05000400/LER-2019-002, B Train Chiller for the Essential Services Chilled Water System Tripped on High Compressor Oil Temperature

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B Train Chiller for the Essential Services Chilled Water System Tripped on High Compressor Oil Temperature
ML19259A072
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 09/16/2019
From: Dills J
Duke Energy Progress
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RA-19-0361 LER 2019-002-00
Download: ML19259A072 (5)


LER-2019-002, B Train Chiller for the Essential Services Chilled Water System Tripped on High Compressor Oil Temperature
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)
4002019002R00 - NRC Website

text

(DUKE ENERGY John R. Dills Plant Manager Shearon Harris Nuclear Power Plant 5413 Shearon Harris Road New Hill, NC 27562-9300 919.362.2000 10 CFR 50.73 September 16, 2019 Serial: RA-19-0361 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 Shearon Harris Nuclear Power Plant, Unit 1 Docket No. 50-400/Renewed License No. NPF-63 Subject: Licensee Event Report 2019-002-00 Ladies and Gentlemen:

Duke Energy Progress, LLC, submits the enclosed Licensee Event Report (LER) 2019-002-00 in accordance with 10 CFR 50. 73 for Shearon Harris Nuclear Power Plant, Unit 1 (HNP). This report describes an event resulting in the 'B' train of the Essential Services Chilled Water System being inoperable for a time period longer than permitted by HNP Technical Specifications. The system has since been restored. This event had no significance with respect to the health and safety of the public.

There are no regulatory commitments contained within this report.

Please refer any questions regarding this submittal to Chuck Yarley at (919) 362-2477.

Sincerely, Enclosure: Licensee Event Report 2019-002-00 cc:

J. Zeiler, NRC Senior Resident Inspector, HNP M. Barillas, NRC Project Manager, HNP NRC Regional Administrator, Region II

John R. Dills Plant Manager Shearon Harris Nuclear Power Plant 5413 Shearon Harris Road New Hill, NC 27562-9300 919.362.2000 10 CFR 50.73 September, 2019 Serial: RA-19-0361 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 Shearon Harris Nuclear Power Plant, Unit 1 Docket No. 50-400/Renewed License No. NPF-63 Subject: Licensee Event Report 2019-002-00 Ladies and Gentlemen:

Duke Energy Progress, LLC, submits the enclosed Licensee Event Report (LER) 2019-002-00 in accordance with 10 CFR 50.73 for Shearon Harris Nuclear Power Plant, Unit 1 (HNP). This report describes an event resulting in the B train of the Essential Services Chilled Water System being inoperable for a time period longer than permitted by HNP Technical Specifications. The system has since been restored. This event had no significance with respect to the health and safety of the public.

There are no regulatory commitments contained within this report.

Please refer any questions regarding this submittal to Chuck Yarley at (919) 362-2477.

Sincerely, John R. Dills Enclosure: Licensee Event Report 2019-002-00 cc:

J. Zeiler, NRC Senior Resident Inspector, HNP M. Barillas, NRC Project Manager, HNP NRC Regional Administrator, Region II

NRC FORM 366 (04-2018)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

(See Page 2 for required number of digits/characters for each block)

(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

NRC FORM 366 (04-2018) 05000

3. Page 1

OF

4. Title
5. Event Date Month Day Year
6. LER Number Year Sequential Number Rev No.
7. Report Date Month Day Year
8. Other Facilities Involved Facility Name Docket Number 05000 Facility Name Docket Number 05000
9. Operating Mode
10. Power Level
11. This Report is Submitted Pursuant to the Requirements of 10 CFR §: (Check all that apply) 20.2201(b) 20.2201(d) 20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(2)(v) 20.2203(a)(2)(vi) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1)(i)(A) 50.36(c)(1)(ii)(A) 50.36(c)(2) 50.46(a)(3)(ii) 50.73(a)(2)(i)(A) 50.73(a)(2)(i)(B) 50.73(a)(2)(i)(C) 50.73(a)(2)(ii)(A) 50.73(a)(2)(ii)(B) 50.73(a)(2)(iii) 50.73(a)(2)(iv)(A) 50.73(a)(2)(v)(A) 50.73(a)(2)(v)(B) 50.73(a)(2)(v)(C) 50.73(a)(2)(v)(D) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(ix)(A) 50.73(a)(2)(x) 73.71(a)(4) 73.71(a)(5) 73.77(a)(1) 73.77(a)(2)(i) 73.77(a)(2)(ii)

Other (Specify in Abstract below or in Page of 05000-

3. LER NUMBER YEAR SEQUENTIAL NUMBER REV NO.

E. Safety Analysis

The ESCW cooling capacity for each train is sized for 100 percent of the plant safety HVAC system cooling demand. This ensures that with the 'A' train of ESCW operable, the site would still be within the analyzed results for all transient and accident conditions, particularly as documented within the HNP Final Safety Analysis Report Chapter 6 and Chapter 15.

No loss of safety function occurred as a result of this event. At no point during the impacted periods was the ESCW system required to mitigate the impact of a design basis event. As such, this event had no significance with respect to the health and safety of the public.

F. Additional Information

The events leading to the WC-2B trip are unique to this event. There have been no LERs submitted in the past three years due to a similar event.

3 3

Shearon Harris Nuclear Power Plant, Unit 1 400 2019 002 00