Over a period of approximately one month, the OB Main Control Room ( MCR) Heating, Ventilating and Air Conditioning ( HVAC) system experienced four failures. Troubleshooting was completed for each of the failures and for three of the failures the cause was determined to be an intermittent dropout or chattering of the Loss of Offsite Power ( LOOP) start relay for two fans ( 0B-V116 MCR Supply and OB-V121 MCR Return Fans). The fourth failure was due to a contactor in the Motor Control Center ( MCC) for the OB-V116 MCR Supply Fan. On 11/29/16 the second failure occurred on the LOOP start relay for the OB-V116 MCR Supply fan. The investigation identified a manufacturing defect of the Agastat/Tyco ETR Relays in the lot of relays used for the recent preventative maintenance ( PM) relay replacements. The relays were determined to be unreliable since the initial PM replacement on 10/19/16 until 12/5/16, when the quality issue was identified and relays from a different lot were installed. The B train of MCR HVAC was determined to be inoperable due to the relay issue for a period of 47 days, which is greater than the allowable Limiting Condition for Operation (LCO) action window of 7 days (per TS 3.7.2.a.1) for an inoperable Control Room Emergency Fresh Air System ( CREFAS) train.
Therefore, this was a condition prohibited by Technical Specifications (TS). |
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Category:Letter
MONTHYEARML24151A3842024-10-31031 October 2024 – Issuance of Amendment Nos. 264 and 226 Support to Digital Modernization Project Installation (EPID L-2023-LLA-0025) and Exemption from the Requirements of 10 CFR 50.62 ML24303A0902024-10-29029 October 2024 Operator Licensing Examination Approval ML24303A2782024-10-29029 October 2024 10 CFR 50.46 Annual Report ML24299A2642024-10-25025 October 2024 Response to Request for Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications IR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24278A3022024-10-0404 October 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10 CFR 50.62 ATWS Rule to Support the Digital Modernization Project Installation - Rev Unit 2 Technical Spec ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24263A0032024-09-27027 September 2024 Generation Station, Units 1 and 2 – Regulatory Audit Plan Supporting Review of the Component Interface Module System of the Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) (Redacted) ML24243A0482024-09-19019 September 2024 Generation Station, Unit Nos. 1 and 2 - Schedule Update for License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24215A4042024-09-18018 September 2024 Request for Withholding Information from Public Disclosure IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) ML24241A1952024-08-28028 August 2024 License Amendment Request for Modification to Technical Specification 3.6.1.2 and Main Steam Isolation Valve Leakage Rate Requirements ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24163A3902024-08-14014 August 2024 Request for Withholding Information from Public Disclosure ML24220A2392024-08-12012 August 2024 Correction to Technical Specification Page 3/4 3-11 in Amendment No. 225 IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24204A0712024-07-29029 July 2024 Issuance of Amendment Nos. 263 and 225 Technical Specifications for Main Steam Line Tunnel Temperature ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24208A1592024-07-25025 July 2024 Regulatory Audit Plan Supporting Review of the System Development Portion of Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML24201A1662024-07-19019 July 2024 Response to Request for Additional Information for License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam L ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24180A1572024-06-28028 June 2024 Request to Return and Replace WEC Documents (EQ-EV-386-GLIM, EQ-QR- 433-GLIM, and APP-GW-GLR-611), to Meet 10CFR2.390 Request to Withdraw from Public Disclosure Requirements ML24170A7702024-06-20020 June 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, Opportunity for Hearing(Epid L-2024-LLA-0079) LTR 05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 ML24166A1142024-06-14014 June 2024 Response to Requests for Additional Information (RAIs 15 Through 23) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24165A2642024-06-13013 June 2024 License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam Line Tunnel Temperature TS 3/4.7.9 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker ML24151A2882024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24151A2012024-06-10010 June 2024 Request for Withholding Information from Public Disclosure 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24149A2112024-05-28028 May 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 ML24124A0432024-05-0303 May 2024 Response to Requests for Additional Information (RAIs 9 Through 14) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24114A3222024-04-23023 April 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) - Pivot to Unit ML24109A0702024-04-18018 April 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFRC50.52 ATWS Rule to Support the Digital Modernization Project Installation . 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2023-001, Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications2023-06-26026 June 2023 Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications 05000352/LER-2022-001, Regarding HPCI Inoperable Due to Inadvertent Isolation Signal2022-12-13013 December 2022 Regarding HPCI Inoperable Due to Inadvertent Isolation Signal 05000352/LER-2021-001, HPCI Inoperable Due to Remote Shutdown Panel Switch Failure2021-11-22022 November 2021 HPCI Inoperable Due to Remote Shutdown Panel Switch Failure 05000352/LER-2017-0012017-01-27027 January 2017 Condition Prohibited by TS due to Parts Quality Issue, LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue 05000353/LER-2016-0012016-07-27027 July 2016 Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error, LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 05000352/LER-2016-0032016-05-18018 May 2016 Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak, LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak 05000352/LER-2016-0022016-04-11011 April 2016 Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements, LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements 05000352/LER-2016-0012016-03-23023 March 2016 Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock, LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function 2024-06-18
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Limerick Generating Station, Units 1 and 2 05000352 & 05000353
3. LER NUMBER
2017 - 00 001 I. Unit Conditions Prior to the Event Limerick Generating Station (LGS) Units 1 and 2 were both operating in Operational Condition (OPCON) 1 at 100 percent power at the time of the event. There were no other structures, systems, or components inoperable at the time of the event that contributed to the event.
II. Description of the Event
Over a period of approximately one month, the Main Control Room (MCR) Heating, Ventilating and Air Conditioning (HVAC) system experienced four failures. Three of the failures were caused by an intermittent dropout, or chattering of the LOOP start relay for two fans (0B-V116 MCR Supply and OB-V121 MCR Return Fans). The fourth failure was due to a contactor in the MCC for the OB-V116 MCR Supply Fan. Each of these events caused an unplanned Limiting Condition for Operation (LCO) entry and inoperability of the Control Room Emergency Fresh Air Supply (CREFAS) system. A timeline of events is as follows:
10/19/16 - KS-078-326B and KS-078-359B relays replaced for Preventative Maintenance (PM).
Post Maintenance Testing (PMT) was performed by running the OB MCR HVAC train.
11/13/2016 - To support chiller swaps the OA MCR HVAC train was secured and Operations attempted to start the OB train. This was the first start attempt since the PMT performance on 10/19/16. When the supply fan handswitch was placed in RUN, the fan did not start. Relay replacements were performed for KS-078-026B, which was found failed, and KS-078-326B, which was found chattering. Following replacements, the supply fan was started successfully.
When Operations attempted to start the OB return fan by placing the handswitch in RUN, it did not start. The KS-078-359B relay was found chattering, thereby preventing the return fan from starting.
11/20/16 - After running the OB train of MCR HVAC for a period of one week, the supply fan tripped. The contactor was observed to be chattering. Breaker maintenance was performed and the contactors were replaced. Additionally, new wiring was installed internal to the breaker cubicle. During troubleshooting, the KS-078-326B and KS-078-026B relays were removed from the field and bench tested satisfactorily.
11/29/16 - To support a MCR chiller swap, the OA MCR fans were secured and Operations attempted to start the OB train. When the supply fan handswitch was placed in RUN, the fan did not start. The cause was determined to be a failed KS-078-326B relay.
12/5/16 - The 'B' MCR Return fan tripped and the 'A' MCR return fan auto-started.
Troubleshooting efforts identified a chattering KS-078-359B relay in the field.
On 11/29/16, the site believed that the relay failure was not an infantile failure and that there may be a common condition that was causing these failures. The relay was sent for testing and evaluation, and on 12/15/16, the station received the analysis which identified a manufacturing issue had caused the relay failures.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Limerick Generating Station, Units 1 and 2 05000352 & 05000353
3. LER NUMBER
2017 - 00 001
III. Analysis of the Event
The identified relay failures were all determined to be attributed to intermittent drop out, or chattering of the installed Agastat/Tyco model ETR1413D004 (ETR TDPU series) relay coil.
These relays were all installed as normally energized, power monitoring/ Loss of Offsite Power (LOOP) start relays. They are installed to allow a 35-second time delay before the fan restarts on re-energization of the associated load center during a LOOP.
The testing determined that the relays were not reliable and failure of the relays could not be predicted. The OB MCR HVAC train was determined to be unreliable since the initial relay replacement on 10/19/16 until when the relays were replaced with relays from a different lot on 12/05/16. The B train of MCR HVAC was conservatively determined to be inoperable for a period of 47 days, which is greater than the allowable LCO action window of 7 days (per TS 3.7.2.a.1) for an inoperable CREFAS train, and therefore was deemed to be a condition prohibited by TS.
IV. Cause of the Event
Bench tests were performed on-site on the removed relays in addition to failure analysis by an offsite testing facility. This testing determined the cause of the relay chattering to be an incorrectly installed capacitor on the internal timing circuit board.
V. Corrective Actions Completed/Planned Extent of condition actions were taken to replace all of the Agastat 2016 ETR relays installed at Limerick. A total of two additional relays, from the same lot, were identified to be installed in the plant and both these relays were proactively replaced.
A Part 21 was generated by TE Connectivity for the manufacturing issue. (ML17006A011) VI. Previous Similar Occurrences There were no previous similar occurrences in the last five years of MCR Supply fan and Return fan trips due to defective relays.
VII. Component data:
System: V Central Control Complex Env. Ctrl. Sys.
Component: RLY Relay, Time- Delay Starting or Closing Component number: KS-078-326B & KS-078-359B Manufacturer: T351 Tyco Instrument DIV Model number: ETR1413D004
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05000352/LER-2017-001 | Condition Prohibited by TS due to Parts Quality Issue LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue | |
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