IR 05000250/1997003

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Integated Insp Repts 50-250/97-03 & 50-251/97-03 on 970216- 0329.No Violations Noted.Major Areas Inspected:Operations, Maint,Engineering & Plant Support
ML17354A500
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/23/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17354A499 List:
References
50-250-97-03, 50-250-97-3, 50-251-97-03, 50-251-97-3, NUDOCS 9705080188
Download: ML17354A500 (88)


Text

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S.

NUCLEAR REGULATORY COMMISSION REGION ll Docket Nos.:

50-250 and 50-251 License Nos.:

DPR-31 and DPR-41 Report Nos.:

50-250/97-03 and 50-251/97-03 Licensee:

Florida Power and Light Company Facility:

Turkey Point Units 3 and 4 Location:

9760 S.

W. 344 Street Florida City, FL 33035 Dates:

February 16 through March 29, 1997 Inspectors:

T.

P. Johnson, Senior Resident Inspector J.

R.

Reyes, Resident Inspector J.

W. York, Acting Resident Inspector F.

N. Wright, Regional Inspector (Sections R1.1-1.5, R5.1, R6.1)

W.

C. Bearden, Regional Inspector (Sections H1.2-1.6, H2. 1.

M2.2, H7.2)

J. J. Blake, Senior Project Manager (Sections M2.7 and H2.9)

Approved by:

C. A. Julian, Acting Chief Reactor Projects Branch

Division of Reactor Projects 9705080i88 970423 PDR ADOCK 05000250

PDR

EXECUTIVE SUMMARY TURKEY POINT UNITS 3 and

Nuclear Regulatory Commission Inspection Report Nos. 50-250.251/97-03 This integrated inspection to assure public health and safety included aspects of licensee operations, maintenance, engineering, and plant support.

The report covers a six week period (February 16 to March 29, 1997) of resident inspection.

In addition. the report includes regional announced inspections of maintenance, health physics, inser vice inspection, and steam generator programs.

0 erations Operator response to a loss of a Unit 4 non-vital motor control center was very. good, including procedure use, command and control, and personnel performance (section 01. 1).

Poorly communicated instructions, a lack of a questioning attitude, and a weak system lineup sheet caused a Unit 3 feedwater transient and power reduction to 85K.

Operator response was excellent and timely, and prevented a unit trip (section 01.2).

Unit 3 shutdown and cooldown activities for the cycle 16 refueling outage were well performed and safely conducted (section 01.3).

Unit 3 draindown activities were generally well performed; however, a personnel error due to conflicting evolutions during post core-offload activities resulted in an unplanned reactor vessel fill (section 01.3).

The license demonstrated conservatism by not entering reactor coolant mid-loop operations.

A full core offload was conducted prior to vessel draindown for refueling work (section 01.3).

Unit 3 core alterations were professionally and efficiently performed.

Strong teamwork, good procedure use.

and effective communications were noted (section 01.4).

Unit 3 post-refueling reactor coolant system fill and vent operations were well performed (section 01.5).

The common high head safety injection system was appi opriately aligned (section'02.1).

Two non-safety related radwaste operating procedures did not comply with licensee administrative procedure and writer's guide requirements.

This was a licensee identified, non-cited violation (section 03.1).

Technical Specification Action Statements were appropriately

'ollowed for activities which affected the operating unit (Unit 4)

I

during refueling unit (Unit 3) evolutions and maintenance activities (section 04.1).

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Non-licensed operator rounds were generally good; however, one instance of poor follow-through and a lack of a questioning attitude by both non-licensed operators and the control room operators was noted.

This resulted in an unplanned Technical Specification entry to the post-accident hydrogen monitor (section 04.2).

~

Poor oversight of a non-licensed operator trainee resulted in an inadvertent trip of an auxiliary feedwater trip and throttle valve.

Licensee actions to immediately reset the valve and corrective actions were appropriate (section 05. 1).

~

Licensee reactivity management oversight and controls were very good (section 06. 1).

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Generally strong oversight and effective risk management were noted during the Unit 3 refueling outage (section 07. 1).

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A weakness was identified because operations personnel missed several opportunities to identify corroding piping during monthly survei llances on penetration alignment verification for containment integrity,(section H2.3).

~

Operator response to a fire and an Unusual Event was noteworthy (section P1.1).

Maintenance Poor work controls associated with a temporary trailer and power and breaker coordination issues caused a power loss to a Unit 4 non-vital motor control center (section 01.1).

Continuing Unit 3 rod control problems resulted in an urgent fai lure alarm, a manual trip to complete the shutdown, and a

licensee event report (section 01.3).

Corrective and preventive maintenance, and testing activities associated with the 3A emergency diesel generator; Unit 3, 4160 volt load center preventive maintenance and testing; and disassembly and inspection of the Unit 3 main steam line B check valve were performed in a good manner (sections M1.2, H1.3, H1.4.

and M1.6).

Leak rate testing of containment penetr ations was performed in a good manner.

As-found leakage values, which did not satisfy established acceptance criteria, were appropriately documented in condition reports and repaired (section Hl.5).

Personnel safety issues were appropriately addressed by the licensee (section H1.7).

Basket strainer cleaning was well performed (section Hl.8).

Unit 3 power operated relief valve testing was appropriately conducted (section M1.9).

Unit 3 turbine-generator overhaul, inspections, and modification activities were appropriately performed (section Hl.10).

Unit 3 reactor pressure vessel work (disassembly and reassembly)

was well performed (section Hl.ll).

Fire protection themolag work was observed and work control was appropriate (section H1.12).

Reactor coolant pump and motor maintenance was appropriately performed (section M1.13).,

Corrective maintenance associated with a fire damaged control rod drive mechanism motor generator was conducted in a good manner, with frequent quality assurance overview (section M2. 1).

Maintenance activities associated with a main steam safety valve which had failed to lift at the expected pressure during testing were conducted in a good manner (section H2.2).

Hotor-operated valve testing and ownership were very good (section H2.4).

Steam generator inspection and cleaning activities were well managed (section H2.5).

The 4A safety injection pump casing leak tempo ary repai r failed and permanent repairs were required (section H2

~ 8).

Welder qualifications for the outage were properly conducted and the personnel conducting these tests were experienced and capable (section M5.1).

Safety-related piping not being stored to regulatory requirements (ANSI 45.2.2)

was a non-cited violation (section M7.1).

Maintenance self-assessment in the area of work coordination provided meaningful feedback to management for performance improvement (section M7.2).

The licensee's ISI activities wer e well documented, and appeared to be representative of good. close coordination between corporate. site.

and contractor activities.

Containment

surveillance procedures had documented acknowledgement of recent changes to NRC regulations (section M2.7).

~

An exception to good coordination was noted regarding the late recognition that permission to use ASNE Code Case N-533 had not been requested due to mis-communication between licensee organizations (section N2.7).

En ineerin Engineering involvement and support of corrective maintenance and preventative maintenance activities associated with the 3A Emergency Diesel Generator, and the main steam line B check valve disassembly and inspection were very good (sections M1.2. N1.3, and M1.6).

Engineering support for maintenance was good as evidenced by resolution of a Unit 4 flange leak in the boric acid system (section E2.1).

Observed Unit 3 modifications associated with the boron injection tank removal, core reload.

intake and turbine plant cooling water, and turbine generator were well performed and appropriately documented (sections E2.2-2.4).

The licensee's program and controls for the intake structure's periodic inspections and maintenance were appropriate, and indicated good engineering involvement (section E2.5).

The licensee's response to Generic Letter 96-01 regarding safety related testing was reviewed (section E3. 1).

Licensee event reports and monthly operating reports were timely and well written (section E3.2).

The licensee has an effective flow-accelerated testing program (section N2.6).

Excellent engineering support for maintenance was observed for repai r on the high head safety injection pump 4A (section N2.8).

Plant~st Use of remote monitoring technology to save collective radiation dose was 'a strength (secti on Rl. 1).

~

The licensee's program for inspection of Steam Generators appeared to be well managed.

The documentation of inspection results was more conservative during the current outage than it had been in the past (section M2.9).

~

.

Adequate radiation protection control measures were in place in the Unit 3 containment.

However, one non-cited violations were identified:

failure to perform meter response checks.

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Radiation areas were properly posted.

No radioactive material was found outside the controlled area (section R1.2).

The ALARA program was a strength (section R1.3).

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Vehicle surveys were thorough and dose rates acceptable (section R1.4).

High radiation areas resulting from spent fuel transfer was appropriately identified (section Rl.5).

~

The new Radiation Protection Manager met regulatory training and qualification requirements (section R5. 1).

A new radiation protection organization was acceptable (section R6.1).

Periodic Unit 3 containment tours and a review of radiation controls during the outage determined that very good health physics controls were in place (section R1.6).

~

Licensee response including fire brigade, emergency preparedness, and station support to an Unusual Event due to a fire was noteworthy (section P1.1).

~

An Emergency Plan and a fire drill were well conducted (sections P4.1 and F5.1).

~

The lice~see appropriately responded to and reported an illegal drug found in the protected area (section Sl.l).

~

Failure to have several personnel included in the random drug and al.cohol testing program was a licensee-identified.

non-cited

. violation (section S8. 1).

TABLE OF CONTENTS Summary of Plant Status...

I.

Operations II.

Maintenance

III.

Engineering

...30 IV.

Plant Support

.33 V.

Management-Meetings

Partial List of Persons Contacted..

List of Items Opened.

Closed and Discussed Items

List of Inspection Procedures Used.

..46 List of Acronyms,and Abbreviations

.47

REPORT DETAILS Summary of Plant Status Unit 3 At the beginning of this reporting period, Unit 3 was operating at or near full reactor power and had been on line since January 16, 1997.

The unit shutdown for the Cycle 16 refueling outage on March 3, 1997.

At the end of the inspection period, the unit was in Node 5 (cold shutdown)

making preparations for its return to service.

Unit 4 At the beginning of this reporting period, Unit 4 was operating at or near full reactor power and had been on line since February 3, 1997.

The unit operated at full power during the entire inspection period.

0 erations Conduct of Operations Unit 4 Loss of Non-Vital Bus 71707 and 93702 At 3:05 p.m.

on February 26, 1997, Unit 4 was operating at full power when a loss of the 4A non-vital motor control center (MCC) occurred.

Operators received several annunciator alarms, and confi rmed that the feeder breaker from the load center to the NCC had tripped.

Non-safety related equipment lost included transformer normal cooling. gland steam (GS) exhauster fan, steam generator (SG) blow-down, steam generator feed

~

~

~

~

ump (SGFP)

room fans, secondary sampling, lighting in the turbine ui lding, heating venti 1,ation and air conditioning (HVAC) equipment, and turbine-generator (TG) auxiliary equipment.

Alarm response procedures (ARPs) were followed, and redundant equipment was verified operating or was manually started.

In the cases where redundant equipment was not available by design or was out-of-service (OOS) (e.g.

GS fan), operators monitored system parameters in the control room and in the field.

Operators determi.ned that an exposed temporary welding outlet cable had been wetted during some Unit 3 pre-outage work.

This shorted the power supply panel from the 4A NCC, causing an overcurrent trip of the supply breaker.

Operators de-energized the temporary outlet.

opened all MCC feeder breakers, re-energized the NCC, and reclosed MCC loads one-at-a-time.

All loads were restored by 4:20 p.m.

Condition Report (CR) No.97-255 was also written.

The. licensee also determined that a lack of coordination between the MCC in-coming breaker and the power panel supply breaker was also a causal factor.

Corrective actions to address this issue are pending.

The inspector heard the public address (PA) announcement and responded to the control room.

The inspector verified that operators were responding per the ARPs, and using controlled load list documents.

The

inspector independently checked alarm and control room indications, and toured the Unit 4 turbine building area.

Local HCC breaker operations were witnessed.

The inspector examined the wetted temporary cable.

Apparently, the cable had supplied a trailer that was recently moved by the maintenance projects group.

The inspector also reviewed logs, the CR, and discussed the event with operators and management.

The inspector concluded that poor work controls associated with a trailer movement operation and with temporary power control for pre-outage work resulted in the loss of the 4A HCC.

Operator response including procedure use, command and control, field activities and control room monitoring, was very good.

CR corrective actions were reviewed and determined to be appropriate.

Unit 3 Feedwater Transient and Load Reduction 71707 and 93702 At 5:51 a.m.

on February 27, 1997, Unit 3 operators received steam generator (SG) steam-feed flow mismatch alarms while at full power.

Operators responded by taking manual control of two feedwater regulating valves, and reduced unit load to 85K power.

This was done as a

recaution due to observed low SGFP suction pressure, a loss of both eater drain pumps, and an automatic,feedwater heater bypass (e.g.

control valve CV-2011 opened on low SGFP pressure).

An Event Response Team (ERT) was established and CR No.97-259 was written.

The licensee concluded that operator alignment activities associated with the Unit 3 condensate polishing system resulted in partial closing of the system bypass pressure control valve (PCV-6325B),

causing a momentary (e.g.,

few seconds)

interruption of condensate and feedwater flow.

At Turkey Point, the full flow condensate polishing system is only used during long outage periods.

Normally at power, the system is OOS and bypassed with PCV-6325B opened.

The operator performing the post-maintenance lineup check repositioned the control switch for PCV-6325B as directed from open to auto per the OP lineup sheet.

The lineup sheet assumed the system to be in operation.

When the operator noted the valve had begun to stroke closed as designed, the switch was returned to open.

The ERT concluded that causal factors included poor instructions to the operator from the control room, a system lineup sheet that only included normal (e.g.,

operating) condition of the condensate polishing system, and a lack of a questioning attitude by.the operator and the control room.

On the positive side, the ERT concluded that the operator's quick action to re-open PCV-6325B probably prevented a unit trip from loss of feedwater.

Further, the ERT noted excellent response by the control room to prevent significant SG level transients and a possible loss of SGFPs.

The inspector reviewed the event.

including logs, the CR.

and the ERT report.

The inspector also discussed the event'with on-shift operators and with plant and operations management personnel.

The inspector verified corrective actions.

The inspector noted this transient to be a

"near miss" caused by poorly communicated instructions, a lack of a

questioning attitude by non-licensed operator, and a poor system lineup sheet.

On the other hand, quick response by the non-licensed operator using Stop-Think-Act-Review (STAR) to re-open the valve, and timely and skilled control room operator response prevented a plant trip.

Unit 3 Shutdown and Cooldown and Reactor Vessel Oraindown Ins ection Sco e

60710 and 71707 The inspectors reviewed and observed portions of the licensee's shutdown and cooldown activities associated with the Unit 3 Cycle 16 refueling outage..

In addition, the inspector s reviewed reactor vessel draindown activities.

Observations and Findin s The licensee commenced power reduction for the Unit 3 Cycle 16 refueling outage on February 28, 1997, to 60K power,.

Subsequently on March 3, 1997, at 12:01 a.m., the generator output breakers were opened.

Operators shut down the reactor, entering Node 3 at 12:41 a.m.

Subsequent testing and cooldown activities were performed and the unit entered Mode 4 at 4:13 p.m.

on March 3.

1997, and Node 5 at 9:10 p.m.

on March 3, 1997.

The unit entered Mode 6 at 10:34 p.m.

on March 6, 1997, when the licensee commenced reactor vessel head stud detensioning..

The inspectors observed portions of the shutdown, cooldown, and related testing activities.

The inspectors verified that these evolutions were performed in accordance with approved procedures, that appropriate oversight was present.

an'd that Technical Specification requirements were followed.

Overall, observed activities were well performed and safely conducted with strong oversight.

The shutdown was performed in accordance with procedure 3-GOP-103, Power Operations to Hot Standby.

During the reactor shutdown (power in the source range), at 12: 12 a.m..

on March 3, 1997, a control rod urgent failure alarm occurred.

The alarm was reset once.

Operators then performed a manual reactor trip from the control room to complete the shutdown.

Control banks A and'

and shutdown banks A and B were fully withdrawn.

Control bank C was partially withdrawn and control bank D was fully inserted prior to the trip.

All rods successfully inserted into the core following the trip as verified through the analog rod position indicating system.

Operators entered emergency operating procedures (EOPs)

as required, and then transitioned to the GOP.

An NRC Emergency Notification System (ENS) call was made at 1:24 a.m.

A CR (No.97-275)

and LER 97-02 were subsequently issued.

The licensee concluded that a phase sensing transformer in the

BD power cabinet failed.

The transformer was replaced.

The inspector noted that the operator performance during the shutdown was deliberate and professional.

Training performed prior to shutdown activities was very good.

Further, the NPS conducted briefings per procedure O-ADH-217, Conduct of Infrequently Performed Tests or

Evolution, prior to initiation of the shutdown.

Performance during the rod problem was per procedures and was conservative.

In order to accommodate reactor pressure vessel (RPV) head detensioning, the reactor coolant system (RCS) was drained to a level of'.5 feet below the RPV flange, Reduced inventory or midloop operation condition exists at 3.0 feet or more.

below the RPV flange.

Therefore, the licensee did not technically go into midloop conditions until after the complete core offload.

However, the inspectors reviewed the following documents:

Generic Letter (GL) No. 88-17, Loss of'ecay Heat Removal, and the

'licensee's responses to this generic letter; Operating procedures 3-0P-041.7, Draining the Reactor Coolant System; 3-0P-041.9, Reduced Inventory Operations; and 3-0P-201, Filling/Draining the Refueling Cavity and the Spent Fuel Pit (SFP)

Transfer Canal; Offnormal operating procedure 3-0NOP-052, Loss of Residual Heat Removal (RHR):

Operations surveillance procedures 3-0SP-051.14.

Reduced Inventory Containment Penetration Alignment Verification; and 3-0SP-201.1, RCO Daily Logs; Various plant drawings; Training lesson plans and system description No.

007, Reactor Coolant System; Control room log books:

and Refueling outage schedules.

Prior to the draindown evolution, the licensee conducted special briefings as required by procedure O-ADA-217, Conduct of Infrequently Performed Tests or Evolutions.

Level was maintained at approximately 49K on'the remote reactor draindown level indicators LI-6421 and LI-6423.

This corresponded to 1.5 feet below the RPV flange.

The inspectors verified that redundant RCS level indications were available and were being monitored by control room operators.

Level devices LI-6421 and LI-6423 provided remote readout in the control room, and a tygon level tube (level device LI-6422) provided local indication in the containment.

The inspectors verified that these devices were available, being used, and recorded accor'dingly and that they indicated within their allowable tolerances..

However, during one containment tour on. Harch 6, 1997, the inspector noted that the drain down devices had a

small leak and the devices were not protected from possible detrimental outage work.

These issues were discussed with operations management, and corrective actions were.taken immediatel.4

,During the post-core offload drain down on March 12, 1997, an event occurred where approximately 10.000 gallons of refueling water storage tank (RWST) water gravity drained into the RCS.

The licensee was performing RCS clearance zone No. 41-01.

A conflict with procedure 3-OP-201, RCS Draindown, allowed a

common valve to be opened (e.g.

valve number 3-887).

This provided a

common flowpath from the RWST through the RHR lines to the RCS via motor operated valve MOV-3-872.

Operators immediately recognized the error and closed MOV-3-872.

Water level increased from 20K to 45K on the draindown indicator.

No water was spilled.

The licensee initiated CR No.97-415 and concluded the cause to be a personnel error when two supervisors e. g., senior reactor operators (SRO) di rected conflicting activities. without the oversight of the on-shift ANPS.

Also.

a lack of a questioning attitude was a

causal factor.

Corrective actions included personnel counselling, nite order entries, shift briefings, and procedure changes.

The inspectors noted that the licensee was proactive in reducing risk and demonstrated conservatism in its decision to complete core offload prior to entering reduced'inventory and midloop operations for RCP and steam generator work.

Further, licensee actions to drain the RCS (with fuel loaded)

were effectively conducted with good procedural compliance and with strong oversight.

Conclusions The inspectors concluded that the licensee demonstrated very good performance during Unit 3 shutdown, cooldown.

and pre-refueling draindown activities.

Actions taken were in accordance with procedures and demonstrated conservative operations.

However, a personnel error due to conflicting evolutions and a lack of a questioning attitude during the post-refueling (e.g.,

core offloaded) draindown caused an unplanned RCS fill.

LER 97-02 was adequate and was closed.

Unit 3 Core Offload and Reload Ins ection Sco e

71707 and 60710 The inspectors reviewed core alterations during the Unit 3 outage.

This included core offload and reload activities.

Observations and Findin s The Unit 3 reactor core was completely offloaded into the SFP during the period March 10-12, 1997.

The licensee implemented procedure 3-OP-040.2, Refueling Core Shuffle.

Procedures 3-OP-038. 1 Preparations for Refueling Activities. and 3-0P-038.9, Refueling Activities Check Off List, were used to ensure that prerequisites, precautions, limitations, and guidance were appropriate for core alteration activities.

During the period March 21-23, 1997, the licensee reloaded the reactor core for Cycle 16.

This was done per the Unit 3 Cycle 16 core reload procedures.

During the reload, a few assemblies were discovered to be

p

moderately bowed'.

Thi.s required extra time and a number of fuel assembly move deviations.

The inspectors verified that these 'deviations were performed per procedure 3-0P-040.2, Attachment 2.

The inspectors reviewed the above mentioned procedures, refueling Technical Specification.

operating procedures for each refueling station, the Updated Final Safety Analysis Report (UFSAR) section 9.5, condition reports associated with equipment problems, and operating and reactor engineering logs.

(See section Rl.5 regarding radiation levels from the SFP transfer canal.)

The inspectors witnessed portions of the Unit 3 refueling activities from the following locations:

Reactor Control Operator (RCO) station in the control room; Reactor engineer station in the control room; RCO, SRO, vendor stations on the manipulator bridge; Containment upender and transfer cart station; SFP upender and transfer cart station.

and RCO and SRO station on the SFP bridge.

01.5

02.1 Conclusions For those evolutions that were directly observed, the inspectors noted that communications were formal, teamwork was effective.

and procedure usage and compliance was strong.

Overall, observed core alteration activities were professionally and efficiently performed.

Unit 3 Reactor Coolant S stem RCS Fill and Vent 60710 The inspectors reviewed the post-refueling RCS fill and vent evolutions.

This included RCS fill, RCP runs, pressurizer bubble evolutions, and OP implementation.

These activities were well performed, with strong oversight.

Operational Status of Facilities and Equipment Hi h Head Safet In ection HHSI S stem Walkdown 71707 The inspector performed a walkdown of the Unit 3 and Unit 4 HHSI systems.

At the time, Unit 4 was at power and Unit 3 was preparing f'r restart from the Cycle 16 refueling outage.

The walkdown included Unit 3 post-maintenance and post-modification activities (sections Nl.l and E2.3).

The inspector reviewed piping drawings, system lineup sheets and related procedures.

The inspector independently walked down the system in field

and in the control room.

Further, the inspector walked portions of the system down with the system engineer.

The.inspector concluded that the common HHSI system was appropriately aligned.

The system engineer was noted as being knowledgeable and as having a strong sense of ownership.

Operations Procedures and Documentation 03. 1 0 eratin Procedures OP a.

Ins ection Sco e

71707 The inspector reviewed the licensee's program for operating procedures.

This included the writing of procedures per administrative procedure (ADM) O-ADM-101, Procedure Writer's Guide; procedure preparation and use per O-ADH-100, Preparation, Revision, Review, Approved and Use of Procedure; and.

procedure use per O-ADM-201, Operations Procedure Use.

Observations and Findin s The following areas were reviewed:

Operations organization to support procedures, Procedure identification, Format and style, Procedure writing and approval.

Basis documents.

Signoffs and verifications, Procedure adherence, On-the-spot-changes (OTSC),

Periodic review of procedures, New procedure verification and validation, and Procedure control and distribution.

The inspector reviewed two licensee CRs (Nos.

97-44 and 45) which were generated in January 1997.

The CRs concluded that the two following procedures did not comply with the ADM writers guide (e.g.

procedure 0-ADM-101) requirements:

O-OP-061.12, Waste Disposal System

- Waste Monitor Tanks and Demineralizer Operation

O-OP-061.13, Waste Disposal System

- Transferring Water to the Portable Demineralizer Skid For Processing.

Specifically. the OPs used procedure notes and cautions as action steps.

Section 5.5. 12 of procedure 0-ADM-101 specifically states that notes and cautions are advisory or administrative information regarding potential hazards.

The CR followup also identified additional deficiencies in these two procedures.

The licensee further concluded that these deficiencies were not causal. factors in the two radwaste building spills that occurred in 1996 (reference NRC Inspection Report Nos.

50-250,251/96-02 and 13).

Licensee corrective actions included the following:

Issued training brief No.

667 delineating writers guide requirements, Committed to revising the above two OPs by August 1997,

\\

  • Will review other OPs for consistency with writer's guide requirements during routine or periodic OP revision, and CR completion Conclusion The inspector concluded that procedures O-OP-061.12 and 13 did not comply with licensee ADN requirements.

These procedures are non-safety related, but required by regulations.

This licensee-identified violation is being treated as a Non-Cited Violation (NCV), consistent with Section VII.B.1 of the NRC Enforcement Policy.

NCV 97-03-01.

Failure to Follow Administrative Procedures For Writing Operating Procedures, was closed.

Operator Knowledge and Performance 04. 1 Technical S ecification Action Statement TSAS Com liance 71707 During the inspection period, scheduled outage work on Unit 3 resulted in TSAS entry on the operating Unit 4.

For example, the following shared equipment resulted in Unit 4 TSAS entry:

E ui ment/S stem Auxiliary Feedwater (AFW)

Emergency Diesel (EDG)

Electrical (AC/DC)

Post-Accident Vent (PACV)

Control Room Vent High Head Safety Injection (HHSI)

Standby Steam Generator Feed Pump (S/B SGFP)

TSAS 3.7.1.2 3.8.1 3.8.1/3.8.2/3.8.3 3.6.6 3.7.5 3.5.2 3.7..2

05.1 The inspector verified that the appropriate TSAS was entered for the operating unit, that operator s were knowledgeable of TS requirements.

that the time was minimized as far as possible, and that the risk was assessed in accordance with ADM requirements.

Further, TS section 3.9 for refueling was also reviewed during core alterations for Unit 3 (see section 01.4).

The inspector concluded that the affected TSASs were adhered to, and that the licensee paid particular attention to risk for the operating unit.

Non-Licensed 0 erator Rounds 71707 During the inspection period, the inspectors observed non-licensed operator performance. during periodic rounds and logkeeping activities.

Turbine building, auxiliary building, and outside area rounds were observed.

This included the Senior, Assistant.

and Nuclear Plant Operators (SNPO, ANPO.

and NPO) positions.

Overall performance was noted as being very good.

The inspector also reviewed an instance during the inspection period where poor non-licensed operator attention to logkeeping was noted.

During an administrative review of SNPO logs on March 25.

1997, the 4B post-accident hydrogen monitor (PAHM) reagent (oxygen)

gas bottle pressure was noted as being low.

The requirement was for greater than 200 psig of oxygen gas.

The licensee immediately entered the 30 action statement per TS 3.6.5 effective March 24, 1997.

This was the last time the gas pressure reading was acceptable.

The oxygen bottle was re-filled, a small leak was repaired, and the 4B PAHM system was returned to service.

The licensee's investigation noted that the log reading did not note this to be a

TS reading.

Further, a poor questioning attitude by both the SNPO and the control room operator was noted.

Corrective actions (CR No.97-584) were reviewed and noted to be adequate.

No TSAS violations occurred as the 4A PAHM remained operable.

The inspector concluded that non-licensed operator rounds were gener ally good.

Further, the licensee appropriately responded to the above mentioned poor attention to logkeeping requirements.

Operator Training and Qualification Auxiliar Feedwater AFW Tri and Throttle Valve Closure b

Trainee 71707 On March 13, 1997. at about 12:15 a.m.,

during a routine tour by a trainee with a field operator (NPO), the trainee inadvertently bumped

.the A AFW trip and throttle valve linkage causing its closure.

Scaffolding in the vicinity of'he AFW system was determined to be a

contributing cause.

This action placed Unit 4 in an unplanned 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> TSAS per TS 3.7.1.2 with AFW train 1 OOS.

This was recognized by an NPS field tour and by the unit RCO dur ing control board walkdowns.

The

06.1

valve was immediately reset.

and the TSAS for the A AFW pump was exited within several minutes at 1:00 a.m.

During this time, the B AFW pump was also technically OOS for planned maintenance.

The redundant train 2 AFW pump (e.g.,

C AFW) was fully operable.

Thus, Unit 4 had a single AFW pump and train available.

The B AFW was available and tested after the planned maintenance; however, the B AFW was awaiting procedure signoffs.

The 8 AFW was declared operable and the entire AFW related TSAS exited at 1:05 a.m.

The licensee initiated CR No.97-419, and concluded that poor NPO oversight of the trainee.

and inattention to detail by the trainee were the causes.

Corrective actions included:

CR followup, shift briefings, trainee and NPO counselling, training program reviews, and nite order entries.

The inspector concluded that the licensee appropriately handled this occurrence.

No TS violation occurred.

Operations Organization and Administration Reactivit Mana ement Controls Ins ection Sco e

71707 The inspector reviewed the licensee's reactivity controls for the Unit 3 shutdown for refueling (February 28 to March 3, 1997),

and overall site reactivity management as documented in two CRs.

b.

Observations and Findin s In order to control reactivity associated with di lutions and borations, and control rods, reactor engineering prepared a plan for the Unit 3 power descent for refueling (section 01.3).

Guidance was developed for slow and deliberate power decreases, and accompanied boron changes and control rod movements.

This assured adequate control of axial flux difference and xenon. peaking.

The information was promulgated to operations through two memos.

The memos did not modify nor supersede the normal shutdown procedures.

In addition, two CRs (Nos.

97-80 and 179) were recently written and answered, which addressed reactivity management issues.

The first CR (No. 97-80)

responded to an operations question concerning the CVCS OP.

In particular, whether or not chemical additions in field (that could affect reactivity) need be supervised by.licensed operators.

The licensee concluded that the evolution was satisfactory since it was per an OP and done with control room knowledge.

The second CR (No.97-179)

addressed operating e'xperience issues and recent industry events.

A number of issues and questions were addressed.

The licensee concluded that their reactivity program was sound, and some enhancements were appropriat ~

c.

07.1

Conclusions The inspector reviewed the shutdown plans and actual implementation, and the CR responses.

Licensee personnel demonstrated a good questioning attitude.

proactive reactivity, management control, and an overall very good program.

Quality Assurance in Operations Unit 3 Refuelin Outa e Oversi ht and Risk a.

Ins ection Sco e

60710 and 40500 The inspectors reviewed the licensee controls and oversight in effect during the Unit 3 refueling outage.

This included the implementation of administrative procedure 0-ADM-051. Outage Risk Assessment and Control.

Observations and findin s

'I The ADM required a risk assessment team to review the refueling schedule, switchyard work, higher risk evolutions, and key safe-shutdown functions and to maintain a risk information notebook.

The team was comprised of engineering, outage, operations, and maintenance personnel.

Minimum required equipment was addressed in the ADM enclosures.

The inspectors verified that important equipment was maintained operable or available as necessary.

Deviations from the ADM requi rements were accomplished by the use of an approved Temporary Change Notice (TCN).

The enclosures were broken into two parts:

large decay heat load (<10 days from shutdown)

and reduced decay heat load (>10 days from shut-down).

The inspectors reviewed the safety equipment necessary to support decay heat removal from Mode 3 to Mode 6 with the vessel and cavity flooded.

In Mode 3, all safety equipment were required to be operable by both technical specification and ADM requirements.

In Mode 4. the licensee maintained all safety equipment operable above any requi rements.

Although not required by the Technical Specifications, the licensee maintained ECCS available for Modes 4. 5, and 6.

For example, the cold leg accumulators, HHSI. and the charging system were available for injection, makeup, and RCS feed/bleed operations.

However, difference

,this outage was that HHSI was temporarily isolated for about two shifts (in Mode 5) in order to accommodate a flange installation to support a

modification to the BIT (see section E2.3).

This was accomplished by use of a TCN approved by both the risk team and management.

Once the cavity was flooded to support core offload. the 3A train equipment was removed from service as allowed by Technical Specifications.

This 3A train outage included the 3A EDG, the 3A 4KV buses, and the 3A RHR and support systems.

Since this occurred in the first 10 days, another TCN was written and approved by both the risk team and managemen The inspectors verified that the outage plan was implemented as scheduled and that Technical Specification and ADM requirements were met.

The inspectors noted conservatism relative to equipment made available to remove decay heat as the licensee transitioned from hot standby (Mode 3) to refueling (Mode 6).

Further, the licensee maintained RPV level above RCS reduced inventory and RCS midloop level.

The licensee continues not to go to midloop with the core loaded in the vessel.

This has been true for the past several years.

Another good ractice noted was system engineering involvement.

Periodically, and at east weekly, the system engineers walked down their systems and wrote a

report.

These reports as well as the TCNs were maintained in risk assessment notebooks located both in the control room and in the outage conference room.

The inspectors noted that the licensee assigned shift directors to cover the outage around the clock.

Senior plant personnel and department managers were assigned this shift direction function.

These shift directors provided oversight and maintained status of the refueling outage activities.

They also conducted the periodic outage status meetings.

The inspectors noted that these shift directors were involved in the field and directly involved in containment activities.

The inspectors noted that QA personnel were involved in outage activities including core offload and reload, core verification, containment tours, EDG maintenance, PC/M implementation, and control rod and integrated safeguards testing.

QA findings were discussed with the appropriate personnel and were documented in QA audit and surveillance reports.

Control room oversight was strengthened during the outages.

The operating shifts were modified from a six-shift to a four-shift rotation.

This provided extra NPSs and ANPSs on each shift to provide SRO coverage for refueling and other outage-related activities.

Further, operations management provided additional oversight for key refueling activities. e.g.,

draindown, core alteration, integrated safeguards testing, unit restart.

etc.

c.

Conclusions In conclusion, the inspectors noted generally strong oversight and effective risk management during the Unit 3 refueling outage.

One example of poor oversight was discussed in section 01.3.

II. Maintenance Conduct of Maintenance Ml. 1 General Comments a.

Ins ection Sco e

61726 62707 62700 and 62702 Maintenance and surveillance test activities were witnessed or reviewe The inspector witnessed or reviewed portions of the following mainte-nance activities in progress.

EDG overhaul and testing (sections M1.2 and 1.3)

Electrical bus work (section Hl.4)

Hain steam check valve overhaul (section H1.6)

Basket strainer cleaning (section H1.8)

PORV maintenance and testing (section M1.9)

Turbine generator overhaul (section H1. 10)

Reactor vessel assembly/disassembly (section Hl. 11)

Thermolag upgrades (secti.on M1.12)

RCP work (section H1.13)

4A HG set repair (section M2. 1)

Hain steam safety valve repai r (section M2.2)

SG inspections (sections H2.5 and H2.9)

4A HHSI pump repair (section M2.8)

The inspectors witnessed or reviewed portions of the following test activities:

Local leak rate testing (section Ml.5)

MOV testing (section M2.4)

Unit 3 BIT modification testing (section E2.3)

Observations and Findin s For those maintenance and surveillance activities observed or reviewed, the inspectors determined that the activities were conducted in a satisfactory manner and that the work was properly performed in accor-dance with approved maintenance work orders.

The inspectors also determined that the above testing activities were performed in a satisfactory manner and met the requirements of the technical specification p

c.

Conclusions Observed maintenance and surveillance activities were well performed.

M1.2 Unit 3 Emer enc Diesel Generator Outa e Activities a.

Ins ection Sco e

62700 The inspectors observed selected ongoing corrective maintenance activities associated with the 3A EDG outage.

b.

Observations and Findin s The inspectors observed portions of the following ongoing corrective maintenance activities:

WO 95022087-01 was issued to replace several sections of eroded pipe in the 3A EDG Air Start System.

The inspectors observed replacement of portions of the air start piping.

WO 96029615-01 was issued to replace belts for the 3A EDG radiator cooling fans and performed troubleshooting of the high vibration on the cooling fan bearing.

The inspectors observed replacement of the fan bearing and inspected the final fan drive belt assem-bly.

WO 95027914-01 was issued to perform troubleshooting associated with an oil leak on the left side cam shaft on the 3A EDG.

The inspectors observed portions of ongoing work in progress.

The inspectors noted that the appropriate work instructions and precau-tions were followed and activities were executed in a meticulous manner.

Members of the licensee's QA organization. were frequently present in the work area and were knowledgeable of ongoing work activities.

The EDG System Engineer and an engineer from the FPL Juno Beach office were also frequently present to provide oversight and assistance for the contrac-tor personnel performing the work activities.

No pr'oblems were noted during the inspectors'bservation of the above work activities.

Conclusions The inspectors concluded that the 3A EDG corrective maintenance activi-ties were satisfactorily completed.

Engineering involvement in the ongoing work activities was very good.

In addition, appropriate work instructions and precautions were followed and activities were executed in a meticulous manne Unit 3 Emer enc Diesel Generator EDG Preventive Maintenance and

~Testin Ins ection Sco e

61726 and 62700 The inspectors observed various preventive maintenance activities associated with the 3A EDG outage.

Observations and Findin s The inspectors observed activities associated with the 3A EDG preventive maintenance as required by Technical Specification 4.8.1.1.2.

The licensee's inspection of the EDG was conducted in accordance with Procedure 3-PHH-022.3, Emergency Diesel Generator 18 Month Preventive Maintenance.

The 18 month PM inspections were accomplished and docu-mented under WO 96011365-01.

The inspections were performed by contrac-tor personnel with assistance from onsite engineering and maintenance groups with offsite support.

Ongoing activities observed by the inspectors included draining and changeout of engine lubricant, flushing and changeout of radiator coolant system, lube oil strainer inspection, engine main lube oil filter inspection, inspection of cooling system including radiator, fan drive belt tensioning, turbo oil filter replace-ment, and soakback oil strainer inspection.

The inspectors noted that licensee QA personnel were present frequently during the maintenance activities.

The EDG inspections did not reveal any notable discrepan-cies requiring further investigation.

The inspectors noted that the appropriate preventive maintenance instructions and precautions were followed.

The EDG engineer from the FPL Juno Beach office was also frequently present to provide oversight and assistance for the contrac-tor personnel performing the work activities.

No problems-were noted during the inspectors'bservation of the above activities.

Conclusions The inspectors concluded that the.3A EDG preventive maintenance and testing activities were satisfactorily completed.

QA,and engineering involvement in the ongoing testing and PMs was very good Unit 3 4160 VAC Switch ear Preventive Maintenance and Testin Ins ection Sco e

62700 The. inspectors observed various preventive maintenance activities associated with the 3A 4160 VAC switchgear outage.

Observations and Findin s The inspectors observed various ongoing preventive maintenance activities associated with the 3A 4160 VAC switchgear outage.

Activities observed included the 18 month PM for cleaning and inspection of electrical switchgear and several other selected work activities.

Additional work activities observed included:

16 WO 96020786-01 was issued to perform required preventive mainte-nance on the 3A Emergency Load Sequencer.

The inspectors observed ongoing activities in Panel 3C23A and noted that activities were conducted in accordance with Procedure.

0-PMI-024. 1, Emergency Bus Load Sequencer 18 Month Maintenance.

RWO 97-017 was issued to perform routine relay calibration using the DOBLE F2350 Test System.

The inspectors observed ongoing over-current relay calibration for relays on the 4160 VAC Intake Cooling Water Pump 3A Breaker 3M19.

The relay calibration activi-ties were performed in accordance with FP8L Protection and Control Group Procedure QTI-5-PS/PTN-2.02.

Turkey Point Plant Instruction for Testing and Independent Verification of Over-current Relays.

RWO 97-015 was issued to perform routine functional checks of trip coils.

The inspectors observed functional checks of breaker trip coils on the 4160 VAC Breakers 3M17, Bus Tie Breaker, 3M15, Breaker'o 3A RHR Pump, and 3M14, Breaker to 3C Load Center.

The breaker trip coil functional checks were performed in accordance with FP&L Protection and Control Group Procedure QTI-5-PS/PTN-2.-

04, Turkey Point Plant Instruction for Testing and Independent Verification of Circuit Breaker Trip Coils.

The inspectors noted that the appropriate work instructions and precautions were followed and activities were executed in a meticulous manner.

No problems were identified during the inspec-tors'bservation of the above work activities.

c.

Conclusions The inspectors concluded that the 3A 4160 VAC switchgear preventive maintenance and testing activities were satisfactorily completed.

Appropriate procedures and precautions were followed.

M1.5 Local Leak Rate Testin LLRT a.

Ins ection Sco e

62700 The inspectors discussed local leak rate testing of containment penetra-tions that was scheduled to be performed on Unit 3 during the outage with the Inservice Test (IST) coordinator and IST supervisor.

Addition-ally. the inspectors observed performance of leak rate testing of selected containment penetrations and reviewed licensee corrective actions associated with one condition report generated as a result of on-going testing.

Observations and Findin s The inspectors held discussions with licensee IST personnel responsible for LLRT testing activities.

The inspectors concluded that the IST coordinator and IST supervisor were knowledgeable and responsive to inspectors questions.

Additionally, the inspectors observed the

I a

e erformance of'LRT testing on Penetration 62A, Containment Pressure ine, and Penetration-65B, ILRT Test Line.

Licensee IST personnel performed the LLRT in accordance with Procedure.

3-0SP-051.5, Local Leak Rate Tests.

No problems were noted with the performance of the leak rate testing observed by the inspectors.

Additionally, the inspectors reviewed the corrective actions associated with the failed LLRT on Penetration 34, Service Air Line.

Penetration 34 had failed to meet the established LLRT acceptance criteria due to excessive leakage during leak rate testing performed on March 6, 1997.

Service Air Check Valve, 3-40-205, had as-found leakage of 155,000 cubic centimeters per minute (cc/min) which exceeded the maximum allowed leakage of 2,000 cc/min.

The licensee documented this fai lure under CR 97-0315.

The inspectors reviewed this CR and held discussions with licensee engineering personnel.

The licensee determined the most likely cause of the LLRT failure was due to internal corrosion of the carbon steel check valve.

Root. cause determination of the failure was still in progress at the end of the inspection period.

The licensee decided to schedule the valve for replacement during the outage.

The inspectors concluded that the licensee had adequately addressed the LLRT failure.

Conclusions LLRT activities observed by the inspectors were performed in an acceptable manner.

The IST coordinator and IST supervisor were knowledgeable 'and responsive to inspectors questions.

Further, the condition report system was appropriately utilized to document failures.

Hain Steam Check Valve Oisassembl and Ins ection a.

Ins ection Sco e

62700 The inspectors observed the portions of the disassembly and inspection of the Unit 3 Main Steam Line B Check Valve, 3-10-005.

Observations and Findin s The inspectors observed portions of ongoing activities associated with WO 96014568-01 which was issued to accomplish the inservice testing and SOER 86-03 inspection of Hain Steam Check Valve,'3-10-005.

These activities were performed in accordance with Procedure O-CMH-072.2, Hain Steam Non-Return Check Valve Repairs.

The site valve component engineer was closely involved in the ongoing activities.

The valve component engineer from the FPL Juno Beach office was also frequently present at the work site to provide oversight and assistance for the personnel performing the disassembly and inspection activities. 'he inspectors observed portions of the ongoing work activities including valve disassembly, removal and inspection of the check valve disk and other internals.

The inspectors noted that most valve internals including the valve disk appeared to be in very good condition.

Two minor scratches were present on the valve disk seating surface which were easily removed.

However, measurements of the rocker shaft revealed excessive

Ml.7 M1. 8

wear and the shaft required replacement.

No problems were identified during observation of the check valve disassembly and inspection activities.

Conclusions The inspectors concluded that the check valve disassembly and inspection activities were satisfactorily completed.

Site and corporate engineering involvement in the ongoing work activity was very good.

Personnel Safet 62707 The inspector reviewed personnel safety practices during the Unit 3 refueling outage.

This included several personnel injuries and associated corrective actions as documented in CR Nos.97-237 and 292.

In these incidents, contract workers were injured during turbine generator work.

One involved the crane and the other involved the high pressure turbine.

Root causes included poor tai lboard meetings, lack of oversight, poor communications, and an apparent lack of worker sensitivity towards safety.

The licensee stopped work and briefed contr actor crews, and provided increased monitoring of contractor activities.

Safety rules and practices were restressed.

Unit 4 Intake Coolin Water ICW Strainer Cleanin 62707 The inspectors observed the mechanical cleaning and inspection of ICW Basket Strainer BS-4-1403.

The journeymen were using the proper procedure, O-PMM-019.7, Intake Cooling Water Basket Strainer Cleaning and Inspection, and were signing off the individual steps.

Ouring the performance of this maintenance activity, operators monitored the ICW flow through the TPCW heat exchangers and the CCW heat exchangers.

The inspectors noted the logging of the values during the cleaning of the strainer.

The inspector concluded that the maintenance was well performed.

Ml.9 Unit 3 Power-0 crated Relief PORV and Valves Testin The licensee tested the Unit 3 PORVs per surveillance procedures.

The PORVs are two-inch, Copes-Vulvan, air -operated, plug valves with an internal cage.

The PORVs have had historical seat leakage problems.

However, none was detected prior to the outage.

The licensee also tested both Unit 3 PORV block valves (MOV-3-535 and 536).

The inspectors reviewed the procedures, PWOs and other related documentation, discussed the testing with licensee personnel, and inspected the valves in the pressurizer cubicle.

The inspectors concluded that test procedure and PWO implementation were appropriat Ml.10 Unit 3 Turbine-Generator Overhaul and Secondar Plant Modifications

~62707 The licensee performed Unit 3 turbine-generator maintenance including high pressure turbine inspections, modifications, and refurbishments, and other related preventive and corrective maintenance activities.

A number of PC/Ms (including 96-61, 96-53 and 95-77) were also completed The inspector reviewed work and selected PC/M packages.

UFSAR Chapter 10, and observed maintenance and modifications in the field.

The inspectors noted excellent supervisory oversight, and positive control of'he turbine heavy load lifting. and rigging activities.

Ml. 11 Unit 3 Reactor Vessel Work 62707 During the Unit'

refueling outage.

the inspectors observed portions of the reactor vessel work including:

reactor head interferences removal and replacement, reactor head detensioning and tensioning, upper internals lifts, cavity seal ring installation and removal, and other related activities.

The inspectors verified that maintenance procedures were being used, that an appropriate level of supervision was present, that operations personnel were cognizant of and appropriately approved those required activities, and that activities were safety conducted.

The inspector reviewed CR No. 97-0362 which addressed an issue with the Unit 3 upper internals connecting pin and lifting tool engagement.

Difficultywas experienced in installing one of'hree lifting screws due to damaged or worn threads.

A special engagement tool and appropriate procedure were developed and used.

Maintenance procedures were revised and Unit 4 applicability will be reviewed for the Fall 1997 outage.

The inspectors concluded that for these observed activities, the licensee was conducting safe and efficient evolutions.

Overall, licensee performance was very good for these vessel related maintenance and testing activities.

CR No. 97-0362 response was appropriate.

Ml.12 Unit 3 Fire Protection Modifications PC/Ms 96-14 and 84 62707 The licensee upgraded thermolag during the Unit 3 refueling outage as follows:

.PC/M 96-14, Thermolag Upgrades in the Unit 3 West Electrical Penetration Room PC/M 96-84, Radiant Energy Shields in Containment The inspector reviewed each PC/M package and observed work in the field.

Work control was appropriat r

H1.13 Reactor Coolant Pum RCP Maintenance 62707 The licensee performed planned maintenance on the 3A 'and 3C RCPs during the outage.

Work scope included pump seal overhauls, motor inspections, and other routine preventive maintenance.

The periodic flywheel inspection as required by TS 4.4. 10 was deferred by NRC letter dated February 11, 1997, approved TS Amendments Nos.

193 and 187.

The inspector observed portions of the RCP maintenance, reviewed procedures and work packages.

and discussed the work with licensee personnel.

The inspector also veri tied that the TS Amendment was appropriately implemented.

The licensee noted that the 3A RCP Number

Seal Runner was out-of-tolerance and required machining.

This may explain the historical low seal leak off flow that was discussed in previous NRC Inspection Reports.

During the 3B RCP pre-start checkout, the motor failed the break-away torque test.

The licensee uncoupled the pump and determined that two internal oil lift lines were severed.

Repairs were effected and the RCP was reassembled.

Subsequent operation was satisfactory.

The inspector concluded that the RCP work was appropriately pertormed.

H2

~

MZ.i Maintenance and Material-Condition of'acilities and Equipment Re airs Followin 4A Control Rod Drive Mechanism Motor Generator CROM

~MG Fi re Ins ection Sco e

62700 The inspectors observed licensee activities associated with repairs following the fire that occurred on March 4, 1997.

The fire had occurred in the 4A CROM HG and resulted in damage to the inboard generator bearing and generator rotor shaft.

Observation and Findin s The inspectors observed portions of the disassembly and reassembly of the 4A CRDH MG along with cleanup activities associated with fire and removal ot fire suppression chemical from various areas in the Cable Spreading Room.

WO 97005677-01 was issued to perform repairs associated with the fire.

The MG disassembly and reassembly activities were accomplished in accordance with Procedure, O-PME-028.3.

CROM HG Set Overhaul.

Work activities observed included electrical determination and retermination of motor, uncoupling and removing motor, heating and removal of HG flywheel, disassembly of'enerator and removal of rotor shaft.

The shaft and inboard MG generator bearing were replaced and the HG reassembled.

Additionally, the damaged bearing was retained for failure analysis to determine cause of the fire.

Root cause determina-tion of the Are was still in progress at the end of the inspection period.

The inspectors noted that licensee QA personnel were present

frequently during the ongoing repair activities.

No problems were noted during observation of the ongoing activities.

Conclusions OA personnel were present frequently during the ongoing repai r activities.

Additionally. the licensee's, corrective actions should be adequate to address the cause of the fire.

M2.2 Main Steam Safet Valve MSSV Activities a.

Ins ection Sco e

62700 The licensee completed set-pressure testing for six main steam safety valved (NSSVs) for Unit 3 on March 1, 1997, immediately prior to starting the refueling outage.

One valve, Hain Steam Line C Safety Valve, RV-3-1412, had failed to lift at the expected pressure during testing.

The as-found set pressure was determined to be 1168 PSIG which was 4.8X above the expected set-point of 1115 PSIG.

The acceptance criteria allows a

3X tolerance band.

Licensee employees had noted that water coming from the tailpipe drain following the lifttest included an unusual amount of corrosion products.

The inspectors reviewed the licensee corrective actions associated with this failure.

~

'bser vation and Findin s The licensee had originally scheduled four out of a total of 12 Unit 3 HSSVs for lifttesting.

As the result of this failure, the licensee immediately declared the NSSV inoperable and reactor power was reduced to less than 53K in accordance with TS 3.7.1.1.

Additionally, two more MSSVs were tested (total of six HSSYs tested)

in accordance with Procedure, 0-ADH-502. In-Service Testing Program, and ASME ON-1987. Part 1. Step 2.1.4.2.

The ASME Code and the licensee's program require that should any valve fai 1 to satisfy its acceptance criteria that two additional valves are tested for each valve failure.

None of the other five NSSVs tested failed to satisfy their acceptance criteria.

The inspectors reviewed CR 97-273 which documented the licensee's corrective actions associated with failure of HSSV RV-3-1412 to meet requi red lift pressure set-point.

The inspectors noted that licensee corrective actions included overhaul of the affected HSSV and inspection of'alve internals for any evidence that might have caused the valve to have not lifted at the expected pressure.

Corrective actions also included drainline inspections on all NSSV tailpipes to determine if excessive corrosion products might be present which might affect the normal operation of the safety valves.

Additionally, two other HSSVs, RV-3-1403 and RV-3-1407, which had been previously scheduled for overhaul due to minor leakage were also scheduled for similar inspec-tions of valve internals.

The inspectors observed the disassembly and inspection of valve inter-nals for NSSV RV-3-1412.

No problems were noted during the valve

H2.3

disassembly and inspection.

Additionally, the inspectors noted that the valve tailpipe appeared free of debris or corrosion products that could have been a possible contributing factor to this failure.

Root cause determination of the failure was still in progress at the end of the inspection period.

Conclusions The inspectors concluded that the NSSV disassembly and inspection was

. performed in an acceptable manner'.

Additionally. the 'licensee's corrective action process was appropriately used to.address this issue.

Corrosion Pi in of Penetration

B and C

Ins ection Sco e

62707 During the local leak rate testing (LLRT) of several containment penetrations for Unit 3. the inspector noted considerable corrosion (rusting)

on one of lines exiting penetrations

B and C.

A review was made of the disposition of the Condition Report (CR) No.97-408.

Observations and Findin s The.inspectors reviewed the CR on this subject.

The inspector noted that these three-'fourths inch diameter lines were used as sensing lines for monitoring containment conditions during integrated leak rate testing ( ILRT) testing.

The corrosion on these Unit 3 lines was located between the penetrations and the outside isolation valves.

The pipes were ground and an ultra-sonic test (UT) meter used to measure the wall thicknesses.

The thinnest wall measured was 0. 110 inch.

The minimum wall thickness was 0.099 inch; therefore.

no operability problem was noted.

The similar penetrations on Unit 4 did not exhibit the same problem.

A similar corrosion problem was repai red by.recoating on June 12.

1996.

A review of the work package indicated that the correct coating proce-dure (SPEC-C-004)

was used for the repair

.

The presence of considerable rusting in such a short period of time raises a question on the surface preparation for the previous recoating.

The inspectors'questioned the licensee about previous opportunities for discovering these corrosion conditions.

A monthly surveillance described in procedure 3-0SP-053.4.

Containment Integrity Penetration Alignment Verification, required operations pers'onnel to verify the valve positions by visual inspection at the valve's location.

The presence of the corrosion on the piping was easily distinguished by the inspectors in the vicinity of the valve.

Records for the last three months indicated that the surveillance had been performed:

however, no abnormalities were detected.

This lack of a questioning attitude by the non-licensed operations personnel to identify corrosion on the lines during the surveillance was identified as a weakness.

S

p J

~

c M2.4 M2.5

M2.6

Conclusions A weakness was identified because the non-licensed operations personnel missed several opportunities to identify corroding piping during monthly surveillances on penetration alignment verification for containment

'ntegrity.

Unit 3 Motor 0 crated Valve HOV Testin 61726 and 62707 The inspector reviewed the scope of MOV related activities scheduled for the Unit 3 Cycle 16 refueling outage.

The licensee performed MOV testing, differential pressure tests, MOV overhauls.

grease inspections, and preventative maintenance inspections.

The inspector received and discussed several condition reports that were generated as a result of these MOV activities, The inspector concluded that the MOV coordinator/responsible engineer was knowledgeable and maintained cognizance and ownership of the MOV related activities ongoing during this outage.

Unit 3 Steam Generator Ins ection and Cleanin Activities 62707 Ouring the current Unit 3 refueling outage, the licensee performed inspections, tube plug replacements and secondary side sludge lancing associated with all three steam generators.

This included involvement among FPL corporate. site, and contractor organizations.

In addition, a

number "alloy 600" Westinghouse mechanical tube plugs were replaced due to industry problems.

This was performed as required by an NRC commit-ment.

Steam generator inspections and associated activities were performed in accordance with approved program plans.

The chemistry department retained overall responsibility for this steam generator work.

The inspectors observed a sampling of the above mentioned activities including field work, data retrieval, and assessment.

Inspection procedures were also reviewed.

and personnel involved in the steam generator activities were interviewed.

The inspectors also reviewed UFSAR Chapter 4.2.

4B and 4C.

The inspectors concluded that the licensee's engineering and chemistry personnel were effectively involved in all phases of these activities.

Strong secondary chemistry programs and controls have resulted in minimal pluggable steam generator tubes (section M2.9).

Unit 3 Flow-Accelerated Corrosion Testin 62707 The inspectors reviewed and discussed the flow-accelerated corrosion inspection plan for the Unit 3 outage.

Highlights of the inspection plan included continued augmented safety related feedwater inspection.

inspection of 50 percent of the turbine crossunder piping, 100 percent of the moisture separator/reheaters, inspection of one steam tr ap header, and a sampling of non-isolable small bore piping.

Some of the Condition Reports concerning the inspection and replacement of some of

the piping were reviewed and were also discussed with the licensee's program manager.

Several of the inspection areas were walked down by the inspector.

No roblems were identified, and the inspectors concluded that the licensee as an effective flow-accelerated corrosion program.

Unit 3 Inservice Ins ection ISI Ins ection Sco e

IP 73753 The inspector reviewed program plans.

procedures, and documentation related to the conduct of the ISI program during the Spring 1997, Unit 3 Outage.

Observations and Findin s Pressure Boundar ISI At the time of the inspection, the ISI examinations planned for this outage had been essentially completed, therefore the inspection focussed on the ISI plan and the documentation of the results.

The inspector partially reviewed ISI-PTN-3/4-Program, Rev 1. dated August 9, 1995.

"Third Ten-Year Inservice inspection Program for Turkey Point Nuclear Power Plants U3 & U4."

The thi rd, ten-year ISI interval for Turkey Point Unit 3 started on February 22, 1994.

The second inspection period of this interval started on February 22, 1997. therefore this refueling outage was the first outage of the second inspection period.

The code of record for the third, ten-year ISI interval is the ASHE B&PV Code Section XI, 1989 edition.

The inspector reviewed the documentation for visual, surface, and volumetric examinations that were conducted during the Spring 1997 refueling outage.

Records reviewed in detail included the following:

~Com onent Examination Comment Valve, LCV-3-460 14" -RHR-2301-9 Pipe to Elbow 14" -RHR-2301-10 Elbow to Pipe 14"-RHR-2301-11 Pipe to Elbow VT-2 UT-45 UT-60. UT-70 UT-45 UT-60, UT-70 UT-45 UT-60 3/8/97 - Accumulation of boric acid at packing and bolting'NRI)

No recordable Indica-tions, Root Geometry, Limited Volume from elbow side due to configuration NRI Root Geometry NRI Root Geometry

~Com anent Examination Comment 14" -RHR-2301-18 UT-45 Valve 3-752A to Pipe UT-60, UT-70 14"-RHR-2301-24 UT-45, UT-60, Pipe to pump casing UT-70 NRI Root Geometry.

No exam from weld or from valve side Root Geometry.

No exam from pump side.

The inspector also reviewed two condition reports involving the ISI

. rogram.

Condition Report 97-0429 documented that inspection of several ocations of Class 1 Bolting during the system overpressure test would be unsafe.

The Condition Report was written to identify a communica-tion/engineering problem in that the licensee had not requested approval for the use of ASME Code Case N-533 at Turkey Point.

(Code Case N-533 allows for the inspection of pressure boundary bolting while the system is depressurized, and had been requested for and approved for use at the licensee's St Lucie plants.)

Condition Report 97-0479 documented

,unacceptable indications found during liquid penetrant examination ot an integrally welded support on RHR heat exchanger A.

Condition Report 97-0429 resolution included discussions with NRR; submittal of request for approval to use Code Case N-533; inspection of bolting in accordance with N-533:

and contingency plans in the case that the request was not granted prior to the end of the outage.

The engineering groups involved were also counseled about the need to take ownership of issues that require NRC approval.

Condition Report 97-0479 was resolved by exploring the unacceptable indication until it was determined that it was the result of a fabrication defect instead of a service induced flaw, and then applying ASME Section XI fracture mechanics resolutions to allow it to stay in service without repai r.

Containment ISI Effective September 9,

1996,

CFR. 50.55a, was amended to include the requi rements of ASME 88PV Code,Section XI, Subsections IWE and IWL 1992 Edition, with 1992 Addenda.

Subsections IWE and IWL provide ISI requirements for concrete containments

~ steel containments, and steel liners for concrete containments.

The amendment to the rule provided a

five-year period, until September 9, 2001, before full implementation of Subsections IWE and IWL.

In correspondence with'he industry, (November 6,

1996 letter to Alex Marion, Nuclear Energy Institute from Gus Lainas, Office of Nuclear Reactor Regulation, concerning

"Implementation of Containment Inspection Rule" )

NRC provided a Staff position that, in response to deficiencies noted prior to the full implementation IWE and IWL, repair'and replacement activities must be conducted in accordance with those subsection On September 3,

1996. the licensee started the 25-year inspection of the Unit 3 containment tendons as requi red by the Technical Specifications.

The inspector discussed the results of the tendon inspections with the licensee's Lead Civil Engineer, to determine if the licensee was aware of the new requirements of 10CFR50.55a for repairs and replacements.

The licensee had documented the change to 10CFR50.55a in the tendon surveillance procedure with a note to the effect that the new require-ments would be implemented during the 30-year inspection of the tendons.

The licensee also showed the inspector documentation for a tendon anchor-head shim replacement for Buttress g3, tendon 35-H-20, due to a

"cracked shim" (which turned out not to be cracked after removal and

'examination;)

as well as anchor-head shim additions for five tendons which had shown low tension during "lift-off"tests.

The application of ASME "Repair and Replacement" considerations will be addressed in the licensee's final report of the Tendon Surveillance.

Conclusions The licensee's ISI activities were well documented.

and appeared to be representative of good, close coordination between corporate, site, and contractor activities.

The only noted exception being the late recogni-tion that permission to use ASME Code Case N-533 had not been requested due to mis-communication between licensee organizations.

Containment surveillance procedures had documented acknowledgement of recent changes to NRC regulations.

Hi h Head Safet In ection HHSI Re air 62707 On March 27, 1997, Unit 4 HHSI 4A pump developed two pump casing flange leaks.

When the licensee retorqued the studs one of the leaks increased to approximately nine to ten gallons per hour.

Engineering calculated that this leak rate was in excess of conservative assumptions for emergency core cooling system (ECCS) recirculation loop leakage assumed in the UFSAR for meeting the requirements of 10 CFR Part 100.

The licensee declared the pump inoperable.

entered a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and made a one hour ENS call.

The pump was isolated and a decision was made to inject a sealant compound (Furmanite) into one of the casing stud cap nuts.

The repair took three attempts to seal the cap nuts and stop the leak.

The inspectors reviewed Condition Report No.97-613, reviewed the Furmanite procedure, and observed the work in progress.

There was excellent engineering support for maintenance on this repair.

The leak reoccurred on April 3.

1997, and the licensee made another ENS call and initiated permanent repairs.

These repairs were completed on April 5, 1997.

The LER will be reviewed in a future inspectio g

Unit 3 Steam Generator SG Ins ection Ins ection Sco e

50002 Through discussions with personnel and review of documentation, the inspector reviewed the Eddy Current (ET) inspection of the Unit 3 SGs.

Observations and Findin s The Unit 3 SGs are Westinghouse replacement Model 51F SGs which were installed in 1982.

The Model 51F SGs contain thermally treated Inconel 600 tubing which is supported by stainless steel, quatrefoil support plates.

To date, the primary reason for plugging of tubes in the Unit 3 SGs has been because of wall thinning in the area of anti-vibration bars (AVBs).

During the current inspection.

two tubes in SG 3B were preventively plugged due to a foreign object lodged against the outer diameter (OD) of the tubes.

(The foreign object had been determined to be a piece of metallic slag formed during arc-cutting of weld prep areas on the SG shell, and introduced during the replacement operations in 1982.)

The inspector reviewed a sample of the Eddy Current (ET) test data representative of SG tubes which were left in service with indications which had been diagnosed as MBM Manufacturing Buff Marks by ET,analysts.

The inspector reviewed the ET Bobbin Coil data recorded this outage, and compared it with data that was recorded during the 1994 refueling outage.

In two of the cases reviewed, the 1994 examination results had been dispositioned as No Detectable Defect, (NDD) while the 1997 data was dispositioned as having MBMs.

The inspector noted that in both cases, the MBM signals recorded in 1997 were present in the 1994 data, at the same location, and with essentially the same signal strength.

Apparently, in 1994 the ET analysts determined that these signals did not represent flaws and dispositioned the tubes as NDD.

The inspector also reviewed the test data from a tube which, during the 1997 outage, had wear signals recorded at three AVB locations: AVl-15X, AV2, - 20K, and AV3 - 13K through-wall.

The 1994 data for this tube was also reviewed, which showed that the signals at AV1 and AV3 were not present; but that the signal at AV2 was present, at essentially the same relative size, during the inspection in 1994.

Conclusions The licensee's program for inspection of SGs appeared to be well managed.

The documentation of inspection results was more conservative during the current outage than it had been in the pas J

Haintenance Staff Training and gualification Trainin and uglification of Welders Ins ection Sco e

62707 The inspectors reviewed and observed the qualification and testing of welders that were brought to the Turkey Point plant for the refueling outage on Unit 3.

Observations and Findin s The licensee had approximately 105 welders to qualify for the Unit 3 outage.

A review was made of parts of ASNE Code Section IX, and procedure O-ADN-046, Control of Welding Special Processes, to ensure that the method used for qualifying the welders met the ASHE Code.

The inspectors determined that the licensee's procedure was compatible with the Code requirements.

The inspectors observed activities in the welder qualification shop, and discussed the requirements and techniques for qualification with the welding personnel performing the work.

The inspector noted that the qualifiers required the identification of the welder, properly controlled and marked weld test coupons, and performing fit up and visual inspections of the finished weld.

The inspectors observed the actual testing on one set of weld bend specimens and the evaluation of a minor linear indication.

The previous day the welding evaluator had failed six out of 14 welder qualifications.

Some of the failed bend specimens and some that had passed were visually examined by the inspector for Code compliance.

The qualification logs and records were adequately explained by the qualification personnel.

The welding engineer performing the qualifications had experience in this area dating back to 1981 and was able to answer all of inspectors'uestions correctly.

A quality surveillance (Ouality Report No. 97-0050)

was performed by the Nuclear Assurance Group over a two day period after the inspectors evaluated the welder qualification area.

The results of this surveillance were that the welder qualification tests were being properly conducted.

In addition, the inspectors briefly observed a few of the welding repai rs and modifications made by some of these welders including weld metal control.

The inspectors reviewed two CRs (Nos.

97-0441 and 97-0488) which raised a possible problem with weld metal control.

Turkey Point personnel did not realize that a St. Lucie heat code was on the welding rod issued for several jobs.

Further investigation cleared up the confusion and the issue of the weld rod had been correctly per-formed.

The inspectors did not identify any welding problem Conclusions The inspectors concluded that the welder qualifications wer e being properly conducted and that the personnel conducting these tests were experienced and capable.

Quality Assurance in Maintenance Activities Stora e of Safet Related Pi in 62707 During a tour of an outside storage area, the inspector noted the absence of protective pipe caps on some piping in an enclosed pipe lay down area.

The inspector requested Quality Control (QC) to determine if the piping was safety related, and to determine if the storage met regulatory requirements.

The inspector reviewed CR No.97-236 that was generated by the QC inspector and then toured the storage area with the QC inspector to examine the stored piping.

Fifteen heat codes with thi rty three pieces of pipe that were safety related were identified as not being stored to the requirement of American National Standards Institute (ANSI) 45.2.2 level D storage, i.e. all openings into items shall be capped, plugged.

and sealed.

Document

CFR Part 50 Appendix 8 Criterion XIII, states in part that measures shall be established to control the handling. storage, shipping, cleaning, and preservation of material... in accordance with work and inspection instructions to prevent damage or deterioration...

Methods for implementing this requirement are in Regulatory Guide 1.38 which endorses ANSI 45.2.2.

The licensee commits to these requirements in their Topical Quality Assurance Report Appendix C.

The implementing procedure is Quality Instructions QI13-PTN-1, Handling, Storage, and Shipping of Items. This failure to proper ly store safety related piping to the requirement of ANSI 45.2.2 constitutes a violation of minor significance and is being treated as a Non-Cited Violation, consistent with Section IV of the NRC Enforcement Policy.

The CR concluded that ANSI No. 45.2.2 storage requirements were not being met.

The licensee is not storing some of thei r safety related piping to the requirements of ANSI 45.2.2.

The condition was identified as NCV 250

'51/97-03-02, Failure to Store Safety Related Piping to ANSI Standards.

The NCV was closed.

Licensee Self Assessment Ins ection Sco e

62702 The inspectors reviewed the licensee report which documented the results of a self-assessment recently performed by the Maintenance Department on January 6 - 10, 1997. This self assessment was in the area of Work Coordination.

The inspectors also held discussions with the Maintenance Manage and other licensee managemen 'L r

Observations and Findin s

III.

E2 E2.1 During the review of this assessment the inspectors noted that although no CRs were initiated by the licensee, several recommended areas for improvement were identified during the assessment.

Areas for improvement were generally associated with fai lures to satisfy management expectations, and included lack of coordination of 2 outage multi-discipline activities, ineffective utilization of maintenance resources, HP support of ongoing maintenance activities. clearance scheduling and coordination. availability of replacement parts, and pre-review of WO packages.

Maintenance management was reviewing the recommended areas for improvement for possible methods of disposition.

Conclusions The team concluded that the licensee's recent self-assessment provided significant and meaningful feedback to management.

En ineerin Engineering Support of Facilities and Equipment Unit 4 Boric Acid Leak Ins ection Sco e

37551 The licensee noted that a boric acid buildup was found on the flange of Unit 4 boric acid to blender flow transmitter (FT-4-113).

The licensee's root cause and operab'i lity determinations for this problem were examined by the inspectors.

Observations and Findin s The inspector and the system engineer observed a

QC technician performing a dye penetrant inspection of the flange and adjacent pipe.

Several linear indications were found on the flange and one on the pipe.

This test was requested because boric acid buildup was noted on the flange during an 18 month visual inspection required by a corrective action to a previous Condition Report (CR).

This leakage appears to be related to the previous discovery of stress corrosion cracking (SCC)

found on various sections of the CVCS boric acid system after removal of thermal insulation and heat tracing.

A review was made of Metallurgical Laboratory report No.95-111 which analyzed the root cause for some of the previous leakage in this system.

The inspector noted that the SCC was the reason for the cracking in the stainless steel 304 fittings and piping.

Condition Report No. 97-0213 was generated for this issue.

The inspectors reviewed the operability assessment and corrective actions.

The flange and related piping will be replaced during the next Unit 4 refueling outage (September 1997).

The flange indications will be periodically monitored by engineering, operations, and Q ~

c.

E2.2 E2.3 Conclusions Engineering support to maintenance was good in resolving the'resence of a leak on a flange in a safety related system.

The root cause analysis, the'operability assessment.

and the corrective actions were appropriate.

Turke Point Unit 3 C cle 16 Reload PC/M No.96-71 37551 The licensee initiated PC/M No. 96-71 for the Unit 3 Cycle 16 core reload.

This PC/M provided for the reload core design and included the replacement of.irradiated assemblies with new 15 x 15 optimized fuel assemblies.

The new assemblies were of the debris resistant design which included several fuel design enhancements.

These were similar to

'he recent previous reload designs.

The inspectors reviewed the documentation package for the PC/M including the design bases and analyses.

the safety evaluation, core loading plan, and other pertinent data.

The inspectors noted that appropriate reviews and approvals were performed by Engineering.

Reactor Engineering, QC, and the PNSC.

The inspectors concluded that PC/M was well documented and adequately implemented by'efueling procedures as discussed in section 01.4 of this report.

Unit 3 Boron In ection Tank BIT Modification PC/M 96-12 37551 The licensee modified the Unit 3 HHSI system piping, such that the BIT was bypassed.

During removal of the boric acid system abandoned heat tracing/insulation, multiple through wall leaks were noted (see NRC

Inspection Report

Nos. 50-250,251/95-04,

06,

and 09).

These defects

were caused

by stress

cracking corrosion

and were all repaired.

The

licensee

concluded that the BIT piping was also subject to this failure

mechanism.

Thus, the decision

was

made to bypass the BIT piping and

abandon the BIT in place.

The BIT function with highly concentrated

boric acid was

removed

from service in the 1980's.

The inspector

verified this as described in the

UFSAR section 6.2 and associated

drawings.

PC/M 96-12 removed the BIT instrumentation

and relocated

one relief

valve.

In addition. the inlet valves

(MOV-3-867A and

B) were eliminated

and replaced

by one manual

valve (3-867).

The

MOV function had been

previously removed.

The SI function remained

unchanged,

included

HHSI

valves

(MOV-3-843A and B), and associated

controls, including the inter

disc equalization function.

A similar PC/M (No.95-172)

was performed

on Unit 4 during the Spring

1996 outage.

The inspector

reviewed the

PC/M package,

including the

CFR 50.59

evaluation,

and other related drawings

and documentation.

The inspector

discussed

the

PC/M with engineering,

operations,

and maintenance

personnel,

including the system engineer.

The inspector witnessed

portions of PC/M in the field, including testing.

Operator training was

addressed

through

a training bulletin.

The inspector concluded the

PC/M

was appropriately

implemente t

l

Unit 3 Intake Coolin

and Turbine Plant Coolin

Water'odifications

PC/Ms-96-49

96-94 and 96-10

37551

The licensee

abandoned

the Unit 3

ICW to TPCW heat exchangers

outlet

valve (CV-3-2201) per

PC/H 96-10.

The valve has histo'rically not

functioned well and was previously bypassed

per

a safety evaluation.

A

spool piece

was put in place of the

CV in parallel to a locked-open

manual

bypass

valve.

A similar PC/M was performed

on Unit 4 last outage

(March 1996).

In addition,

PC/M 96-49 modified the

TPCW valves CV-3-

2200 and 2203.

These are for the turbine lube oil and hydrogen

gas

coolers.

PC/M 96-94 installed flow instrumentation

on the Unit 3

ICW

headers.

The inspector verified that

UFSAR section 9.6 for the

ICW system

was

being revised to reflect these

PC/Ms.

The inspector also reviewed the

PC/M packages.

procedure

changes,

safety evaluations,

drawings, training

briefs,

and other related documentation.

The PC/M was discussed

with

engineering

and operations

personnel.

In addition, portions of the work

were observed in the field.

The inspector concluded that the

PC/Ms were appropriately

implemented.

Intake Structure

Ins ection

37551

The inspector

reviewed the licensee's

program plan for the Unit 3 and

Unit 4 intake structure inspections.

Historical degradation

'due to the

salt water corrosion

and erosion

was noted during the mid 1980's.

Since

then, the licensee

embarked

on an inspection

and repair program.

These

activities were reviewed in previous

NRC Inspection Reports.

The inspector noted that the licensee controls intake inspection/repair

activities per Speci,fication

No. CM-2.28, Nuclear Engineering

Intake

Structure Inspection

and Repair.

No inspections

or repair activities

were scheduled for the 1997 Unit 3 or Unit 4 outages.

The next

activities are scheduled for Unit 3 Cycle 17 (Fall 1998).and Unit 4

Cycle 18 (Spring 1999).

The inspector verif'ied that these future

activities were budgeted

and approved

by the

PRB,

and were on the "Top

20" modification lists.

In addition. engineering

evaluation

PTN-ENG-

SECS-96-043'.

was also reviewed.

The inspector concluded that the licensee's

program and controls for the

intake structure periodic inspections

and repairs were appropriate,

and

indicated

good engineering

involvement.

Engineering

Procedures

and Documentation

Generic Letter

GL 96-01

Res

onse

37551

GL 96-01 required the licensee to review their testing of safety related

circuits to assure

TS compliance,

and to verify that systems

would

function when called upon.

These actions were required to be complete

for Unit 3 prior to the restart

from the Cycle 16 refueling outag e

E3.2

The licensee identified three instances

of non-compliance.

which was

reported to the

NRC in LER No. 96-04 and subsequent

supplements.

These

issues

were reviewed in previous

NRC Inspection Reports.

The licensee

completed thei r review per the GL, and documented this in safety

evaluation

No. JPN-PTN-SEIS-97-001.

The

PNSC reviewed

and approved the

safety evaluation

on March 18,

1997.

The inspector

reviewed the safety evaluation,

attended

the

PNSC meeting,

and discussed this issue with engineering

personnel.

Final

NRC review

and closeout of the

GL will be documented

in future correspondence.

Re orts

90712

90713

and 92700

The inspectors

reviewed the monthly operating reports for January

and

February

1997,

and

LER 97-021 (section 01.3).

The reports were timely

and well written.

IV. Plant

Su

ort

R1

~

Rl.l

Radiological Protection

and Chemistry

(RPEC) Controls

The purpose of this inspection effort was to evaluate radiological

protection program effectiveness

during outage conditions.

External

Ex osure Controls

Ins ection Sco

e

83750

The adequacy of radiation protection controls in containment

were

reviewed.

Observations

and Findin s

The review included performance of independent

radiation surveys,

review

of radiological boundaries

and postings,

checks

on security of high

radiation areas.

reviews of records

and procedures,

and observations

of

work activities in progress.

The inspector

observed interactions of

radiation workers

and Health Physics

(HPs) technicians

in containment

and conducted interviews with Turkey Point and contract personnel

concerning

adequacy of radiation protection controls.

The licensee did not have

a

HP control area inside the containment

building but did station

HPs in containment to monitor work and assist

radiation workers

as needed.

Personnel

entering containment

were

provided Radiation

Work Permit

(RWP) briefings and any special

dosimetry

needed in the

HP building.

HPs could control work in high radiation

areas

from the

HP building. observing activities with video monitoring

equipment,

communicating

and directing workers with radio headsets,

and

monitoring individual radiation doses with teledosimetry

on the

radiation workers'he

licensee

was making good use of radio head sets

for communications

between the roving HPs in containment

and the

HPs in

the

HP bui lding.

Use of technology in monitoring and controlling work

in high radiation areas

from low dose areas

was

a radiation protection

program strength.

The air conditioning of containment

made the envi ronment safer

as

temperatures

were comfortable.

The air conditioning helped

keep

protective clothing dry which helped

reduce contamination

leaching

problems

and lower personnel

contaminations.

In interviews with

radiation workers, the inspector inqui red about working conditions

inside containment

and the adequacy of radiation protection support.

Specifically were breaks outside containment sufficient and was

HP

support available when needed.

Workers reported that they were able to

take breaks

when needed

and that they had not had any problems getting

HP support.

Licensee

procedures

O-HPT-013,

"Portable Survey Instruments," revision

dated

November 2,

1994, provided specifications

and operational

instructions for HP portable survey instruments.

Section 9.2,

"Heter

Checkout

and Use," stated,

in part. that the

HP technician shall

choose

an instrument that will detect the expected

type and range of radiation

and or radioactivity.

Additionally, step 9.2.4 requires the technician

ensure the instrument being used

has

been daily response

checked for

that date by checking the date

on the response

check sticker attached to

the instrument.

On Harch 25.

1997, the inspector noticed that the licensee

was using

a

portable thin window Geiger Huller

(GN) count rate contamination

monitor

on the refueling floor that had not been source

checked since Harch 5,

1997.

The instrument

had

"For Information Only" written across

the

daily response

check chart attached to the monitor

.

The background

where the instrument

was utilized was approximately 1,200 - 1,400 counts

per minute (cpm).

The inspector observed

HP technicians

using the

monitor to obtain contamination levels

on items being

removed from the

reactor

cavity.

Licensee

procedures

required

a daily source

check of

the radiation survey instruments.

The inspector

asked

why the

instruments

were not being response

checked daily and licensee

personnel

reported that they did not believe the source

check was necessary

since

the instruments

were used in high background

areas

and were not utilized

to measure

radioactive contamination for "official surveys"

or release

purposes.

The inspector

found that the licensee's

procedures

did not

address

"For Information Only" portable radiation survey instruments.

The procedures

did not address

requirements,

limitations, or the method

to distinguish

"For Information Only" instruments

from other

instrumentation.

The licensee

also did not have

any training describing

proper

and improper uses of such instrumentation.

The inspector

reported that failure to response

check the monitors in containment

daily appeared to be

a violation of licensee

procedures.

This is being

treated

as

a minor violation per Section

IV of the

NRC Enforcement

Policy.

NCV 50-250.251/97-03-03,

Failure to perform daily response

checks

on radiation monitoring equipment in accordance

with licensee

procedure

requirements

was close I

The licensee

reported that the procedures

would be modified to permit

the'use of the friskers without a daily source

check.

The inspectors

were unable to find radiation surveys

where the instrument

had been

used

to quantify radioactive contamination levels.

While response

checks

can

be used to determine efficiency of an instrument,

one of the purposes

is

to look for changes

in monitor performance

and to verify that the

detector

and ratemeter

were still operating properly.

The licensee's

persistence

to use

an instrument that was not receiving daily Quality

Control

(QC) checks,

for any monitoring purpose,

was imprudent.

Licensee

procedure

0-ADM-605. "Control of Radioactive Tools,

Equipment,

and Components,"

revision dated

December

31,

1996, required in step

5.9.1, that tools and equipment designated

for use only on the

RCA shall

be conspicuously

painted with purple paint.

While observing work in upper

containment

on March 26,

1997. the

inspectors

examined contents of'ool boxes.

The tool boxes contained

hundreds of various small tools used for refuel floor work during

outages.

The inspectors

found that most of the tools were painted

purple.

However,

a significant number (approximately

20 - 40 percent)

were not painted purple as required

by licensee

procedures.

The

inspector reported that failure to paint tools used for work in the

RCA

purple appeared to be

a violation of licensee

procedures.

Subsequently,

the licensee

presented

documents to the resident inspectors to

demonstrate

that they had already identified this matter

and that

corrective action was in process to be completed 4/15/97.

This matter

will be treated

as

an inspector followup item IFI 50/250.

251/97-03-04.

Failure to conspicuously identify tools used in RCA in accordance

with

licensee

procedure

requirements.

The inspectors identified other examples of poor attention to detail.

For example.

the licensee

had established

a radiation control boundary

around the reactor

cavity and the equipment

pool

as

a high radiation

and

hot particle area.

The licensee

had

removed that zone

and established

a

smaller one at the top of the personnel

ladder into the equipment

and

reactor cavity.

While surveying the refuel floor area,

the inspectors

found one of the signs f'r the previous

zone still hanging

on

a guard

rai'1

and another

propped

up against

a guard rail post.

The inspector

reported

th'e posting discrepancy to a

HP on the refuel floor who

promptly removed the signs.

The licensee

had established

a radioactive materials storage

area in

containment that was used to store trash until it could be removed from

containment.

The inspectors

found bags of trash bulging out of zone

with some bags outside the boundary

on the floor and hanging over the

boundary ribbon.

The materials. boundary could have

been easily extended

such that all material

was within the radioactive materials

area.

This

was pointed out to a

HP technician

and all of the material

on and

outside the boundary

was moved back into the storage

are r

Concl us ion

In general,

the inspectors

found adequate

radiation protection control

measures

in place inside Unit 3 Containment Building.

Good use of

remote monitoring technology to save collective dose

was

a program

strength.

However,

a non-cited violation was identified and other

observations

indicated poor attention to detail.

Ins ection of Plant Areas

Ins ection Sco

e

83750

The inspectors

toured plant areas for radiation protection issues

Observations

and Findin s

On tours within the

RCA, the inspectors

made independent

radiation

surveys,

examined the adequacy of the licensee's

radiation protection

boundaries

and radiological postings,

examined labeling of containers,

verified radiation monitoring equipment in use was calibrated

and

receiving periodic source

checks,

checked the security of high radiation

area doors,

observed

housekeeping,

observed radiation worker compliance

with radiation protection controls.

obser yed

HP technicians

performing

radiation surveys.

and.interviewed radiation workers.

The inspectors

made independent

radiation surveys in the

RCA including

the auxiliary building, dry storage faci lity, yard areas within the

RCA.

Radiation surveys

were also

made outside the

RCA in the turbine

building, warehouses,

yard,

and

RCA boundary.

Conclusion

Radiation

and high radiation areas

were properly posted

and secured.

Control of radioactive material in the

RCA was adequate

and no

radioactive material

was found in areas

outside the licensee's

RCA.

As Low As Reasonabl

Achievable

ALARA

Ins ection Sco

e

83750

The inspectors

interviewed licensee

personnel

and reviewed records of

ALARA program results

and activities to determine whether the ALARA

program was effective in maintaining doses

ALAR ~

b.

C.

Observations

and Findin s

The 1996 site collective dose

was approximately 186.0 person-rem of 275

person-rem objective'and

was the site's

lowest operating

exposure.

The

Unit 4 Re-Fueling

Outage

(RFO) in 1996 was

35 days in length

and the

total collective dose

was approximately 158.0 person-rem.

The outage

goal

was 215 person-rem.

The licensee attributed the 1996 successes

rimarily to effective scheduling,

pre-job planning,

department

man-rem

udget program,

and increased

plant involvement and accountability.

Non-outage

dose

was approximately 27.7 person-rem.

Short notice outage

dose

was approximately 0.3 person-rem.

In 1996 the licensee cut outage

dose

by approximately

16 person-rem

and non-outage

dose

by about

person-rem

from the doses in 1995. which was also

a year with a single

.

35 day

RFO.

To increase

the plant staff's involvement in dose reduction activities,

the licensee

implemented

an ALARA dose budget process

in 1995.

The

process allotted dose to various work groups depending

upon their

assigned

responsibilities.

Managers of the various departments

of the

site organization

were expected to complete assignments

without

exceeding allotted doses.

The dose budget

was similar to their

financial budgets.

This caused

managers to plan tasks better or face

the possibility of exhausting

dose allotments

and failure to meet

assigned

goals.

One of the most important elements

in the program was

the strong

upper

management

support

and involvement in the process.

The

people responsible

for the work were caused to perform it more

efficiently and,

as

a result,

reduce

dose.

The licensee

planned to

improve the process further through additional

involvement of personnel

at lower levels within the organization.

The personnel

experienced

in

performing the various tasks in radiation areas

know how.to perform the

work more efficiently that anyone else.

The licensee

plans to have

those personnel

more involved in processes

to lower their radiation

doses.

The licensee

had two RFOs planned for 1997.

The most recent years

having two RFOs were 1991

and 1994.

The licensee

had 939 and 474

person-rem f'r those years respectively.

The 1997 goal

was 475 person-

rem with 165 person-rem allotted for each

RFO.

The licensee

had

expended,

159 person-rem of the

165 person-rem Unit 3 goal through day

40 of the planned

35 RFO.

Another licensee

goal

was

110 person-rem/unit

3 year average.

Evidence of site management

involvement with ALARA was

observed in the 1997

ALARA plan that also included individual department

ALARA plans.

Conclusion

The licensee's

ALARA activities in 1996 were very good and the licensee

continued to be successful

in reducing the site collective doses in

1997.

The inspector

found the licensee's

ALARA successes

were due to

several

factors including strong

management

support,

improved

participation of plant staff'n implementing the ALARA dose budget,

and

shorter refueling outages.

The licensee

had

a very good program for'

R1.4

establishing

and tracking performance related to ALARA goals

and

objectives.

Vehicle Surve

s

a.

Ins ection Sco

e

83750

Independent

radiation surveys of a loaded exclusive

use vehicle were

made to evaluate the licensee's ability to identify highest

dose rates

on the vehicle and to verify the dose rates

were within regulatory

limits.

Observations

and Findin s

'L

The inspectors

made independent

radiation surveys

on an exclusive use

vehicle just prior to its release

from the site.

The inspectors

found

that the radiation levels identified by the licensee's

HP technician

agreed with the inspector's

and were within regulatory limits for

transportation of radioactive materials

by an exclusive

use vehicle.

The

HP technician performing the survey was thorough

and completed the

survey in accordance with licensee

procedures.

Conclusion

The licensee radiation surveys of an exclusive use vehicle were thorough

and all dose rates

were below applicable regulatory limits.

R1.5

a.

Unit 3 Fuel Transfer

Canal

Radiation Surve

s

Ins ection Sco

e

83750

This area

was reviewed to determine whether the licensee

was properly

evaluating plant radiation levels during the transfer of spent fuel from

the reactor to the Spent

Fuel

Pool

(SFP) storage.

Observations

and Findin s

On Harch 15,

1996, during core alterations,

HP personnel

noted higher

than expected radiation levels

on the Unit 4 auxiliary building roof in

the vicinity of the SFP transfer canal

outer wall.

Dose rates

were as

high as 1.500 mrem/hr on contact with the concrete wall and

900 mrem/hr

at 12 inches.

One of the'licensee's

corrective actions in response to

the event was to monitor the Unit 3 areas that may have elevated

radiation levels during fuel movement in the next Unit 3 refueling

outage.

The program included use of portable radiation surveys

by HP technicians

during initial fuel movements

and the u'se of radiation monitoring

equipment continuously recording radiation levels throughout the fuel

transfer

process.

The licensee's

documentation

showed the highest

radiation dose rate to be approximately

600 mrem/hr at

a point in the

Cask

Washdown

Room

(CWR).

The radiation levels

on the auxiliary

h

building roof were much lower that those

seen

on Unit 4 due to extra

shielding provided by Boric Acid Storage

Tanks

(BAST).

Areas that were

posted

as high radiation areas

during the fuel movement included the

auxiliary building roof'bove the

BAST,

BAST Room,

New Fuel

Room,

CWR,

and

SFP Heat Exchanger

room.

Conclusion

The inspector

concluded that the licensee

adequately identified the

temporary high radiation areas

resulting from the transfer of spent fuel

from the Unit 3 reactor to the Unit 3 SFP.

Radiation Controls Durin

the Unit 3 Outa

e

71750

Periodically during the Unit 3 outage,

the inspectors

made containment

entries to review work in progress.

radiological conditions.

and assess

housekeeping

and general

material conditions.

The inspectors

also

reviewed the licensee's

radiological controls to minimize dose, to

prevent contamination

spread,

and to protect workers.

The inspectors

noted

good practices

including remote monitoring by the use of cameras

including closed circuit television

and dose telemetry.

Observed. jobs

included

RPV and cavity work,

SG primary work,

CVCS heat exchanger

repai r, and other containment work.

Overall dose performance will be

reviewed in a subsequent

inspection.

Staff Trainin

and

uali fications in Radiation Protection

and Chemistr

83750

Ins ection Sco

e

The qualifications of a new HP Supervisor

were reviewed against

qualification criteria in Technical Specification (TS) 6.3.1.

Observations

and Findin s

Licensee

TS 6.3. 1 required

each

member of the unit staff meet or exceed

the minimum qualifications of ANSI N18. 1-1971 for comparable positions,

except, for the Health Physics Supervisor

who shall

meet or exceed the

qualifications of Regulatory Guide (RG) 1.8,

"Personnel

Selection

and

Training," revision dated

September

1975.

Regulatory Guide 1.8. prescribed specific qualifications for Supervisor

of Radiation Protection referred to as the Radiation Protection

Manager

(RPM).

The

RG stated the

RPM should have

a bachelor's

degree

or the

equivalent in a science

or engineering subject.

including some formal

training in radiation protection.

The

RPM sh'ould also have at least

five years of professional

experience

in applied radiation protection.

At least three years of the professional

experience

should

be in applied

radiation protection work in a nuclear facility dealing with

'

R6

R6.1

radiological

problems similar to those encountered

in nuclear

power

stations preferably in an actual

nuclear

power station.

The inspector

reviewed the qualifications of the new

HP Supervisor.

Overall, the

HP Supervisor

had been

a supervisor

in some radiation

rotection capacity at Turkey Point for approximately eighteen years.

he supervisor

had also received National Registry of Radiation

Protection Technologist

(NRRPT) certification.

The

HP Supervisor

did

not have

a bachelors

degree but did possess

the equivalent in

experience.

The

NRC has considered

four years of applied radiation

protection experience

at

a nuclear facility equivalent to the bachelors

degree

requirement.

Conclusion

The inspectors

concluded the new

RPM met the qualification requirements

of TS 6.3.1.

RP&C Organization

and Administration

Radiation Protection

and Chemistr

Or anization

and Administration

83750

Ins ection Sco

e

The inspectors

evaluated the recent organization

changes for their

affect in the licensee's

program for control of radiation exposures,

especially

any changes that result in a lessening of the ability of the

radiation protection manager to have direct recourse to the onsite plant

or station manager in order to resolve questions

related to the conduct

of the radiation protection program.

Observations

and Findin s

The licensee

had recently combined the chemistry

and health physics

departments.

The reorganization

was

made to allow more efficient use of

available resources

and to allow individuals an opportunity to work in

new positions of responsibility.

The new organization

had Chemistry,

HP,

and Technical sections,

with each having an assigned

supervisor.

The Technical section

was

a new group.

An HP/Chemistry Supervisor

position was also created to manage the three sections.

The

HP/Chemistry supervisor

would report to the operations

manager.

The

former

HP Supervisor

was

made the Technical section supervisor

and the

ALARA coordinator

was

made the supervisor of Health Physics.

The

licensee did not know when the manager

position would be filled.

In accordance with licensee

TS 6.2 the

HP supervisor

shall

have di rect

access to the senior site management for resolving issues affecting

implementation of the radiation protection program.

The new

organization did affect the

RPHs chain of command to senior

management,

in that.

another

manager

had been

added to the chain of command.

However, the route through the operations

manager

to the plant manager

remained the same.

HP personnel

reported

good access

to upper

management.

c.

Conclusion

The inspector

concluded the

new organization did not adversely

impact

the licensee's ability control radiation exposures.

Pl

Conduct of EP Activities

Pl. 1

Notification of Unusual

Event

UE

Due to Fire

93702

and 71750

At about 7: 15 a.m.

on March 4,

1997, Control, room operators

received

fire alarms f'r the invertor rooms

and cable spreading

room (CSR),

and

observed

some

smoke in the invertor room behind the control

room.

A

public address

(PA) announcement

was

made

and the fire brigade

responded

to'the affected areas.

Subsequently,

one of the invertor room halon

systems

automatically initiated.

The fire brigade observed

sparks

and

fire emanating

from the inboard generator

bearing

on the 4A control rod

drive motor-generator

(MG) set.

The 4A MG set

was secured locally, and

the fire brigade extinguished the fire using portable carbon dioxide and

dry chemical extinguishers.

Other licensee

actions

included the following:

Called for outside assistance,

Declared

an

UE due to fire lasting more than ten minutes at 7:37

a.m.,

r

Notified the State

(FL) and

NRC as required,

Declared the control

room ventilation system

OOS,

Downgraded the

UE when fire was confirmed out at 8:00 a.m.,

Organized

an

ERT to determine root cause,

Debriefed the fire brigade

and other involved personnel,

and

Repaired the 4A MG set

(see section M2.1).

The effects

on each unit was

as follows:

Unit 3 was in mode 5, in the second

day of the refueling outage.

RHR was in service,

and no immediate concerns

were noted.

(2)

Unit 4 was at 100'ower.

The 4B

MG set

remained in service

providing rod control power.

(3)

The licensee

reviewed control

room evacuation

procedures

based

on

the proximity of the fire and smok p5

P5.1

S1

S1.1

.

The resident

and region based

inspectors

heard the

PA announcement,

and

reported

immediately to the scene

and the control

room.

Procedure

implementation (e.g.. fire ONOPs),

TSAS,

and

Emergency

Plan activation

were independently verified to be appropriate.

Timely and effective

response

by the fire brigade

was noted.

Strong oversight

by the fire

brigade leader.

the

NPS,

and licensee

management

was noted.

The

ERT

efforts were noteworthy and comprehensive.

A fire brigade debrief was

held by fire protection personnel,

and

ERT members,

and plant manage-

- ment.

This debrief was proactive.

informative,

and well executed.

In conclusion;

the licensee's

response to the fire. and the

UE,

and

followup activities were noteworthy.

Staff Training and Oualification in

EP'mer

enc

Plan Drill

71750

On February 24,

1997. the licensee

conducted

an Emergency

Preparedness

(EP) drill, including actuation of the Technical

Support Center

(TSC)

and the Operations

Support Center

(OSC).

The inspectors

monitored

portions, of the drill in the control

room simulator

as well as the

TSC

and

OSC.

The inspectors

concluded that the

EP drill was appropriately conducted

and critiqued.

Overall licensee

performance

was very good.

New and

recently promoted personnel

were used in their

EP positions for the

first time.

This provided good training for these individuals.

Conduct of Security and Safeguards Activities

Ille al

Dru

Found In the Protected

Ar ea

PA

71750

On February

19.

1997. at 12:20 p.m.,

a licensee security officer

discovered

a glass tube with a white powder substance

at one end of the

tube.

The tube was found in a portable toilet, inside the protected

area just north of the spare transformer.

The tube fell from a ledge

above the door while the portable toilet was being cleaned.

Metro-Dade

Police were notified,

and took possession

of the glass tube.

Confirmatory testing identified the substance

as containing crack

cocaine.

The licensee

inspected all the similar portable toilets on-

site and no other material

was found.

Subsequent

inspections of the Protected

Area and site by heightened

security and operations

personnel

did not identify any other material.

The licensee

also initiated Condition Report

No. 97-0227

and

made

a 24-

hour notification

ENS to the

NRC at 8:52 p.m. per

CFR 36.73.

Additional corrective actions

included maintaining

a heightened

awareness

during the refueling outage

due to a large number of extra

personnel

onsite.

increased

Protected

Area searches,

and increased

random testing per fitness-for-duty requirement r

S8

S8.1

The inspector

reviewed the licensee's

investigation,

examined the

material,

independently toured

and inspected

the Protected

Area and

site, verified corrective actions.

and reviewed the

ENS worksheet

and

CR.

The inspector concluded that the licensee appropriately

responded

to this issue,

including reportabi lity assessment

and corrective

actions.

A regional specialist

intends to review this item in a future

inspection.

Hiscellaneous

Security and Safeguards

Issues

Closed

URI 95-21-01

Failure to Include Individuals in A Dru

Testin

Pro

ram

Enforcement Action

EA

No. 97-86

92904

On September

26.

1995, the licensee identified that several

individuals

were missing from the Nuclear Employee Plant Access

(NEPA) System.

This

omission from the computer

system also excluded these individuals from

the required

random drug testing pool.

The discrepancy

was detected

when another licensee

requested

transfer of access

of affected

individuals.

Upon investigation

and through

an audit conducted

by the

licensee, it was confirmed that information for several

individuals was

not input to the

NEPA system.

The licensee

determined that

a contract security officer failed to

complete the procedure

and upon realizing the licensee's

investigation

was proceeding,

decided to input the data without informing the

licensee.

The employee

was subsequently

terminated

as

a result of this

action.

The individuals who were not under the random drug screening

program were not aware of their exclusion.

The time-frame of exclusion

of the various individuals was approximately

19 to 30 days.

The licensee

concluded root cause

was

a personnel

error.

The

individual's inattention to detail also contributed to falsification of

records.

The individual failed to perform job related tasks in a timely

manner, getting behind in duties.

Upon learning of the pending

investigation,

the individual attempted to input the data using the

dates the data

was supposed

to be entered,

rather than the date the data

was actually entered in the

NEPA System.

CFR 26.24 requires

licensees

to have unannounced

drug and alcohol

tests

imposed in a statistically

random and unpredictable

manner.

Thus,

all persons

in the population subject to testing

have

an equal

probability of being selected

and tested.

For approximately

19 to 30

days,

during the period July 1995 to September

1995, several

individuals

were excluded

from the licensee's

required

random drug and alcohol

testing program.

The inspector

reviewed the licensee's

corrective actions

and

NRC

enforcement criteria.

This licensee-identified

and corrected violation

is being treated

as

a Non-Cited Violation (NCV), consistent with Section

VII.B.1 of the

NRC Enforcement Policy.

NCV 50-250.251/97-03-03,

Failure

to Include Individuals in a Drug Testing

Program,

and the URI and

EA

were close P

t

F5

Fire Protection Staff Training and Qualification

75.1

~Fi

Il 111

71755

The inspector

observed

a routine. unannounced fire drill conducted

on

February

19.

1997, at the Unit 3 lube oil reservoir.

The inspector

observed activities from the control

room and locally at the scene.

The

inspector

concluded that personnel

appropriately

and adequately

responded to the simulated fire.

The response

included operators

and

HP

personnel

assigned to the fire team,

chemistry

and medical

personnel

assigned

as the emergency

medical

team,

and security personnel.

The inspector

concluded that the fire drill was well conducted

and

critiqued.

V.

Mana ement Meetin s

Xl Exit Meeting Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on April 11,

1997.

The

licensee

acknowledged

the tindings presented.

Licensee representatives

presented their views that the item on failure to paint all tools used

in the

RCA had been prior identified by them and that corrective action

was in progress,

therefore it should not be cited by the

NRC as

a

violation.

The inspector

acknowledged their comments.

The inspectors

asked the licensee

whether

any materials

examined during

the inspection should

be considered proprietary.

No proprietary

information was identified.

Partial List of Persons

Contacted

Licensee

T.

V: Abbatiello. Site Quality Manager

G. Alexander,

Supervisor

Inspections/CSI

R. J. Acosta, Director, Nuclear Assurance

J.

C. Balaguero,

Plant Operations

Support Supervisor

P.

M. Banaszak.

Electrical/18C Engineering Supervisor

R.

M. Brown,

HP Supervisor

T. J. Carter,

Mechanical

Maintenance Supervisor

S. Chaviano,

Lead Civil Engineer

B.

C.

Dunn, Mechanical

Systems

Supervisor

R. J. Earl,

QC Supervisor

S.

M. Franzone,

Electrical Maintenance

Supervisor

R. J. Gianfrancesco.

Maintenance

Support Supervisor

J.

R. Hartzog.

Business

Systems

Manager

G.

E. Hollinger, Licensing Manager

R. J.

Hovey, Site Vice-President

M.

P.

Huba,

Nuclear Materials Manager

D.

E. Jernigan,

Plant General

Manager

T. 0. Jones,

Operations

Supervisor

M. D. Jurmain,

IKC Maintenance

Supervisor

V. A. Kaminskas.

Services

Manager

J.

E. Kirkpatrick, Fire Protection,

EP, Safety Supervisor

J.

E. Knorr, Regulatory Compliance Analyst

G.

D. Kuhn, Procurement

Engineering Supervisor

R. J.

Kundalkar,

Vice President,

Engineering

and Licensing

M. L. Lacal, Training Manager

J.

D. Lindsay, Health Physics

Support Supervisor

E. Lyons, Engineering Administrative Supervisor

F.

E. Marcussen,

Security Supervisor

R.

B. Marshall,

Human Resources

Manager

C. Mowrey. Licensing Specialist

H.

N.

Paduano,

Manager,

Licensing and Special

Projects

M. O.. Pearce,

Maintenance

Manager

K.

W. Petersen,

Site Superintendent

T. F. Plunkett,

President,

Nuclear Division

K. L. Remington,

System Performance

Group Supervisor

R.

E.

Rose,

Outage

Manager

C.

V. Rossi.

QA and Assessments

Supervisor

W. Skelley, Plant Engineering

Manager

R.

N. Steinke,

Chemistry Super visor

E. A. Thompson.

Engineering

Manager

D. J.

Tomaszewski,

Systems

Engineering

Manager

R. Turner, Inservice Inspection Coordinator

G. A. Warriner, Quality Surveillance Supervisor

R.

G. West, Operations

Manager

Other licensee

employees

contacted

included construction

craftsmen,

engineers,

technicians,

operators,

mechanics,

and

electricians.

NRC Resident

Inspectors:

T.

P. Johnson,

Senior

Resident

Inspector

J.

W. York, Resident

Inspector

J.

R.

Reyes,

Resident

Inspector

Partial List of Opened,

Closed,

and Discussed

Items

~0ened

50-250.251/97-03-04

Closed

IFI, Failure to Conspicuously

mark tools in the

RCA (R1.1).

50-250,251/95-21-01

URI, Failure to Include Individuals in A Drug

Testing Program (section

SB. 1).

50-250.251/97-03-01

NCV, Failure to Follow the

ADM for Operating

Procedures

(section

03. 1).

50-250,251/97-03-02

NCV, Failure to Meet ANSI N45.2.2 Storage

Requirements

for

Piping (section M7.1).

50-250,251/97-03-03

NCV. Failure to Perform Daily Radiation Meter

Response

Checks (Rl.l).

50-250.251/97-03-05

LER 50-250/97-02,

Discussed

None

NCV, Failure to Include Individuals in a Drug

Testing

Program (section S8.1)

Manual Reactor Trip (section 01.3)

List of Inspection

Procedures

Used

'IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying,

Resolving,

and Preventing

Problems

IP 50002:

Steam Generators

IP 60705:

Preparation

for Refueling

IP 60710:

Refueling Activities

IP 61726:

Surveillance

Observations

IP 62700:

Maintenance

Program Implementation

IP 62702:

Maintenance

Program

IP 62707:

'aintenance

Observations

IP 71707:

Plant Operation

IP 71750:

Plant Support Activities

IP 73753:

Inservice Inspection

IP 83750:

Occupational

Radiation

Exposure

IP 90712:

Inoffice Review of Written Reports

IP 90713:

Review of Periodic Reports

IP 92700:

IP 92904:

IP 93702:

Onsite Followup of Written Reports of Nonroutine Events at

Power Reactor Facilities

Followup - Plant Support

Prompt Onsite

Response

to Events at Operating

Power Reactors

List of Acronyms and Abbreviations"

AC

ADM

AFW

ALARA

a.m.

ANPO

ANPS

ANSI

ARB

ARP

ASME

AVB

B&PV

BIT

CC

CCW

CFR

CMM

CR

CRDM

CSR

CV

CVCS

DB/DBD

DC

DOT

dpm

DPR

DRS

EA

ECCS

EDG

e.g

ENG

ENS

, EOP

EP

ERT

ET

etal

oF

F

FCV

FL

FPL

FT

Alternating Current

Administrative (Procedure)

Auxiliary Feedwater

As Low As Reasonably

Achievable

Ante Meridiem

Associate

Nuclear Plant Operator

Assistant

Nuclear Plant Supervisor

American National Standards

Institute

Alara Review Board

Annunciator

Response

Procedure

American Society of Mechanical

Engineers

Anti-Vibration Bar

Boiler and Pressure

Vessel

Boron Injection Tank

cubic centimeter

Component Cooling Water

Code of Federal

Regulations

Corrective Maintenance

- Mechanical

Condition Report

Control

Rod Drive Mechanism

Cable Spreading

Room

Control Valve

Chemical

Volume Control System

Design Basis

(Document)

Direct Current

Department of Transportation

Disintegrations

Per

Minute

Power Reactor

License

Division of Reactor Safety

Enforcement Action

Emergency

Core Cooling System

Emergency Diesel Generator

For Example

Engineering

Emergency Notification System

Emergency Operating

Procedure

Emergency

Preparedness

Event Response

Team

Eddy Current

"and the rest"

Degrees

Fahrenheit

Fuse

Flow Control Valve

Florida

Florida Power and Light

Flow Transmitter

GL

GOP

gpm

GS

HEPA

HHSI

HP

HPA

HPES

HPS

HPSS

HPT

hr

HRA

HVAC

'&C

ICW

i.e.

IEEE

IG(SCC)

ILRT

IP

ISI

IST

IWE,

IWL

JPN

JPNS

KV

L

LC

LCO

LCV

LER

LI

LLRT

LPDR

MBM

MCC

MG

MOV

'OVATS

MSSV

NCY

NDD

NDE

NEPA

No.

NO(UE)

NPO

NPS

NRC

Generic Letter

General

Operating

Procedure

Gallons

Per Minute

Gland Steam

High Efficiency Particulate Air

High Head Safety Injection

Health Physics

Health Physics

- Administrative

Human Performance

Evaluation System

Health Physics

- Surveillance

HP Shift Supervisor

Health Physics

- Technical

hour

High Radiation Area

Heating Ventilation and Air Conditioning

Instrumentation

and Control

Intake Cooling Water

That Is

Institute of Electrical

and Electronics

Engineers

Intergranular

(Stress

Corrosion Cracking)

Integrated

Leak Rate Testing

Inspection

Procedure

Inservice Inspection

Inservice Test

Subsections

of ASME B&PV Code, Section

XI

Juno Project Nuclear (Nuclear Engineering)

Juno Project Nuclear Safety

Kilovolt

Letter (licensing)

Level Controller

Limiting Condition for Operation

Level Control Valve

Licensee

Event Report

Level Indicator

Local Leak Rate Test

Local

PDR

milli

Manufacturing Buff Marks

Motor Control Center

Motor Generator

Motor-Operated

Valve

MOV Acceptance Testing System

Main Steam Safety Valve

Non-Cited Violation

No Detectable

Defect

Nondestructive.Examination

Nuclear Employee Plant Access

Number

Notification of (Unusual

Event)

Nuclear Plant Operator

Nuclear Plant Supervisor

Nuclear Regulatory Commission

NRI

NRR

OD

ONOP

OOS

OP

OSC

OSP

PA

PACV

PAHH

PC

PCE

PC/H

PCV

PDR

p.m.

PM

PMI

PHM

PNSC

PORV

Pslg

PTN

PWO

QA

QAO

QC

QI

RCA

RCO

RCP

RCS

rem

(

RG

RHR

RO

RPM

RP(H)

PRV

RWO

RWP

RWST

RV

S/B

S

SEC/S

SER

SFP

SG

SI

SGFP

SNPO

No Recordable

Indications

Office of Nuclear Reactor Regulation

Outside Diameter

Off-Normal Operating

Procedure

Out-of-Service

Operating

Procedure

Operational

Support Center

Operations Surveillance

Procedure

Public Address

Post-Accident

Containment Ventilation

Post-Accident

Hydrogen Monitor

Protective.Clothing

Personnel

Contamination

Event

Plant Change/Modification

Pressure

Control Valve

Public Document

Room

Post Meridiem

Preventive

Maintenance

Preventive

Maintenance

- I8C

Preventive

Maintenance

- Mechanical

Plant Nuclear Safety Committee

Power-Operated

Relief Valve

Pounds

Per Square

Inch Gauge

Project Turkey Nuclear

Plant Work Order

Quality Assurance

Quality Assurance

Organization

Quality Control

Quality Instruction

Radiation Control Area

Reactor Control Operator

Reactor

Coolant

Pump

Reactor Coolant System

m rem) Roentgen

Equivalent

Man (milli)

Regulatory Guide

(NRC)

Residual

Heat Removal

Reactor Operator

Radiation Protection

Manager

Radiation Protection

(men)

Reactor

Pressure

Vessel

Relay Work Order

Radiation

Work Permit

Refueling Water Storage

Tank

Relief Valve

GFP

Standby

SGFP

Safety Evaluation Civil - Site

Safety Evaluation Report

Spent

Fuel

Pit'team

Generator

Safety Injection

s/g Feedwater

Pump

Senior Nuclear Plant Operator

~

~

~

wi;,

SOER

SRO

STAR

TCN

TG

TS

TSAS

TSC

UFSAR

URI

UT

V

VAC

VAR

VCT

VIO

VMR

VT

W

WGDT

WHT

WO

WR

Significant Operating

Experience

Review

Senior Reactor Operator

Stop-Think-Act-Review

Temporary

Change Notice

Turbine Generator

Technical Specification

TS Action Statement

Technical

Support Center

Updated Final Safety Analysis Report

Unresolved

Item

Ultrasonic Examination

Volt

Volt AC

Volts Amperes Reactive

Volume Control Tank

Violation

Voltage Metering Relay

Visual Examination

Westinghouse

Waste

Gas

Decay Tank

Waste Holdup Tank

Work Order

Work Request

~(~

t

l

4