IR 05000263/2014007

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IR 05000263/2014007; on 09/22/2014 - 10/10/2014; Monticello Nuclear Generating Plant; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML14322A309
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 11/18/2014
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Fili K
Northern States Power Co
References
IR 2014007
Download: ML14322A309 (25)


Text

November 18, 2014

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT PROBLEM IDENTIFICATION AND RESOLUTION AND POWER UPRATE INSPECTION REPORT 05000263/2014007

Dear Ms. Fili:

On October 10, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at your Monticello Nuclear Generating Plant.

The enclosed report documents the inspection results, which were discussed on October 10, 2014, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the inspection sample, the inspection team concluded that the implementation of the corrective action program and overall performance related to identifying, evaluating, and resolving problems at Monticello was generally effective. Issues were entered into the corrective action program at a low threshold and were generally prioritized and evaluated commensurate with their safety significance. Corrective actions were generally implemented in a timely manner and addressed the associated causes. Lessons learned from industry operating experience were generally reviewed and applied when appropriate. Audits and self-assessments were generally used to identify problems and appropriate actions.

No violations or findings were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket No. 50-263 License No. DPR-22

Enclosure:

Inspection Report 05000263/2014007 w/Attachment: Supplemental Information

REGION III==

Docket No.

50-263 License No.

DPR-22 Report No:

05000263/2014007 Licensee:

Northern States Power Company, Minnesota Facility:

Monticello Nuclear Generating Station Location:

Monticello, MN Dates:

September 22 through October 10, 2014 Inspectors:

N. Shah, Project Engineer-Team Lead

R. Lerch, Project Engineer

P. Zurawski, Senior Resident Inspector-Monticello

B. Jose, Senior Reactor Engineer

J. Rutkowski, Project Engineer

Approved by:

K. Riemer, Chief Branch 2 Division of Reactor Projects

SUMMARY OF FINDINGS

Inspection Report 05000263/2014007; 09/22/2014-10/10/2014; Monticello Nuclear Generating

Plant; Biennial Baseline Inspection of the Identification and Resolution of Problems.

This team inspection was performed by four regional inspectors and the senior resident inspector. No violations or findings were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process Revision 5, dated February 2014.

Identification and Resolution of Problems Overall, the Corrective Action Program (CAP) was generally effective at identifying, evaluating and correcting problems. A strong safety conscious work environment was evident, based on interviews with workers and a review of CAP issues and the Employee Concerns Program (ECP). Nuclear Oversight (NOS) audits and department self-assessments were generally critical and identified issues that were captured in the CAP. Operating Experience (OE) was appropriately evaluated.

Although recent efforts to hold workers accountable to the process have resulted in some improvement, there continued to be examples where process requirements were not followed.

Some of these issues may have resulted from frequent cross-referencing of CAPs, which increased the susceptibility for issues to be lost in the process. There were also examples where self-imposed limitations or common practice behaviors potentially impacted the efficacy of the CAP, particularly in the review of OE during cause evaluations and processing of escalated NOS findings.

The licensees efforts to address underlying human performance issues which had led to several, past plant events, appeared good, but recent events involving reactivity control raised questions about whether these actions would be effective in the long term.

REPORT DETAILS

OTHER ACTIVITIES

4OA2 Problem Identification and Resolution

The activities documented in Sections

.1 through.4 constituted one biennial sample of

PI&R as defined in Inspection Procedure (IP) 71152.

.1 Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees CAP implementing procedures and attended CAP program meetings to assess the implementation of the CAP by site personnel.

The inspectors reviewed risk and safety significant issues in the licensees CAP since the last NRC PI&R inspection in 2012. The issues selected were appropriately varied across the NRC cornerstones, and were identified through routine daily plant activities, licensee audits and self-assessments, industry operating experience reports, and NRC inspection activities. The inspectors also reviewed a selection of apparent, common and root cause evaluations for more significant CAP items.

The inspectors performed a more extensive review going back 5 years of the licensees efforts to address issues with contractor control and aging management. This review consisted primarily of a 5-year search of related issues identified in the CAP and discussions with appropriate licensee staff to assess the licensees corrective actions.

The inspectors also reviewed the licensees efforts to address the underlying issues for the substantive cross-cutting issues (SCCIs) in H7, Documentation, and H14, Conservative Bias. These issues were identified in the licensees 2014 mid-cycle assessment letter dated September 2, 2014.

During the reviews, the inspectors evaluated whether the licensee staffs actions were in compliance with the facilitys CAP and 10 CFR Part 50, Appendix B requirements.

Specifically, whether licensee personnel were identifying plant issues at the proper threshold, entering the plant issues into the stations CAP in a timely manner, and assigning the appropriate prioritization for resolution of the issues. The inspectors determined whether the licensee staff assigned the appropriate investigation method to ensure the proper determination of root, apparent, and contributing causes. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC findings.

All documents reviewed during this inspection were listed in the Attachment to this report.

Assessment

(1) Effectiveness of Problem Identification The licensees implementation of the CAP was generally good. This was evident by the large number of CAP items generated annually, which were reasonably distributed across the various departments. A shared computerized database was used for creating individual reports and for subsequent management of the processes of issue evaluation and response. Workers were generally familiar with using this database and were encouraged to identify issues. Of note, were that many workers felt that management feedback on these issues had improved since the 2012 NRC PI&R inspection. The inspectors also verified that workers were familiar with the various avenues (CAP, ECP, NRC, etc.) for raising concerns.

Observations The inspectors noted a number of CAP issues documenting apparent trends identified through the binning of issues or via the quarterly department roll-up meeting (DRUM)reports. The inspectors reviewed a selective sample of these trends and concluded that they were generally well handled. However, the inspectors identified a potential adverse trend where several issues were not entered into the CAP in a timely matter. Of note, was that a similar trend had been identified during a recent licensee assessment (CAP 1444328, PI&R Prep CAP Initiation Review, dated 10/1/14). The licensee documented this issue as CAP 1449939.

From February 17-24, 2014, the licensee took several steps to reduce the CAP backlog from about 3000 to 2400 items. The effort consisted of having department CAP liaisons identifying lower level issues that could be closed. These items were then screened by licensee management to validate that there was no significant risk toward closing the actions. The inspectors reviewed a sample of these issues and identified no problems.

b. Findings

No findings were identified.

(1) Effectiveness of Prioritization and Evaluation of Issues Identified problems were generally prioritized and evaluated commensurate with their safety significance, including an appropriate consideration of risk. Most issues were either closed to trend or at a level appropriate for a condition evaluation. Those issues assigned to higher level evaluations, such as root and apparent cause evaluations, were generally technically accurate and of sufficient depth to effectively identify the cause and extent of condition. There were no items in the operations, engineering, or maintenance backlogs that were risk-significant, individually or collectively. The inspectors noted that the licensee generally, adequately evaluated equipment operability and functionality after identifying a degraded or non-conforming condition.

Observations The licensee had implemented several actions since the 2012 NRC PI&R inspection to improve worker adherence to the CAP process. However, the inspectors did identify several examples where process requirements were still not being followed, including:

some examples where CAPs were not timely initiated, the failure to document the basis for CAP downgrades; inappropriate closure of corrective actions; and the failure to properly cross-reference CAPs. Some of these examples resulted, in part, from the licensees frequent practice of cross-referencing CAPs. This often made it difficult to determine whether issues were properly addressed and increased the probability that issues may be lost in the CAP process. Although none of the individual examples were significant, they collectively indicated that additional licensee attention was warranted.

The licensee documented this issue as CAPs 1449939 and 1448223.

Aging Management Programs All engineers had received training on aging management, including refresher training, just after entering the period of extended operation. The training was also given to managers and supervisors. The team did not observe active questioning about possible aging issues during management review of CAPs at the PARB meeting; however, the team observed that this was specifically covered in the pre-screening meetings. The inspectors review of associated procedures and CAP documents did not identify any significant aging management issues.

CAP 1415802, Reactor Building Closed Cooling Water In-Leakage: Historical Review of Event, 1/22/2014 Between August 9, 2013 and January 17, 2014, the licensee was responding to potential reactor coolant system leakage into the reactor building closed cooling water in-leakage (RBCCW) system. This leakage was eventually determined to be reactor pressure boundary leakage, a condition prohibited by Technical Specifications that required a forced shutdown to repair. As documented in Inspection Report 05000263/2014002, the NRC identified several weaknesses with the licensees oversight and technical evaluation/decision-making for this event. Subsequently, the licensee did a root cause evaluation on the issue.

The root cause focused specifically on why plant operators did not initially request a formal operability evaluation. The other aspects of the oversight/decision-making were subsumed in another root cause (which was cross-referenced to the above root cause)looking at common elements related to inadequate oversight/decision-making for the RBCCW and other plant events.

The inspectors identified several concerns with the licensees review of the RBCCW issue:

  • In the root cause for the operability recommendation, the licensee concluded that there was insufficient procedural guidance in Operational Work Instruction 03-02, Safety Related and Fire Protection Related System Operability Determination and Verification. However, the inspectors noted that fleet procedure FP-OP-OL-01, Operability/Functionality Determination, had sufficient guidance to prompt a formal operability recommendation; the root cause did not evaluate why the operators did not follow the fleet procedure.
  • The second root cause looking at the common elements, did not evaluate the specific circumstances of the RBCCW event; therefore, it was uncertain whether there were specific issues associated with that event for which corrective action was not being taken.

The inspectors also considered the licensees handling of the RBCCW issue as another example where cross-referencing may result in issues not being properly addressed.

The licensee documented these concerns as CAP 1450086.

Findings No findings were identified.

(2) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. Those corrective actions addressing selected NRC documented violations were also generally effective and timely. The inspectors review of the contractor control and aging management issues did not identify any negative trend or inability by the licensee to address long term issues.

Observations Potential Adverse Trend Regarding Lack of Integrated Plant Knowledge Between 2013 and 2014, the licensee has had several significant events resulting in potential violations of Technical Specifications, challenges to operability/functionality and a forced shutdown. For each event, the licensee performed an apparent or root cause as appropriate and instituted corrective action. Although the individual evaluations and actions were generally adequate, the inspectors noted an apparent common element regarding a lack of integrated plant knowledge (licensing and plant design basis)among engineers and plant operators. This element was not identified as a potential adverse trend/common issue warranting independent review. It was unclear whether collectively; the individual corrective actions for the specific events would address this common concern. The licensee documented this observation as CAP 1450057.

Licensee Actions to Address Substantive Cross-Cutting Issues Currently, Monticello has two open SCCIs, as assessed through the NRC operating reactor assessment program. Specifically, a substantive cross-cutting theme in Human Performance, Documentation (H.7) was identified during the 2013 End-of-Cycle assessment. A second substantive cross-cutting theme in Human Performance, Conservative Bias (H.14) was identified during the 2014 Mid-Cycle assessment. The licensee completed a root cause analysis for each substantive cross cutting theme in May 2014. Although the inspectors determined that, the corrective actions to mitigate each issue appear adequate, these actions have not yet been proven effective and sustained performance has not been observed Findings No findings were identified.

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors reviewed whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits.

The inspectors reviewed implementing OE program procedures, attended CAP meetings to observe the use of OE information, attended the weekly OE screening meeting, reviewed evaluations of OE issues and events, and reviewed self-assessments of the OE program. The inspectors also assessed if corrective actions, as a result of OE experience, were identified and effectively and timely implemented.

Documents reviewed during this inspection are listed in the Attachment to this report.

Assessment The inspectors determined that overall OE was effectively used at the station. OE was discussed as part of the daily planning meetings, and at operations and maintenance pre-job briefings. Generally, OE was appropriately reviewed during causal evaluations; however, as stated below, the review was limited. During interviews, workers stated that OE was seen as a valuable learning too and that its use was encouraged by management. No issues were identified through the inspectors review of selective OE evaluated by the station over the past 2 years.

Observations While reviewing licensee cause evaluations, the inspectors noted that the procedural threshold for industry OE preventable events was too restrictive, in that only industry events of high significance (such as those documented in NRC Information Notices)involving the same circumstances were considered. This high threshold essentially meant that the failure to use OE would likely never be identified as a potential precursor for events. There were several examples where the licensee had identified lower level industry events, involving similar issues and causes, which were discounted, as they did not meet the procedural threshold. The inspectors also noted that similar observations had been made during prior PI&R inspections in 2010 and 2012. The licensee documented this concern in CAPs 1448087, 1450065 and 1448222.

b. Findings

No findings were identified.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors assessed the licensee staffs ability to identify and enter issues into the CAP program, prioritize and evaluate issues, and implement effective corrective actions, through efforts from departmental assessments and NOS audits.

Documents reviewed during this inspection are listed in the Attachment to this report Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold level. The audits and self-assessments were completed by personnel knowledgeable in the subject area and the NOS audits were thorough and critical. Where changes to the operating experience process were too recent for inspectors to assess, the NOS organization was monitoring the stations performance.

The inspectors observed that CAP items had been initiated for issues identified through the NOS audits and self-assessments. The inspectors reviewed the self-assessment performed on the CAP, found no issues and generally agreed with the overall results and conclusions drawn. The self-assessment of CAP was a very thorough look at the process which concluded that the process was effective.

Observations The inspectors noted some issues with how the licensee handled escalated NOS findings. These findings were issued when NOS had concerns with how the licensee was addressing previously identified NOS issues. They were considered more significant than regular NOS findings (which were handled commensurate with their significance in the CAP), but less significant than adverse findings (which were typically assigned a minimum CAP significance of B and an apparent cause evaluation).

By contrast, escalated findings were assigned a lower CAP significance level (C) and were resolved using an NOS specific process. This separate process did not evaluate why the issue had been escalated, but instead focused on those corrective actions necessary for NOS to close the issue. Once resolved, the associated CAP was closed with a cross-reference to the associated NOS documentation. This practice prevented the licensee from investigating why the CAP process did not adequately address the original NOS concern and potentially diminished the role of NOS as an independent overseer of station performance.

The licensee documented this observation as CAP 1449547.

b. Findings

No findings were identified.

.4 Assessment of Safety-Conscious Work Environment

a. Inspection Scope

The inspectors assessed the licensees safety conscious work environment (SCWE)through the reviews of the facilitys employee concern program implementing procedures, discussions with coordinators of the employee concern program, interviews with personnel from various departments, and reviews of issue reports. The inspectors also reviewed the results from a Safety Culture Survey and partial results of an organization effectiveness survey.

As part of the overall inspection effort, inspectors discussed department and station programs with a variety of people. In addition, the inspectors interviewed approximately 30 individuals from various departments to assess their willingness to raise nuclear safety issues. Other items discussed included:

  • knowledge and understanding of the CAP;
  • effectiveness and efficiency of the CAP;
  • willingness to use the CAP; and
  • knowledge and understanding of the ECP.

Documents reviewed during this inspection are listed in the Attachment to this report.

Assessment The inspectors did not identify any issues of concern regarding the licensees safety conscious work environment. Information obtained during the interviews indicated that an environment was established where licensee personnel felt free to raise nuclear safety issues without fear of retaliation; licensee personnel were aware of and generally familiar with the CAP and other processes, including the ECP and the NRC, through which concerns could be raised, and safety significant issues could be freely communicated to supervision. Documents provided to the inspectors regarding safety culture surveys and monitoring of the safety culture and SCWE generally supported the conclusions from the interviews.

Documents reviewed are listed in the Attachment to this report.

Observations Interviewed personnel generally expressed the view the CAP was serving its intended functions and stated that they were aware of and complied with the expectations to document concerns in the CAP.

The licensee had a Safety Culture Survey completed in August 2013, which concluded that overall the plant had a safety culture that supported the traits of a healthy nuclear safety culture, had a respect for nuclear safety, and assured that nuclear safety was not compromised by production priorities. The survey and the team that conducted the survey identified several positive observations and several weakness observations where action for improvement might be warranted. The weakness observations were associated with a respectful work environment and leadership safety values and actions.

The report documented that some employees believed that the communications from management on changes could be improved and management did not show respect for employees and their opinions. Several workers interviewed by the inspectors stated that following several management changes in 2014 that communication between workers and licensee management had improved since the survey.

The licensee had an organizational effectiveness survey in December 2013 that also looked at various traits associated with an effective safety culture. While generally the results of the survey were positive for the overall station, there were some indications of decline in some departments from 2011, the last previous equivalent survey, to the present survey. When the inspectors questioned personnel for the reasons for the indicated declines and for any follow-up action, the majority of licensee personnel interviewed were not aware of the survey results or of any action, including the generation of CAP inputs that resulted from the survey. During the inspection, the licensee did not provide any documents that indicated that the results from the December 2013 were considered as items that should be addressed.

b. Findings

No findings were identified.

4OA5 Other Activities

.1 Power Uprate Related Inspection Activities

a. Inspection Scope

As part of the biennial PI&R inspection, the inspectors reviewed selected, routine items entered into the licensee CAP concerning the power uprate amendment.

Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings were identified.

4OA6 Management Meeting

.1

Exit Meeting Summary

On October 10, 2014, the inspectors presented the inspection results to Ms. Fili and other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was considered proprietary.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

PLANT PROCEDURES

Number

Description or Title

Date or Revision

FP-OP-COO-15

Conservative Decision Making

FP-STND-NSC-01

Nuclear Safety Culture Monitoring Process

CD 2.1

Nuclear Oversight Corporate Directive

DP-NO-IA

Internal Assessments

DP-NOIA-07

Internal Assessment: Topic Selection, Scheduling,

And Cycle Reporting

FG-PA-CTC-01

CAP Trend Code Manual

FG-PA-EVAL-01

Evaluation Methods

FP-PA-DRUM-01

Department Roll-Up Meeting (DRUM) Manual

FP-PA-ACE-01

Apparent Cause Evaluation Manual

and 2

FP-PA-ARP-01

CAP Action Request Process

35, 37 and 39

FP-PA-SA-01

Focused Self-Assessment Planning, Conduct, and

Reporting

FP-PA-PAR-01

Performance Assessment Review Board and

Performance Assessment Oversight

OWI-03.02

Safety Related and Fire Protection System

Operability Determination and Verification

FP-E-EVL-01

Engineering Evaluations

FP-E-SE-04

Conduct of System Engineering

FP-OP-OL-01

Operability/Functionality Determination

QF0398

Security Change/Activity Screening and Evaluation 5

FG-PA-KPI-01

Performance Assessment Data Reporting

CP 0021

Employee Concerns Program

FP-EC-ECP-01

Employee Concerns Program

FP-PA-ECE-01

Equipment Cause Evaluation Manual

FP-PA-EFR-01

Effectiveness Review Manual

FP-PA-OE-01

Operating Experience Program

FP-PA-RCE-01

Root Cause Evaluation Manual

FP-PA-SOER-01

Significant Operating Experience Report (SOER)

Processing

NSPM-1

Quality Assurance Topical Report

FP-NO-IA-12

Nuclear Oversight Finding Development, Issuance

Tracking, and Issue Escalation

271

Memo Distribution, PCR 01313901

07/23/13

3802

Visual Inspection of Heat Exchanger Condition

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

Number

Description or Title

28268

Age Degradation Evaluation for Bolting Integrity Program

26605

GE Part 21 Notice (SC05-03) - Potential to Exceed Low Pressure

Safety Limit

951636

Administrative Controls Documents Will be Revised

1008261

Change Commitment Cross-Reference Location for M87005A

1131704

Breaker Racking or Alignment Issues

1176715

  1. 17 Battery's Capacity Calculation Contains Wrong Assumptions

1181868

Leaking Manifold Valve for DPIS-2-117A B Steam Line Flow

1185959

RCIC HELB at MO-2078 and Its Affect On MOC-311

1197202

CDBI-Calculation Quality Adverse Trend

205719

APM S&C Refurbishment Not Performed In Accordance With Tech

Manual

210803

Appropriate License Renewal Frequency Not Established

217223

Gap to Excellence in License Renewal System Walkdowns

21315

RBCCW Piping Thickness Below Expected Value

21333

MO-2009 Failed To Properly Operate During Procedure 1381

23696

Leak Discovered on SBLC Tank

27961

  1. 11 Offgas Compressor Flex Conduit Brocken

28061

Reactor Feed Pump Control Cable Exposed to Elevated

Temperatures

28167

Cable Tray in Turbine Building Has Corrosion Deposit

28174

FP-13 Has Evidence of Selective Leaching

265183

Ready To Install Task Caviats Could Cause Issues as Written

266454

Recovery Plan for HELB Improvement Potentially Off Track

268207

New LS-7211 EDG Level Switch Did Not Function as Expected

274758

Potential HU Error Trap In Electrical Modification WOs

280199

AR 1279926 Inappropriately Closed With No Actions

280599

Insulation Nick In MCC-141 Refeed Connector

298620

MO-2-53A/B Low Capability Margin for NSR Scenario

1300308

Main Access SCT Airlock EFR Acceptance Criteria Not Met

1307848

Class 1E Agastat Relay Replacement PM should be 10 Years

1309439

Core Spray Testable Check Valve Shows Dual Position

1314222

Potential Adverse Trend in Raw Water Pump Performance

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

Number

Description or Title

1316022

CV-1378 Cannot Control Pressure With Current Configuration

22841

Safety Related Equipment Impacted by Tech Spec Allowed Frequency

23839

MO-2021 Found With Dual Indication

28206

Actions from ACE 01266100 Found Not Effective

1330947

Questions About Equipment Safety Classification In Passport

1331618

NRC 2012 CDBI-Harmonics Issue with Degraded Voltage Relays

1332185

FME Found In New 13.8kv Switchgear

1334789

NRC Cross-Cutting Issue Potential In Human Performance

1337178

CRD HCU Piston Accumulators Do Not Meet HELB Environment

1337186

License Renewal PN Changes Not In Accordance With AWI

1342363

ODMI for Cable A602-G40/2 per Cable Program EWI-08.19.01

1343416

Adverse Trend In Equipment Re-Greasing Practices

1350445

MO-2010, Exceeded Maximum Closing Thrust

1351259

Discrepancy Between Fleet Process and Tec Spec

1353905

Adverse TrendBechtel Work Package Quality

1354966

MRule Unplanned SCRAMs Has Exceeded Criteria

1362098

Foreign Material Identified in 11 RHRSW Upper Reservoir

1368457

Rust Discovered in Feed Water Heater Nozzles

1373085

Leaks Identified on RHR-25-2 During DW Walkdown

1375410

Crack found in the P-1A, CD Pump Can / Suction Nozzle Weld

1376596

Support FW-17 Rigid Strut Recieved Not Correct Length

1378391

Inferior Bolts Found On New Valve - MS-116

1378744

E SRV Low-Low Set Tailpipe dP Root Valve Found Closed

1383340

EPU - Unacceptable Radiography (RT) Result On Piping Welds

1385118

Manufacturer Label Confusing To Personnel

1385313

Evaluate Shelf Life Guidance for Oil/Grease

1389519

IST Cold Shutdown Tests Not Scheduled Properly

1389604

NRC Question Regarding SR 3.0.2 and 3.0.3 Applicability

1390285

RF026 Was Planned 87 Days; Actual Will Be About 139 Days

1395575

NRC Questioning Results in Submitting 50.72 Unanalyzed Condition

1398625

NOS EscalationLevel 1 Performance Assessment

1402240

AO-13-22 Furmanite Injection Process Question

1402246

NRC Question on DSC PT Examination Times

1405367

NRC: Issues with Calculation 10-219

1405518

What Superseded Calc.00-082

1406284

NRC Inspection: Information Provided is Incorrect

1407041

HPCI Flow Time Delay Calculation Does Not Support HELB

1407385

NRC Inspection: Requirements for Soldering Electrical Connections

Not Met

1410620

Floating FME Found in Cell #7 On #17 Battery

1412267

OE: NRC Pt 21 Event No. 49667 Cracking in KCR-13 Standby

1419279

PT Exam on DSC-16 - Linear Indication Found on Re-Exam

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

Number

Description or Title

24048

Potential Adverse Trend on Accuracy of NRC Submittals

25172

Strain Gauge Location Configuration Question on C MSL

1430435

Inaccurate Info Transmitted to NRC for EPU

1432184

Review Adequacy of EOC for Inaccurate Info in EPU Submittals

1440002

ARP-01 CAQ Definition More Restrictive than QATR

1442205

No Follow-Up Actions Taken For Increase in Sum Of Six Result

OPERATING EXPERIENCE

Number

Description or Title

1446300

LPCI During RHR Torus Cooling

QF0463

NSPM OE Screen Team Meeting Template, Incoming Operating

Experience Package 09/15/2014

QF0463

NSPM OE Screen Team Meeting Template, incoming Operating

Experience Package 09/22/2014

SE-0401

List of Open Operating Experience CAPs as of 9/25/2014

24761

OE Evaluation of SOER 10-01

297249

OE-IERL2-11-2, 2009-2010 Scram Analysis

1308589

Issue at PI May Impact Monticello Maintenance Instructions

1312510

OE IERL2-11-46, Extended Emergency Power Operations

1313396

OE: NRC Green Violation-Failure to Establish Inspection Procedures

1314536

OE: NRC IN 2011-20 Concrete Degradation

25353

OE: IERL2-12-14 Automatic Reactor Scram Resulting from a Design

Vulnerability in the 4.16-kV Bus Undervoltage Protection Scheme

1335244

OE IERL2-12-38 Reactor Trip and Generator Lockout

1357468

Prairie Island AR-During Round, Outplant Operator Discovered 121

Safeguards Traveling Screen Differential Pressure Switch Pegged

Low

1357487

GE SIL 433 Sup. 2 Shroud Head Bolt Inspection Recommendations

1359840

Prairie Island AR-Update of CAP 1354059 That Event Was

Considered A Minor NRC Violation

1382652

GE SIL 438 R2 Main Steam Line High Flow Trip Setting

1391239

GEH SIL 409 Rev3 Incore Dry Tube Cracks

1402093

Prairie Island AR-No Combustible Permits for Lead Shielding

1407735

OE: IERL2-13-53 Loss of Off-Site Power (LOOP) Analysis

1416736

ICES 19861 Reactor Feed Pump High Vibration

1431296

OE-IERL2-14-25 Heavy Snow and a Design Flaw Result in a Dual

Unit Scram

ROOT CAUSE and APPARENT CAUSES

Number

Description or Title

141582

RBCCW In-Leakage Historical Review of Event

276006

Near Miss MSIV Bleeds Closed In Unplanned Fashion

1309399

Bus Failed to Re-energize

ROOT CAUSE and APPARENT CAUSES

Number

Description or Title

1334146

CDBI: Technical Specification Degraded Voltage Time Value

1334571

CDBI: Instrument Panel Y20 Voltage Nonconformance with USAR

1337244

RSW Pump Performance Trends Not Predictable

1343360

Adverse Trend Door #45 AEP Board Failures

1345334

Snubber Examinations Not Performed Per Code Requirements

1348567

CRD 18-07 Exceeds Friction Limit

1348931

Welder Qualification on Supports for 4kV HELB Barrier

1351292

V-FE-11: Negative DP During 0472-01 Testing

1351317

2-202 Initially Failed to Close During Planned Transfer

1351664

RMCS Failure During CRD Exercise Test 0074

1352773

Reactor Scram 130

1352778

Lockout of 4 kV Bus 12 During WO:446500-01

1353605

HPCI Concern With Y81 Inverter Out of Service

1353869

Danger Tagged Lifted Lead was Landed for P-903A Motor

1354309

HELB Barrier Bolts Found Loosened for Lower 4kV

1356091

Operability Concerns for Safety Related Inverter Supplied Loads

1356474

Potential Adverse Trend for Plant Configuration Control During Mods

1356625

Monticello HU Events

1357606

Four Findings in P.1© Cross-Cutting Aspect

1358371

Relay 10A-K35 for LPCI Loop Select Did Not Drop Out

1358924

RCIC System Found Inoperable and Unavailable

1367175

P-25B, #12 Reactor Building Floor Drain Pump Found Tripped

1367915

4-C-23 Recirc Pump Motor B Low Oil Level Alarm Received

1374981

Incorrect Cable Cut During Demolition

1378051

TI 2515 187, Inadequate Flooding Walkdowns

1378713

Work Hours Not Updated in WHM Tool IAW Procedure

1379117

NOS Finding: Adverse Trend With Common Cause Identified

1379814

Loss of Instrument Air Caused by PS-1469 Being Isolated

1381637

EDG Air Inlet Abstructed by Herculite

1383202

Agastat Relays Discovered Beyond Vendor Recommended

Qualification Life

1384157

Essential Bus Transfer Occurred While Performing 2R Testing

1384157

Essential Bus Transfer Occurred while Performing 2R Testing

1385754

Reactor Water Level Controlled With an Inaccurate Instrument

1385754

Temporary Vessel Level Instrumentation Rise

1386518

Breaker 152-101 Fault Resulting in Loss of Offsite Power

1386536

Shutdown of 11 & 12 EDGs after LONOP

1388760

NOS: AAF: MNGP Leadership Nuclear Safety Concerns

1389520

NRC Findings In H.2.C Cross-Cutting Aspect

1390092

Diesel Oil Service Pump P-77 Low Flow T-45B

1390785

Loose Circuit Card for Alarm C-04-A-11

1391665

Security 1 Hour Report Under 10 CFR 73.71

ROOT CAUSE and APPARENT CAUSES

Number

Description or Title

1392528

Multiple EPU Design Issues Discovered During Plant Startup

1394150

TIA 2012-03 Final Response EDG Fuel Oil Supply NCV 2013007-04

1394150

NRC TIA 2012-03 Final Response EDG Fuel Oil Supply

1394412

Area Radiation Monitor UP-and DOWNSCALE Trips Out of Spec.

1394877

Recirc Pump Runback, Investigate Circuitry

1394877

Recirc Pump Runback, Investigate Circuitry

1395575

NRC Questioning Results In Submitting 50.72 Unanalyzed Condition

1395722

NOS Escalation Level 1Power Uprate Readiness

1397406

Door 85/86 Plenum Room Airlock Failed Interlock Testing

1398300

2013 INPO Mid-Cycle FSA: AFI MA-2-25

1402240

AO-13-22 Furmanite Injection Process Question

1405035

Potential Adverse Trend in Ineffective CAPR EFRs

1405518

NRC Question: What Superseded Calc 00-082 HPCI Trip?

1406283

Improperly Identified Inputs Impact HRLB Calcs

1406283

Improperly Identified Inputs Impact HELB Calculation

1409551

NRC INSP: Failure to Maintain IEEE Qualifications of Relay

1411443

CV-1728 Went Closed When Only 13 RHRSW Pump Running

1418321

SR 3.8.1.12 Was Not Met By TS LOP Instrument Alone

1418669

Diesel Generator Output Breaker Failed to Close

23979

Inaccurate Scaling Used on EPU Testing on DAS for Steam Dryer

24346

LCB-083 Trip Interlock Bent Causing Unexpected Lockout/Alarm

25443

Six NRC Findings in H.14 Cross-Cutting Aspect

26098

Findings in Work Management H.5 Cross-Cutting Aspect

29810

Preconditioning Evaluation Was Not Documented

1430165

C4.2-1 Auxiliary System Chemistry Parameters

1430930

Opening Identified in Fire Barrier Separating Both Divisions

1432015

E CS&RHR Area ARM Out of As Found Criteria During 1024

1433756

Diesel Oil Pump (P-77) Lost Flow, Pressure

AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS

Number

Description or Title

Revision

USA Nuclear Safety Culture Assessment

09/17/2013

SAR 01436575

NEI 09-07 Nuclear Safety Culture 1st Quarter

2014

05/30/2014

Organizational Effectiveness Survey - Partial

Results

01/2014

01437361

Principles for Maintaining an Effective Technical

Conscience

07/28/2014

Nuclear Oversight 1st Trimester 2014 Executive

Summary

06/09/2014

SAR 01405321

Operations DRUM Report - 3rd Quarter 2013

11/16/2013

AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS

Number

Description or Title

Revision

SAR 01440695

Operations DRUM Report - 2nd Quarter 2014

07/31/2014

01437361

Principles for Maintaining an Effective Technical

Conscience

07/11/2014

2014-02-011

NOS Assessment of Corrective Action Program

07/21/2014

CAP 01290035

ECP Snapshot Self-Assessment

06/09/2011

SAR 01290035

ECP Snapshot Self-Assessment

08/12/2013

SAR 01404684

Pre-Problem Identification and Resolution

Inspection Assessment

03/10/2014

CAP 01447174

PI&R NRC Inspection Readiness Snapshot

Evaluation

07/28/2014

SAR 1356920

Site DRUM Report3rd Quarter 2012

SAR 01390911

Site DRUM Report4th Quarter 2013

2013-01-001

NOS Observation Report - Performance

Assessment/Corrective Action Program

2013-02-005

NOS Observation Report - Performance

Assessment/Corrective Action Program

2013-03-003

NOS Observation Report - Monticello/Corrective

Action Program

2013-04-006

NOS Observation Report - Performance

Assessment/Corrective Action Program

CY2014

Nuclear Oversight NOS Assessment Cycle

Schedule

2014-02-031

NOS Observation Report - MT/Production

Planning

2014-02-043

NOS Observation Report - MT/Maintenance

QF0434

Maintenance Department DRUM Report, 4th QTR

2013

SAR 01365272

Maintenance Department DRUM Report, 4th QTR

2012

QF0434

Maintenance Department DRUM Report, 3rd QTR

2012

SAR 01437435

Maintenance Department DRUM Report, 2nd QTR

2014

SAR 01429022

Maintenance Department DRUM Report, 1st QTR

2014

SAR 01407517

Maintenance Department DRUM Report, 3rd QTR

2013

QF0434

Maintenance Department DRUM Report, 1st & 2nd

QTR 2013

NOS Trimester Report

1C14

Nuclear Oversight 1st Trimester 2014 (January -

April) Executive Summary

NOS 4Q2013 Report

Nuclear Oversight 4th Quarter 2013 Executive

Summary

NOS 3Q2013 Report

Nuclear Oversight 3rd Quarter 2013 Executive

AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS

Number

Description or Title

Revision

Summary

NOS 2Q2013 Report

Nuclear Oversight 2nd Quarter 2013 Executive

Summary

NOS 1Q2013 Report

Nuclear Oversight 1st Quarter 2013 Executive

Summary

NOS 4Q2012 Report

Nuclear Oversight 4th Quarter 2012 Executive

Summary

NOS 3Q2012 Report

Nuclear Oversight 3rd Quarter of 2012 for

Monticello

23944

Snapshot Assessment of Operating Experience

Evaluation for Significant Regulatory Events

List of Assessments, Benchmarking And

Self-Assessments For 2014 And 2015

1388760

NOS Adverse Assessment Finding on Leadership

Nuclear Safety Culture Concerns

2013-04-021

NOS Observation Report-Monticello Surveillance

2014-02-021

NOS Observation Report-Special Process

Control

2014-02-008

NOS Observation Report-Spent Fuel; Pool Level

Instrumentation Project

WORK ORDERS AND DRAWINGS

Number

Description or Title

Revision

486966

Inject Sealant Into AO-13-22 Packing

2/14/14

487258

V-EF-26 Low Flow Light Lit

09/10/14

489570

P-39 Pump Seal Failure

10/08/14

493201

POI-2942 Not Indicating Position of CV-2942

2/18/14

496046

Operate 12 Reactor Recirc Pump with One Seal

Water HX

2/04/14

497230

AO-2382A Dual Indication When Stroking

09/16/14

498423

V-AC-12A Replace Circuit 1 Compressor

04/25/14

2913

Sudden Pressure Alarms on Main Transformer

09/29/14

504480

FP-37 Inability To Close For Isolation

09/10/14

CONDITION REPORTS GENERATED DURING INSPECTION

Number

Description or Title

28206

Actions for ACE 01266100 Found Not Effective

1447666

PI&R: CAP Screening Missed Assignment of Some Evaluations

1447689

PI&R: Individual in Protected Area Without TLD

1447715

PI&R Question Response Was Not Complete Within 24 Hours

1447778

PI&R: ACE Grading Comments Not Incorporated in ACE 01276006-

CONDITION REPORTS GENERATED DURING INSPECTION

Number

Description or Title

1447784

PI&R: NRC Inspector Access to OCA Denied

1447847

PI&R: PCR01410247 Progression is Not Timely

1447870

PI&R: Interview Delayed Due to Miscommunication

1447927

PI&R: Question on Performing 3-2-1 Results Assessment

1447970

PI&R: Question on the Use of CAPR Designation for Sustainability

1448036

PI&R: Level A CAP Action Inappropriately Closed

1448056

PI&R: Parent OE CAPs Not Assigned Keywords

1448087

PI&R: OE Preventable Event May Be Too Narrowly Defined

1448102

PI&R: RCE1391665 Missing Tracking Action for PCR01348402

1448106

PI&R: NRC Inspector Shown Unqualified When Logging Into RCA

1448117

PI&R: Potential IA by PI Planning Identified in B level CAP

1448123

PI&R: Some Station Personnel Not Proficient In Passport

1448129

PI&R: RCE and ACE Procedures Inconsistent Around OE

Requirements

1448161

PI&R: Question Not Responded to Within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

1448222

PI&R: ACE01402240 Lacked Industry OE

1448223

PI&R: Actions Not Properly Cross-Referenced

1448228

PI&R: CA Inappropriately Closed to Another Action

1448901

PI&R: FP-E-RTC-01 Equipment Classification

1449520

PI&R: Question Not Responded to Within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

1449547

PI&R: Question on NOS Escalation Process

1449629

PI&R: CAP Assignment was Incorrectly Labeled EFR

1449678

New Interim EFR Not Created After Original EFR Failed

1449742

PI&R: Difficult to Follow CAP Issues Through Multiple

Cross-Referencing

1449785

PI&R: Action Closed Contrary to Statement in CA 1354309-08

1449863

PI&R 2014: Severity Classification Question for HU Events

1449939

PI&R Adverse Trend: CAP ARs Were Not Initiated Promptly

1449944

PI&R: Reactivity Control Formality

1450057

PI&R: Potential Common Cause With Integrated Plant Knowledge

1450065

PI&R: Observation on OE Preventable

1450086

PI&R: Observation on the RBCCW RCE

OTHER

Number

Description or Title

Licensees We Get It

Licensees 95002 and Safety Culture

Licensees 95002 Inspection

SAR 01405363

Monticello Operations Department Excellence Plan, Rev 5

Dashway Report Book (Performance Indicators) January to July 2014

TIA 2012-03

Design And Licensing Basis On Diesel Fuel Oil Supply Of The

OTHER

Number

Description or Title

Emergency Diesel Generators At Monticello Nuclear Generating Plant

NOS 2013-04-016

Engineering/Operations Interface 11/04 to 11/08/2013

1/22/2014

Performance Assessment Functional Area MRM

8/25/2014

DashWay Report Book

QF0145

Nuclear Oversight Escalation Letter, Rev. 1

RFI 13-A-002

Concern with AMES valve work

RFI 13-A-018

Concern with HPCI and RCIC alignment work and grease used in

couplings

2011-A-0028

Concern with work done by DZ

WPC 11-26

Contractor concerned that cable was nicked during installation and not

repaired/replaced

AT-0075

CAP Prescreening Report, 09/23/2014

AT-0075 / QF0429

NSPM CAP Screen Team Meeting Template / CAP Screening Report,

09/23/2014

AT-0075 / QF0429

NSPM CAP Screen Team Meeting Template / CAP Screening Report,

09/24/2014

Plant Managers weekly communications package from 10/05/14

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

P. Albares, Operations Manager
D. Bosnic, Director, Business Support
H. Butterworth, Manager, Nuclear Oversight (Prairie Island)
D. Collins, Interim Manager, Regulatory Affairs
C. England, Manager, Radiation Protection
K. Fili, Site Vice-President
P. Gardner, Director, Site Operations
H. Hanson, Plant Manager
M. Kelly, Manager, Performance Assessment
M. Lingenfeter, Director, Site Engineering
M. Murphy, Director, Regulatory Affairs (Xcel Corporate)
K. Nyberg, Manager, Site Security

Nuclear Regulatory Commission

K. Riemer, Chief, Branch 2, Division of Reactor Projects
P. Voss, Resident Inspector (Monticello)

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

None.

LIST OF ACRONYMS USED

ADAMS

Agency wide Document Access Management System

CAP

Corrective Action Program

CFR

Code of Federal Regulations

DRUM

Department roll-up meeting

ECP

Employee Concerns Program

IP

Inspection Procedure

NOS

Nuclear Oversight

NRC

U.S. Nuclear Regulatory Commission

OE

Operating Experience

PARS

Publicly Available Records System

PI&R

Problem Identification & Resolution

RBCCW

Reactor Building Closed Cooling Water In-Leakage

SSCIs

Substantive Cross-Cutting Issues

SCWE

Safety-Conscious Work Environment

K. Fili

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket No. 50-263

License No. DPR-22

Enclosure:

Inspection Report 05000263/2014007

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

DISTRIBUTION w/encl:

John Jandovitz

RidsNrrDorlLpl3-1 Resource

RidsNrrPMMonticello

RidsNrrDirsIrib Resource

Cynthia Pederson

Darrell Roberts

Steven Orth

Allan Barker

Carole Ariano

Linda Linn

DRPIII

DRSIII

Carmen Olteanu

ROPassessment.Resource@nrc.gov

DOCUMENT NAME: Monticello 2014 007

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with

attach/encl "N" = No copy

OFFICE

RIII

NAME

NShah:mt

KRiemer

DATE

11/18/14

11/18/14

OFFICIAL RECORD COPY