requalification written examinations and the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators Licenses. The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations, written examinations, and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the three issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. In addition, the inspectors performed a review of quality control activities to ensure the licensee was in compliance with their Quality Assurance Program requirements. Documents reviewed are listed in the Attachment.

  • Quality Control Sample - EDG-1 activities and safety-related cable verifications
  • EVAL-2016-BNP-6235-985 - Unit 1 Reactor Building Floor Drains Multiple Sump Pump Failures

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.

Documents reviewed are listed in the Attachment.

  • Yellow risk - Unit 2 B train RHR outage
  • Yellow risk - U1 Hardened Vent Wet well Modification and EDG-4 Planned Maintenance
  • EDG-4 extended outage beyond the 14-day limiting condition for operation
  • Emergent failure of Unit 1 HPCI steam admission valve

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors selected the operability evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment.

  • NCR 2059551 - Unit 2 A Core Spray pump venting (operator work around)
  • NCR 2126899 - Unit 2 RCIC water intrusion
  • NCR 2163106 - EDG-3 loading exceeds 3850 kW
  • NCR 2171772 - Master and slave breaker trip from Bus 1C to Bus E-2 during EDG-2 run

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • WO 11970471, NSW pump 1B The inspectors evaluated these activities for the following:
  • Acceptance criteria were clear and demonstrated operational readiness
  • Effects of testing on the plant were adequately addressed
  • Test instrumentation was appropriate
  • Tests were performed in accordance with approved procedures
  • Equipment was returned to its operational status following testing
  • Test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the surveillance tests listed below and either observed the test or reviewed test results to verify testing activities adequately demonstrated that the affected SSCs remained capable of performing the intended safety functions (under conditions as close as practical to design bases conditions or as required by technical specifications) and maintained their operational readiness.

The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.

Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.

Routine Surveillance Tests

  • 0PT-12.2A, No. 1 Diesel Generator Monthly Load Test, Rev. 116
  • 0OI-02.3, Drywell leakage Control, Revision 7

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the simulator evaluation conducted on November 14, 2017.

The inspectors observed licensee activities in the simulator to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (6 samples)

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator (PI) data submitted by the licensee for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between October 2016 and September 2017 to verify the accuracy and completeness of the data reported for the station. Additionally, the RHR Mitigating System Performance Index (MSPI) data from July 2016 through September 2016 was also reviewed. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.

Documents reviewed are listed in the Attachment.

Cornerstone: Mitigating Systems

  • MSPI: High Pressure Injection System (HPCI)
  • MSPI: Heat Removal System (RCIC)
  • MSPI: RHR System

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

a. Inspection Scope

.1 Routine Review

The inspectors screened items entered into the licensees CAP to identify repetitive equipment failures or specific human performance issues for followup. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Semi-Annual Trend Review

The inspectors reviewed issues entered in the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on human performance trends, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of July 2017 through December 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the Attachment.

b. Findings and Observations

No findings were identified. The inspectors noted a negative human performance trend for the last six months where operators were challenged by human performance errors.

The three examples below exhibited gaps in operator performance with respect to plant status control and electrical theory. The inspectors discussed this negative trend with the licensee and the weaknesses were acknowledged by the licensee.

  • NCR 2138147 - Operator inadvertently secured EDG during testing
  • NCR 2163106 - Operators exceeded kW limit during testing
  • NCR 2151329 - Operators failed to utilize procedure to reclose normal feeder breaker during testing (see section 4OA3)

4OA3 Follow-up of Events

(Closed) Licensee Event Report (LER) 05000325/2017-004-00, Emergency Diesel Generator and Primary Containment Isolation System Actuations

a. Inspection Scope

On September 17, 2017, the 4160 volt emergency bus E-4 was momentarily de-energized as a result of the operations crew opening the EDG-4 output breaker during planned surveillance testing. At the time of the event, the EDG-4 was solely carrying the loads on E-4 bus due to a spurious trip of the normal feeder breaker. The operators did not recognize this off normal condition and failed to transfer the power source back to the normal bus, 2C. Subsequently, the E-4 bus momentarily became de-energized until the EDG-4 output breaker automatically reclosed due to the safeguards logic detecting an under voltage condition. At this point, frequency control swapped from the droop mode to the isochronous mode. Upon recognition of the condition, the operators subsequently restored the normal power configuration which required paralleling across the normal feeder breakers. The inspectors evaluated plant status, mitigating actions, and the licensee's classification of the event, to enable the NRC to determine an appropriate NRC response. The events were reported to the NRC as event notification (EN) 52974 and documented in the licensees corrective action program as NCR 2151329.

The inspectors discussed the event with operations, maintenance, engineering, and licensee management personnel to gain an understanding of the conditions leading up to the event and assess licensee actions taken in response to the event. Additionally, the inspectors reviewed the licensees causal analysis to assess the detail and thoroughness of the evaluation and the adequacy of the proposed corrective actions.

The inspectors reviewed the LER and associated NCR to verify that the cause of the under-voltage condition was identified and whether corrective actions were appropriate.

The cause of the spurious opening of the normal feeder breaker (master and slave) was due to a faulty 81PK relay. This relay was designed to open the normal feeder breaker during an under frequency condition. However this relay is effectively bypassed during a design basis LOOP event. The licensees root cause evaluation identified the direct cause to be the operators failure to recognize that EDG-4 was the only power source to the E-4 bus due to spurious tripping of the normal feeder breakers. The inspectors concluded that the licensees corrective actions to this event were appropriate, including the disabling of the failed 81PK relay. The inspectors also verified that timely notifications were made in accordance with 10 CFR 50.72, that licensee staff properly restored the bus using the appropriate plant procedures, and that available plant equipment performed as required during the event. One finding was identified as discussed below. This LER is closed.

b. Findings

Introduction.

A Green self-revealing NCV was identified for the licensees failure to properly transfer power to the E-4 4160 volt emergency bus from the E-4 EDG, to the normal switchgear bus 2C, as required by procedure 0OP-50.1 Diesel Generator Emergency Power System Operating Procedure. This resulted in a momentary under voltage condition followed by a re-energization of the E-4 emergency bus by EDG-4.

Description.

On September 17, 2017, the licensee attempted to perform the monthly EDG-4 surveillance in accordance with 0PT-12.2D, No. 4 Diesel Generator Monthly Load Test. This evolution involved paralleling EDG-4 to the E-4 emergency 4160V bus and loading it to approximately 3500 kW to satisfy the monthly technical specification surveillance requirement. Following closure of the EDG-4 output breaker to the E-4 emergency bus, the operators noted what they deemed to be anomalous indications of the real and reactive power. After 45 minutes of troubleshooting, the operators decided to open the EDG-4 output breaker and consult with plant engineering. At the time, the operators failed to note that slightly after the initial closing of the EDG-4 output breaker, the feeder breakers (master and slave) from the normal power source, 2C bus had opened. At this time, EDG-4 was the only power source supplying the E-4 emergency bus. Upon opening of the EDG-4 output breaker, the E-4 bus experienced an under voltage condition and the EDG-4 output breaker immediately reclosed to resupply power to the bus. In this condition, the only change of state to the EDG-4 was the frequency control swapped from the droop mode to the isochronous mode, which was the safety mode for an under-voltage condition. Additionally, the voltage control swapped from droop to unity.

Soon after this event occurred, the operators realized that the master and slave feeder breakers had previously opened. The operators paralleled across the breakers and secured the EDG-4. Subsequent troubleshooting determined that the cause of the opening of the master and slave breaker was due to a failed 81PK relay. This relay provides under frequency protection only when the EDG is operating in parallel with the normal power supply and is bypassed during accident conditions (i.e., LOOP). The licensee disabled the 81PK relay and the surveillance was completed. This event was entered into the licensees CAP as NCR 2151329. The licensee performed a causal evaluation and determined that the operators failed to note the initial tripping of the normal feeder breakers which led them to incorrectly open the EDG-4 output breaker without first reclosing the normal feeder breakers.

Analysis.

The licensees failure to parallel across (i.e., reclose) the normal feeder breakers prior to unloading the EDG-4 and opening the EDG-4 output breaker which resulted in a valid and automatic actuation of the EDG-4 was a performance deficiency.

The finding was determined to be greater than minor because it was associated with the human performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Using IMC 0609.04, Initial Characterization of Findings, Exhibit 1, the issue was classified as a transient initiator contributor because it was associated with a LOOP. Finally, using Appendix A of IMC 0609, SDP for Findings at-Power, the finding was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating systems will not be available. The cause of this finding was determined to have a cross-cutting aspect in the area of human performance associated with procedural adherence. Specifically, the operators failed to properly utilize an existing procedure pertinent to their particular situation and this directly resulted in the momentary loss of an emergency 4160 volt bus.

Enforcement.

Unit 1 and Unit 2 TS 5.4.1 required, in part, that written procedures be established, implemented, and maintained covering the activities specified in Appendix A, Typical Procedures for Pressurized Water Reactors and Boiling Water Reactors, of Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operations), Revision 2, dated November 1972. Appendix A of RG 1.33 required, in part, that procedures be used for EDG operation. Brunswick plant procedure 0OP-50.1 provides procedural guidance for transferring power to the normal bus from the E-4 emergency bus when the EDG-4 is the sole power source. Contrary to the above, on September 17, 2017, the licensee failed to implement procedure 0OP-50.1 as required and this failure resulted in an automatic actuation of EDG-4. Because the finding was of very low safety significance and has been entered into the licensees CAP as NCR 2151329, this violation is being treated as an NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy: NCV 05000325,324/2017004-01, Loss of Emergency 4160V Bus Due to Failure to Implement Procedure.

4OA5 Other Activities

.1 World Association of Nuclear Operators (WANO) Report Review

In accordance with Executive Director of Operations Procedure 0220, Coordination with the Institute of Nuclear Power Operations, the inspectors reviewed the most recent WANO evaluation report dated January 2017 to determine if this report identified safety or training issues not previously identified by NRC evaluations. The report contained no safety issues that were not already known by the NRC.

.2 Operation of an Independent Spent Fuel Storage Installation (ISFSI)

(60855.1 - 1 sample)

a. Inspection Scope

The inspectors performed a walkdown of the onsite ISFSI and monitored the activities associated with the dry fuel storage campaign completed on December 21, 2017. The inspectors reviewed changes made to the ISFSI programs and procedures, including associated 10 CFR 72.48, Changes, Tests, and Experiments, screens and evaluations to verify that changes made were consistent with the license or certificate of compliance.

The inspectors reviewed records to verify that the licensee recorded and maintained the location of each fuel assembly placed in the ISFSI. The inspectors also reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On January 23, 2018, the resident inspectors presented the inspection results to Mr. Gideon and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

4OA7 Licensee-Identified Violation

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of the NRC Enforcement Policy, for being dispositioned as a NCV.

Unit 1 and Unit 2 facility operating license DPR-71 and DPR-62 condition 2.B.(6)requires, in part, that the licensee shall implement and maintain in effect all provisions of the approved fire protection program. Procedure AD-EG-ALL-1522, Duties of a Fire Watch, requires periodic fire watches to be performed within their designated time periods including any allowed grace periods. Contrary to the above, during the spring 2017 Unit 2 refueling outage, between March 1 and March 19, selected periodic fire watches were missed or not performed within the required grace periods.

The finding was screened using IMC 0609, Appendix F - Fire Protection Significance Determination Process, and was determined to be of very low safety significance (Green), because the reactor was able to reach and maintain safe shutdown. This issue was documented in the licensees CAP as NCR 2115035.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

K. Allen Director, Design Engineering

B. Bagwell Environmental & Chemistry

A. Baker Supervisor, Environmental & Chemistry
J. Berry Supervisor, LOCT Training
A. Brittain Director, Nuclear Plant Security
P. Brown Manager, Nuclear Performance Improvement
B. Bryant Manager, Nuclear Oversight

J. Bryant Regulatory Affairs

R. Carpenter Radiation Monitor Engineer

P. Dubrouillet Director, Nuclear Engineering, Mechanical Systems
C. Dunsmore Manager, Nuclear Outage

W. Gideon Vice President

L. Grzeck Manager, Nuclear Regulatory Affairs
J. Hicks Manager, Nuclear Training
B. Houston Manager, Nuclear Maintenance
J. Johnson Manager, Nuclear Chemistry
K. Krueger Manager, Nuclear Operations
J. McAdoo Manager, Nuclear Rad Protection
M. McPherson Director, Nuclear Organizational Effectiveness

K. Moser Plant Manager

B. Murray Licensing

J. Nolin General Manager, Nuclear Engineering
W. Orlando Superintendent, E/I&C

O. Paladiy Welding Engineer/Repair & Replacement Engineer

A. Padleckas Assistant Ops Manager, Training
D. Petrusic Superintendent, Environmental & Chemistry
J. Pierce Manager, Nuclear Work Management

E. Rau Operations Training

M. Regan Project Manager, Major Projects

L. Rohrbaugh Operator Training

M. Smiley Manager, Nuclear Ops Training

L. Spencer Operator Training

R. Wiemann Director, Nuclear Engineering, Electrical Reactor Systems

E. Williams Operations Manager

S. Williams BWRVIP Program Engineer

C. Winslow ISI Program Engineer

State of North Carolina

P. Cox Department of Health and Human Services

NRC Personnel

S. Rose Chief, Reactor Projects Branch 4, DRP

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000325,324/2017004-01 NCV Loss of Emergency 4160V Bus Due to Failure to Implement Procedure (Section 4OA3)

Closed

005000325;324/2017-004 LER Emergency Diesel Generator and Primary Containment Isolation System Actuations (Section 4OA3)

LIST OF DOCUMENTS REVIEWED