On June 28, 2002, at 1343 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.110115e-4 months <br />, a notification was made to the NRC to report a potential operation outside of License Condition 2.0 (1), which authorizes PSEG Nuclear LLC to operate the facility at reactor core power levels not in excess of 3339 megawatts thermal (100 percent rated power).
On 5/26/02, operators identified that the feedwater cross-flow correction factor was lower after returning to normal operations from a down power evolution. Balance of plant indications led operators to suspect the indicated reactor power with the correction factor applied might be non-conservative. If the plant were operating with a non-conservative correction factor, the calculation of core thermal power was lower than actual power and resulted in the plant being operated above the license thermal power limit. Detailed analyses have confirmed that a malfunction of the crossflow instrumentation correction factor caused the plant to operate by as much as 0.47% overpower. The apparent cause of the event is attributed to a malfunction of the crossflow correction factor instrumentation as a result of cracked insulation becoming lodged between the crossflow meter's clamp and the pipe. Immediate corrective actions included removing crossflow from service and reducing power to the pre 1.4% uprate value. Additional corrective actions included the installation of new crossflow transducers and validation of current crossflow performance. The mounting configuration was changed to prevent similar occurrences.
This Special Report is being submitted in accordance with the requirements of License Condition 2.F. There were no safety consequences associated with this event since significant margins were available to all power distribution thermal limits. |
LER-2002-005, P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236
JUL 2 5 2002 0 0 PSEG
Nuclear LLC
LR-NO2-0243
U. S. Nuclear Regulatory Commission
Document Control Desk
Washington, DC 20555
SPECIAL REPORT 354/2002-005-00
HOPE CREEK GENERATING STATION
FACILITY OPERATING LICENSE NO. NPF-57
DOCKET NO 50-354
Gentlemen:
This Special Report entitled Potential to Exceed Licensed Power Level Due to
Malfunction of The Crossflow Correction Factor Instrumentation", is being submitted
pursuant to the requirements of License Conditions 2.C. (1) and 2.F. The attached
Special Report contains no commitments.
D. F. Gar how
Vice Pres' ent - Operations
Attachment
/MGM
C D Distribution
LER File 3.7
95-2168 REV 7,99
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004
(7-2001) COMMISSION Estimated burden per response to comply with this mandatory. information collection rec,u,:st: 50 hours. Reported lessons learned are incorporated into the licensing process and fen back to
industry. Send comments regarding burden estimate to the Records Management Branch (T-6
E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intern% e-mail to LICENSEE EVENT REPORT (LER) bislnrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-
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Ho • e Creek Generatin • Station 05000354 1 OF 4
Potential to Exceed Licensed Power Level Due to Malfunction of The Crossflow Correction Factor
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FACILITY NAME (1) DOCKET (2) OF1 4 Hope Creek Generating Station 05000354 2 2002 0 0 5 � 00
PLANT AND SYSTEM IDENTIFICATION
General Electric — Boiling Water Reactor (BWR/4) Feedwater System — EIIS Identifier {SJ/—} * *Energy Industry Identification System {EllS} codes and component function identifier codes appear as (SS/CCC)
IDENTIFICATION OF OCCURRENCE
Event Date: May 26, 2002 Discovery Date: June 28, 2002
CONDITIONS PRIOR TO OCCURRENCE
Mode 1 — 100% power. No structures, systems, or components were inoperable at the time of the occurrence that contributed to the event.
DESCRIPTION OF OCCURRENCE
On 5/26/02, operators identified that the feedwater cross-flow correction factor was lower after returning to normal operations from a down power evolution (0.982 vice 0.987). Balance of plant indications led operators to suspect the indicated reactor power with the correction factor applied might be non-conservative. However, other plant indications did not support the conclusion of a non- conservative correction factor. If the plant were operating with a non-conservative correction factor, the calculation of core thermal power was lower than actual power and resulted in the plant being operated above the license thermal power limit. Detailed analyses have confirmed that a malfunction of the crossflow instrumentation factor caused the plant to operate by as much as 0.47% overpower.
This condition resulted from an error in the crossflow meter correction factor calculated by the crossflow computer and applied to the power calculation by the plant computer, which was recognized along with other plant parameters as a deviation from historical plant operation. A review of the historical data indicates that this is the only occurrence of a non-conservative failure of the crossflow meter. A review of Salem data indicates that this event has not occurred at Salem. The Salem installations did not use the same insulation method as Hope Creek and therefore are not susceptible to the same failure mechanism.
Once the condition was identified as possibly resulting in a non-conservative power calculation, the operations department took the appropriate steps to ensure conservative operations by removing crossflow from service and reducing power to pre 1.4% uprate value.
LER NUMBER6) 2002 0 FACILITY NAME (1) Hope Creek Generating Station DOCKET (2) (.1 SEQUENTIAL REVISION 0 5 00 DESCRIPTION OF OCCURRENCE (Cont'd) Several plant parameters indicated conflicting evidence concerning the actual plant power level.
Those that could be associated with an overpower condition were: 1) increased first stage pressure, 2) increased final feedwater temperature, 3) increase in condenser temperature rise, and 4) increase in secondary condensate pump flow. Other parameters that support correct crossflow operation and no overpower condition are: 1) low megawatts, 2) increase in #5 and #6 heater extraction pressures beyond what would be expected from the first stage pressure increase and, 3) increase in final feedwater temperature was attributed to the extraction pressure increase.
On June 28, 2002, at 1343 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.110115e-4 months <br />, a notification was made to the NRC to report a potential operation outside of License Condition 2.0 (1), which authorizes PSEG Nuclear LLC to operate the facility at reactor core power levels not in excess of 3339 megawatts thermal (100 percent rated power).
CAUSE OF OCCURRENCE
The apparent cause of the event was a non-conservative correction factor caused by Crossflow error.
A frequency scan was performed which indicated a degradation in the signal strength occurred. A failure mechanism was identified that could have resulted in the signal strength degradation and introduced the error in crossflow measurement of feedwater flow. Significant thermal cycling of the feed piping occurred during single loop operation when returning to power from the scheduled down- power event to repair the EHC system. This could have caused a foreign material to lodge between the crossflow meter's clamp and the pipe resulting in reduced load on the transducers thus introducing a bias. When the bracket was removed a large amount of insulation debris was found on top of the pipe. The source of the debris was calcium silicate insulation used around the crossflow meter.
PRIOR SIMILAR OCCURRENCES
Prior Hope Creek LERs and Special Reports were reviewed for similar potential overpower events. Several events that have resulted in Operating in Excess of 100 Percent of Rated Core Thermal Power have been reported for Hope Creek within the last two years. However, none of the previous events involved the cross flow correction factor. Previous corrective actions would not have prevented this event.
SAFETY CONSEQUENCES AND IMPLICATIONS
The power measurement error introduced by the error in the crossflow correction factor could have resulted in a potential overpower condition of up to 0.47%. A review of the Cycle 11 reload licensing report indicated that a significant margin was available to all power distribution FACILITY NAME (1) DOCKET (2) SAFETY CONSEQUENCES AND IMPLICATIONS (Cont'd) fuel thermal limits. Therefore, since adequate margin to all power distribution fuel thermal limits remained during the time period, there was no safety significance associated with the potential overpower condition due to the non-conservative cross-flow correction factor. Based on the above this event did not present an undue risk to the health and safety of the public.
A review of this condition determined that a Safety System Functional Failure (SSFF) has not occurred as defined in Nuclear Energy Institute (NEI) 99-02.
CORRECTIVE ACTIONS
1. Immediate corrective actions included the installation of new crossflow transducers and validation of current crossflow performance. Configuration was changed to increase the low limit on the correction factor to prevent similar occurrences and Calcium Silicate Insulation was removed from crossflow meter.
2. Temporary insulation that had been installed on crossflow meter will be replaced with fiberglass cloth insulation. The Corrective Action Program will track this.
3. Crossflow preventive maintenance will be changed to add requirement to perform a Received Signal Strength Indicator (RSSI) scan when a plant transient where feedwater temperature decreases by greater than 100 degrees F or greater than 100 degrees F per minute is experienced. The Corrective Action Program will track this.
COMMITMENTS
The corrective actions cited in this Special Report are voluntary enhancements and do not constitute commitments.
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05000255/LER-2002-001 | NONCOMPLIANCE WITH TECHNICAL SPECIFICATION REQUIREMENTS FOR SAFETY INJECTION TANK T-82D | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000219/LER-2002-001 | | 10 CFR 50.73(a)(2)(i) | 05000305/LER-2002-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000313/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2002-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000368/LER-2002-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000247/LER-2002-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii) | 05000261/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2002-001 | Mechanical Pressure Regulator Failure Causes Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000266/LER-2002-001 | | 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000277/LER-2002-001 | | | 05000289/LER-2002-001 | | | 05000301/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2002-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000400/LER-2002-001 | | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000397/LER-2002-001 | | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000361/LER-2002-001 | | | 05000454/LER-2002-001 | Multiple Main Steam Safety Valve Relief Tests Exceeded Required Tolerance Due to Disk to Nozzle Metallic Bonding and Setpoint Drift | 10 CFR 50.73(a)(2)(i)(b) | 05000483/LER-2002-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000370/LER-2002-001 | | | 05000362/LER-2002-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2002-001 | | | 05000348/LER-2002-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2002-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) | 05000368/LER-2002-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2002-002 | Failure of the High Pressure Core Spray Pump to Start | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000247/LER-2002-002 | | 10 CFR 50.73(a)(2)(i) | 05000346/LER-2002-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000331/LER-2002-002 | | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000266/LER-2002-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000282/LER-2002-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000361/LER-2002-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000289/LER-2002-002 | | | 05000301/LER-2002-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000352/LER-2002-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2002-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000483/LER-2002-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2002-003 | | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000346/LER-2002-003 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2002-003 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii) | 05000313/LER-2002-003 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000400/LER-2002-003 | Reactor Trip Due to Momentary Grid Undervoltage | | 05000454/LER-2002-003 | Two Automatic Reactor Trips Due to Reactor Coolant Overtemperature Conditions Caused by Digital Electrohydraulic Control System Circuit Card Failure Causing the Turbine Governor Valves To Close | | 05000348/LER-2002-003 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000397/LER-2002-003 | | | 05000247/LER-2002-003 | | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000483/LER-2002-003 | 1 OF 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000270/LER-2002-003 | | |
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