05-18-2016 | Reactor coolant system pressure boundary leakage was identified by a drywell leak inspection team during a planned shutdown for a Unit 1 refueling outage. This event resulted in a plant shutdown required by Technical Specifications. The Unit 1 'A' RHR Shutdown Cooling Return Check Valve equalizing line developed a crack at the toe of a weld due to high cyclic fatigue induced by vibration from the reactor recirculation system. The Unit 1 welds were reworked to EPRI 2x1 at select locations on the "A" and "B" RHR Shutdown Cooling Return check valve equalizing lines for HV-051-1F050A and 50B. The similar Unit 2 welds on equalizing lines for HV-051-2F050A and 50B will be examined and reinforced. The scope will be added into the next refueling outage (2R14) currently scheduled for April 2017. |
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Category:Letter
MONTHYEARML24151A3842024-10-31031 October 2024 – Issuance of Amendment Nos. 264 and 226 Support to Digital Modernization Project Installation (EPID L-2023-LLA-0025) and Exemption from the Requirements of 10 CFR 50.62 ML24303A0902024-10-29029 October 2024 Operator Licensing Examination Approval ML24303A2782024-10-29029 October 2024 10 CFR 50.46 Annual Report ML24299A2642024-10-25025 October 2024 Response to Request for Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications IR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24278A3022024-10-0404 October 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10 CFR 50.62 ATWS Rule to Support the Digital Modernization Project Installation - Rev Unit 2 Technical Spec ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24263A0032024-09-27027 September 2024 Generation Station, Units 1 and 2 – Regulatory Audit Plan Supporting Review of the Component Interface Module System of the Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) (Redacted) ML24243A0482024-09-19019 September 2024 Generation Station, Unit Nos. 1 and 2 - Schedule Update for License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24215A4042024-09-18018 September 2024 Request for Withholding Information from Public Disclosure IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) ML24241A1952024-08-28028 August 2024 License Amendment Request for Modification to Technical Specification 3.6.1.2 and Main Steam Isolation Valve Leakage Rate Requirements ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24163A3902024-08-14014 August 2024 Request for Withholding Information from Public Disclosure ML24220A2392024-08-12012 August 2024 Correction to Technical Specification Page 3/4 3-11 in Amendment No. 225 IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24204A0712024-07-29029 July 2024 Issuance of Amendment Nos. 263 and 225 Technical Specifications for Main Steam Line Tunnel Temperature ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24208A1592024-07-25025 July 2024 Regulatory Audit Plan Supporting Review of the System Development Portion of Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML24201A1662024-07-19019 July 2024 Response to Request for Additional Information for License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam L ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24180A1572024-06-28028 June 2024 Request to Return and Replace WEC Documents (EQ-EV-386-GLIM, EQ-QR- 433-GLIM, and APP-GW-GLR-611), to Meet 10CFR2.390 Request to Withdraw from Public Disclosure Requirements ML24170A7702024-06-20020 June 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, Opportunity for Hearing(Epid L-2024-LLA-0079) LTR 05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 ML24166A1142024-06-14014 June 2024 Response to Requests for Additional Information (RAIs 15 Through 23) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24165A2642024-06-13013 June 2024 License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam Line Tunnel Temperature TS 3/4.7.9 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker ML24151A2882024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24151A2012024-06-10010 June 2024 Request for Withholding Information from Public Disclosure 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24149A2112024-05-28028 May 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 ML24124A0432024-05-0303 May 2024 Response to Requests for Additional Information (RAIs 9 Through 14) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24114A3222024-04-23023 April 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) - Pivot to Unit ML24109A0702024-04-18018 April 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFRC50.52 ATWS Rule to Support the Digital Modernization Project Installation . 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2023-001, Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications2023-06-26026 June 2023 Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications 05000352/LER-2022-001, Regarding HPCI Inoperable Due to Inadvertent Isolation Signal2022-12-13013 December 2022 Regarding HPCI Inoperable Due to Inadvertent Isolation Signal 05000352/LER-2021-001, HPCI Inoperable Due to Remote Shutdown Panel Switch Failure2021-11-22022 November 2021 HPCI Inoperable Due to Remote Shutdown Panel Switch Failure 05000352/LER-2017-0012017-01-27027 January 2017 Condition Prohibited by TS due to Parts Quality Issue, LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue 05000353/LER-2016-0012016-07-27027 July 2016 Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error, LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 05000352/LER-2016-0032016-05-18018 May 2016 Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak, LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak 05000352/LER-2016-0022016-04-11011 April 2016 Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements, LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements 05000352/LER-2016-0012016-03-23023 March 2016 Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock, LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function 2024-06-18
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
2. DOCKET
Unit Conditions Prior to the Event Unit 1 was in Operational Condition (OPCON) 1 (Power Operation) at approximately 14.5 percent power performing a planned Unit 1 shutdown to support a refueling outage. There were no structures, systems or components out of service that contributed to this event.
Description of the Event
On Sunday March 20, 2016, Limerick Unit 1 was operating at 14.5 percent power performing a planned Unit 1 shutdown to support a refueling outage (1R16). At 2154 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.19597e-4 months <br />, the drywell leak inspection team identified a 0.5 gpm pressure boundary leak on the shutdown cooling (BO:EllS) testable check valve (ISV:EllS) equalizing line. The control room supervisor (CRS) entered Technical Specification (TS) 3.4.3.2 Reactor Coolant System - Operational Leakage Action "a" which requires being in at least Hot Shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Cold Shutdown within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> Hot Shutdown TS Action was met at 0133 hours0.00154 days <br />0.0369 hours <br />2.199074e-4 weeks <br />5.06065e-5 months <br /> and the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Cold Shutdown Action was met at 1401 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.330805e-4 months <br />.
An investigation determined that Unit 1 Unidentified Leakage increased from 0.03 gpm to 0.06 gpm between January 16, 2016 and January 18, 2016. Leakage increased to 0.24 gpm on January 19, 2016 and continued to vary with reactor recirculation pump speed for the remainder of the cycle. The maximum leakage recorded was 1.2 gpm which stabilized at 1.0 gpm following power reduction to 95 percent. On March 20, 2016 Maintenance Technicians performed a planned drywell entry at 14.5 percent power and identified a leak on the 3/4 inch reactor side equalizing line of the 1A Shutdown Cooling (SDC) Return Line Inboard Testable Check Primary Containment Isolation Valve, HV-051-1F050A. The leak was located approximately 1/4 inch from the valve body weld and was determined to be pressure boundary leakage.
A 4-hour ENS (#51809) was completed at 2351 hours0.0272 days <br />0.653 hours <br />0.00389 weeks <br />8.945555e-4 months <br /> as required by 10CFR50.72(b)(2)(i) for the initiation of a plant shutdown required by TS. The ENS also reported an event that resulted in the condition of the plant principal safety barriers being seriously degraded per 10CFR50.72(b)(3)(ii). Therefore, this LER is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(i)(A) and 10CFR50.73(a)(2)(ii)(A).
Analysis of the Event
There was no actual safety consequence associated with this event. The potential safety consequences of this event were minimal. The Unidentified Leakage remained a small fraction of the 5 gpm TS 3.4.3.2 LCO. HPCI was unavailable less than 29 minutes due to testing and RCIC was unavailable for less than 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> due to maintenance and testing during the three month period (January, February and March of 2016) of elevated drywell leakage. HPCI is designed to prevent the actuation of the automatic depressurization system (ADS) and ensure that the reactor core remains covered in the event of a small pipe break size of one-inch diameter or less.
The SDC return is a 12-inch diameter line equipped with an outboard motor operated valve (MOV) primary containment isolation valve (PCIV) and an inboard testable check valve PCIV.
The testable check valve has a bypass line that is equipped with an air operated valve (AOV) PCIV which is used to equalize the differential pressure across the testable check valve disc when the valve is opened during stroke testing. Testable check valves are also used in similar applications on low pressure coolant injection (LPCI) and core spray (CS) injection lines. The SDC valve is subject to vibration induced high cycle fatigue due to recirculation pump flow induced vibration. The LPCI and CS injection lines' socket welds are not subject to vibration induced high cycle fatigue.
The affected section of bypass line piping was replaced with a new socket weld with a 2x1 weld to improve pipe stability and minimize stresses at the toe as a result of the 2x1 weld configuration. A 2x1 weld was also applied at the similar valve body socket welds for the HV- 051-1F050A residual heat removal (RHR) side and HV-051-1F050B RHR and reactor side welds.
Cause of the Event
The Unit 1 `A' RHR Shutdown Cooling Return Check Valve equalizing line developed a crack at the toe of the weld due to high cyclic fatigue induced by vibration from the reactor recirculation system (Apparent Cause).
Corrective Action Completed The Unit 1 welds were reworked to EPRI 2x1 at select locations on the "A" and "B" RHR Shutdown Cooling Return check valve equalizing lines for HV-051-1F050A and 50B.
Corrective Action Planned The similar Unit 2 welds on equalizing lines for HV-051-2F050A and 50B will be examined and reinforced. The scope will be added into the next refueling outage (2R14) currently scheduled for April 2017.
Previous Similar Occurrences There were no previous similar occurrences of pressure boundary leakage in the past 5 years.
Component data:
System BO RHR/Low Pressure Coolant Injection System Component ISV Valve, Isolation Component number HV-051-1F050A Manufacturer A585 Weir Valves & Controls USA Inc.
Model number 50301-A Serial Number 2-50301-A
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05000353/LER-2016-001 | Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000352/LER-2016-001 | Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000352/LER-2016-002 | Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2016-003 | Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
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