IR 05000324/2018001
| ML18122A331 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 05/02/2018 |
| From: | Steven Rose NRC/RGN-II/DRP/RPB4 |
| To: | William Gideon Duke Energy Progress |
| References | |
| IR 2018001 | |
| Download: ML18122A331 (22) | |
Text
May 2, 2018
SUBJECT:
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT 05000325/2018001 AND 05000324/2018001
Dear Mr. Gideon:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Steam Electric Plant, Units 1 and 2. On April 19, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in this report. This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violation or the significance of the violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the NRC Resident Inspector at the Brunswick Steam Electric Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC resident inspector at the Brunswick Steam Electric Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects
Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62
Enclosure:
IR 05000325/2018001 and 05000324/2018001
Inspection Report
Docket Numbers:
50-325, 50-324
License Numbers:
Report Numbers:
05000325/2018001, 05000324/2018001
Enterprise Identifier: I-2018-001-0053
Licensee:
Duke Energy Progress, LLC
Facility:
Brunswick Steam Electric Plant, Units 1 & 2
Location:
Southport, NC
Inspection Dates:
January 1, 2018 to March 31, 2018
Inspectors:
G. Smith, Senior Resident Inspector
J. Steward, Resident Inspector
M. Schwieg, Reactor Inspector
W. Loo, Senior Health Physicist
J. Panfel, Health Physicist
B. Collins, Reactor Inspector
S. Freeman, Senior Reactor Analyst
Approved By:
S. Rose, Chief
Reactor Projects Branch 4
Division of Reactor Projects
Enclosure
SUMMARY
The NRC continued monitoring licensees performance by conducting a quarterly integrated inspection at Brunswick Steam Electric Plant Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to http://www.nrc.gov/NRR/OVERSIGHT/ASSESS/index.html for more information. Any NRC and self-revealed findings, violations, and additional items are summarized in the table below.
List of Findings and Violations
Inadequate Instruction to Perform Inspections on Emergency Ventilation Dampers Cornerstone Significance Cross-cutting Aspect Report Section Barrier Integrity Green NCV 05000324/2018001-01 05000325/2018001-01 Closed H.5 - Work Management 71153 A self-revealing Green NCV of TS 5.4.1a, Procedures, was identified when the licensee failed to properly provide adequate work instructions associated with the control room emergency damper inspections. Specifically, the licensee disconnected the damper air supply line without adequate work instruction guidance, which caused a loss of Control Building Heating,
Ventilation and Air Conditioning (HVAC) and Control Room Emergency Ventilation (CREV)
Systems resulting in a safety system functional failure.
Additional Tracking Items
Type Issue number Title Report Section Status LER 05000325/2017-003-00 Unplanned Inoperability of CREV and Control Building HVAC 71153 Closed
PLANT STATUS
Unit 1 began the inspection period at 100 percent rated thermal power and operated there until January 28, 2018, when operators began a coast down into a refueling outage. On March 3, 2018, Unit 1 was shut down from 85 percent and remained shut down in a refueling outage for the remainder of the period.
Unit 2 began the period at 100 percent rated thermal power and operated there until February 16, 2018, when the unit was taken off-line for a forced outage due to a hot spot on the main turbine generator disconnect link (A phase). Following repairs, the unit was returned to 100 percent rated thermal power on February 20, 2018, and essentially operated at this level for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather (1 Sample)
The inspectors evaluated readiness for impending adverse weather conditions for winter storm Grayson on January 8, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 Standby Liquid Control System following maintenance on January 11, 2018
- (2) Unit 2 B and C Conventional Service Water (CSW) while 2 A CSW pump was out-of-service (OOS) for planned maintenance on February 17, 2018
- (3) Emergency Diesel Generator (EDG)-1 while EDG-2 was OOS for installation of an automatic voltage regulator on February 28, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the control rod drive system between February 12 and March 23, 2018.
71111.05AQ - Fire Protection Annual/Quarterly
Quarterly Inspection (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas between February 8 and March 23, 2018:
- (1) Unit 2 reactor building 20 elevation
- (2) Unit 1 drywell
- (3) Unit 1 turbine building 20 elevation
- (4) Unit 1 turbine building 45 elevation
- (5) Unit 1 turbine building 70 elevation
Annual Inspection (1 Sample)
The inspectors evaluated the fire brigade performance during a fire drill on February 8, 2018.
71111.08 - Inservice Inspection Activities
The inspectors evaluated boiling water reactor non-destructive testing by observing/reviewing the following examinations from February 5 to February 9, 2018:
- (1) Ultrasonic Examination a) 10 core spray system nozzle inner radius (1-B11-RPV-N5A-IRS), ASME Class 1 (observed)b) Reactor pressure vessel Ring 1 longitudinal seam weld @ 255° (1B11-RPV-E4B),
ASME Class 1 (observed)c) 12 feedwater system nozzle extension-to-safe end weld (1B21N4A-2-SW1-2),
ASME Class 1 (observed)
- (2) Liquid Penetrant Examination a) WO 20191808-1, 20 service water system reducer-to-flange weld (1-SW-911),
ASME Class 3 (reviewed; associated with welding package, which was also reviewed)
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (1 Sample)
The inspectors observed and evaluated Cycle 1 of operator retraining on March 2, 2018.
Operator Performance (2 Samples)
The inspectors observed and evaluated:
- (1) Unit 1 Final Feed water Temperature Reduction on January 18, 2018
- (2) Unit 2 EDG-4 Monthly Load Test on January 18, 2018
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 2 high pressure coolant injection (HPCI) valve packing failure on March 9, 2018
Quality Control (QC) (1 Sample)
The inspectors evaluated the below quality control activities between March 8 and March 22, 2018:
- (1) QC inspection of Unit 1 reactor coolant system (RCS) level indicator LI-R610 installation
- (2) QC torqueing inspection of U-clamp on the Unit 1 D residual heat removal service water system booster pump
- (3) QC cleanliness inspection of backup nitrogen check valves1-RNA-V-305 and -307
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) EDG-3/2A nuclear service water (SW) pump/supplemental EDG outage, on January 9, 2018
- (2) EDG-2 outage automatic voltage regulator modification, on March 2, 2018
- (3) Yellow plant status control risk as a result of electrical power on March 8, 2018, due to U1 unit auxiliary transformer outage
- (4) Emergent failure of the 1B1 battery during following a test discharge failure, on March 16, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) CR 2174081 - ISFSI HSM-001 prompt determination of operability for concrete spalling noted behind roof vent, on January 8, 2018
- (2) CR 2178808 - complex programmable logic device (CPLD) relays installed in EDGs, on February 7, 2018
- (3) CR 2175636 - Shells found in EDG-3 Jacket water heat exchanger, on February 12, 2018
- (4) CR 2172700 - HPCI steam valve packing leak, on March 23, 2018
71111.19 - Post Maintenance Testing
The inspectors evaluated the following post maintenance tests:
- (1) WO 20019415, 2A Conventional SW pump conduit rerouting, on March 2, 2018
- (2) WO 20040133, 2-SW-V-685, check valve removal and inspection, on March 2, 2018
- (3) WO 20062954, EDG-2 post maintenance test (PMT) from automatic voltage regulator (AVR) modification, on March 9, 2018
- (4) WO 20040132, 1-SW-V-685, check valve exam, on March 23, 2018
- (5) Control Rm In-leakage Test, Final Report via Vendor, on March 29, 2018
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated refueling outage B1R-22 activities from March 2, 2018, to March 31, 2018.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine
- (1) 0PT-12.2D Rev.118, EDG-4 Monthly Load Test, on January 26, 2018
- (2) WO 20180054, Functional Test of Service Water Building Sump Pump, on February 28, 2018
- (3) 0PT-46.6 Rev 6, Control Room In leakage Tracer Gas Test, on February 16, 2018
- (4) 0PT-12.1A, Rev. 5, No. 1 Diesel Generator LOOP/LOCA Loading Test, on March 23, 2018
Containment Isolation Valve (1 Sample)
- (1) 0PT-20.3A.5 Rev. 13, MSIV Leak Test, 1-B21-F028B, post maintenance LLRT per WO 20238741, on March 21,
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls
Radiological Hazard Assessment (1 Sample)
The inspectors evaluated radiological hazards assessments and controls.
Instructions to Workers (1 Sample)
The inspectors evaluated worker instructions.
Contamination and Radioactive Material Control (1 Sample)
The inspectors evaluated contamination and radioactive material controls.
Radiological Hazards Control and Work Coverage (1 Sample)
The inspectors evaluated radiological hazards control and work coverage.
High Radiation Area and Very High Radiation Area Controls (1 Sample)
The inspectors evaluated risk-significant high radiation area and very high radiation area controls.
Radiation Worker Performance and Radiation Protection Technician Proficiency (1 Sample)
The inspectors evaluated radiation worker performance and radiation protection technician proficiency.
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,
and Transportation
Radioactive Material Storage
The inspectors evaluated the licensees radioactive material storage.
Radioactive Waste System Walk-down (1 Sample)
The inspectors evaluated the licensees radioactive waste processing facility during plant walkdowns.
Waste Characterization and Classification (1 Sample)
The inspectors evaluated the licensees radioactive waste characterization and classification.
Shipment Preparations (1 Sample)
The inspectors evaluated the licensees radioactive material shipment preparation processes.
Shipment Records (1 Sample)
The inspectors evaluated the licensees non-excepted package shipment records.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified on March 16, 2018, the licensees performance indicators submittals listed below for the period from January 1, 2017 through December 31, 2017.===
- (1) Unit 1 and Unit 2 Unplanned Scrams per 7000 Critical Hours
- (2) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
- (3) Unit 1 and Unit 2 Unplanned Scrams with Complications
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issue:
- (1) CR 2097378 - Tracer gas test failure on main control room on March 23, 2018
71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports
The inspectors evaluated the following licensee event report which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
- (1) Licensee Event Report (LER) 05000325/2017-003-00, Unplanned Inoperability of CREV and Control Building HVAC, on March 30,
INSPECTION RESULTS
Inadequate Instruction to Perform Inspections on Emergency Ventilation Dampers Cornerstone Significance Cross-cutting Aspect Report Section Barrier Integrity
Green NCV 05000324/2018001-01 05000325/2018001-01 Closed H.5 - Work Management 71153
Introduction:
A self-revealing Green NCV of TS 5.4.1a, Procedures, was identified when the licensee failed to properly preplan and perform work instructions associated with the control room emergency ventilation (CREV) damper inspections. Specifically, the licensee disconnected the damper airline without work instruction guidance, which caused a loss of control building heating, ventilation and air conditioning (HVAC) and CREV systems, resulting in a safety system functional failure.
Description:
The first event occurred at 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br /> on June 5, 2017. The licensee was performing a work order (WO) 20036198-02 task to inspect 2-VA-2J-D-CB, Emergency Recirculation Damper. During the task, but without WO guidance, the licensee disconnected a damper actuator instrument airline to cycle the 2J damper to the open position. Afterwards, it was determined that disconnecting the damper actuator instrument airline had caused the Emergency Recirculation Damper 2J to become non-functional rendering both divisions of the CREV system inoperable. The CREV system was restored to operable status by 1009 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.839245e-4 months <br />.
The second event occurred at 1352 hours0.0156 days <br />0.376 hours <br />0.00224 weeks <br />5.14436e-4 months <br /> on June 5, 2017. The licensee was performing a WO 20036198-04 task to inspect 2-VA-2A-EAD-CB, Control Room Emergency Supply Fan A Inlet Isolation Damper. During the task, but without WO guidance, the licensee disconnected a damper actuator instrument airline to cycle the 2A damper to the open position. When the damper actuator airline was disconnected, the control building instrument air system pressure decrease resulted in subsequent loss of the control building HVAC and CREV systems. This event was self-revealing with the trip of both running control building HVAC units (1D-CU-CB and 2D-CU-CB control building air conditioning and Supply Fans). The technical specifications for this condition requires both units to be placed in MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and MODE 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The affected systems were restored by 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />.
In both events, the CREV system dampers were temporarily disabled by the loss of their pneumatic supply. With the CREV dampers unable to respond as required, the CREV system was inoperable and its safety function was lost. The CREV safety function is to minimize infiltration of contaminated air by removing radioactive particles, smoke and toxic gases from the control room envelope. The combined duration of inoperability was 54 minutes. The control building HVAC system was inoperable only during the second event.
The duration of inoperability was 15 minutes. There was no adverse impact on temperature or humidity in the control building during this event.
The licensee performed a root cause evaluation and determined the work order instructions did not contain precautions or limitations about operating dampers and the maintenance leadership has failed to effectively enforce work control standards to align workers and their behaviors to achieve successful maintenance execution.
Additionally, in August of 2015, Brunswick transitioned from PassPort to Consolidated Asset Suite. When this change happened, the instructions for all of the damper seal inspection tasks were revised, removing critical aspects that the damper seal should be inspected in the damper-closed position.
Inspectors determined from August 2015 until June 2017, the work order instruction was not maintained or properly planned when the instruction was revised to remove the damper inspection while in the closed position.
Corrective Actions: Corrective actions included restoring the affected pneumatic air supply, revising work order instructions to prevent damper operation, and improvements in crew performance standards.
Corrective Action Reference: NCR 2129139
Performance Assessment:
Performance Deficiency: The inspectors determined that the licensees failure to properly preplan and establish adequate work instructions for the emergency damper inspections was a performance deficiency.
Screening: The performance deficiency was more than minor because it was associated with Procedural Quality attribute of the Barrier Integrity cornerstone, and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. The CREV safety function is to minimize infiltration of contaminated air by removing radioactive particles was lost from the control room envelope.
Significance: The finding was screened in accordance with IMC 0609, Appendix A, The Significance Determination Process (SDP) For Findings At-Power dated June 19, 2012.
The finding was screened by Exhibit 3 - Barrier Integrity Screening Questions, under Section C - Control Room, Auxiliary, Reactor, or Spent Fuel Pool Building. Since the control room radiological barrier function and the barrier function against smoke or a toxic atmosphere were inoperable, a detailed risk evaluation was required. A regional senior reactor analyst (SRA) conducted the risk assessment using SAPHIRE software Version 8.1.6 and the Standardized Plant Analysis Risk (SPAR) Models, Version 8.50, for each of Units 1 and 2. Because the control room ventilation systems were not specifically modeled in SPAR, the SRA used human error probability (HEP) as a surrogate for the degraded condition. Also, given that no human errors were actually made and control room temperature remained less than 70 degrees Fahrenheit, the SRA increased each HEP by a factor of 10 for the degraded condition. The exposure time was one hour. The dominant sequences, which accounted for approximately 50 percent of the change, included loss of conventional service water with operator failure to initiate suppression pool cooling, fire water injection, or control low pressure coolant injection at low pressures, and loss of condenser heat sink with operator failure to depressurize the reactor or vent containment. The result was a change in core damage frequency of less than 1E-7/year for each unit and was primarily mitigated by the short exposure time. Because the change was less than 1E-7/year, no further analysis was needed for external events or large early release, and this finding was determined to be of very low safety significance (Green).
Cross-cutting Aspect: The finding had a cross-cutting aspect in the Work Management component of the Human Performance cross-cutting area (H.5), which required the organization to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority. Specifically, the licensee failed to plan, control, and execute the CREV work activities, which resulted in a loss of the CREV and control room HVAC systems.
Enforcement:
Violation: Technical Specification 5.4.1a, Procedures, states that written procedures shall be established, implemented, and maintained covering the following activities: a) the applicable procedures recommended in Regulatory Guide 1.33, Appendix A, November 1972 (Safety Guide 33, November 1972). Regulatory Guide 1.33, Appendix A, November 1972 (Safety Guide 33, November 1972),Section I, states in part that maintenance which can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstance. WO 20036198 was a documented instruction for safety-related ventilation system dampers.
Contrary to the above, from August 2015 until June 2017, the licensee failed to properly preplan and maintain adequate work instructions for the damper inspections on the CREV and control room HVAC systems. As a result, the CREV and control room HVAC systems became inoperable and could not perform their safety function.
Disposition: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors confirmed that proprietary information was controlled to protect from public disclosure.
- On April 19, 2018, the inspectors presented the inspection results to R. Gideon, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Common Documents Reviewed
Updated Final Safety Analysis Report
Individual Plant Examination
Individual Plant Examination of External Events
Technical Specifications and Bases
Technical Requirements Manual
Control Room Narrative Logs
Plan of the Day
71111.01 - Adverse Weather Protection
Procedures
0OI-01.03, Non-Routine Activities, Rev 70
0AP-062, Seasonal Preparations, Rev. 6
71111.04 - Equipment Alignment
Procedures
0OP-39, Diesel Generator Operating Procedure, Rev. 190
2OP-43, Service Water System Operating Procedure, Rev. 166
2OP-05, Standby Liquid Control System, Rev. 69
SD-05, Standby Liquid Control System, Rev.11
1OP-08, Control Rod Drive Hydraulic System Operating Procedure, Rev. 100
2OP-08, Control Rod Drive Hydraulic System Operating Procedure, Rev. 106
DBD-08, Control Rod Drive System, Rev. 9
SD-08, CRD Hydraulic System, Rev 13
Drawings
D-02547, Rev. 34
71111.05AQ - Fire Protection Annual/Quarterly
Procedures
0FPP-060 Fire Drill Program, Rev. 2
99-F-RB-03, Fire Drill Scenario Guide, Rev. 2
0PFP-013, General Fire Plan, Rev. 52
CSD-BNP-PFP-1RB, Unit 2 Reactor Building Pre-fire Plans Rev. 1
CSD-BNP-PFP-2RB, Unit 2 Reactor Building Pre-fire Plans Rev. 0
CSD-BNP-PFP-1TB, Turbine Building Pre-fire Plans, Rev. 3
71111.08 - Inservice Inspection Activities
Work Orders
20181808-011-SW-142-30-157: Repair Conventional and Vital Headers Drain Pipe, 3/13/18
Procedures
NDE-NE-ALL-6213, Utilization of PDI-UT-13 Procedure for Manual Phased Array Ultrasonic
Examination of Reactor Pressure Vessel Nozzle to Shell Welds and Nozzle Inner Radius
Regions Rev. 001
ISwT-PDI-AUT5 IHI Southwest Technologies, Inc. Operating Procedure: Automated Inside
Surface Ultrasonic Examination of Pressure Vessel Welds Using Phased Array Rev. 2
ISwT-NDE2 IHI Southwest Technologies, Inc. Operating Procedure: Ultrasonic Linearity
Measurements Rev. 0
54-ISI-869-000 AREVA Inc. Nondestructive Examination Procedure: Procedure for Encoded
Phased Array Ultrasonic Examination of Dissimilar Metal Piping Welds Rev. 000
AD-NE-ALL-1103 Calibration and Control of NDE Examination Equipment Rev. 0
Corrective Action
2194822 NCR: WO 20191808-01 Material Issued not in accordance with Spec 248-117,
3/28/18
2190611 AR: Nozzle N4A Weld 1B21N4A-2-SW1-2 Flaw Identified, 3/12/18
Other
VEN-18-003 Ultrasonic Examination Record (N5A Inner Radius), 3/13/18
Z3668 Zetec Calibration Certificate: TOPAZ 32/128PR (SN 665462), 1/16/17
Z3987 Zetec Calibration Certificate: DYNARAY-128/128PR, 1/29/18
N1051823 Weldstar Certificate of Compliance/Conformance, 9/19/14
N845297 Weldstar Certificate of Compliance, 10/12/09
Carolina Power & Light Company Procedure Qualification Record, 8/26/76
Carolina Power & Light Company Procedure Qualification Record, 10/20/80
243 Carolina Power & Light Company Procedure Qualification Record, 4/5/94
53320 AREVA Certificate of Calibration: Digital Thermometer (SN 160067), 2/9/18
51-9280231-000 AREVA Inc. Engineering Information Record: Automated Dissimilar Metal
Weld Examination Phased Array Technique Sheets for Brunswick Unit 1 B122 Spring 2018
Rev. 0
1-B11-0968 IHI Southwest Technologies Examination Summary Record (Ring 1 Longitudinal
Weld @ 255°), 3/20/18
1-FW-115-VIP Framatome Automated Ultrasonic Phased Array Examination Summary Sheet
(1B21N4A-2-SW1-2), 3/12/18
WPS 08 2 30 Carolina Power & Light Company Welding Procedure Specification Rev. 1
MAGNAFLUX Certificate of Certification: Ultragel II (Batch 14M076), 12/19/14
Duke Energy Certificate of Method Qualification: UT LII-N (May), 9/12/17
Duke Energy Visual Acuity Record (May), 9/6/17
Standards Laboratory Instrument Certification: IR Thermometer (ID G503098), 6/5/17
Day & Zimmerman Vision Acuity Record (Masey), 3/12/18
Day & Zimmerman Certification Record: PT LII (Masey), 5/4/16
Duke Energy Record of Welder Performance Qualification Test (Edwards), 8/30/17
Duke Energy Record of Welder Performance Qualification Test (Maloney), 2/24/16
MAGNAFLUX Certification: Spotcheck, SKC-S (Batch 16G17K), 7/29/16
MAGNAFLUX Certification: Spotcheck, SKL-SP2 (Batch 17B04K), 2/8/17
MAGNAFLUX Certification: Spotcheck, SKD-S2 (Batch 16L16K), 2/5/16
Review and Acceptance of Vendor Personnel and Examinations: UT LIII (Delgado), 3/3/18
Framatome Indication Notification Report: N4A Safe End to Pipe DM Weld
(1B21N4A-2-SW1-2), 3/12/18
Framatome Certificate of Personnel Qualification: UT LIII (Breza), 3/26/18
71111.11 - Licensed Operator Requalification Program and Licensed Operator
Performance
Procedures
0GP-13, Increasing Unit Capacity at End of Core Cycle, Rev. 48
Lesson Plans
OPS-EDG-DLA, Manual Transfer of Emergency Bus Supply from EDG to Normal Feeder,
Rev. 0
Other
LOR Exam 18-1 Version A Rev. 0
LOR Exam 18-1 Version B Rev. 0
71111.12 - Maintenance Effectiveness
Procedures
AD-EG-ALL-1210, Maintenance Rule Program, Rev. 1
Condition Reports
CR 2172700, Unit 2 HPCI Team Supply Packing Failure
Work Orders (WO)
WO20104840
WO12100402
Miscellaneous
NUMARC 93-01, Industry Guidelines for monitoring the effectiveness of maintenance at Nuclear
Power Plants, Rev. 4A
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Procedures
AD-OP-ALL-0201, Protected Equipment, Rev. 04
0AP-022, BNP Outage Risk Management, Rev. 56
AD-WC-ALL-0250, Work Implementation and Completion, Rev. 04
AD-WC-ALL-0410, Work Activity Integrated Risk Management, Rev. 03
AD-WC-ALL-0200, Online Work Management, Rev. 08
AD-OP-ALL-0201, Protected Equipment, Rev. 04
AD-WC-ALL-0430, Outage Risk Review, Rev. 02
0AP-025, BNP Integrated Scheduling, Rev. 56
71111.15 - Operability Determinations and Functionality Assessments
Procedures
NUHOMS Amend 10, Technical Specifications, Transnuclear, Inc., Storage System, Rev. 1
0ISFS-100, Horizontal Storage Module Assembly, Rev. 2
FP-86004, Transnuclear Dry Fuel Storage System, Rev. A
AD-OP-ALL-0105, Operability Determinations and Functionality Assessments, Rev. 4
AD-OP-ALL-0100, Corrective Action Program, Rev. 11
Condition Reports
CR 02174081, Inspection of ISFSI HSM and Prompt Operability Determination
CR 02178808, CPLD relays installed in EDGs
CR 2175636, Shells found in EDG-3 Jacket water HX
CR 2172700, HPCI steam valve packing leak
Drawings
F-08602, sheet 8, ISFSI Project Horizontal Storage Module Layout Details
71111.19 - Post Maintenance Testing
Procedures
0PLP-20, Post-Maintenance Testing Program, Rev. 49
Work Orders
WO 20019415, 2A Conventional SW pump conduit rerouting
WO 20040133, 2-SW-V-685, Check valve removal and inspection
WO 20062954, EDG-2 PMT from AVR modification
WO 20040132 1-SW-V-685 Check valve exam
Miscellaneous
Control Room In-leakage Test - Final Report from Vendor on January 18, 2018
71111.20 - Refueling and Other Outage Activities
Procedures
0FH-11, Fuel Handling, Rev. 107
0ENP-24.12, Preparation of Core Component Sequence Sheets, Rev. 50
0GP-05, Unit Shutdown, Rev 185
0GP-08, Refueling to Cold Shutdown, Rev 51
0GP-07, Preparations for Core Alterations, Rev 63
0GP-01, Pre-startup Checklist, Rev 197
0GP-02, Approach to Criticality and Pressurization of the Reactor, Rev 114
0GP-03, Unit Startup and Synchronization, Rev 88
0GP-04, Increasing Turbine Load to Rated Power, Rev 121
Clearance
25660
71111.22 - Surveillance Testing
Procedures
0PT-12.2D, NO.4 Diesel Generator Monthly Load Test, Rev. 118
0PT-46-6, Control Room Inleakage Tracer Gas Test, Rev. 6
0OI-2.3, Drywell Leakage Control, Rev.7
0PT-12.1B, No. 2 Diesel Generator LOOP/LOCA Loading Test, Rev. 5
AD-OP-ALL-1000, Conduct of Operations, Attachment 1, Adverse Condition Monitoring and
Contingency Planning Form for Unit 2 elevated drywell floor drain leakage, Rev. 9
IMC 2515 Appendix D, Plant Status, Attachment 1, Assessing RCS Unidentified Leakage Rate
Trend, effective January 1, 2018
0PT-20.3A.5, MSIV Leak Test, sec 7.3.3; Rev. 13
0ENP-16.4, Use of Leak Detection Equipment, Rev. 23
Condition Reports
2190194
Work Orders
2097378
20180054
Drawings
D-25021 sheet 1B, Rx Bldg Nuc Stm Supply Piping Diagram, Rev. 55
Miscellaneous
Lagus Applied Technology, Inc ltr dtd Feb 12, 2018, addressing preliminary tracer gas test
results from testing performed 2/7 - 2/9/18
71124.01 - Radiological Hazard Assessment and Exposure Controls
Procedures, Guidance Documents and Manuals
0AI-112, Control of Materials In Spent Fuel Pool, Rev. No. 27
0E&RC-0040, Administrative Controls for High Radiation Areas, Locked High Radiation Areas,
and Very High Radiation Areas, Rev. 43
0E&RC-0101, Performance and Tracking of Routine Surveillances, Rev. 8
0E&RC-0112, Discrete Radioactive Particle Control, Rev. 6
0E&RC-0115, Use and Calibration of the Small Article Monitors, Rev. 21
0E&RC-0117, Control of Work in the Hot Machine Shop, Rev. 5
0E&RC-0118, Decontamination for Areas, Materials, and Tools, Rev. 19
0E&RC-0229, Control and Use HEPA Air Filtration Units, Rev. 11
0E&RC-0241, Health Physics Coverage in Drywells During Fuel and Irradiated Component
Movement, Rev. 19
0E&RC-0261, Drywell Entry, Rev. 29
0E&RC-0500, Inventory Control and Leak Testing of Radioactive Sources, Rev. 27
0E&RC-0598, Control of Radwaste Containers in Interim Storage, Rev. 5
AD-PI-ALL-0100, Corrective Action Program, Rev. 13
AD-RP-ALL-0002, Radiation and Contamination Surveys, Rev. 0
AD-RP-ALL-0003, Radiological Air Sampling, Rev. 0
AD-RP-ALL-0004, Radiological Posting and Labeling, Rev. 0
AD-RP-ALL-0005, Access Controls for High and Locked High Radiation Areas, Rev. 0
AD-RP-ALL-0006, Personnel Contamination Monitoring, Rev. 0
AD-RP-ALL-0007, Control of Radioactive Material, Rev. 0
AD-RP-ALL-0008, Use and Control of HEPA Filtration and Vacuum Equipment, Rev. 0
AD-RP-ALL-0010, Radiological Job Coverage, Rev. 0
AD-RP-ALL-0011, Radiological Protection Fundamentals, Rev. 0
AD-RP-ALL-1000, Conduct of Radiation Protection, Rev. 4
AD-RP-ALL-2000, Preparation and Management of Radiation Work Permits, Rev. 3
AD-RP-ALL-2003, Investigation of Unusual Radiological Occurrences, Rev. 3
AD-RP-ALL-2004, Management of Large Scale Contamination Events, Rev. 0
AD-RP-ALL-2007, Radiation Protection Outage Readiness, Rev. 1
AD-RP-ALL-2007, Remote Monitoring, Rev. 4
AD-RP-ALL-2011, Radiation Protection Briefings, Rev. 3
AD-RP-ALL-2014, Work in Alpha Environments, Rev. 6
AD-RP-ALL-2015, Alpha Radiation Characterization, Rev. 2
AD-RP-ALL-2020, Radiological Controls for Diving Operations, Rev. 2
AD-RP-ALL-3002, Unconditional Release of Material, Rev. 1
AD-RP-ALL-3003, Outside Radioactive Material Container Inventory and Control, Rev. 2
AD-RP-ALL-7004, Operation of Air Sampling Equipment, Rev. 3
Records and Data
Analysis Report for Sample IDs: 180457_2, HP Charcoal Air Sample U1 TB 70 I/S Tb Shell,
03/03/18; 180464_1, HP Charcoal Air Sample U/1 Turbine 70 Manway, 03/04/18;
180465_2, HP Charcoal Air Sample U1 Turbine 70 Manway, 03/04/18; and 180467_1, HP
Charcoal Air Sample U/1 70 TB, 03/04/18
3, Clean Material Survey - Container Contents, 0E&RC-0216, Control and
Monitoring of Nonradioactive Plant Waste and Scrap, Rev. 31, Survey No. 082917-005,
08/29/17
7, Radioactive Source Inventory Reports, 0E&RC-0500, Inventory Control and Leak
Testing of Radioactive Sources, Rev. 27, 08/04/17 and 02/05/18
BNP 10 CFR Part 61 Radioactive Waste Stream Sample Information, 02/08/18
Brunswick Nuclear Plant Radiological Survey, Survey Nos: BNP-M-20180303-2, Map 2,
DW01_DW-5.001, 03/03/18, and Map 3, DW02_DW-17.001, 03/03/18; BNP-M-20180303-
26, DW03_DW-38.001, 03/03/18; BNP-M-20180304-7, DW05_DW67.001, 03/04/18; BNP-
M-20180304-11, DW05_DW67.001, 03/04/18; BNP-M-20180304-17, U1 RB Torus Pre Dive
Survey, 03/04/18; BNP-M-20180305-7, DW05_DW-67.001, 03/05/18; BNP-M-20180306-1,
DW05_DW-67.001, 03/06/18; BNP-M-20180306-7, DW05_DW-67.001, 03/06/18, 05:03;
BNP-M-20180306-7, DW05_DW-67.001, 03/06/18, 21:03; BNP-M-20180306-9, DW05_DW-
67.001, 03/06/18; BNP-M-20180306-11, DW09_DW-17 SRMA Replace/Remove,
03/06/18; and BNP-M-20180307-3, DW05_DW-67.001, 03/07/18
Brunswick Nuclear Project, Radiological Survey Record, One Line Air Sample Survey Form,
Survey No. 030718-009, Sampler Nos. HD-11825 (U1 DW Equip Hatch) and PA-12925 (U1 DW
PH), 03/07/18
National Source Tracking System, Annual Inventory Reconciliation Report, 01/11/18
Radiation Work Permit (RWP) Number (No.) 1500, Misc - High Radiological Risk Activities
LHRA/HCA (High Risk Activities), Task No. 3, RB, Torus Diving (Divers Only) - High Risk -
HRA/CA
RWP No. 1500, Misc - High Radiological Risk Activities LHRA/HCA (High Risk Activities), Task
No. 11, DW - Nuclear Instrumentation Activities (SRM/IRM Remove/Replace) - IER 11-41
High Risk Activities (LHRA/HCA/ARA), Rev. 1
RWP No. 1530, Operations Activities, Task No. 1, DW - OPS Activities - Medium Risk -
LHRA/HCA, Rev. 3
RWP No. 1539, TB Turbine/Generator System - Inspection & Repairs - Crew, Task No. 1, TB
Turbine Generator System - Inspections and Repairs - Low Risk Activities (RA/CA), Rev. 2
RWP No. 1540, Circ Water Activities, Task No. 1, TB, Circ Water System - Inspections and
Repairs - Low Risk Activities (RA/CA), Rev. 1
RWP No. 1554, RB Emergent RWCU Piping Replacement, Task No. 1, RB - RWCU Piping
Replacement L86 and Support - Low Risk - (RA/CA), Rev. 2
RWP No. 1574, NDE Complex Inspections, Task No. 1, DW NDE Complex Inspection
Activities - Medium Risk in LHRA/CA, Rev. 1
Work Order Package (WOP) 20143242 01, 2-F16-MIS, Perform Quarterly U/2 Spent Fuel Pool
Inspection, 12/05/17, Procedure No. 0AI-112, Control of Materials In Spent Fuel Pool,
Rev. No. 27, 12/05/17
WOP 20157065 01, Perform the Unit 1 Spent Fuel Pool Inspection, 02/06/18, Procedure No.
0AI-112, Control of Materials In Spent Fuel Pool, Rev. No. 27, 02/06/18
Corrective Action Program (CAP) Documents
2111178
2114719
2147461
2189186
Quick-Hitter Self-Assessment Report, No. 02086194-05, RP Field Operations, Undated
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling,
Storage, and Transportation
Procedures, Guidance Documents and Manuals
AD-PI-ALL-0100, Corrective Action Program, Rev. 13
AD-RP-ALL-0007, Control of Radioactive Material, Rev. 0
AD-RP-ALL-3003, Outside Radioactive Material Container Inventory and Control, Rev. 2
AD-RP-ALL-5000, Preparation and Shipment of Radioactive Material, Rev. 1
AD-RP-ALL-5002, 10 CFR 61 Radioactive Waste Classification, Rev. 0
Carolina Power & Light Company, Brunswick Nuclear Plant, Process Control Program (PCP),
Rev. 5
HPS-NGGC-0002, Vendor Cask Utilization Procedure, Rev. 24
0OI-03.10, Transferring Spent Resins of Filter Media to the Radwaste Processing Area, Rev. 12
Shipping Records and Radwaste Data
2015 and 2016 Annual Radioactive Effluent Release Report, Brunswick Steam Electric Plant
BNP 10 CFR Part 61 Radioactive Waste Stream Sample Information, 02/08/2018
List of All Abandoned Solid and Liquid Radwaste Processing Equipment, 2018
Shipment No.16-139
Shipment No.16-154
Shipment No.17-145
Shipment No.17-151
Shipment No.17-158
Shipment No.17-216
Shipping Logbook, Jan 2016 - Feb 2018
RC6C003G, Radiation Control Technicians Lesson Plan - Radioactive Material Shipping and
Regulatory Awareness, 05/2016
CAP Documents
2016-BNP-RP-01, Nuclear Oversight - Audit of Brunswick Radiation Protection, 06/02/16
2016944
2019275
2027786
2032219
2032676
2033531
2035377
2041791
2042597
2042953
2043481
2045838
2099171
2103619
2136550
2147461
2190058
2033860
2090604
71151 - Performance Indicator Verification
Other
Operator narrative logs from 2017
71152 - Problem Identification and Resolution
Procedures
AD-HU-ALL-0001, Human Performance Program, Rev. 12
AD-PI-ALL-0100, Corrective Action Program, Rev. 18
AD-SY-ALL-0401, Fitness for Duty Program, Rev. 2
AD-SY-ALL-0460, Managing Fatigue and Work Hour Limits, Rev. 1
AD-SY-ALL-1000, Conduct of Security, Rev. 2
AD-SY-ALL-0520, Security Training, Rev. 3
AD-PI-ALL-0101, Root Cause Evaluation, Rev. 04
AD-PI-ALL-0102, Apparent Cause Evaluation, Rev. 04
AD-PI-ALL-0103, Quick Cause Evaluation, Rev. 04
AD-PI-ALL-0400, Operating Experience Program, Rev. 05
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Report
2129139; Unplanned Inoperability of CREV and Control Building HVAC, Rev. 1
2185263; Unit 2 Phase A Main Generator No Load Disconnect indicating 282 degrees
Fahrenheit
Drawings
F-04080 Sheet1; Control Room Air Flow Diagram, Rev. 15
F-04080 Sheet1; Control Room Air Flow Diagram, Rev. 5
Miscellaneous
LER 2017-003-000; Control Room Air Conditioning and Emergency Ventilation Systems
Rendered Inoperable, Rev. 0
RCE 02129139; Unplanned Inoperability of CREV and Control Building HVAC, Rev. 1
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
245 PEACHTREE CENTER AVENUE NE, SUITE 1200
ATLANTA, GEORGIA 30303-1257
May 2, 2018
William R. Gideon
Site Vice President
Brunswick Steam Electric Plant
8470 River Rd. SE (M/C BNP001)
Southport, NC 28461
SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION
REPORT 05000325/2018001 AND 05000324/2018001
Dear Mr. Gideon:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Brunswick Steam Electric Plant, Units 1 and 2. On April 19, 2018, the NRC inspectors
discussed the results of this inspection with you and other members of your staff. The results of
this inspection are documented in the enclosed report.
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in
this report. This finding involved a violation of NRC requirements. The NRC is treating this
violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement
Policy.
If you contest the violation or the significance of the violation, you should provide a response
within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with
copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the
NRC Resident Inspector at the Brunswick Steam Electric Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the
- U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the
NRC resident inspector at the Brunswick Steam Electric Plant.
W. Gideon
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for
Withholding.
Sincerely,
/RA/
Steven
- D. Rose, Chief
Reactor Projects Branch 4
Division of Reactor Projects
Docket Nos.: 50-325, 50-324
Enclosure:
cc w/ encl: Distribution via ListServ
OFFICE
RII:DRP
RII:DRP
RII:DRS
RII:DRS
RII:DRS
RII:DRP
NAME
GSmith
JSteward
BCollins
JPanfel/Loo
WLoo
DJackson
DATE
4/30/2018
5/01/2018
4/30/2018
5/2/2018
4/30/18
5/2/2018
OFFICE
RII:DRP
RII:DRP
RII:DRP
RII:DRP
NAME
MSchwieg
JDodson
SFreeman
SRose
DATE
5/1/2018
5/2/2018
5/2/2018
5/2/2018
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Numbers:
50-325, 50-324
License Numbers:
Report Numbers:
05000325/2018001, 05000324/2018001
Enterprise Identifier: I-2018-001-0053
Licensee:
Duke Energy Progress, LLC
Facility:
Brunswick Steam Electric Plant, Units 1 & 2
Location:
Southport, NC
Inspection Dates:
January 1, 2018 to March 31, 2018
Inspectors:
- G. Smith, Senior Resident Inspector
- J. Steward, Resident Inspector
- M. Schwieg, Reactor Inspector
- W. Loo, Senior Health Physicist
- J. Panfel, Health Physicist
- B. Collins, Reactor Inspector
- S. Freeman, Senior Reactor Analyst
Approved By:
- S. Rose, Chief
Reactor Projects Branch 4
Division of Reactor Projects
SUMMARY
The NRC continued monitoring licensees performance by conducting a quarterly integrated
inspection at Brunswick Steam Electric Plant Units 1 and 2 in accordance with the Reactor
Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the
safe operation of commercial nuclear power reactors. Refer to
http://www.nrc.gov/NRR/OVERSIGHT/ASSESS/index.html for more information. Any NRC and
self-revealed findings, violations, and additional items are summarized in the table below.
List of Findings and Violations
Inadequate Instruction to Perform Inspections on Emergency Ventilation Dampers
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Green NCV 05000324/2018001-01
05000325/2018001-01
Closed
H.5 - Work
Management
A self-revealing Green NCV of TS 5.4.1a, Procedures, was identified when the licensee failed
to properly provide adequate work instructions associated with the control room emergency
damper inspections. Specifically, the licensee disconnected the damper air supply line without
adequate work instruction guidance, which caused a loss of Control Building Heating,
Ventilation and Air Conditioning (HVAC) and Control Room Emergency Ventilation (CREV)
Systems resulting in a safety system functional failure.
Additional Tracking Items
Type
Issue number
Title
Report
Section
Status
Unplanned Inoperability of
CREV and Control Building
Closed
PLANT STATUS
Unit 1 began the inspection period at 100 percent rated thermal power and operated there until
January 28, 2018, when operators began a coast down into a refueling outage. On
March 3, 2018, Unit 1 was shut down from 85 percent and remained shut down in a refueling
outage for the remainder of the period.
Unit 2 began the period at 100 percent rated thermal power and operated there until
February 16, 2018, when the unit was taken off-line for a forced outage due to a hot spot on the
main turbine generator disconnect link (A phase). Following repairs, the unit was returned to
100 percent rated thermal power on February 20, 2018, and essentially operated at this level for
the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather (1 Sample)
The inspectors evaluated readiness for impending adverse weather conditions for winter
storm Grayson on January 8, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1) Unit 2 Standby Liquid Control System following maintenance on January 11, 2018
(2) Unit 2 B and C Conventional Service Water (CSW) while 2 A CSW pump was out-of-
service (OOS) for planned maintenance on February 17, 2018
(3) Emergency Diesel Generator (EDG)-1 while EDG-2 was OOS for installation of an
automatic voltage regulator on February 28, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the control
rod drive system between February 12 and March 23, 2018.
71111.05AQ - Fire Protection Annual/Quarterly
Quarterly Inspection (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas between February 8 and March 23, 2018:
(1) Unit 2 reactor building 20 elevation
(2) Unit 1 drywell
(3) Unit 1 turbine building 20 elevation
(4) Unit 1 turbine building 45 elevation
(5) Unit 1 turbine building 70 elevation
Annual Inspection (1 Sample)
The inspectors evaluated the fire brigade performance during a fire drill on
February 8, 2018.
71111.08 - Inservice Inspection Activities (1 Sample)
The inspectors evaluated boiling water reactor non-destructive testing by
observing/reviewing the following examinations from February 5 to February 9, 2018:
(1) Ultrasonic Examination
a) 10 core spray system nozzle inner radius (1-B11-RPV-N5A-IRS), ASME Class 1
(observed)
b) Reactor pressure vessel Ring 1 longitudinal seam weld @ 255° (1B11-RPV-E4B),
ASME Class 1 (observed)
c) 12 feedwater system nozzle extension-to-safe end weld (1B21N4A-2-SW1-2),
ASME Class 1 (observed)
(2) Liquid Penetrant Examination
a) WO 20191808-1, 20 service water system reducer-to-flange weld (1-SW-911),
ASME Class 3 (reviewed; associated with welding package, which was also
reviewed)
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (1 Sample)
The inspectors observed and evaluated Cycle 1 of operator retraining on March 2, 2018.
Operator Performance (2 Samples)
The inspectors observed and evaluated:
(1) Unit 1 Final Feed water Temperature Reduction on January 18, 2018
(2) Unit 2 EDG-4 Monthly Load Test on January 18, 2018
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated
with the following equipment and/or safety significant functions:
(1) Unit 2 high pressure coolant injection (HPCI) valve packing failure on March 9, 2018
Quality Control (QC) (1 Sample)
The inspectors evaluated the below quality control activities between March 8 and
March 22, 2018:
(1) QC inspection of Unit 1 reactor coolant system (RCS) level indicator LI-R610 installation
(2) QC torqueing inspection of U-clamp on the Unit 1 D residual heat removal service water
system booster pump
(3) QC cleanliness inspection of backup nitrogen check valves1-RNA-V-305 and -307
71111.13 - Maintenance Risk Assessments and Emergent Work Control (4 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent
work activities:
(1) EDG-3/2A nuclear service water (SW) pump/supplemental EDG outage, on
January 9, 2018
(2) EDG-2 outage automatic voltage regulator modification, on March 2, 2018
(3) Yellow plant status control risk as a result of electrical power on March 8, 2018, due to
U1 unit auxiliary transformer outage
(4) Emergent failure of the 1B1 battery during following a test discharge failure, on
March 16, 2018
71111.15 - Operability Determinations and Functionality Assessments (4 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1) CR 2174081 - ISFSI HSM-001 prompt determination of operability for concrete spalling
noted behind roof vent, on January 8, 2018
(2) CR 2178808 - complex programmable logic device (CPLD) relays installed in EDGs, on
February 7, 2018
(3) CR 2175636 - Shells found in EDG-3 Jacket water heat exchanger, on February 12,
2018
(4) CR 2172700 - HPCI steam valve packing leak, on March 23, 2018
71111.19 - Post Maintenance Testing (5 Samples)
The inspectors evaluated the following post maintenance tests:
(1) WO 20019415, 2A Conventional SW pump conduit rerouting, on March 2, 2018
(2) WO 20040133, 2-SW-V-685, check valve removal and inspection, on March 2, 2018
(3) WO 20062954, EDG-2 post maintenance test (PMT) from automatic voltage regulator
(AVR) modification, on March 9, 2018
(4) WO 20040132, 1-SW-V-685, check valve exam, on March 23, 2018
(5) Control Rm In-leakage Test, Final Report via Vendor, on March 29, 2018
71111.20 - Refueling and Other Outage Activities (1 Sample)
The inspectors evaluated refueling outage B1R-22 activities from March 2, 2018, to
March 31, 2018.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine (4 Samples)
(1) 0PT-12.2D Rev.118, EDG-4 Monthly Load Test, on January 26, 2018
(2) WO 20180054, Functional Test of Service Water Building Sump Pump, on
February 28, 2018
(3) 0PT-46.6 Rev 6, Control Room In leakage Tracer Gas Test, on February 16, 2018
(4) 0PT-12.1A, Rev. 5, No. 1 Diesel Generator LOOP/LOCA Loading Test, on
March 23, 2018
Containment Isolation Valve (1 Sample)
(1) 0PT-20.3A.5 Rev. 13, MSIV Leak Test, 1-B21-F028B, post maintenance LLRT per
WO 20238741, on March 21, 2018
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls
Radiological Hazard Assessment (1 Sample)
The inspectors evaluated radiological hazards assessments and controls.
Instructions to Workers (1 Sample)
The inspectors evaluated worker instructions.
Contamination and Radioactive Material Control (1 Sample)
The inspectors evaluated contamination and radioactive material controls.
Radiological Hazards Control and Work Coverage (1 Sample)
The inspectors evaluated radiological hazards control and work coverage.
High Radiation Area and Very High Radiation Area Controls (1 Sample)
The inspectors evaluated risk-significant high radiation area and very high radiation area
controls.
Radiation Worker Performance and Radiation Protection Technician Proficiency (1 Sample)
The inspectors evaluated radiation worker performance and radiation protection technician
proficiency.
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,
and Transportation
Radioactive Material Storage (1 Sample)
The inspectors evaluated the licensees radioactive material storage.
Radioactive Waste System Walk-down (1 Sample)
The inspectors evaluated the licensees radioactive waste processing facility during plant
walkdowns.
Waste Characterization and Classification (1 Sample)
The inspectors evaluated the licensees radioactive waste characterization and
classification.
Shipment Preparations (1 Sample)
The inspectors evaluated the licensees radioactive material shipment preparation
processes.
Shipment Records (1 Sample)
The inspectors evaluated the licensees non-excepted package shipment records.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified on March 16, 2018, the licensees performance indicators submittals
listed below for the period from January 1, 2017 through December 31, 2017. (6 Samples)
(1) Unit 1 and Unit 2 Unplanned Scrams per 7000 Critical Hours
(2) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
(3) Unit 1 and Unit 2 Unplanned Scrams with Complications
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program
related to the following issue:
(1) CR 2097378 - Tracer gas test failure on main control room on March 23, 2018
71153 - Follow-up of Events and Notices of Enforcement Discretion
Licensee Event Reports (1 Sample)
The inspectors evaluated the following licensee event report which can be accessed at
https://lersearch.inl.gov/LERSearchCriteria.aspx:
(1) Licensee Event Report (LER) 05000325/2017-003-00, Unplanned Inoperability of CREV
and Control Building HVAC, on March 30, 2018
INSPECTION RESULTS
Inadequate Instruction to Perform Inspections on Emergency Ventilation Dampers
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Green
05000325/2018001-01
Closed
H.5 - Work
Management
Introduction: A self-revealing Green NCV of TS 5.4.1a, Procedures, was identified when the
licensee failed to properly preplan and perform work instructions associated with the control
room emergency ventilation (CREV) damper inspections. Specifically, the licensee
disconnected the damper airline without work instruction guidance, which caused a loss of
control building heating, ventilation and air conditioning (HVAC) and CREV systems, resulting
in a safety system functional failure.
Description: The first event occurred at 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br /> on June 5, 2017. The licensee was
performing a work order (WO) 20036198-02 task to inspect 2-VA-2J-D-CB, Emergency
Recirculation Damper. During the task, but without WO guidance, the licensee disconnected
a damper actuator instrument airline to cycle the 2J damper to the open position. Afterwards,
it was determined that disconnecting the damper actuator instrument airline had caused the
Emergency Recirculation Damper 2J to become non-functional rendering both divisions of the
CREV system inoperable. The CREV system was restored to operable status by 1009 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.839245e-4 months <br />.
The second event occurred at 1352 hours0.0156 days <br />0.376 hours <br />0.00224 weeks <br />5.14436e-4 months <br /> on June 5, 2017. The licensee was performing a
WO 20036198-04 task to inspect 2-VA-2A-EAD-CB, Control Room Emergency Supply Fan A
Inlet Isolation Damper. During the task, but without WO guidance, the licensee disconnected
a damper actuator instrument airline to cycle the 2A damper to the open position. When the
damper actuator airline was disconnected, the control building instrument air system pressure
decrease resulted in subsequent loss of the control building HVAC and CREV systems. This
event was self-revealing with the trip of both running control building HVAC units (1D-CU-CB
and 2D-CU-CB control building air conditioning and Supply Fans). The technical
specifications for this condition requires both units to be placed in MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />
and MODE 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The affected systems were restored by 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />.
In both events, the CREV system dampers were temporarily disabled by the loss of their
pneumatic supply. With the CREV dampers unable to respond as required, the CREV
system was inoperable and its safety function was lost. The CREV safety function is to
minimize infiltration of contaminated air by removing radioactive particles, smoke and toxic
gases from the control room envelope. The combined duration of inoperability was
minutes. The control building HVAC system was inoperable only during the second event.
The duration of inoperability was 15 minutes. There was no adverse impact on temperature
or humidity in the control building during this event.
The licensee performed a root cause evaluation and determined the work order instructions
did not contain precautions or limitations about operating dampers and the maintenance
leadership has failed to effectively enforce work control standards to align workers and their
behaviors to achieve successful maintenance execution.
Additionally, in August of 2015, Brunswick transitioned from PassPort to Consolidated Asset
Suite. When this change happened, the instructions for all of the damper seal inspection
tasks were revised, removing critical aspects that the damper seal should be inspected in the
damper-closed position.
Inspectors determined from August 2015 until June 2017, the work order instruction was not
maintained or properly planned when the instruction was revised to remove the damper
inspection while in the closed position.
Corrective Actions: Corrective actions included restoring the affected pneumatic air supply,
revising work order instructions to prevent damper operation, and improvements in crew
performance standards.
Corrective Action Reference: NCR 2129139
Performance Assessment:
Performance Deficiency: The inspectors determined that the licensees failure to properly
preplan and establish adequate work instructions for the emergency damper inspections was
a performance deficiency.
Screening: The performance deficiency was more than minor because it was associated with
Procedural Quality attribute of the Barrier Integrity cornerstone, and adversely affected the
cornerstone objective to provide reasonable assurance that physical design barriers protect
the public from radionuclide releases caused by accidents or events. The CREV safety
function is to minimize infiltration of contaminated air by removing radioactive particles was
lost from the control room envelope.
Significance: The finding was screened in accordance with IMC 0609, Appendix A, The
Significance Determination Process (SDP) For Findings At-Power dated June 19, 2012.
The finding was screened by Exhibit 3 - Barrier Integrity Screening Questions, under
Section C - Control Room, Auxiliary, Reactor, or Spent Fuel Pool Building. Since the
control room radiological barrier function and the barrier function against smoke or a toxic
atmosphere were inoperable, a detailed risk evaluation was required. A regional senior
reactor analyst (SRA) conducted the risk assessment using SAPHIRE software Version 8.1.6
and the Standardized Plant Analysis Risk (SPAR) Models, Version 8.50, for each of Units 1
and 2. Because the control room ventilation systems were not specifically modeled in SPAR,
the SRA used human error probability (HEP) as a surrogate for the degraded condition. Also,
given that no human errors were actually made and control room temperature remained less
than 70 degrees Fahrenheit, the SRA increased each HEP by a factor of 10 for the degraded
condition. The exposure time was one hour. The dominant sequences, which accounted for
approximately 50 percent of the change, included loss of conventional service water with
operator failure to initiate suppression pool cooling, fire water injection, or control low
pressure coolant injection at low pressures, and loss of condenser heat sink with operator
failure to depressurize the reactor or vent containment. The result was a change in core
damage frequency of less than 1E-7/year for each unit and was primarily mitigated by the
short exposure time. Because the change was less than 1E-7/year, no further analysis was
needed for external events or large early release, and this finding was determined to be of
very low safety significance (Green).
Cross-cutting Aspect: The finding had a cross-cutting aspect in the Work Management
component of the Human Performance cross-cutting area (H.5), which required the
organization to implement a process of planning, controlling, and executing work activities
such that nuclear safety was the overriding priority. Specifically, the licensee failed to plan,
control, and execute the CREV work activities, which resulted in a loss of the CREV and
control room HVAC systems.
Enforcement:
Violation: Technical Specification 5.4.1a, Procedures, states that written procedures shall be
established, implemented, and maintained covering the following activities: a) the applicable
procedures recommended in Regulatory Guide 1.33, Appendix A, November 1972 (Safety
Guide 33, November 1972). Regulatory Guide 1.33, Appendix A, November 1972 (Safety
Guide 33, November 1972),Section I, states in part that maintenance which can affect the
performance of safety-related equipment should be properly preplanned and performed in
accordance with written procedures, documented instructions, or drawings appropriate to the
circumstance. WO 20036198 was a documented instruction for safety-related ventilation
system dampers.
Contrary to the above, from August 2015 until June 2017, the licensee failed to properly
preplan and maintain adequate work instructions for the damper inspections on the CREV
and control room HVAC systems. As a result, the CREV and control room HVAC systems
became inoperable and could not perform their safety function.
Disposition: This violation is being treated as a Non-Cited Violation, consistent with
Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors confirmed that proprietary information was controlled to protect from public
disclosure.
On April 19, 2018, the inspectors presented the inspection results to
- R. Gideon, Site Vice
President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Common Documents Reviewed
Updated Final Safety Analysis Report
Individual Plant Examination
Individual Plant Examination of External Events
Technical Specifications and Bases
Technical Requirements Manual
Control Room Narrative Logs
Plan of the Day
71111.01 - Adverse Weather Protection
Procedures
0OI-01.03, Non-Routine Activities, Rev 70
0AP-062, Seasonal Preparations, Rev. 6
71111.04 - Equipment Alignment
Procedures
0OP-39, Diesel Generator Operating Procedure, Rev. 190
2OP-43, Service Water System Operating Procedure, Rev. 166
2OP-05, Standby Liquid Control System, Rev. 69
SD-05, Standby Liquid Control System, Rev.11
1OP-08, Control Rod Drive Hydraulic System Operating Procedure, Rev. 100
2OP-08, Control Rod Drive Hydraulic System Operating Procedure, Rev. 106
DBD-08, Control Rod Drive System, Rev. 9
SD-08, CRD Hydraulic System, Rev 13
Drawings
D-02547, Rev. 34
71111.05AQ - Fire Protection Annual/Quarterly
Procedures
0FPP-060 Fire Drill Program, Rev. 2
99-F-RB-03, Fire Drill Scenario Guide, Rev. 2
0PFP-013, General Fire Plan, Rev. 52
CSD-BNP-PFP-1RB, Unit 2 Reactor Building Pre-fire Plans Rev. 1
CSD-BNP-PFP-2RB, Unit 2 Reactor Building Pre-fire Plans Rev. 0
CSD-BNP-PFP-1TB, Turbine Building Pre-fire Plans, Rev. 3
71111.08 - Inservice Inspection Activities
Work Orders
20181808-011-SW-142-30-157: Repair Conventional and Vital Headers Drain Pipe, 3/13/18
Procedures
NDE-NE-ALL-6213, Utilization of PDI-UT-13 Procedure for Manual Phased Array Ultrasonic
Examination of Reactor Pressure Vessel Nozzle to Shell Welds and Nozzle Inner Radius
Regions Rev. 001
ISwT-PDI-AUT5 IHI Southwest Technologies, Inc. Operating Procedure: Automated Inside
Surface Ultrasonic Examination of Pressure Vessel Welds Using Phased Array Rev. 2
ISwT-NDE2 IHI Southwest Technologies, Inc. Operating Procedure: Ultrasonic Linearity
Measurements Rev. 0
54-ISI-869-000 AREVA Inc. Nondestructive Examination Procedure: Procedure for Encoded
Phased Array Ultrasonic Examination of Dissimilar Metal Piping Welds Rev. 000
AD-NE-ALL-1103 Calibration and Control of NDE Examination Equipment Rev. 0
Corrective Action
2194822 NCR: WO 20191808-01 Material Issued not in accordance with Spec 248-117,
3/28/18
2190611 AR: Nozzle N4A Weld 1B21N4A-2-SW1-2 Flaw Identified, 3/12/18
Other
VEN-18-003 Ultrasonic Examination Record (N5A Inner Radius), 3/13/18
Z3668 Zetec Calibration Certificate: TOPAZ 32/128PR (SN 665462), 1/16/17
Z3987 Zetec Calibration Certificate: DYNARAY-128/128PR, 1/29/18
N1051823 Weldstar Certificate of Compliance/Conformance, 9/19/14
N845297 Weldstar Certificate of Compliance, 10/12/09
Carolina Power & Light Company Procedure Qualification Record, 8/26/76
Carolina Power & Light Company Procedure Qualification Record, 10/20/80
243 Carolina Power & Light Company Procedure Qualification Record, 4/5/94
53320 AREVA Certificate of Calibration: Digital Thermometer (SN 160067), 2/9/18
51-9280231-000 AREVA Inc. Engineering Information Record: Automated Dissimilar Metal
Weld Examination Phased Array Technique Sheets for Brunswick Unit 1 B122 Spring 2018
Rev. 0
1-B11-0968 IHI Southwest Technologies Examination Summary Record (Ring 1 Longitudinal
Weld @ 255°), 3/20/18
1-FW-115-VIP Framatome Automated Ultrasonic Phased Array Examination Summary Sheet
(1B21N4A-2-SW1-2), 3/12/18
WPS 08 2 30 Carolina Power & Light Company Welding Procedure Specification Rev. 1
MAGNAFLUX Certificate of Certification: Ultragel II (Batch 14M076), 12/19/14
Duke Energy Certificate of Method Qualification: UT LII-N (May), 9/12/17
Duke Energy Visual Acuity Record (May), 9/6/17
Standards Laboratory Instrument Certification: IR Thermometer (ID G503098), 6/5/17
Day & Zimmerman Vision Acuity Record (Masey), 3/12/18
Day & Zimmerman Certification Record: PT LII (Masey), 5/4/16
Duke Energy Record of Welder Performance Qualification Test (Edwards), 8/30/17
Duke Energy Record of Welder Performance Qualification Test (Maloney), 2/24/16
MAGNAFLUX Certification: Spotcheck, SKC-S (Batch 16G17K), 7/29/16
MAGNAFLUX Certification: Spotcheck, SKL-SP2 (Batch 17B04K), 2/8/17
MAGNAFLUX Certification: Spotcheck, SKD-S2 (Batch 16L16K), 2/5/16
Review and Acceptance of Vendor Personnel and Examinations: UT LIII (Delgado), 3/3/18
Framatome Indication Notification Report: N4A Safe End to Pipe DM Weld
(1B21N4A-2-SW1-2), 3/12/18
Framatome Certificate of Personnel Qualification: UT LIII (Breza), 3/26/18
71111.11 - Licensed Operator Requalification Program and Licensed Operator
Performance
Procedures
0GP-13, Increasing Unit Capacity at End of Core Cycle, Rev. 48
Lesson Plans
OPS-EDG-DLA, Manual Transfer of Emergency Bus Supply from EDG to Normal Feeder,
Rev. 0
Other
LOR Exam 18-1 Version A Rev. 0
LOR Exam 18-1 Version B Rev. 0
71111.12 - Maintenance Effectiveness
Procedures
AD-EG-ALL-1210, Maintenance Rule Program, Rev. 1
Condition Reports
CR 2172700, Unit 2 HPCI Team Supply Packing Failure
Work Orders (WO)
WO20104840
WO12100402
Miscellaneous
NUMARC 93-01, Industry Guidelines for monitoring the effectiveness of maintenance at Nuclear
Power Plants, Rev. 4A
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Procedures
AD-OP-ALL-0201, Protected Equipment, Rev. 04
0AP-022, BNP Outage Risk Management, Rev. 56
AD-WC-ALL-0250, Work Implementation and Completion, Rev. 04
AD-WC-ALL-0410, Work Activity Integrated Risk Management, Rev. 03
AD-WC-ALL-0200, Online Work Management, Rev. 08
AD-OP-ALL-0201, Protected Equipment, Rev. 04
AD-WC-ALL-0430, Outage Risk Review, Rev. 02
0AP-025, BNP Integrated Scheduling, Rev. 56
71111.15 - Operability Determinations and Functionality Assessments
Procedures
NUHOMS Amend 10, Technical Specifications, Transnuclear, Inc., Storage System, Rev. 1
0ISFS-100, Horizontal Storage Module Assembly, Rev. 2
FP-86004, Transnuclear Dry Fuel Storage System, Rev. A
AD-OP-ALL-0105, Operability Determinations and Functionality Assessments, Rev. 4
AD-OP-ALL-0100, Corrective Action Program, Rev. 11
Condition Reports
CR 02174081, Inspection of ISFSI HSM and Prompt Operability Determination
CR 02178808, CPLD relays installed in EDGs
CR 2175636, Shells found in EDG-3 Jacket water HX
CR 2172700, HPCI steam valve packing leak
Drawings
F-08602, sheet 8, ISFSI Project Horizontal Storage Module Layout Details
71111.19 - Post Maintenance Testing
Procedures
0PLP-20, Post-Maintenance Testing Program, Rev. 49
Work Orders
WO 20019415, 2A Conventional SW pump conduit rerouting
WO 20040133, 2-SW-V-685, Check valve removal and inspection
WO 20062954, EDG-2 PMT from AVR modification
WO 20040132 1-SW-V-685 Check valve exam
Miscellaneous
Control Room In-leakage Test - Final Report from Vendor on January 18, 2018
71111.20 - Refueling and Other Outage Activities
Procedures
0FH-11, Fuel Handling, Rev. 107
0ENP-24.12, Preparation of Core Component Sequence Sheets, Rev. 50
0GP-05, Unit Shutdown, Rev 185
0GP-08, Refueling to Cold Shutdown, Rev 51
0GP-07, Preparations for Core Alterations, Rev 63
0GP-01, Pre-startup Checklist, Rev 197
0GP-02, Approach to Criticality and Pressurization of the Reactor, Rev 114
0GP-03, Unit Startup and Synchronization, Rev 88
0GP-04, Increasing Turbine Load to Rated Power, Rev 121
Clearance
25660
71111.22 - Surveillance Testing
Procedures
0PT-12.2D, NO.4 Diesel Generator Monthly Load Test, Rev. 118
0PT-46-6, Control Room Inleakage Tracer Gas Test, Rev. 6
0OI-2.3, Drywell Leakage Control, Rev.7
0PT-12.1B, No. 2 Diesel Generator LOOP/LOCA Loading Test, Rev. 5
AD-OP-ALL-1000, Conduct of Operations, Attachment 1, Adverse Condition Monitoring and
Contingency Planning Form for Unit 2 elevated drywell floor drain leakage, Rev. 9
IMC 2515 Appendix D, Plant Status, Attachment 1, Assessing RCS Unidentified Leakage Rate
Trend, effective January 1, 2018
0PT-20.3A.5, MSIV Leak Test, sec 7.3.3; Rev. 13
0ENP-16.4, Use of Leak Detection Equipment, Rev. 23
Condition Reports
2190194
Work Orders
2097378
20180054
Drawings
D-25021 sheet 1B, Rx Bldg Nuc Stm Supply Piping Diagram, Rev. 55
Miscellaneous
Lagus Applied Technology, Inc ltr dtd Feb 12, 2018, addressing preliminary tracer gas test
results from testing performed 2/7 - 2/9/18
71124.01 - Radiological Hazard Assessment and Exposure Controls
Procedures, Guidance Documents and Manuals
0AI-112, Control of Materials In Spent Fuel Pool, Rev. No. 27
0E&RC-0040, Administrative Controls for High Radiation Areas, Locked High Radiation Areas,
and Very High Radiation Areas, Rev. 43
0E&RC-0101, Performance and Tracking of Routine Surveillances, Rev. 8
0E&RC-0112, Discrete Radioactive Particle Control, Rev. 6
0E&RC-0115, Use and Calibration of the Small Article Monitors, Rev. 21
0E&RC-0117, Control of Work in the Hot Machine Shop, Rev. 5
0E&RC-0118, Decontamination for Areas, Materials, and Tools, Rev. 19
0E&RC-0229, Control and Use HEPA Air Filtration Units, Rev. 11
0E&RC-0241, Health Physics Coverage in Drywells During Fuel and Irradiated Component
Movement, Rev. 19
0E&RC-0261, Drywell Entry, Rev. 29
0E&RC-0500, Inventory Control and Leak Testing of Radioactive Sources, Rev. 27
0E&RC-0598, Control of Radwaste Containers in Interim Storage, Rev. 5
AD-PI-ALL-0100, Corrective Action Program, Rev. 13
AD-RP-ALL-0002, Radiation and Contamination Surveys, Rev. 0
AD-RP-ALL-0003, Radiological Air Sampling, Rev. 0
AD-RP-ALL-0004, Radiological Posting and Labeling, Rev. 0
AD-RP-ALL-0005, Access Controls for High and Locked High Radiation Areas, Rev. 0
AD-RP-ALL-0006, Personnel Contamination Monitoring, Rev. 0
AD-RP-ALL-0007, Control of Radioactive Material, Rev. 0
AD-RP-ALL-0008, Use and Control of HEPA Filtration and Vacuum Equipment, Rev. 0
AD-RP-ALL-0010, Radiological Job Coverage, Rev. 0
AD-RP-ALL-0011, Radiological Protection Fundamentals, Rev. 0
AD-RP-ALL-1000, Conduct of Radiation Protection, Rev. 4
AD-RP-ALL-2000, Preparation and Management of Radiation Work Permits, Rev. 3
AD-RP-ALL-2003, Investigation of Unusual Radiological Occurrences, Rev. 3
AD-RP-ALL-2004, Management of Large Scale Contamination Events, Rev. 0
AD-RP-ALL-2007, Radiation Protection Outage Readiness, Rev. 1
AD-RP-ALL-2007, Remote Monitoring, Rev. 4
AD-RP-ALL-2011, Radiation Protection Briefings, Rev. 3
AD-RP-ALL-2014, Work in Alpha Environments, Rev. 6
AD-RP-ALL-2015, Alpha Radiation Characterization, Rev. 2
AD-RP-ALL-2020, Radiological Controls for Diving Operations, Rev. 2
AD-RP-ALL-3002, Unconditional Release of Material, Rev. 1
AD-RP-ALL-3003, Outside Radioactive Material Container Inventory and Control, Rev. 2
AD-RP-ALL-7004, Operation of Air Sampling Equipment, Rev. 3
Records and Data
Analysis Report for Sample IDs: 180457_2, HP Charcoal Air Sample U1 TB 70 I/S Tb Shell,
03/03/18; 180464_1, HP Charcoal Air Sample U/1 Turbine 70 Manway, 03/04/18;
180465_2, HP Charcoal Air Sample U1 Turbine 70 Manway, 03/04/18; and 180467_1, HP
Charcoal Air Sample U/1 70 TB, 03/04/18
3, Clean Material Survey - Container Contents, 0E&RC-0216, Control and
Monitoring of Nonradioactive Plant Waste and Scrap, Rev. 31, Survey No. 082917-005,
08/29/17
7, Radioactive Source Inventory Reports, 0E&RC-0500, Inventory Control and Leak
Testing of Radioactive Sources, Rev. 27, 08/04/17 and 02/05/18
BNP 10 CFR Part 61 Radioactive Waste Stream Sample Information, 02/08/18
Brunswick Nuclear Plant Radiological Survey, Survey Nos: BNP-M-20180303-2, Map 2,
DW01_DW-5.001, 03/03/18, and Map 3, DW02_DW-17.001, 03/03/18; BNP-M-20180303-
26, DW03_DW-38.001, 03/03/18; BNP-M-20180304-7, DW05_DW67.001, 03/04/18; BNP-
M-20180304-11, DW05_DW67.001, 03/04/18; BNP-M-20180304-17, U1 RB Torus Pre Dive
Survey, 03/04/18; BNP-M-20180305-7, DW05_DW-67.001, 03/05/18; BNP-M-20180306-1,
DW05_DW-67.001, 03/06/18; BNP-M-20180306-7, DW05_DW-67.001, 03/06/18, 05:03;
BNP-M-20180306-7, DW05_DW-67.001, 03/06/18, 21:03; BNP-M-20180306-9, DW05_DW-
67.001, 03/06/18; BNP-M-20180306-11, DW09_DW-17 SRMA Replace/Remove,
03/06/18; and BNP-M-20180307-3, DW05_DW-67.001, 03/07/18
Brunswick Nuclear Project, Radiological Survey Record, One Line Air Sample Survey Form,
Survey No. 030718-009, Sampler Nos. HD-11825 (U1 DW Equip Hatch) and PA-12925 (U1 DW
PH), 03/07/18
National Source Tracking System, Annual Inventory Reconciliation Report, 01/11/18
Radiation Work Permit (RWP) Number (No.) 1500, Misc - High Radiological Risk Activities
LHRA/HCA (High Risk Activities), Task No. 3, RB, Torus Diving (Divers Only) - High Risk -
HRA/CA
RWP No. 1500, Misc - High Radiological Risk Activities LHRA/HCA (High Risk Activities), Task
No. 11, DW - Nuclear Instrumentation Activities (SRM/IRM Remove/Replace) - IER 11-41
High Risk Activities (LHRA/HCA/ARA), Rev. 1
RWP No. 1530, Operations Activities, Task No. 1, DW - OPS Activities - Medium Risk -
LHRA/HCA, Rev. 3
RWP No. 1539, TB Turbine/Generator System - Inspection & Repairs - Crew, Task No. 1, TB
Turbine Generator System - Inspections and Repairs - Low Risk Activities (RA/CA), Rev. 2
RWP No. 1540, Circ Water Activities, Task No. 1, TB, Circ Water System - Inspections and
Repairs - Low Risk Activities (RA/CA), Rev. 1
RWP No. 1554, RB Emergent RWCU Piping Replacement, Task No. 1, RB - RWCU Piping
Replacement L86 and Support - Low Risk - (RA/CA), Rev. 2
RWP No. 1574, NDE Complex Inspections, Task No. 1, DW NDE Complex Inspection
Activities - Medium Risk in LHRA/CA, Rev. 1
Work Order Package (WOP) 20143242 01, 2-F16-MIS, Perform Quarterly U/2 Spent Fuel Pool
Inspection, 12/05/17, Procedure No. 0AI-112, Control of Materials In Spent Fuel Pool,
Rev. No. 27, 12/05/17
WOP 20157065 01, Perform the Unit 1 Spent Fuel Pool Inspection, 02/06/18, Procedure No.
0AI-112, Control of Materials In Spent Fuel Pool, Rev. No. 27, 02/06/18
Corrective Action Program (CAP) Documents
2111178
2114719
2147461
2189186
Quick-Hitter Self-Assessment Report, No. 02086194-05, RP Field Operations, Undated
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling,
Storage, and Transportation
Procedures, Guidance Documents and Manuals
AD-PI-ALL-0100, Corrective Action Program, Rev. 13
AD-RP-ALL-0007, Control of Radioactive Material, Rev. 0
AD-RP-ALL-3003, Outside Radioactive Material Container Inventory and Control, Rev. 2
AD-RP-ALL-5000, Preparation and Shipment of Radioactive Material, Rev. 1
AD-RP-ALL-5002, 10 CFR 61 Radioactive Waste Classification, Rev. 0
Carolina Power & Light Company, Brunswick Nuclear Plant, Process Control Program (PCP),
Rev. 5
HPS-NGGC-0002, Vendor Cask Utilization Procedure, Rev. 24
0OI-03.10, Transferring Spent Resins of Filter Media to the Radwaste Processing Area, Rev. 12
Shipping Records and Radwaste Data
2015 and 2016 Annual Radioactive Effluent Release Report, Brunswick Steam Electric Plant
BNP 10 CFR Part 61 Radioactive Waste Stream Sample Information, 02/08/2018
List of All Abandoned Solid and Liquid Radwaste Processing Equipment, 2018
Shipment No.16-139
Shipment No.16-154
Shipment No.17-145
Shipment No.17-151
Shipment No.17-158
Shipment No.17-216
Shipping Logbook, Jan 2016 - Feb 2018
RC6C003G, Radiation Control Technicians Lesson Plan - Radioactive Material Shipping and
Regulatory Awareness, 05/2016
CAP Documents
2016-BNP-RP-01, Nuclear Oversight - Audit of Brunswick Radiation Protection, 06/02/16
2016944
2019275
2027786
2032219
2032676
2033531
2035377
2041791
2042597
2042953
2043481
2045838
2099171
2103619
2136550
2147461
2190058
2033860
2090604
71151 - Performance Indicator Verification
Other
Operator narrative logs from 2017
71152 - Problem Identification and Resolution
Procedures
AD-HU-ALL-0001, Human Performance Program, Rev. 12
AD-PI-ALL-0100, Corrective Action Program, Rev. 18
AD-SY-ALL-0401, Fitness for Duty Program, Rev. 2
AD-SY-ALL-0460, Managing Fatigue and Work Hour Limits, Rev. 1
AD-SY-ALL-1000, Conduct of Security, Rev. 2
AD-SY-ALL-0520, Security Training, Rev. 3
AD-PI-ALL-0101, Root Cause Evaluation, Rev. 04
AD-PI-ALL-0102, Apparent Cause Evaluation, Rev. 04
AD-PI-ALL-0103, Quick Cause Evaluation, Rev. 04
AD-PI-ALL-0400, Operating Experience Program, Rev. 05
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Report
2129139; Unplanned Inoperability of CREV and Control Building HVAC, Rev. 1
2185263; Unit 2 Phase A Main Generator No Load Disconnect indicating 282 degrees
Fahrenheit
Drawings
F-04080 Sheet1; Control Room Air Flow Diagram, Rev. 15
F-04080 Sheet1; Control Room Air Flow Diagram, Rev. 5
Miscellaneous
LER 2017-003-000; Control Room Air Conditioning and Emergency Ventilation Systems
Rendered Inoperable, Rev. 0
RCE 02129139; Unplanned Inoperability of CREV and Control Building HVAC, Rev. 1