IR 05000263/2014007
| ML14322A309 | |
| Person / Time | |
|---|---|
| Site: | Monticello |
| Issue date: | 11/18/2014 |
| From: | Kenneth Riemer NRC/RGN-III/DRP/B2 |
| To: | Fili K Northern States Power Co |
| References | |
| IR 2014007 | |
| Download: ML14322A309 (25) | |
Text
November 18, 2014
SUBJECT:
MONTICELLO NUCLEAR GENERATING PLANT PROBLEM IDENTIFICATION AND RESOLUTION AND POWER UPRATE INSPECTION REPORT 05000263/2014007
Dear Ms. Fili:
On October 10, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at your Monticello Nuclear Generating Plant.
The enclosed report documents the inspection results, which were discussed on October 10, 2014, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the inspection sample, the inspection team concluded that the implementation of the corrective action program and overall performance related to identifying, evaluating, and resolving problems at Monticello was generally effective. Issues were entered into the corrective action program at a low threshold and were generally prioritized and evaluated commensurate with their safety significance. Corrective actions were generally implemented in a timely manner and addressed the associated causes. Lessons learned from industry operating experience were generally reviewed and applied when appropriate. Audits and self-assessments were generally used to identify problems and appropriate actions.
No violations or findings were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's Agencywide Documents Access and Management System (ADAMS),
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Kenneth Riemer, Chief
Branch 2
Division of Reactor Projects
Docket No. 50-263 License No. DPR-22
Enclosure:
Inspection Report 05000263/2014007 w/Attachment: Supplemental Information
REGION III==
Docket No.
50-263 License No.
DPR-22 Report No:
05000263/2014007 Licensee:
Northern States Power Company, Minnesota Facility:
Monticello Nuclear Generating Station Location:
Monticello, MN Dates:
September 22 through October 10, 2014 Inspectors:
N. Shah, Project Engineer-Team Lead
R. Lerch, Project Engineer
P. Zurawski, Senior Resident Inspector-Monticello
B. Jose, Senior Reactor Engineer
J. Rutkowski, Project Engineer
Approved by:
K. Riemer, Chief Branch 2 Division of Reactor Projects
SUMMARY OF FINDINGS
Inspection Report 05000263/2014007; 09/22/2014-10/10/2014; Monticello Nuclear Generating
Plant; Biennial Baseline Inspection of the Identification and Resolution of Problems.
This team inspection was performed by four regional inspectors and the senior resident inspector. No violations or findings were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process Revision 5, dated February 2014.
Identification and Resolution of Problems Overall, the Corrective Action Program (CAP) was generally effective at identifying, evaluating and correcting problems. A strong safety conscious work environment was evident, based on interviews with workers and a review of CAP issues and the Employee Concerns Program (ECP). Nuclear Oversight (NOS) audits and department self-assessments were generally critical and identified issues that were captured in the CAP. Operating Experience (OE) was appropriately evaluated.
Although recent efforts to hold workers accountable to the process have resulted in some improvement, there continued to be examples where process requirements were not followed.
Some of these issues may have resulted from frequent cross-referencing of CAPs, which increased the susceptibility for issues to be lost in the process. There were also examples where self-imposed limitations or common practice behaviors potentially impacted the efficacy of the CAP, particularly in the review of OE during cause evaluations and processing of escalated NOS findings.
The licensees efforts to address underlying human performance issues which had led to several, past plant events, appeared good, but recent events involving reactivity control raised questions about whether these actions would be effective in the long term.
REPORT DETAILS
OTHER ACTIVITIES
4OA2 Problem Identification and Resolution
The activities documented in Sections
.1 through.4 constituted one biennial sample of
PI&R as defined in Inspection Procedure (IP) 71152.
.1 Corrective Action Program Effectiveness
a. Inspection Scope
The inspectors reviewed the licensees CAP implementing procedures and attended CAP program meetings to assess the implementation of the CAP by site personnel.
The inspectors reviewed risk and safety significant issues in the licensees CAP since the last NRC PI&R inspection in 2012. The issues selected were appropriately varied across the NRC cornerstones, and were identified through routine daily plant activities, licensee audits and self-assessments, industry operating experience reports, and NRC inspection activities. The inspectors also reviewed a selection of apparent, common and root cause evaluations for more significant CAP items.
The inspectors performed a more extensive review going back 5 years of the licensees efforts to address issues with contractor control and aging management. This review consisted primarily of a 5-year search of related issues identified in the CAP and discussions with appropriate licensee staff to assess the licensees corrective actions.
The inspectors also reviewed the licensees efforts to address the underlying issues for the substantive cross-cutting issues (SCCIs) in H7, Documentation, and H14, Conservative Bias. These issues were identified in the licensees 2014 mid-cycle assessment letter dated September 2, 2014.
During the reviews, the inspectors evaluated whether the licensee staffs actions were in compliance with the facilitys CAP and 10 CFR Part 50, Appendix B requirements.
Specifically, whether licensee personnel were identifying plant issues at the proper threshold, entering the plant issues into the stations CAP in a timely manner, and assigning the appropriate prioritization for resolution of the issues. The inspectors determined whether the licensee staff assigned the appropriate investigation method to ensure the proper determination of root, apparent, and contributing causes. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC findings.
All documents reviewed during this inspection were listed in the Attachment to this report.
Assessment
- (1) Effectiveness of Problem Identification The licensees implementation of the CAP was generally good. This was evident by the large number of CAP items generated annually, which were reasonably distributed across the various departments. A shared computerized database was used for creating individual reports and for subsequent management of the processes of issue evaluation and response. Workers were generally familiar with using this database and were encouraged to identify issues. Of note, were that many workers felt that management feedback on these issues had improved since the 2012 NRC PI&R inspection. The inspectors also verified that workers were familiar with the various avenues (CAP, ECP, NRC, etc.) for raising concerns.
Observations The inspectors noted a number of CAP issues documenting apparent trends identified through the binning of issues or via the quarterly department roll-up meeting (DRUM)reports. The inspectors reviewed a selective sample of these trends and concluded that they were generally well handled. However, the inspectors identified a potential adverse trend where several issues were not entered into the CAP in a timely matter. Of note, was that a similar trend had been identified during a recent licensee assessment (CAP 1444328, PI&R Prep CAP Initiation Review, dated 10/1/14). The licensee documented this issue as CAP 1449939.
From February 17-24, 2014, the licensee took several steps to reduce the CAP backlog from about 3000 to 2400 items. The effort consisted of having department CAP liaisons identifying lower level issues that could be closed. These items were then screened by licensee management to validate that there was no significant risk toward closing the actions. The inspectors reviewed a sample of these issues and identified no problems.
b. Findings
No findings were identified.
- (1) Effectiveness of Prioritization and Evaluation of Issues Identified problems were generally prioritized and evaluated commensurate with their safety significance, including an appropriate consideration of risk. Most issues were either closed to trend or at a level appropriate for a condition evaluation. Those issues assigned to higher level evaluations, such as root and apparent cause evaluations, were generally technically accurate and of sufficient depth to effectively identify the cause and extent of condition. There were no items in the operations, engineering, or maintenance backlogs that were risk-significant, individually or collectively. The inspectors noted that the licensee generally, adequately evaluated equipment operability and functionality after identifying a degraded or non-conforming condition.
Observations The licensee had implemented several actions since the 2012 NRC PI&R inspection to improve worker adherence to the CAP process. However, the inspectors did identify several examples where process requirements were still not being followed, including:
some examples where CAPs were not timely initiated, the failure to document the basis for CAP downgrades; inappropriate closure of corrective actions; and the failure to properly cross-reference CAPs. Some of these examples resulted, in part, from the licensees frequent practice of cross-referencing CAPs. This often made it difficult to determine whether issues were properly addressed and increased the probability that issues may be lost in the CAP process. Although none of the individual examples were significant, they collectively indicated that additional licensee attention was warranted.
The licensee documented this issue as CAPs 1449939 and 1448223.
Aging Management Programs All engineers had received training on aging management, including refresher training, just after entering the period of extended operation. The training was also given to managers and supervisors. The team did not observe active questioning about possible aging issues during management review of CAPs at the PARB meeting; however, the team observed that this was specifically covered in the pre-screening meetings. The inspectors review of associated procedures and CAP documents did not identify any significant aging management issues.
CAP 1415802, Reactor Building Closed Cooling Water In-Leakage: Historical Review of Event, 1/22/2014 Between August 9, 2013 and January 17, 2014, the licensee was responding to potential reactor coolant system leakage into the reactor building closed cooling water in-leakage (RBCCW) system. This leakage was eventually determined to be reactor pressure boundary leakage, a condition prohibited by Technical Specifications that required a forced shutdown to repair. As documented in Inspection Report 05000263/2014002, the NRC identified several weaknesses with the licensees oversight and technical evaluation/decision-making for this event. Subsequently, the licensee did a root cause evaluation on the issue.
The root cause focused specifically on why plant operators did not initially request a formal operability evaluation. The other aspects of the oversight/decision-making were subsumed in another root cause (which was cross-referenced to the above root cause)looking at common elements related to inadequate oversight/decision-making for the RBCCW and other plant events.
The inspectors identified several concerns with the licensees review of the RBCCW issue:
- In the root cause for the operability recommendation, the licensee concluded that there was insufficient procedural guidance in Operational Work Instruction 03-02, Safety Related and Fire Protection Related System Operability Determination and Verification. However, the inspectors noted that fleet procedure FP-OP-OL-01, Operability/Functionality Determination, had sufficient guidance to prompt a formal operability recommendation; the root cause did not evaluate why the operators did not follow the fleet procedure.
- The second root cause looking at the common elements, did not evaluate the specific circumstances of the RBCCW event; therefore, it was uncertain whether there were specific issues associated with that event for which corrective action was not being taken.
The inspectors also considered the licensees handling of the RBCCW issue as another example where cross-referencing may result in issues not being properly addressed.
The licensee documented these concerns as CAP 1450086.
Findings No findings were identified.
- (2) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. Those corrective actions addressing selected NRC documented violations were also generally effective and timely. The inspectors review of the contractor control and aging management issues did not identify any negative trend or inability by the licensee to address long term issues.
Observations Potential Adverse Trend Regarding Lack of Integrated Plant Knowledge Between 2013 and 2014, the licensee has had several significant events resulting in potential violations of Technical Specifications, challenges to operability/functionality and a forced shutdown. For each event, the licensee performed an apparent or root cause as appropriate and instituted corrective action. Although the individual evaluations and actions were generally adequate, the inspectors noted an apparent common element regarding a lack of integrated plant knowledge (licensing and plant design basis)among engineers and plant operators. This element was not identified as a potential adverse trend/common issue warranting independent review. It was unclear whether collectively; the individual corrective actions for the specific events would address this common concern. The licensee documented this observation as CAP 1450057.
Licensee Actions to Address Substantive Cross-Cutting Issues Currently, Monticello has two open SCCIs, as assessed through the NRC operating reactor assessment program. Specifically, a substantive cross-cutting theme in Human Performance, Documentation (H.7) was identified during the 2013 End-of-Cycle assessment. A second substantive cross-cutting theme in Human Performance, Conservative Bias (H.14) was identified during the 2014 Mid-Cycle assessment. The licensee completed a root cause analysis for each substantive cross cutting theme in May 2014. Although the inspectors determined that, the corrective actions to mitigate each issue appear adequate, these actions have not yet been proven effective and sustained performance has not been observed Findings No findings were identified.
.2 Assessment of the Use of Operating Experience
a. Inspection Scope
The inspectors reviewed whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits.
The inspectors reviewed implementing OE program procedures, attended CAP meetings to observe the use of OE information, attended the weekly OE screening meeting, reviewed evaluations of OE issues and events, and reviewed self-assessments of the OE program. The inspectors also assessed if corrective actions, as a result of OE experience, were identified and effectively and timely implemented.
Documents reviewed during this inspection are listed in the Attachment to this report.
Assessment The inspectors determined that overall OE was effectively used at the station. OE was discussed as part of the daily planning meetings, and at operations and maintenance pre-job briefings. Generally, OE was appropriately reviewed during causal evaluations; however, as stated below, the review was limited. During interviews, workers stated that OE was seen as a valuable learning too and that its use was encouraged by management. No issues were identified through the inspectors review of selective OE evaluated by the station over the past 2 years.
Observations While reviewing licensee cause evaluations, the inspectors noted that the procedural threshold for industry OE preventable events was too restrictive, in that only industry events of high significance (such as those documented in NRC Information Notices)involving the same circumstances were considered. This high threshold essentially meant that the failure to use OE would likely never be identified as a potential precursor for events. There were several examples where the licensee had identified lower level industry events, involving similar issues and causes, which were discounted, as they did not meet the procedural threshold. The inspectors also noted that similar observations had been made during prior PI&R inspections in 2010 and 2012. The licensee documented this concern in CAPs 1448087, 1450065 and 1448222.
b. Findings
No findings were identified.
.3 Assessment of Self-Assessments and Audits
a. Inspection Scope
The inspectors assessed the licensee staffs ability to identify and enter issues into the CAP program, prioritize and evaluate issues, and implement effective corrective actions, through efforts from departmental assessments and NOS audits.
Documents reviewed during this inspection are listed in the Attachment to this report Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold level. The audits and self-assessments were completed by personnel knowledgeable in the subject area and the NOS audits were thorough and critical. Where changes to the operating experience process were too recent for inspectors to assess, the NOS organization was monitoring the stations performance.
The inspectors observed that CAP items had been initiated for issues identified through the NOS audits and self-assessments. The inspectors reviewed the self-assessment performed on the CAP, found no issues and generally agreed with the overall results and conclusions drawn. The self-assessment of CAP was a very thorough look at the process which concluded that the process was effective.
Observations The inspectors noted some issues with how the licensee handled escalated NOS findings. These findings were issued when NOS had concerns with how the licensee was addressing previously identified NOS issues. They were considered more significant than regular NOS findings (which were handled commensurate with their significance in the CAP), but less significant than adverse findings (which were typically assigned a minimum CAP significance of B and an apparent cause evaluation).
By contrast, escalated findings were assigned a lower CAP significance level (C) and were resolved using an NOS specific process. This separate process did not evaluate why the issue had been escalated, but instead focused on those corrective actions necessary for NOS to close the issue. Once resolved, the associated CAP was closed with a cross-reference to the associated NOS documentation. This practice prevented the licensee from investigating why the CAP process did not adequately address the original NOS concern and potentially diminished the role of NOS as an independent overseer of station performance.
The licensee documented this observation as CAP 1449547.
b. Findings
No findings were identified.
.4 Assessment of Safety-Conscious Work Environment
a. Inspection Scope
The inspectors assessed the licensees safety conscious work environment (SCWE)through the reviews of the facilitys employee concern program implementing procedures, discussions with coordinators of the employee concern program, interviews with personnel from various departments, and reviews of issue reports. The inspectors also reviewed the results from a Safety Culture Survey and partial results of an organization effectiveness survey.
As part of the overall inspection effort, inspectors discussed department and station programs with a variety of people. In addition, the inspectors interviewed approximately 30 individuals from various departments to assess their willingness to raise nuclear safety issues. Other items discussed included:
- knowledge and understanding of the CAP;
- effectiveness and efficiency of the CAP;
- willingness to use the CAP; and
- knowledge and understanding of the ECP.
Documents reviewed during this inspection are listed in the Attachment to this report.
Assessment The inspectors did not identify any issues of concern regarding the licensees safety conscious work environment. Information obtained during the interviews indicated that an environment was established where licensee personnel felt free to raise nuclear safety issues without fear of retaliation; licensee personnel were aware of and generally familiar with the CAP and other processes, including the ECP and the NRC, through which concerns could be raised, and safety significant issues could be freely communicated to supervision. Documents provided to the inspectors regarding safety culture surveys and monitoring of the safety culture and SCWE generally supported the conclusions from the interviews.
Documents reviewed are listed in the Attachment to this report.
Observations Interviewed personnel generally expressed the view the CAP was serving its intended functions and stated that they were aware of and complied with the expectations to document concerns in the CAP.
The licensee had a Safety Culture Survey completed in August 2013, which concluded that overall the plant had a safety culture that supported the traits of a healthy nuclear safety culture, had a respect for nuclear safety, and assured that nuclear safety was not compromised by production priorities. The survey and the team that conducted the survey identified several positive observations and several weakness observations where action for improvement might be warranted. The weakness observations were associated with a respectful work environment and leadership safety values and actions.
The report documented that some employees believed that the communications from management on changes could be improved and management did not show respect for employees and their opinions. Several workers interviewed by the inspectors stated that following several management changes in 2014 that communication between workers and licensee management had improved since the survey.
The licensee had an organizational effectiveness survey in December 2013 that also looked at various traits associated with an effective safety culture. While generally the results of the survey were positive for the overall station, there were some indications of decline in some departments from 2011, the last previous equivalent survey, to the present survey. When the inspectors questioned personnel for the reasons for the indicated declines and for any follow-up action, the majority of licensee personnel interviewed were not aware of the survey results or of any action, including the generation of CAP inputs that resulted from the survey. During the inspection, the licensee did not provide any documents that indicated that the results from the December 2013 were considered as items that should be addressed.
b. Findings
No findings were identified.
4OA5 Other Activities
.1 Power Uprate Related Inspection Activities
a. Inspection Scope
As part of the biennial PI&R inspection, the inspectors reviewed selected, routine items entered into the licensee CAP concerning the power uprate amendment.
Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings were identified.
4OA6 Management Meeting
.1
Exit Meeting Summary
On October 10, 2014, the inspectors presented the inspection results to Ms. Fili and other members of the licensee staff. The licensee acknowledged the issues presented.
The inspectors confirmed that none of the potential report input discussed was considered proprietary.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
PLANT PROCEDURES
Number
Description or Title
Date or Revision
FP-OP-COO-15
Conservative Decision Making
FP-STND-NSC-01
Nuclear Safety Culture Monitoring Process
CD 2.1
Nuclear Oversight Corporate Directive
DP-NO-IA
Internal Assessments
DP-NOIA-07
Internal Assessment: Topic Selection, Scheduling,
And Cycle Reporting
FG-PA-CTC-01
CAP Trend Code Manual
FG-PA-EVAL-01
Evaluation Methods
FP-PA-DRUM-01
Department Roll-Up Meeting (DRUM) Manual
FP-PA-ACE-01
Apparent Cause Evaluation Manual
and 2
FP-PA-ARP-01
CAP Action Request Process
35, 37 and 39
FP-PA-SA-01
Focused Self-Assessment Planning, Conduct, and
Reporting
FP-PA-PAR-01
Performance Assessment Review Board and
Performance Assessment Oversight
OWI-03.02
Safety Related and Fire Protection System
Operability Determination and Verification
FP-E-EVL-01
Engineering Evaluations
FP-E-SE-04
Conduct of System Engineering
FP-OP-OL-01
Operability/Functionality Determination
QF0398
Security Change/Activity Screening and Evaluation 5
FG-PA-KPI-01
Performance Assessment Data Reporting
CP 0021
Employee Concerns Program
FP-EC-ECP-01
Employee Concerns Program
FP-PA-ECE-01
Equipment Cause Evaluation Manual
FP-PA-EFR-01
Effectiveness Review Manual
FP-PA-OE-01
Operating Experience Program
FP-PA-RCE-01
Root Cause Evaluation Manual
FP-PA-SOER-01
Significant Operating Experience Report (SOER)
Processing
NSPM-1
Quality Assurance Topical Report
FP-NO-IA-12
Nuclear Oversight Finding Development, Issuance
Tracking, and Issue Escalation
271
Memo Distribution, PCR 01313901
07/23/13
3802
Visual Inspection of Heat Exchanger Condition
CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED
Number
Description or Title
28268
Age Degradation Evaluation for Bolting Integrity Program
26605
GE Part 21 Notice (SC05-03) - Potential to Exceed Low Pressure
Safety Limit
951636
Administrative Controls Documents Will be Revised
1008261
Change Commitment Cross-Reference Location for M87005A
1131704
Breaker Racking or Alignment Issues
1176715
- 17 Battery's Capacity Calculation Contains Wrong Assumptions
1181868
Leaking Manifold Valve for DPIS-2-117A B Steam Line Flow
1185959
RCIC HELB at MO-2078 and Its Affect On MOC-311
1197202
CDBI-Calculation Quality Adverse Trend
205719
APM S&C Refurbishment Not Performed In Accordance With Tech
Manual
210803
Appropriate License Renewal Frequency Not Established
217223
Gap to Excellence in License Renewal System Walkdowns
21315
RBCCW Piping Thickness Below Expected Value
21333
MO-2009 Failed To Properly Operate During Procedure 1381
23696
Leak Discovered on SBLC Tank
27961
- 11 Offgas Compressor Flex Conduit Brocken
28061
Reactor Feed Pump Control Cable Exposed to Elevated
Temperatures
28167
Cable Tray in Turbine Building Has Corrosion Deposit
28174
FP-13 Has Evidence of Selective Leaching
265183
Ready To Install Task Caviats Could Cause Issues as Written
266454
Recovery Plan for HELB Improvement Potentially Off Track
268207
New LS-7211 EDG Level Switch Did Not Function as Expected
274758
Potential HU Error Trap In Electrical Modification WOs
280199
AR 1279926 Inappropriately Closed With No Actions
280599
Insulation Nick In MCC-141 Refeed Connector
298620
MO-2-53A/B Low Capability Margin for NSR Scenario
1300308
Main Access SCT Airlock EFR Acceptance Criteria Not Met
1307848
Class 1E Agastat Relay Replacement PM should be 10 Years
1309439
Core Spray Testable Check Valve Shows Dual Position
1314222
Potential Adverse Trend in Raw Water Pump Performance
CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED
Number
Description or Title
1316022
CV-1378 Cannot Control Pressure With Current Configuration
22841
Safety Related Equipment Impacted by Tech Spec Allowed Frequency
23839
MO-2021 Found With Dual Indication
28206
Actions from ACE 01266100 Found Not Effective
1330947
Questions About Equipment Safety Classification In Passport
1331618
NRC 2012 CDBI-Harmonics Issue with Degraded Voltage Relays
1332185
FME Found In New 13.8kv Switchgear
1334789
NRC Cross-Cutting Issue Potential In Human Performance
1337178
CRD HCU Piston Accumulators Do Not Meet HELB Environment
1337186
License Renewal PN Changes Not In Accordance With AWI
1342363
ODMI for Cable A602-G40/2 per Cable Program EWI-08.19.01
1343416
Adverse Trend In Equipment Re-Greasing Practices
1350445
MO-2010, Exceeded Maximum Closing Thrust
1351259
Discrepancy Between Fleet Process and Tec Spec
1353905
Adverse TrendBechtel Work Package Quality
1354966
MRule Unplanned SCRAMs Has Exceeded Criteria
1362098
Foreign Material Identified in 11 RHRSW Upper Reservoir
1368457
Rust Discovered in Feed Water Heater Nozzles
1373085
Leaks Identified on RHR-25-2 During DW Walkdown
1375410
Crack found in the P-1A, CD Pump Can / Suction Nozzle Weld
1376596
Support FW-17 Rigid Strut Recieved Not Correct Length
1378391
Inferior Bolts Found On New Valve - MS-116
1378744
E SRV Low-Low Set Tailpipe dP Root Valve Found Closed
1383340
EPU - Unacceptable Radiography (RT) Result On Piping Welds
1385118
Manufacturer Label Confusing To Personnel
1385313
Evaluate Shelf Life Guidance for Oil/Grease
1389519
IST Cold Shutdown Tests Not Scheduled Properly
1389604
NRC Question Regarding SR 3.0.2 and 3.0.3 Applicability
1390285
RF026 Was Planned 87 Days; Actual Will Be About 139 Days
1395575
NRC Questioning Results in Submitting 50.72 Unanalyzed Condition
1398625
NOS EscalationLevel 1 Performance Assessment
1402240
AO-13-22 Furmanite Injection Process Question
1402246
NRC Question on DSC PT Examination Times
1405367
NRC: Issues with Calculation 10-219
1405518
What Superseded Calc.00-082
1406284
NRC Inspection: Information Provided is Incorrect
1407041
HPCI Flow Time Delay Calculation Does Not Support HELB
1407385
NRC Inspection: Requirements for Soldering Electrical Connections
Not Met
1410620
Floating FME Found in Cell #7 On #17 Battery
1412267
OE: NRC Pt 21 Event No. 49667 Cracking in KCR-13 Standby
1419279
PT Exam on DSC-16 - Linear Indication Found on Re-Exam
CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED
Number
Description or Title
24048
Potential Adverse Trend on Accuracy of NRC Submittals
25172
Strain Gauge Location Configuration Question on C MSL
1430435
Inaccurate Info Transmitted to NRC for EPU
1432184
Review Adequacy of EOC for Inaccurate Info in EPU Submittals
1440002
ARP-01 CAQ Definition More Restrictive than QATR
1442205
No Follow-Up Actions Taken For Increase in Sum Of Six Result
OPERATING EXPERIENCE
Number
Description or Title
1446300
QF0463
NSPM OE Screen Team Meeting Template, Incoming Operating
Experience Package 09/15/2014
QF0463
NSPM OE Screen Team Meeting Template, incoming Operating
Experience Package 09/22/2014
List of Open Operating Experience CAPs as of 9/25/2014
24761
OE Evaluation of SOER 10-01
297249
OE-IERL2-11-2, 2009-2010 Scram Analysis
1308589
Issue at PI May Impact Monticello Maintenance Instructions
1312510
OE IERL2-11-46, Extended Emergency Power Operations
1313396
OE: NRC Green Violation-Failure to Establish Inspection Procedures
1314536
OE: NRC IN 2011-20 Concrete Degradation
25353
OE: IERL2-12-14 Automatic Reactor Scram Resulting from a Design
Vulnerability in the 4.16-kV Bus Undervoltage Protection Scheme
1335244
OE IERL2-12-38 Reactor Trip and Generator Lockout
1357468
Prairie Island AR-During Round, Outplant Operator Discovered 121
Safeguards Traveling Screen Differential Pressure Switch Pegged
Low
1357487
GE SIL 433 Sup. 2 Shroud Head Bolt Inspection Recommendations
1359840
Prairie Island AR-Update of CAP 1354059 That Event Was
Considered A Minor NRC Violation
1382652
GE SIL 438 R2 Main Steam Line High Flow Trip Setting
1391239
GEH SIL 409 Rev3 Incore Dry Tube Cracks
1402093
Prairie Island AR-No Combustible Permits for Lead Shielding
1407735
OE: IERL2-13-53 Loss of Off-Site Power (LOOP) Analysis
1416736
ICES 19861 Reactor Feed Pump High Vibration
1431296
OE-IERL2-14-25 Heavy Snow and a Design Flaw Result in a Dual
Unit Scram
ROOT CAUSE and APPARENT CAUSES
Number
Description or Title
141582
RBCCW In-Leakage Historical Review of Event
276006
Near Miss MSIV Bleeds Closed In Unplanned Fashion
1309399
Bus Failed to Re-energize
ROOT CAUSE and APPARENT CAUSES
Number
Description or Title
1334146
CDBI: Technical Specification Degraded Voltage Time Value
1334571
CDBI: Instrument Panel Y20 Voltage Nonconformance with USAR
1337244
RSW Pump Performance Trends Not Predictable
1343360
Adverse Trend Door #45 AEP Board Failures
1345334
Snubber Examinations Not Performed Per Code Requirements
1348567
CRD 18-07 Exceeds Friction Limit
1348931
Welder Qualification on Supports for 4kV HELB Barrier
1351292
V-FE-11: Negative DP During 0472-01 Testing
1351317
2-202 Initially Failed to Close During Planned Transfer
1351664
RMCS Failure During CRD Exercise Test 0074
1352773
Reactor Scram 130
1352778
Lockout of 4 kV Bus 12 During WO:446500-01
1353605
HPCI Concern With Y81 Inverter Out of Service
1353869
Danger Tagged Lifted Lead was Landed for P-903A Motor
1354309
HELB Barrier Bolts Found Loosened for Lower 4kV
1356091
Operability Concerns for Safety Related Inverter Supplied Loads
1356474
Potential Adverse Trend for Plant Configuration Control During Mods
1356625
Monticello HU Events
1357606
Four Findings in P.1© Cross-Cutting Aspect
1358371
Relay 10A-K35 for LPCI Loop Select Did Not Drop Out
1358924
RCIC System Found Inoperable and Unavailable
1367175
P-25B, #12 Reactor Building Floor Drain Pump Found Tripped
1367915
4-C-23 Recirc Pump Motor B Low Oil Level Alarm Received
1374981
Incorrect Cable Cut During Demolition
1378051
TI 2515 187, Inadequate Flooding Walkdowns
1378713
Work Hours Not Updated in WHM Tool IAW Procedure
1379117
NOS Finding: Adverse Trend With Common Cause Identified
1379814
Loss of Instrument Air Caused by PS-1469 Being Isolated
1381637
EDG Air Inlet Abstructed by Herculite
1383202
Agastat Relays Discovered Beyond Vendor Recommended
Qualification Life
1384157
Essential Bus Transfer Occurred While Performing 2R Testing
1384157
Essential Bus Transfer Occurred while Performing 2R Testing
1385754
Reactor Water Level Controlled With an Inaccurate Instrument
1385754
Temporary Vessel Level Instrumentation Rise
1386518
Breaker 152-101 Fault Resulting in Loss of Offsite Power
1386536
Shutdown of 11 & 12 EDGs after LONOP
1388760
NOS: AAF: MNGP Leadership Nuclear Safety Concerns
1389520
NRC Findings In H.2.C Cross-Cutting Aspect
1390092
Diesel Oil Service Pump P-77 Low Flow T-45B
1390785
Loose Circuit Card for Alarm C-04-A-11
1391665
Security 1 Hour Report Under 10 CFR 73.71
ROOT CAUSE and APPARENT CAUSES
Number
Description or Title
1392528
Multiple EPU Design Issues Discovered During Plant Startup
1394150
TIA 2012-03 Final Response EDG Fuel Oil Supply NCV 2013007-04
1394150
NRC TIA 2012-03 Final Response EDG Fuel Oil Supply
1394412
Area Radiation Monitor UP-and DOWNSCALE Trips Out of Spec.
1394877
Recirc Pump Runback, Investigate Circuitry
1394877
Recirc Pump Runback, Investigate Circuitry
1395575
NRC Questioning Results In Submitting 50.72 Unanalyzed Condition
1395722
NOS Escalation Level 1Power Uprate Readiness
1397406
Door 85/86 Plenum Room Airlock Failed Interlock Testing
1398300
2013 INPO Mid-Cycle FSA: AFI MA-2-25
1402240
AO-13-22 Furmanite Injection Process Question
1405035
Potential Adverse Trend in Ineffective CAPR EFRs
1405518
NRC Question: What Superseded Calc 00-082 HPCI Trip?
1406283
Improperly Identified Inputs Impact HRLB Calcs
1406283
Improperly Identified Inputs Impact HELB Calculation
1409551
NRC INSP: Failure to Maintain IEEE Qualifications of Relay
1411443
CV-1728 Went Closed When Only 13 RHRSW Pump Running
1418321
SR 3.8.1.12 Was Not Met By TS LOP Instrument Alone
1418669
Diesel Generator Output Breaker Failed to Close
23979
Inaccurate Scaling Used on EPU Testing on DAS for Steam Dryer
24346
LCB-083 Trip Interlock Bent Causing Unexpected Lockout/Alarm
25443
Six NRC Findings in H.14 Cross-Cutting Aspect
26098
Findings in Work Management H.5 Cross-Cutting Aspect
29810
Preconditioning Evaluation Was Not Documented
1430165
C4.2-1 Auxiliary System Chemistry Parameters
1430930
Opening Identified in Fire Barrier Separating Both Divisions
1432015
E CS&RHR Area ARM Out of As Found Criteria During 1024
1433756
Diesel Oil Pump (P-77) Lost Flow, Pressure
AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS
Number
Description or Title
Revision
USA Nuclear Safety Culture Assessment
09/17/2013
SAR 01436575
NEI 09-07 Nuclear Safety Culture 1st Quarter
2014
05/30/2014
Organizational Effectiveness Survey - Partial
Results
01/2014
01437361
Principles for Maintaining an Effective Technical
Conscience
07/28/2014
Nuclear Oversight 1st Trimester 2014 Executive
Summary
06/09/2014
SAR 01405321
Operations DRUM Report - 3rd Quarter 2013
11/16/2013
AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS
Number
Description or Title
Revision
SAR 01440695
Operations DRUM Report - 2nd Quarter 2014
07/31/2014
01437361
Principles for Maintaining an Effective Technical
Conscience
07/11/2014
2014-02-011
NOS Assessment of Corrective Action Program
07/21/2014
CAP 01290035
ECP Snapshot Self-Assessment
06/09/2011
SAR 01290035
ECP Snapshot Self-Assessment
08/12/2013
SAR 01404684
Pre-Problem Identification and Resolution
Inspection Assessment
03/10/2014
CAP 01447174
PI&R NRC Inspection Readiness Snapshot
Evaluation
07/28/2014
SAR 1356920
Site DRUM Report3rd Quarter 2012
SAR 01390911
Site DRUM Report4th Quarter 2013
2013-01-001
NOS Observation Report - Performance
Assessment/Corrective Action Program
2013-02-005
NOS Observation Report - Performance
Assessment/Corrective Action Program
2013-03-003
NOS Observation Report - Monticello/Corrective
Action Program
2013-04-006
NOS Observation Report - Performance
Assessment/Corrective Action Program
CY2014
Nuclear Oversight NOS Assessment Cycle
Schedule
2014-02-031
NOS Observation Report - MT/Production
Planning
2014-02-043
NOS Observation Report - MT/Maintenance
QF0434
Maintenance Department DRUM Report, 4th QTR
2013
SAR 01365272
Maintenance Department DRUM Report, 4th QTR
2012
QF0434
Maintenance Department DRUM Report, 3rd QTR
2012
SAR 01437435
Maintenance Department DRUM Report, 2nd QTR
2014
SAR 01429022
Maintenance Department DRUM Report, 1st QTR
2014
SAR 01407517
Maintenance Department DRUM Report, 3rd QTR
2013
QF0434
Maintenance Department DRUM Report, 1st & 2nd
QTR 2013
NOS Trimester Report
1C14
Nuclear Oversight 1st Trimester 2014 (January -
April) Executive Summary
NOS 4Q2013 Report
Nuclear Oversight 4th Quarter 2013 Executive
Summary
NOS 3Q2013 Report
Nuclear Oversight 3rd Quarter 2013 Executive
AUDITS, ASSESSMENTS, SELF-ASSESSMENTS, AND EVALUATIONS
Number
Description or Title
Revision
Summary
NOS 2Q2013 Report
Nuclear Oversight 2nd Quarter 2013 Executive
Summary
NOS 1Q2013 Report
Nuclear Oversight 1st Quarter 2013 Executive
Summary
NOS 4Q2012 Report
Nuclear Oversight 4th Quarter 2012 Executive
Summary
NOS 3Q2012 Report
Nuclear Oversight 3rd Quarter of 2012 for
Monticello
23944
Snapshot Assessment of Operating Experience
Evaluation for Significant Regulatory Events
List of Assessments, Benchmarking And
Self-Assessments For 2014 And 2015
1388760
NOS Adverse Assessment Finding on Leadership
Nuclear Safety Culture Concerns
2013-04-021
NOS Observation Report-Monticello Surveillance
2014-02-021
NOS Observation Report-Special Process
Control
2014-02-008
NOS Observation Report-Spent Fuel; Pool Level
Instrumentation Project
WORK ORDERS AND DRAWINGS
Number
Description or Title
Revision
486966
Inject Sealant Into AO-13-22 Packing
2/14/14
487258
V-EF-26 Low Flow Light Lit
09/10/14
489570
P-39 Pump Seal Failure
10/08/14
493201
POI-2942 Not Indicating Position of CV-2942
2/18/14
496046
Operate 12 Reactor Recirc Pump with One Seal
Water HX
2/04/14
497230
AO-2382A Dual Indication When Stroking
09/16/14
498423
V-AC-12A Replace Circuit 1 Compressor
04/25/14
2913
Sudden Pressure Alarms on Main Transformer
09/29/14
504480
FP-37 Inability To Close For Isolation
09/10/14
CONDITION REPORTS GENERATED DURING INSPECTION
Number
Description or Title
28206
Actions for ACE 01266100 Found Not Effective
1447666
PI&R: CAP Screening Missed Assignment of Some Evaluations
1447689
PI&R: Individual in Protected Area Without TLD
1447715
PI&R Question Response Was Not Complete Within 24 Hours
1447778
PI&R: ACE Grading Comments Not Incorporated in ACE 01276006-
CONDITION REPORTS GENERATED DURING INSPECTION
Number
Description or Title
1447784
PI&R: NRC Inspector Access to OCA Denied
1447847
PI&R: PCR01410247 Progression is Not Timely
1447870
PI&R: Interview Delayed Due to Miscommunication
1447927
PI&R: Question on Performing 3-2-1 Results Assessment
1447970
PI&R: Question on the Use of CAPR Designation for Sustainability
1448036
PI&R: Level A CAP Action Inappropriately Closed
1448056
PI&R: Parent OE CAPs Not Assigned Keywords
1448087
PI&R: OE Preventable Event May Be Too Narrowly Defined
1448102
PI&R: RCE1391665 Missing Tracking Action for PCR01348402
1448106
PI&R: NRC Inspector Shown Unqualified When Logging Into RCA
1448117
PI&R: Potential IA by PI Planning Identified in B level CAP
1448123
PI&R: Some Station Personnel Not Proficient In Passport
1448129
PI&R: RCE and ACE Procedures Inconsistent Around OE
Requirements
1448161
PI&R: Question Not Responded to Within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
1448222
PI&R: ACE01402240 Lacked Industry OE
1448223
PI&R: Actions Not Properly Cross-Referenced
1448228
PI&R: CA Inappropriately Closed to Another Action
1448901
PI&R: FP-E-RTC-01 Equipment Classification
1449520
PI&R: Question Not Responded to Within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
1449547
PI&R: Question on NOS Escalation Process
1449629
PI&R: CAP Assignment was Incorrectly Labeled EFR
1449678
New Interim EFR Not Created After Original EFR Failed
1449742
PI&R: Difficult to Follow CAP Issues Through Multiple
Cross-Referencing
1449785
PI&R: Action Closed Contrary to Statement in CA 1354309-08
1449863
PI&R 2014: Severity Classification Question for HU Events
1449939
PI&R Adverse Trend: CAP ARs Were Not Initiated Promptly
1449944
PI&R: Reactivity Control Formality
1450057
PI&R: Potential Common Cause With Integrated Plant Knowledge
1450065
PI&R: Observation on OE Preventable
1450086
PI&R: Observation on the RBCCW RCE
OTHER
Number
Description or Title
Licensees We Get It
Licensees 95002 and Safety Culture
Licensees 95002 Inspection
SAR 01405363
Monticello Operations Department Excellence Plan, Rev 5
Dashway Report Book (Performance Indicators) January to July 2014
Design And Licensing Basis On Diesel Fuel Oil Supply Of The
OTHER
Number
Description or Title
Emergency Diesel Generators At Monticello Nuclear Generating Plant
NOS 2013-04-016
Engineering/Operations Interface 11/04 to 11/08/2013
1/22/2014
Performance Assessment Functional Area MRM
8/25/2014
DashWay Report Book
QF0145
Nuclear Oversight Escalation Letter, Rev. 1
RFI 13-A-002
Concern with AMES valve work
RFI 13-A-018
Concern with HPCI and RCIC alignment work and grease used in
2011-A-0028
Concern with work done by DZ
WPC 11-26
Contractor concerned that cable was nicked during installation and not
repaired/replaced
AT-0075
CAP Prescreening Report, 09/23/2014
AT-0075 / QF0429
NSPM CAP Screen Team Meeting Template / CAP Screening Report,
09/23/2014
AT-0075 / QF0429
NSPM CAP Screen Team Meeting Template / CAP Screening Report,
09/24/2014
Plant Managers weekly communications package from 10/05/14
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- P. Albares, Operations Manager
- D. Bosnic, Director, Business Support
- H. Butterworth, Manager, Nuclear Oversight (Prairie Island)
- D. Collins, Interim Manager, Regulatory Affairs
- C. England, Manager, Radiation Protection
- K. Fili, Site Vice-President
- P. Gardner, Director, Site Operations
- H. Hanson, Plant Manager
- M. Kelly, Manager, Performance Assessment
- M. Lingenfeter, Director, Site Engineering
- M. Murphy, Director, Regulatory Affairs (Xcel Corporate)
- K. Nyberg, Manager, Site Security
Nuclear Regulatory Commission
- K. Riemer, Chief, Branch 2, Division of Reactor Projects
- P. Voss, Resident Inspector (Monticello)
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
None.
LIST OF ACRONYMS USED
Agency wide Document Access Management System
Corrective Action Program
CFR
Code of Federal Regulations
DRUM
Department roll-up meeting
Employee Concerns Program
IP
Inspection Procedure
NOS
Nuclear Oversight
NRC
U.S. Nuclear Regulatory Commission
Operating Experience
Publicly Available Records System
Problem Identification & Resolution
Reactor Building Closed Cooling Water In-Leakage
SSCIs
Substantive Cross-Cutting Issues
Safety-Conscious Work Environment
K. Fili
-2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's Agencywide Documents Access and Management System (ADAMS),
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public
Electronic Reading Room).
Sincerely,
/RA/
Kenneth Riemer, Chief
Branch 2
Division of Reactor Projects
Docket No. 50-263
License No. DPR-22
Enclosure:
Inspection Report 05000263/2014007
w/Attachment: Supplemental Information
cc w/encl: Distribution via LISTSERV
DISTRIBUTION w/encl:
John Jandovitz
RidsNrrDorlLpl3-1 Resource
RidsNrrPMMonticello
RidsNrrDirsIrib Resource
Cynthia Pederson
DRPIII
DRSIII
ROPassessment.Resource@nrc.gov
DOCUMENT NAME: Monticello 2014 007
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Non-Publicly Available
Sensitive
Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with
attach/encl "N" = No copy
OFFICE
RIII
NAME
NShah:mt
KRiemer
DATE
11/18/14
11/18/14
OFFICIAL RECORD COPY