IR 05000282/2019004

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Integrated Inspection Report 05000282/2019004 and 05000306/2019004
ML20028F249
Person / Time
Site: Prairie Island  
Issue date: 01/27/2020
From: Hironori Peterson
Region 3 Branch 3
To: Sharp S
Northern States Power Company, Minnesota
References
IR 2019004
Download: ML20028F249 (22)


Text

January 27, 2020

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT - INTEGRATED INSPECTION REPORT 05000282/2019004 AND 05000306/2019004

Dear Mr. Sharp:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Prairie Island Nuclear Generating Plant. On January 16, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff.

The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Hironori Peterson, Chief Branch 3 Division of Reactor Projects

Docket Nos. 05000282 and 05000306 License Nos. DPR-42 and DPR-60

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000282 and 05000306

License Numbers:

DPR-42 and DPR-60

Report Numbers:

05000282/2019004 and 05000306/2019004

Enterprise Identifier: I-2019-004-0056

Licensee:

Northern States Power Company, Minnesota

Facility:

Prairie Island Nuclear Generating Plant

Location:

Welch, Minnesota

Inspection Dates:

October 01, 2019 to December 31, 2019

Inspectors:

S. Bell, Health Physicist

E. Fernandez, Reactor Inspector

L. Haeg, Senior Resident Inspector

K. Pusateri, Resident Inspector

N. Shah, Project Engineer

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Prairie Island Nuclear Generating Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 operated at or near full power for the entirety of the inspection period. Unit 2 began the inspection period at approximately 74 percent power, coasting down for a refueling outage that began on October 4, 2019. The unit was returned to full power on October 31, 2019, and operated at full power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures on 12/16/2019 for the following systems:

Unit 2 emergency diesel generators and cooling water systems

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 A train 480V and 4160V systems with B train equipment out-of-service during

2R31 on 10/17/2019 (2)

Unit 2 A train containment spray system following surveillance testing on 11/07/2019

(3) 22 diesel-driven cooling water pump seal water system on 11/13/2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 2 containment on 10/16/2019
(2) Unit 2 A containment spray pump room on 11/07/2019
(3) Plant screenhouse during fire header maintenance on 11/12/2019
(4) Unit 2 emergency diesel generator D5/D6 building on 12/19/2019
(5) Bus 150/160 and no. 22 battery rooms on 12/19/2019

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) 22 component cooling water heat exchanger on 10/10/2019

===71111.08P - Inservice Inspection Activities (PWR)

PWR Inservice Inspection Activities Sample (IP Section 03.01)===

(1) The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from 10/07/2019 to 10/11/2019:

03.01.a - Nondestructive Examination and Welding Activities.

  • H-4/IA
  • Visual Examination (VT-1) of Intergal Attachment (Snubber), CCH-182/IA
  • Repair Cracked Weld on Alignment Lugs for Equipment Hatch

(WO-700001472)

03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

  • Issue ID-501000005225 Boric Acid Evaluation of Bolted Connection on 22 RHR Pump Discharge Line
  • Issue ID-501000004041 Boric Acid Evaluation of Bolted Connection on Valve CV-31229 RCP Loop BPRPZR Spray CV
  • Issue ID-501000005466 Boric Acid Evaluation of Bolted Connection on Valve 2VC-28-2 22 Charging Pump Discharge Relief

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room on 12/27/2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated operator re-qualification in the simulator on 12/05/2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Maintenance effectiveness for cooling water system components on 11/14/2019

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Quality control program regarding equipment approaching end of qualified life on 10/15/2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Maintenance risk during reduced inventory in preparation for reactor head lift on 10/7/2019
(2) Emergent work associated with D5 emergency diesel generator fuel oil transfer system leak on 12/4/2019
(3) Maintenance risk during work week beginning 12/22/2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2 letdown orifice isolation valve issue past operability review (AR 501000032151)on 10/11/2019
(2) U2 B train residual heat removal void issue past operability review (AR 501000031667) on 10/08/2019
(3) Cooling water piping corrosion issue (AR 501000032539) on 10/02/2019 (4)22 turbine-driven auxiliary feedwater pump high outboard bearing temperature issue (AR 501000033986) on 10/28/2019
(5) Passive motor-operated valve usage procedural issue (AR 501000031050) on 10/31/2019
(6) Fuel oil leak on D5 emergency diesel generator (AR 501000034334) on 11/04/2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Bus 26 following refueling outage modifications and maintenance on 11/05/2019
(2) D6 diesel generator following refueling outage maintenance on 10/15/2019 (3)22 component cooling water heat exchanger following maintenance on 10/17/2019 (4)21 safety injection pump following seal replacement on 10/22/2019 (5)22 containment spray pump following seal replacement on 10/19/2019
(6) D2 diesel generator air start solenoid following failure to close after surveillance testing on 11/12/2019 (7)12 motor-driven auxiliary feed water pump following replacement of auxiliary lubricating oil pump auxiliary relay on 11/26/2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Unit 2 refueling outage 2R31 activities from 10/04/2019 to 10/31/2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) SP 2314; 22 Battery Discharge Test on 10/15/2019
(2) SIP 2036; Unit 2 Turbine Overspeed Trip Test on 10/28/2019

Inservice Testing (IP Section 03.01) (1 Sample)

(1) SP 2083B, Unit 2 Integrated SI Test With a Simulated Loss of Offsite Power Train B on 10/22/2019

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) SP 2072.11; Local Leakage Rate Test of Penetration 11 (Letdown Line) on 10/09/2019

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes.
  • PI-2018-617, 12/17/18
  • PI-2018-633, 01/31/19
  • PI-2019-656, 02/22/19
  • PI-2019-679, 06/18/19

This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Licensed operator re-qualification training with Drill and Exercise Performance Indicator opportunities on 11/20/2019

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls.

(1) The inspectors reviewed the following:

Radiological Surveys

  • U2 Containment Refueling Floor 10/02/2019 through 10/10/2019
  • U2 Containment Reactor Cavity 10/02/2019 through 10/10/2019
  • U1 Containment 10/07/2019 through 10/10/2019

Risk Significant Radiological Work Activities

  • U1 Containment Entry at Full Reactor Power
  • U2 Containment Reactor Refueling Activities

Air Sample Survey Records

  • U2 Containment 10/02/2019 23:32
  • U2 Containment Upper Reactor Cavity 10/08/2019 13:45
  • U1 Containment 10/09/2019 01:06
  • U2 Containment Reactor Cavity 10/10/201901:32

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas.

(1) The inspectors reviewed the following:

Radiation Work Packages

  • Radiation Work Permit 190002; U1 Containment and Annulus at Power Activities - Online; Revision 01
  • Radiation Work Permit 190000; GL-08 Work - Online; Revision 01
  • Radiation Work Permit 192042; 2R31 Reactor (Rx) Head Disassembly

/Reassembly; Revision 01

  • Radiation Work Permit 192040; 2R31 Refuel Work; Revision 00

Electronic Alarming Dosimeter Alarms

  • Electronic dosimeter dose rate alarm 12/07/2018 09:42
  • Electronic dosimeter dose rate alarm 12/19/2018 08:35
  • Electronic dosimeter dose rate alarm 10/02/2019 19:47
  • Electronic dosimeter dose rate alarm 10/05/2019 22:45

Labeling of Containers

  • Five equipment storage containers in the radioactive waste barrel yard

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material.

(1) The inspectors verified the following sealed sources are accounted for and are intact:

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and observation of radiological work activities.

(1) There were no radiological work package for areas with airborne radioactivity available for inspection.

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)

(1) The inspectors evaluated risk-significant high radiation area and very high radiation area controls.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)

(1) The inspectors evaluated radiation worker performance and radiation protection technician proficiency.

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning.

(1) The inspectors reviewed the following activities:
  • RWP 192040; 2R31 Refuel Work
  • RWP 192042; Reactor Head Disassembly/Reassembly

Implementation of ALARA and Radiological Work Controls (IP Section 02.03) (1 Sample)

The inspectors reviewed as low as reasonably achievable practices and radiological work controls.

(1) The inspectors reviewed the following activities:
  • RWP 192040; 2R31 Refuel Work
  • RWP 192042; Reactor Head Disassembly/Reassembly

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Self-Contained Breathing Apparatus for Emergency Use (IP Section 02.03) (1 Sample)

The inspectors evaluated self-contained breathing apparatus program implementation.

(1) The inspectors reviewed the following:

Status and Surveillance Records for Self-Contained Breathing Apparatus

===090900SG

  • 095924KS
  • 090920SG

Self-Contained Breathing Apparatus Fit for On-Shift Operators

  • On-shift crew number #1; 12/04/2019

Self-Contained Breathing Apparatus Maintenance Check

  • 090890SG
  • 095933KS
  • 090900SG

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) Unit 1 between 10/01/2018 and 9/30/2019
(2) Unit 2 between 10/01/2018 and 9/30/2019

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 between 10/01/2018 and 09/30/2019
(2) Unit 2 between 10/01/2018 and 09/30/2019

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 between 10/01/2018 and 09/30/2019
(2) Unit 2 between 10/01/2018 and 09/30/2019

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)

(1)

(1) Unit 1 July 1, 2018 through September 30, 2019 (2)
(2) Unit 2 July 1, 2018 through September 30, 2019

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1)

(1) July 1, 2018 through September 30, 2019

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1)

(1) July 1, 2018 through September 30, 2019

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed existing Unit 2 degraded, non-conforming, and adverse condition monitoring issues resolved during 2R31 on 10/17/2019

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) AR 501000030644, "NRC Question: Flood Barriers" and internal flood program on 12/03/2019
(2) Apparent Cause Evaluation 501000031050 regarding equipment classifications on 12/06/2019

71153 - Followup of Events and Notices of Enforcement Discretion Reporting (IP Section 03.05)

(1) The inspectors reviewed LER 2019-001-00 and the subsequent cancellation of this LER on 12/16/2019

INSPECTION RESULTS

Minor Violation 71152 Minor Violation: On August 12, 2019, the inspectors identified a Unit 2 RHR flood barrier that was shorter in height than other similar flood barriers. Specifically, a steel sleeve surrounding the floor penetration of Unit 2 RHR heat exchanger discharge piping was 15.5 inches tall, while similar sleeves installed on adjacent RHR piping were 24 inches tall. The inspectors questioned the discrepancy and the licensee evaluated this issue under AR 501000030644, NRC Question: Flood Barriers. The inspectors reviewed the licensees evaluation of this AR, the corrective actions, and they also performed a corrective action program review of the licensees internal flooding program.

The licensee determined that the existing auxiliary building design basis flooding analysis, ENG-ME-448, Auxiliary Building Flooding Analysis, Revision 1B, dated November 28, 2013, did not differentiate between postulated flooding caused by high energy line break (HELB)events and postulated flooding caused by ruptures of non-high energy piping. Additionally, the analysis did not distinguish between those systems specifically credited for safe shutdown following the different postulated flood events. The licensee also determined that RHR was not a credited system for safe shutdown following flooding from HELB-induced actuation of the fire protection system; however, RHR was credited for safe shutdown following postulated flooding caused by ruptures involving certain non-high energy piping. The licensee refined the calculation methodology and adjusted inputs to account for the shorter barrier. Based on this, the licensee determined that with the shorter barrier, RHR room flooding would not begin until 513 minutes after the onset of the postulated flood. This conclusion provided additional margin to the USAR Section 6.1.2.8.2 stated time of 296 minutes for this scenario. Because margin was added following re-calculation, and the associated time critical operator action to isolate flood water for this scenario was validated to occur within approximately 37 minutes, Unit 2 RHR operability was not affected by the shorter flood barrier.

Screening: The inspectors determined the performance deficiency was minor. Although the licensee's internal flooding design basis analysis for the auxiliary building contained an incorrect input for the maximum postulated flood height, revision of the analysis demonstrated that more margin existed than was previously understood. Therefore, the performance deficiency did not have the potential to lead to a more significant safety concern if left uncorrected.

Enforcement:

The failure to assure that the postulated internal flood design basis was correctly translated into the specifications for a Unit 2 RHR flood barrier per the requirements of Title 10 CFR, Appendix B, Criterion III, "Design Control," constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. To restore compliance, the licensee revised ENG-ME-448, and planned to update Prairie Island USAR Section 6.1.2.8.2.

Observation: Apparent Cause Evaluation for Containment Isolation Valve Active/Passive Concern 71152 The inspectors reviewed an apparent cause evaluation associated with AR 501000031050 regarding Technical Specification testing requirements for 12 sample containment isolation valves. The inspectors reviewed the apparent cause, corrective actions, and extent of condition/cause, and did not identify any issues of concern.

Observation: Unit 2 Refueling Outage Item Resolution 71152 The inspectors performed a trend review of corrective action program items scheduled for resolution during the Unit 2 refueling outage conducted in October of 2019. These items included degraded, non-conforming, and adverse condition monitoring issues, as well as removal of any temporary modifications that were scoped into the outage schedule. The inspectors reviewed whether any trends existed in the bases for deferred items and/or aggregate impacts. The inspectors also reviewed final corrective actions taken for those issues that were addressed during the refueling outage. The inspectors did not identify any concerns during these reviews.

Observation: Cancellation of LER 2019-001-00 on 12/16/2019 71153 The inspectors reviewed LER 2019-001-00 and the subsequent cancellation of this LER on 12/16/2019. The inspectors reviewed the reporting basis under a partial sample in Section 71153 of Prairie Island Inspection Report 2019003. After the LER was submitted, the licensee subsequently determined during inspections and testing during a Unit 2 refueling outage that a condition prohibited by Technical Specifications did not occur. Therefore, the licensee cancelled the LER. The inspectors reviewed the basis for the cancellation and did not identify any issues of concern. This LER is closed.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 16, 2020, the inspectors presented the integrated inspection results to Mr. S. Sharp, Site Vice President and other members of the licensee staff.
  • On October 10, 2019, the inspectors presented the Radiation Protection Baseline inspection results to Mr. S. Sharp, Site Vice President and other members of the licensee staff.
  • On October 24, 2019, the inspectors presented the ISI Inspection for Prairie Island 2R31 inspection results to Ms. S. Schwartz, Fleet Regulatory Affairs and other members of the licensee staff.
  • On December 5, 2019, the inspectors presented the radiation protection baseline inspection results to Mr. H. Hanson, Plant Manager and other members of the licensee staff.
  • On January 16, 2020, the inspectors presented the Integrated Inspection Report inspection results to Mr. S. Sharp, Site Vice President and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed an Institute of Nuclear Power Operations report that was issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

AR

501000034574

Seasonal Readiness Preparation

11/12/2019

AR

501000035542

No Prompt Exists for Cold Temperature Checks

2/10/2019

Procedures

TP 1637

Winter Plant Operation

71111.04Q Corrective Action

Documents

Resulting from

Inspection

AR

501000034697

DDCLP Filter Question from NRC Resident

11/14/2019

Drawings

NF-39216-1

Flow Diagram Cooling Water - Screenhouse Unit 1 & Unit 2

04/11/2007

NF-39237

Flow Diagram Containment Spray System Units 1 and 2

NF-39252

Flow Diagram Caustic Addition System Units 1 and 2

Procedures

C1.1.20.5-2

Unit 2 4.16kV System Switches and Indication Checklist

C1.1.20.6-2A

Unit 2 480V System Switches and Indication Checklist

71111.05Q Drawings

F5 Appendix A

Fire Detection Zone 35; 21 and 22 Battery Rooms; Floor

Elevation 695'

Fire Plans

F5 Appendix A

Fire Detection Zone 54; Fire Area 71; Reactor Building Unit

2; Elevation 755'

F5 Appendix A

Fire Detection Zone 52; Fire Area 71; Reactor Building Unit

2; Elevation 733' 9"

F5 Appendix A

Fire Detection Zone 42; Fire Area 71; Reactor Building Unit

2, Elevation 697' 6"'

F5 Appendix A

Fire Detection Zone 56; Fire Area 71; Reactor Building Unit

2; Elevation 711' 6"

Procedures

F5 APP K

Fire Protection Systems Functional Requirements

Fire Detection

Zone 40-

Appendix A

Unit 2 Auxiliary Building, Elevation 695'

71111.07A

Procedures

GMP YUBA-001

CC Heat Exchanger Periodic Maintenance

H21

Generic Letter 89-13 Implementing Program

Work Orders

GMP YUBA-001

WO 498516; GMP YUBA-001

10/30/2015

71111.08P

Corrective Action

20015381

Shelf Life for Liquid Penetrant Materials

07/26/2011

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

501000031647

Framatone SG Welding Issues

09/23/2019

NDE Reports

2019P001

Liquid Penetrant Examination (PT) of Class 1 Intergral

10/10/2019

2019U014

Ultrasonic Examination (UT) of Elbow to Pipe Weld on

Reactor Coolant System, Component ID W-6

10/10/2019

2019U016

Ultrasonic Examination (UT) of Elbow to Elbow Weld on

Reactor Coolant System, Component ID W-5

10/10/2019

2019V013

Visual Examination (VT) of Intergal Attachment (Snubber)

Component ID CCH-182/IA

10/09/2019

Procedures

2000004765

PDI Generic Procedure for Ultrasonic Examination of

Austenitic Pipe Welds PDI-UT-2

10/04/2017

FP-PE-NDE-200

Solvent Removable Visual Dye Penetrant Examination

FP-PE-NDE-402

Ultrasonic Examination of Austenitic Pipe Welds-

Supplement 2

FP-PE-NDE-408

Straight Beam Ultrasonic Examination of Bolts and Studs

FP-PE-NDE_510

Visual Examination, VT-1

01/13/2017

71111.11Q Work Orders

WO 700055782

SP 1106B-22 DD CL PMP (245-392) 1 M Test

2/27/2019

71111.13

Corrective Action

Documents

AR

501000035273

Hole Found in 3" Fuel Oil Supply Line

2/02/2019

AR

501000036061

Oil Addition 22 CC PMP OB

2/24/2019

71111.15

Corrective Action

Documents

AR

501000028115

Auxiliary Building Roof Leak

06/06/2019

AR

501000031050

Passive MOV Usage Procedural Steps

08/21/2019

AR

501000031973

Missed Surveillance on Sampling CIVs

09/16/2019

AR

501000031991

MOVs to be Rescoped to GL PGM

09/16/2019

AR

501000032539

Prompt Operability Determination POD 500000300508

AR

501000033348

D6 FO Valves Forming Signs of Drip

10/15/2019

AR

High Temperature Cycle 8 Engine 1 D6

10/15/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

501000033349

AR

501000033362

D6 Electric Governor Fail

10/15/2019

AR

501000033567

245-071, 21 SI PMP Outboard Seal Leak

10/19/2019

AR

501000033567

245-071, 21 SI Pump Outboard Seal Leak

10/19/2019

AR

501000033944

TDAFP Governor Adjustment

10/26/2019

AR

501000033975

PMT Work Plan has PEG Step Prevention SUPR

10/26/2019

AR

501000033986

TD AFWP High Outboard BRG Temperature

10/28/2019

Procedures

FP-E-MR-03

Maintenance Rule Monitoring

FP-E-MR-07

Maintenance Rule - Structures Monitoring

H24.3

Structures Monitoring Program

PM 3586-10

Periodic Structures Inspection

PM 3586-10

Periodic Structures Inspection

PM 3586-11

Shield Building Caulking Inspection

SP 2036

Turbine Overspeed Trip Exercise

SP 2088A

Train A Safety Injection Quarterly Test

SP 2103B

Unit 2 Train B AFW Comprehensive IST Pump and Valve

Test

71111.19

Corrective Action

Documents

AR

501000033056

Bus 26 Inspection

10/09/2019

AR

501000033362

D6 Electric Governor Fail

10/15/2019

SP 2083B

Unit 2 Integrated SI Test with a Simulated Loss of Offsite

Power Train B

71111.20

Corrective Action

Documents

AR

501000033397

Entered C17 AOP3

10/15/2019

AR

501000033412

Bowed Fuel Bundle Critical Path Lost Time

10/14/2019

Procedures

2C1-3-M5

Unit 2 Shutdown to Mode 5

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2C4.1

RCS Inventory Control Refueling

2R31

Prairie Island Refueling Outage October 2019

09/03/2019

CP# 2R31-1

Outage Contingency Planning Form-Decay Heat Removal

Single Point Vulnerability to Orange

06/04/2019

CP# 2R31-2

Outage Contingency Planning Form - Protect SFP CC Flow

for all Alignments

06/04/2019

CP# 2R31-3

Lowered Inventory Pre-Refuel

06/04/2019

CP# 2R31-4

Outage Contingency Planning Form - 2R31 Lowered

Inventory Post-Refuel

06/04/2019

CP# 2R31-5

Outage Contingency Planning Form-SSA Power Single

Point Vulnerability to Orange

06/04/2019

CP# 2R31-8

Outage Contingency Planning Form-CC HX Open Flood

Plan

06/04/2019

D2-15

Unit 2 Reduced Inventory SI Lineup

D2-9

Draining the Reactor Coolant System Unit 2-MV-32169

Open Breaker Off Highlighted

D30

Post Refueling Startup Testing

PRA No:

V.SMN.17.002

Reactor Cavity GOTHIC Time to Boil

SP 2294

Installation/Removal of Automatic SI Reset Bypasses

71111.22

Corrective Action

Documents

AR

501000033076

CV-31620 Exceeded Admin Limit on LLRT

10/09/2019

Operability

Evaluations

2C20.9 AOP4

Failure of 22 Battery Charger

Procedures

H19

Containment Leakage Rate Testing

SP 2072.11

Local Leakage Rate Test of Penetration 11 (Letdown Line)

SP 2083B

Unit 2 Integrated SI Test With a Simulated Loss of Offsite

Power Train B

SP 2314

Battery Refueling Outage Discharge Test

Work Orders

SP 2083B

Protected Equipment Work Approval Form - Bus 25-1

10/22/2019

WO 700025162

Install Temp Charger on 22 Battery

WO 700030150

SP 2083B-Integrated SI Test w/Simulated Loop B Train

08/14/2019

WO 700038207

SP 2072.11-LLRT 2 PEN 11 Post-Maintenance

06/10/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO 70029825

SP 2072.11-LLRT 2PEN Letdown Line

10/09/2019

71114.04

Corrective Action

Documents

05000022935

NOS ID: Question Regarding EAL Calculation

2/08/2019

501000022887

NOS-ID: Emergency Plan PAR Dose Rate Estimate

2/07/2019

Miscellaneous

PI-2018-617

50.54(q) Screening/Evaluation

2/17/2018

PI-2018-633

50.54(q) Screening/Evaluation

01/31/2019

PI-2019-656

50.54(q) Screening/Evaluation

2/22/2019

PI-2019-679

50.54(q) Screening/Evaluation

06/18/2019

71124.01

Corrective Action

Documents

501000020798

Invalid Dose Rate Alarm Received

2/07/2018

501000032736

Potential for Unbriefed Dose Rate Alarm

10/05/2019

501000032786

Radiological Near Miss HRA Posting

10/07/2019

Corrective Action

Documents

Resulting from

Inspection

501000032971

Dose Rates Missing from Routine Survey

10/09/2019

Miscellaneous

Prairie Island Plant Alpha Characterization Study

03/29/2019

National Source Tracking System Annual Reconciliation

01/02/2019

Procedures

RPIP 1118

Conducting Radiological Surveys

RPIP 1120

Posting of Restricted Areas

RPIP 1201

Airborne Radioactive Particulate and Iodine Sampling

Self-Assessments

Inspection Procedure 71124.01 Self-Assessment

10/07/2019

Work Orders

700050449

Radioactive Source Inventory/Leak Test

08/16/2019

71124.02

ALARA Plans

181071

1R31 Steam Generator Primary Work

2040

2R31 Reactor Refueling

2042

2R31 Reactor Dissassebly/Re-assembly

Corrective Action

Documents

AR

501000012071

Work Order Over Dose Estimate

05/16/2018

AR

501000018176

Station Alara Committee Dose Estimate Increased

10/07/2018

AR

501000031456

SP-1544 Over Dose Estimate

09/04/2019

Miscellaneous

1R31 Radiation Protection Post Outage Report

01/08/2019

2R31 Radiation Protection Post Outage Report

11/22/2019

181071

1R31 11 & 12 Steam Generator Primary Side Work Post

2/16/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Job Evaluation

181071

50% Work In Progress Review Steam Generator Primary

Side Work

10/06/2018

181071

80% Work In Progress Review Steam Generator Primary

Side Work

10/08/2018

2040

50% Work In Progress Review 2R31 Refuel Work

10/15/2019

2040

80% Alara Work In Progress Review 2R31 Refuel Work

10/16/2019

2042

50% Alara Work In Progress Review 2R31 Reactor

Disassembly/Re-assembly

10/18/2019

2042

80% Work In Progress Review 2R31 Reactor

Disassembly/Re-assembly

10/19/2019

Procedures

FP-RP-SAC-01

Station Alara Committees

Radiation Work

Permits (RWPs)

181071

1R31 11 & 12 Steam Generator Primary Side Work

2040

2R31 Refuel Work

2042

2R31 Reactor Disassebly/Re-assembly

71124.03

Corrective Action

Documents

Resulting from

Inspection

AR

501000008440

SCBA Inspection Incomplete

2/15/2018

Miscellaneous

Operations RO/SRO Dayshift Crew #1 Respiratory

Protection Records

2/04/2019

Respiratory Protection Checks

07/05/2019

Respiratory Protection Checks

08/21/2019

Respiratory Protection Checks

09/13/2019

Procedures

C40.5

Control Room Breathing Air System

H26

Respiratory Protection Program

RPIP 1215

Respiratory Equipment Control

71152

Calculations

ENG-ME-448

Auxiliary Building Flooding Analysis

Corrective Action

Documents

AR

501000031131

Improvement Opp in CAP Evaluation and Closure

08/23/2019

AR

501000034128

Decline in Licensee ID Finding/Violation

10/30/2019

Procedures

H36

Plant Flooding

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71153

Corrective Action

Documents

AR

501000030520

Potential Diaphragm Degraded: MV-32410

08/07/2019

Procedures

SP 2072.17

Local Leakage Rate Test of Penetration 17 (Hot Leg Loop B

Sample Line)

19