03-23-2016 | Unit 1 reactor enclosure secondary containment integrity was briefly declared inoperable when both doors on a reactor enclosure 201' elevation pipe tunnel airlock were simultaneously opened. The cause of the event was a degraded closing mechanism on the airlock inboard door. The airlock doors were closed to restore reactor enclosure secondary containment integrity. The degraded inboard door closing mechanism was repaired. |
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Category:Letter
MONTHYEARML24151A3842024-10-31031 October 2024 – Issuance of Amendment Nos. 264 and 226 Support to Digital Modernization Project Installation (EPID L-2023-LLA-0025) and Exemption from the Requirements of 10 CFR 50.62 ML24303A0902024-10-29029 October 2024 Operator Licensing Examination Approval ML24303A2782024-10-29029 October 2024 10 CFR 50.46 Annual Report ML24299A2642024-10-25025 October 2024 Response to Request for Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications IR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24278A3022024-10-0404 October 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10 CFR 50.62 ATWS Rule to Support the Digital Modernization Project Installation - Rev Unit 2 Technical Spec ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24263A0032024-09-27027 September 2024 Generation Station, Units 1 and 2 – Regulatory Audit Plan Supporting Review of the Component Interface Module System of the Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) (Redacted) ML24243A0482024-09-19019 September 2024 Generation Station, Unit Nos. 1 and 2 - Schedule Update for License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24215A4042024-09-18018 September 2024 Request for Withholding Information from Public Disclosure IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) ML24241A1952024-08-28028 August 2024 License Amendment Request for Modification to Technical Specification 3.6.1.2 and Main Steam Isolation Valve Leakage Rate Requirements ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24163A3902024-08-14014 August 2024 Request for Withholding Information from Public Disclosure ML24220A2392024-08-12012 August 2024 Correction to Technical Specification Page 3/4 3-11 in Amendment No. 225 IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24204A0712024-07-29029 July 2024 Issuance of Amendment Nos. 263 and 225 Technical Specifications for Main Steam Line Tunnel Temperature ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24208A1592024-07-25025 July 2024 Regulatory Audit Plan Supporting Review of the System Development Portion of Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML24201A1662024-07-19019 July 2024 Response to Request for Additional Information for License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam L ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24180A1572024-06-28028 June 2024 Request to Return and Replace WEC Documents (EQ-EV-386-GLIM, EQ-QR- 433-GLIM, and APP-GW-GLR-611), to Meet 10CFR2.390 Request to Withdraw from Public Disclosure Requirements ML24170A7702024-06-20020 June 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, Opportunity for Hearing(Epid L-2024-LLA-0079) LTR 05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 ML24166A1142024-06-14014 June 2024 Response to Requests for Additional Information (RAIs 15 Through 23) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24165A2642024-06-13013 June 2024 License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam Line Tunnel Temperature TS 3/4.7.9 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker ML24151A2882024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24151A2012024-06-10010 June 2024 Request for Withholding Information from Public Disclosure 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24149A2112024-05-28028 May 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 ML24124A0432024-05-0303 May 2024 Response to Requests for Additional Information (RAIs 9 Through 14) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24114A3222024-04-23023 April 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) - Pivot to Unit ML24109A0702024-04-18018 April 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFRC50.52 ATWS Rule to Support the Digital Modernization Project Installation . 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2023-001, Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications2023-06-26026 June 2023 Emergency Diesel Generator Lube Oil Pressure Sensing Line Leak Resulting in a Condition Prohibited by Technical Specifications 05000352/LER-2022-001, Regarding HPCI Inoperable Due to Inadvertent Isolation Signal2022-12-13013 December 2022 Regarding HPCI Inoperable Due to Inadvertent Isolation Signal 05000352/LER-2021-001, HPCI Inoperable Due to Remote Shutdown Panel Switch Failure2021-11-22022 November 2021 HPCI Inoperable Due to Remote Shutdown Panel Switch Failure 05000352/LER-2017-0012017-01-27027 January 2017 Condition Prohibited by TS due to Parts Quality Issue, LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue 05000353/LER-2016-0012016-07-27027 July 2016 Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error, LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 05000352/LER-2016-0032016-05-18018 May 2016 Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak, LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak 05000352/LER-2016-0022016-04-11011 April 2016 Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements, LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements 05000352/LER-2016-0012016-03-23023 March 2016 Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock, LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function 2024-06-18
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry.
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Unit Conditions Prior to the Event Unit 1 was in Operational Condition (OPCON) 1 (Power Operation) at 100 percent power.
There were no structures, systems or components out of service that contributed to this event.
Description of the Event
On Monday, January 25, 2016, Limerick Unit 1 was operating at 100 percent power with maintenance ongoing in the residual heat removal service water (RHRSW) / emergency service water (ESW) pipe tunnel. At approximately 1819 hours0.0211 days <br />0.505 hours <br />0.00301 weeks <br />6.921295e-4 months <br />, the main control room supervisor (CRS) was notified that the local airlock open door alarm (EIIS:ALM) was activated when a worker in the pipe tunnel opened the airlock outboard (pipe tunnel side) door (El IS:DR). The alarm indicated that both air lock doors were briefly opened for one reactor enclosure airlock. The reactor enclosure low pressure alarm setpoint is 0.20 inches of vacuum water gauge (WG) and the reactor enclosure low pressure alarm did not actuate during the event. The airlock was open for less than 10 seconds; therefore, the main control room airlock open alarm did not actuate. The reactor enclosure secondary containment integrity (El IS:NH) was declared inoperable for the period when both doors were open.
An investigation determined that a worker using the airlock properly verified that the door open blue light indication was not lit and then opened the outboard airlock door which activated the local airlock open alarm. The most likely cause of the alarm was a degraded inboard door closing mechanism that resulted in the inboard door opening far enough to activate the alarm when the outboard door was opened. The worker immediately reclosed the open outboard door when the local alarm actuated and the breach of secondary containment was terminated. The airlock was open for a period of less than 10 seconds.
The worker notified Operations shift management of the containment breach.
TS 3.6.5.1.1 Reactor Enclosure Secondary Containment Integrity surveillance requirement 4.6.5.1.1.a requires verification that reactor enclosure pressure is greater than or equal to 0.25 inches of vacuum water gauge on a 24-hour frequency. The TS surveillance requirement 4.6.5.1.1.b.2 requires at least one door in each access to the reactor enclosure be verified closed on a 31-day frequency. TS 3.6.5.1.1 is applicable in operational conditions (OPCON) 1, 2, and 3.
This LER is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(v)(C) for a condition that could have prevented the fulfillment of the safety function of structures or systems needed to control the release of radioactive material.
NEI 99-02 (Revision 7), Regulatory Assessment Performance Indicator Guideline, section 2.2 Mitigating Systems Cornerstone, Safety System Functional Failures, Clarifying Notes, states the following:
Engineering analyses: events in which the licensee declared a system inoperable but an engineering analysis later determined that the system was capable of performing its safety function are not counted, even if the system was removed from service to perform the analysis.
This event will not be reported in the NRC performance indicator (PI) for safety system functional failures (SSFF) since an engineering analysis (technical evaluation) was performed which determined that the system was capable of performing its safety function during events when the airlock was open for less than 10 seconds. The post-LOCA dose calculation does not credit reactor enclosure secondary containment integrity for mitigation of on-site and off- site doses for the first 15.5 minutes of the event. Therefore, this event is bounded by the existing dose calculation.
Analysis of the Event
There was no actual safety consequence associated with this event. The potential safety consequences of this event were minimal. Both doors on the airlock were open simultaneously for less than 10 seconds.
To prevent a breach of secondary containment each reactor enclosure airlock is equipped with door open indicating lights that are used to locally verify the door status. If both doors are opened simultaneously a local alarm is actuated. If both doors remain open for greater than 10 seconds, an alarm is actuated in the main control room and operators are dispatched to verify that the airlock doors are closed.
UFSAR 6.2.3.2.1 describes the secondary containment design. The reactor enclosure secondary containment (Zones I and II) is designed to limit the inleakage to 200% of their zone free volume per day, and the refueling area secondary containment (Zone III) is designed to limit the inleakage to 50% of its zone free volume per day. These inleakage rates are based on a negative interior pressure of 0.25 inches wg, while operating the standby gas treatment system (SGTS). Following a LOCA the affected zone is maintained at this negative pressure by operation of the SGTS.
Cause of the Event
The cause of the event was a degraded closing mechanism on the airlock inboard door. This event was not prevented by the design of the reactor enclosure airlocks since there is no mechanical interlock and the door open indicating light does not prevent simultaneous opening of both airlock doors.
Corrective Action Completed The airlock doors were closed to restore reactor enclosure secondary containment integrity.
The degraded inboard door closing mechanism was adjusted.
Previous Similar Occurrences Unit 2 LER 2015-006, Unit 2 LER 2014-007, Unit 2 LER 2014-004, Unit 2 LER 2014-003, Unit 1 LER 2014-003, Unit 2 LER 2014-002, Unit 2 LER 2014-001, Unit 1 LER 2014-002, Unit 1 LER 2014-001, and Unit 2 LER 2013-003 were submitted due to reactor enclosure airlock breaches allowed by the airlock design. Unit 2 LER 2013-002 was submitted due to a reactor enclosure airlock breach caused by a non-functional airlock door open indicating light not providing the correct door status. Unit 2 LER 2014-006 was submitted due to a reactor enclosure airlock breach caused by a door improperly latched closed.
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05000353/LER-2016-001 | Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000352/LER-2016-001 | Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000352/LER-2016-002 | Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2016-003 | Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
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