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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000305/LER-1998-003, :on 980203,RCS Low Flow Trip Logic Were Identified as Not Been Tested IAW Tss.Caused by Personnel Error.Testing Was Conducted IAW Requirements of Section 4 of TS1998-03-0505 March 1998
- on 980203,RCS Low Flow Trip Logic Were Identified as Not Been Tested IAW Tss.Caused by Personnel Error.Testing Was Conducted IAW Requirements of Section 4 of TS
05000305/LER-1996-007, :on 961023,identified Design Deficiency in Containment Isolation Function.Caused by Oversight During Plant Design.Implemented Administrative Controls to Preclude Subject Condition Prior to Plant start-up1996-11-22022 November 1996
- on 961023,identified Design Deficiency in Containment Isolation Function.Caused by Oversight During Plant Design.Implemented Administrative Controls to Preclude Subject Condition Prior to Plant start-up
05000305/LER-1995-003, :on 950516,failed to Adequately Assess Consequences During Recovery from Switch Misposition Resulted in Turbine/Rt.Reminded Nco of Importance of Self Checking1995-06-14014 June 1995
- on 950516,failed to Adequately Assess Consequences During Recovery from Switch Misposition Resulted in Turbine/Rt.Reminded Nco of Importance of Self Checking
05000305/LER-1990-005, :on 900404,intergranular Attack & IGSCC Results in Both Steam Generators a & B Being Categorized as C-3.All Defective Tubes Plugged & Sludge Lancing & Crevice Flushing Conducted1990-05-0404 May 1990
- on 900404,intergranular Attack & IGSCC Results in Both Steam Generators a & B Being Categorized as C-3.All Defective Tubes Plugged & Sludge Lancing & Crevice Flushing Conducted
05000305/LER-1989-009, :on 890401,during Repositioning of Ventilation Dampers,Jumper Inadvertently Detached from Terminal Block Contact,Causing Damper Actuation.Caused by Procedural Inadequacies.Weidmuller Blocks Installed1989-05-0101 May 1989
- on 890401,during Repositioning of Ventilation Dampers,Jumper Inadvertently Detached from Terminal Block Contact,Causing Damper Actuation.Caused by Procedural Inadequacies.Weidmuller Blocks Installed
05000305/LER-1989-006, :on 890315,audit Identified Failure to Implement Tech Spec Re Testing of Fan Coil Emergency Discharge Dampers & Backfit Dampers.Caused by Procedural Inadequacy.Procedure Updated1989-04-14014 April 1989
- on 890315,audit Identified Failure to Implement Tech Spec Re Testing of Fan Coil Emergency Discharge Dampers & Backfit Dampers.Caused by Procedural Inadequacy.Procedure Updated
05000305/LER-1989-005, :on 890310,insp of Diesel Generator Start Up Air Sys Finds Deficiencies That Could Render Both Diesel Generators Inoperable Due to Inadequate Design.Cause Unknown.Generic Implications Will Be Examined1989-04-10010 April 1989
- on 890310,insp of Diesel Generator Start Up Air Sys Finds Deficiencies That Could Render Both Diesel Generators Inoperable Due to Inadequate Design.Cause Unknown.Generic Implications Will Be Examined
05000305/LER-1987-002, :on 870224,reactor Tripped When Source Range Nuclear Flux Detectors 1 & 2 Erroneously Reached Nominal Reactor Trip Setpoint of 1.0E05 Counts/S.Caused by Seepage of Borated Refueling Water Into Instrument1987-03-26026 March 1987
- on 870224,reactor Tripped When Source Range Nuclear Flux Detectors 1 & 2 Erroneously Reached Nominal Reactor Trip Setpoint of 1.0E05 Counts/S.Caused by Seepage of Borated Refueling Water Into Instrument
05000305/LER-1987-001, :on 870223 & 24,series of High Radiation Alarms Received in Control Room.Caused by Primary to Secondary Leak in Steam Generator 1A.Results of Eddy Current Testing Will Be Submitted1987-03-25025 March 1987
- on 870223 & 24,series of High Radiation Alarms Received in Control Room.Caused by Primary to Secondary Leak in Steam Generator 1A.Results of Eddy Current Testing Will Be Submitted
05000305/LER-1985-015, :on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 211987-03-0606 March 1987
- on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 21
05000305/LER-1986-015, :on 861229,svc Water Inlet Valve for Radiation Monitor R-16 Found Closed.Caused by Personnel Error.Sight Flow Meter Cleaned & Operating Procedure Used to Perform Flushing Process Reviewed1987-01-28028 January 1987
- on 861229,svc Water Inlet Valve for Radiation Monitor R-16 Found Closed.Caused by Personnel Error.Sight Flow Meter Cleaned & Operating Procedure Used to Perform Flushing Process Reviewed
05000305/LER-1986-014, :on 861202,during Full Power,Boric Acid Transfer Pumps Inoperable.Caused by Burned Off Section of Heat Tape Around Pump Casing.Insulation on Pump Replaced & Extended to Cover Mechanical Seal & Casing1986-12-31031 December 1986
- on 861202,during Full Power,Boric Acid Transfer Pumps Inoperable.Caused by Burned Off Section of Heat Tape Around Pump Casing.Insulation on Pump Replaced & Extended to Cover Mechanical Seal & Casing
05000305/LER-1986-013, :on 861030,gate to Waste Metering Tank Room, Posted as High Contamination & Radiation Hazard Area, Discovered Unlocked & Open.Caused by Personnel Error.Survey of Area Performed & Procedures Revised1986-11-26026 November 1986
- on 861030,gate to Waste Metering Tank Room, Posted as High Contamination & Radiation Hazard Area, Discovered Unlocked & Open.Caused by Personnel Error.Survey of Area Performed & Procedures Revised
05000305/LER-1986-012, :on 860926,auxiliary Bldg Vent Stack Radiation Monitor Indications Elevated Due to Radioactive Ar-41 Gas & on 861006,zone Special Ventilation Sys Automatically Started on High Radiation Signal Due to Low Setpoints1986-10-24024 October 1986
- on 860926,auxiliary Bldg Vent Stack Radiation Monitor Indications Elevated Due to Radioactive Ar-41 Gas & on 861006,zone Special Ventilation Sys Automatically Started on High Radiation Signal Due to Low Setpoints
05000305/LER-1984-006, :on 840416,containment Isolation Valves Found W/Excessive Leakage Rates Due to Degraded Seal Ring Gaskets. Repairs Performed on Inboard Valves & Design Change Implemented to Relocate Valves1986-09-23023 September 1986
- on 840416,containment Isolation Valves Found W/Excessive Leakage Rates Due to Degraded Seal Ring Gaskets. Repairs Performed on Inboard Valves & Design Change Implemented to Relocate Valves
05000305/LER-1986-011, :on 860811,during Performance of Monthly Fire Pump Flow Test,Both Fire Pumps Simultaneously Out of Svc for Approx 10 S.Caused by Personnel Failure to Follow Procedure.Personnel Counseled1986-09-10010 September 1986
- on 860811,during Performance of Monthly Fire Pump Flow Test,Both Fire Pumps Simultaneously Out of Svc for Approx 10 S.Caused by Personnel Failure to Follow Procedure.Personnel Counseled
05000305/LER-1986-010, :on 860801,ESF Actuation Occurred Due to Electrical Jumper Shorting to Ground.Caused by Low Profile Design of Connecting Screws on Terminal Strip.Banana Jacks Added Where Jumpers Used1986-08-28028 August 1986
- on 860801,ESF Actuation Occurred Due to Electrical Jumper Shorting to Ground.Caused by Low Profile Design of Connecting Screws on Terminal Strip.Banana Jacks Added Where Jumpers Used
05000305/LER-1986-008, :on 860513,reactor/turbine Trip Occurred During Performance of Surveillance Procedure on power-range Nuclear Instrumentation.Caused by Personnel Error.Labeling of Instrumentation Upgraded1986-06-12012 June 1986
- on 860513,reactor/turbine Trip Occurred During Performance of Surveillance Procedure on power-range Nuclear Instrumentation.Caused by Personnel Error.Labeling of Instrumentation Upgraded
05000305/LER-1986-007, :on 860424,reactor Tripped Due to Low Steam Generator Level Coincident W/Steam & Feedwater Flow Mismatch.Caused by Defective Main Feedwater Control Valve. Valve Stroked & Cycled Until Operable1986-05-23023 May 1986
- on 860424,reactor Tripped Due to Low Steam Generator Level Coincident W/Steam & Feedwater Flow Mismatch.Caused by Defective Main Feedwater Control Valve. Valve Stroked & Cycled Until Operable
05000305/LER-1986-006, :on 860420,turbine Trip & Reactor Trip Occurred.Caused by Main Feedwater Control Valve Sticking. Valve Inspected,Adjusted & Cycled to Verify Operability Prior to Restart1986-05-20020 May 1986
- on 860420,turbine Trip & Reactor Trip Occurred.Caused by Main Feedwater Control Valve Sticking. Valve Inspected,Adjusted & Cycled to Verify Operability Prior to Restart
05000305/LER-1986-005, :on 860417,reactor Trip Occurred During Performance of Work Request on Intermediate-Range Nuclear Channel N35.Caused by Premature Removal of Control Power Fuse1986-05-16016 May 1986
- on 860417,reactor Trip Occurred During Performance of Work Request on Intermediate-Range Nuclear Channel N35.Caused by Premature Removal of Control Power Fuse
05000305/LER-1986-004, :on 860401,nonspring-assisted Fire Dampers Mechanically Bound in Intermediate Position.Caused by Not Testing Dampers.Testing of Dampers Continuing & Damper Design Changes Initiated1986-05-14014 May 1986
- on 860401,nonspring-assisted Fire Dampers Mechanically Bound in Intermediate Position.Caused by Not Testing Dampers.Testing of Dampers Continuing & Damper Design Changes Initiated
05000305/LER-1986-003, :on 860326,potential Problem Found w/long-term Reliability of Both Backup Emergency Ac Diesel Generators. Caused by Numerous Fast Starts of Diesel Generator W/O Full Main Lube Oil Pressure1986-04-25025 April 1986
- on 860326,potential Problem Found w/long-term Reliability of Both Backup Emergency Ac Diesel Generators. Caused by Numerous Fast Starts of Diesel Generator W/O Full Main Lube Oil Pressure
05000000/LER-1986-005-03, Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points1986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000305/LER-1986-002, :on 860318,local Leak Rate Test Results Exceeded Tech Spec Limit.Caused by Degraded Component Performance at Three Penetrations.Valves Lapped,Repacked & Satisfactorily Retested1986-04-17017 April 1986
- on 860318,local Leak Rate Test Results Exceeded Tech Spec Limit.Caused by Degraded Component Performance at Three Penetrations.Valves Lapped,Repacked & Satisfactorily Retested
05000305/LER-1986-001, :on 860211,review of Retest Requirements Re Solenoid Valve Replacement Revealed Valve Timing Test Not Performed During 1985.Caused by Erroneous Deletion from Procedures.Test Performed1986-03-13013 March 1986
- on 860211,review of Retest Requirements Re Solenoid Valve Replacement Revealed Valve Timing Test Not Performed During 1985.Caused by Erroneous Deletion from Procedures.Test Performed
05000305/LER-1985-023, :on 851212,loss of Power to Instrument Bus I Occurred.Caused by Failure of Constant Voltage Transformer. Constant Voltage Transformer Replaced & Instrument Bus Returned to Normal Power Supply1986-01-10010 January 1986
- on 851212,loss of Power to Instrument Bus I Occurred.Caused by Failure of Constant Voltage Transformer. Constant Voltage Transformer Replaced & Instrument Bus Returned to Normal Power Supply
05000305/LER-1985-022, :on 851203,discovered That Surveillance Procedure Sp 48-046,conducted on 851127,performed Outside of Required Time Interval.Caused by Calibr of Nuclear Instrumentation Due to 851113 Trip1986-01-0202 January 1986
- on 851203,discovered That Surveillance Procedure Sp 48-046,conducted on 851127,performed Outside of Required Time Interval.Caused by Calibr of Nuclear Instrumentation Due to 851113 Trip
05000305/LER-1985-021, :on 851114,high Flux Shutdown Bistable Trip Value Recorded in Place of High Flux Level Trip Setpoint on Both Source Range Channels.Caused by Personnel Error. Individuals Counseled on Procedure Performance1985-12-26026 December 1985
- on 851114,high Flux Shutdown Bistable Trip Value Recorded in Place of High Flux Level Trip Setpoint on Both Source Range Channels.Caused by Personnel Error. Individuals Counseled on Procedure Performance
05000305/LER-1985-020, :on 851113,failure of Train a Main Feedwater Control Valve Caused lo-lo Water Level in Steam Generator 1A & Reactor Trip.Caused by Two of Four Cap Screws Holding Valve Actuator to Yoke Shearing1985-12-13013 December 1985
- on 851113,failure of Train a Main Feedwater Control Valve Caused lo-lo Water Level in Steam Generator 1A & Reactor Trip.Caused by Two of Four Cap Screws Holding Valve Actuator to Yoke Shearing
05000305/LER-1985-019, :on 851107,at 100% Power,Test of Undervoltage Trip Attachment Conducted for Each Reactor Trip Breaker to Verify Existence of 20 Oz of Force Margin,Per IE Bulletin 85-002.Two Breakers Failed1985-12-0606 December 1985
- on 851107,at 100% Power,Test of Undervoltage Trip Attachment Conducted for Each Reactor Trip Breaker to Verify Existence of 20 Oz of Force Margin,Per IE Bulletin 85-002.Two Breakers Failed
05000305/LER-1985-018, :on 850820,discovered That Fire Hose Insp Required by Tech Spec 4.15.2 Performed Outside Required 18-month (Plus or Minus 25%) Time Interval.Caused by Mgt Oversight When Procedure Modified1985-09-19019 September 1985
- on 850820,discovered That Fire Hose Insp Required by Tech Spec 4.15.2 Performed Outside Required 18-month (Plus or Minus 25%) Time Interval.Caused by Mgt Oversight When Procedure Modified
05000305/LER-1985-017, :on 850808,reactor Tripped Manually to Isolate Ruptured Excess Steam Vent Line.Caused by Carbon Steel Piping Erosion.Ruptured Vent Lines Replaced.Program Implemented to Examine Steam Line Piping1985-09-0606 September 1985
- on 850808,reactor Tripped Manually to Isolate Ruptured Excess Steam Vent Line.Caused by Carbon Steel Piping Erosion.Ruptured Vent Lines Replaced.Program Implemented to Examine Steam Line Piping
05000305/LER-1985-016, :on 850725,control Operator Observed That Position Indication for Containment Isolation Valves & Steam Exclusion Dampers Changed Position.Caused by Power Interruption & Loss of Sys Redundancy1985-08-26026 August 1985
- on 850725,control Operator Observed That Position Indication for Containment Isolation Valves & Steam Exclusion Dampers Changed Position.Caused by Power Interruption & Loss of Sys Redundancy
05000305/LER-1985-015, :on 850617,Fluor Engineers Notified Util That Seismic Qualification of Emergency Diesel Generator Differential Relays Could Not Be Conclusively Determined. Resolution Under Review1985-07-17017 July 1985
- on 850617,Fluor Engineers Notified Util That Seismic Qualification of Emergency Diesel Generator Differential Relays Could Not Be Conclusively Determined. Resolution Under Review
05000305/LER-1985-014, :on 850615,concrete Block Preventing Access to Spent Resin Storage Tank Room Found Removed.Caused by Design Change & Maint Work on Tank.Requirements for Securing High Radiation Areas Discussed1985-07-15015 July 1985
- on 850615,concrete Block Preventing Access to Spent Resin Storage Tank Room Found Removed.Caused by Design Change & Maint Work on Tank.Requirements for Securing High Radiation Areas Discussed
05000305/LER-1985-013, :on 850404 & 0505,heat Tracing Circuit on Suction Line to Containment Hydrogen Analyzer 1A Discovered Inoperable.Caused by Failed Amphenol Connector.Spare Parts Ordered & Failed Connector Bypassed1985-06-12012 June 1985
- on 850404 & 0505,heat Tracing Circuit on Suction Line to Containment Hydrogen Analyzer 1A Discovered Inoperable.Caused by Failed Amphenol Connector.Spare Parts Ordered & Failed Connector Bypassed
05000305/LER-1985-012, :on 850410,reactor Tripped.Caused by Differences in Ground Potential Between Ni & Test Equipment. Purchase of New Portable Picoammeter Being Considered1985-05-10010 May 1985
- on 850410,reactor Tripped.Caused by Differences in Ground Potential Between Ni & Test Equipment. Purchase of New Portable Picoammeter Being Considered
05000305/LER-1985-011, :on 850407,auxiliary Bldg Special Ventilation Sys Actuated from Steam Exclusion Signal.Caused by Steam Issuing Through Blown Rupture Disk on Boric Acid Evaporator Condenser.Ventilation Sys Reset1985-05-0707 May 1985
- on 850407,auxiliary Bldg Special Ventilation Sys Actuated from Steam Exclusion Signal.Caused by Steam Issuing Through Blown Rupture Disk on Boric Acid Evaporator Condenser.Ventilation Sys Reset
05000305/LER-1985-010, :on 850405,reactor Trip Occurred Due to Steam Flow Greater than Feed Flow Signal Coincident W/Lo Steam Generator Level Signal.Caused by One Feed Flow & One Steam Low Transmitter Out of Calibr1985-05-0303 May 1985
- on 850405,reactor Trip Occurred Due to Steam Flow Greater than Feed Flow Signal Coincident W/Lo Steam Generator Level Signal.Caused by One Feed Flow & One Steam Low Transmitter Out of Calibr
05000305/LER-1984-018, :on 840928,investigation of Fan Coil Units W/Less than Design Air Flow Revealed Svc Water Side of Cooling Coils Partially Plugged W/Silt.Caused by Equipment Deficiencies.Fan Coil Units Cleaned1985-04-17017 April 1985
- on 840928,investigation of Fan Coil Units W/Less than Design Air Flow Revealed Svc Water Side of Cooling Coils Partially Plugged W/Silt.Caused by Equipment Deficiencies.Fan Coil Units Cleaned
05000305/LER-1985-007, :on 850225,w/red Pressurizer Channel Tripped & White Channel Calibr,Safety Injection Signal Occurred. Caused by Technician Requesting Wrong Channel Be Tripped. Surveillance Procedure Revised1985-03-27027 March 1985
- on 850225,w/red Pressurizer Channel Tripped & White Channel Calibr,Safety Injection Signal Occurred. Caused by Technician Requesting Wrong Channel Be Tripped. Surveillance Procedure Revised
05000305/LER-1985-008, :on 850225,alarm 47001-34 for Condenser Low Vacuum Turbine Trip,Cleared & Alarmed Again & Both Diesel Generators Started.Caused by Maint to Turbine Trip Mechanism.Start Signal Will Be Removed1985-03-27027 March 1985
- on 850225,alarm 47001-34 for Condenser Low Vacuum Turbine Trip,Cleared & Alarmed Again & Both Diesel Generators Started.Caused by Maint to Turbine Trip Mechanism.Start Signal Will Be Removed
05000305/LER-1985-006, :on 850220,steam Generator Tube Found Incorrectly Plugged.Possibly Caused by Mismarked Tube Sheet. Template Marked to Identify Tubes to Be Plugged1985-03-15015 March 1985
- on 850220,steam Generator Tube Found Incorrectly Plugged.Possibly Caused by Mismarked Tube Sheet. Template Marked to Identify Tubes to Be Plugged
05000305/LER-1985-004, :on 850210,control Room Operator Noticed Reactor Coolant Pump 1B Running.Caused by Grounded Condition in Actuation Circuitry Due to Water Accumulation in Pressure Switch.Hardware Mod Being Evaluated1985-03-13013 March 1985
- on 850210,control Room Operator Noticed Reactor Coolant Pump 1B Running.Caused by Grounded Condition in Actuation Circuitry Due to Water Accumulation in Pressure Switch.Hardware Mod Being Evaluated
05000305/LER-1985-005, :on 850211,exhaust Fan 1A of Auxiliary Bldg Special Ventilation Sys Found Running.Caused by Burnt Out Coil in Solenoid Valve Controlling Air to Zone SV Exhaust Filter 1A Inlet Damper.Valve Replaced1985-03-13013 March 1985
- on 850211,exhaust Fan 1A of Auxiliary Bldg Special Ventilation Sys Found Running.Caused by Burnt Out Coil in Solenoid Valve Controlling Air to Zone SV Exhaust Filter 1A Inlet Damper.Valve Replaced
05000305/LER-1985-003, :on 850208,reactor Tripped.Caused by Decrease in Steam Generator Vol to Low Level Alarm Setpoints. Corrective Action Being Investigated1985-03-0808 March 1985
- on 850208,reactor Tripped.Caused by Decrease in Steam Generator Vol to Low Level Alarm Setpoints. Corrective Action Being Investigated
05000305/LER-1985-002, :on 850125,seismic Analysis for nonsafety- Related Piping Section of Containment Integrated Leak Rate Test Penetration Could Not Be Located.Design Change Will Be Completed During 1985 Refueling Shutdown1985-02-24024 February 1985
- on 850125,seismic Analysis for nonsafety- Related Piping Section of Containment Integrated Leak Rate Test Penetration Could Not Be Located.Design Change Will Be Completed During 1985 Refueling Shutdown
05000305/LER-1985-001, :on 850122,inadvertent Actuation of Internal Containment Spray Sys 1B Occurred,Discharging Approx 2,500 Gallons Borated Water Into Containment Bldg.Operator Secured Sys & Reset Containment Spray1985-02-21021 February 1985
- on 850122,inadvertent Actuation of Internal Containment Spray Sys 1B Occurred,Discharging Approx 2,500 Gallons Borated Water Into Containment Bldg.Operator Secured Sys & Reset Containment Spray
05000305/LER-1984-021, :on 841218,boric Acid Tank Selector Switch Misaligned.Caused by Personnel Error.Switch Returned to Proper Position.Meeting Conducted on Job Attentiveness1985-01-17017 January 1985
- on 841218,boric Acid Tank Selector Switch Misaligned.Caused by Personnel Error.Switch Returned to Proper Position.Meeting Conducted on Job Attentiveness
1998-03-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000305/LER-1998-003, :on 980203,RCS Low Flow Trip Logic Were Identified as Not Been Tested IAW Tss.Caused by Personnel Error.Testing Was Conducted IAW Requirements of Section 4 of TS1998-03-0505 March 1998
- on 980203,RCS Low Flow Trip Logic Were Identified as Not Been Tested IAW Tss.Caused by Personnel Error.Testing Was Conducted IAW Requirements of Section 4 of TS
ML20140E9181997-06-0707 June 1997 Safety Evaluation Supporting Amend 133 to License DPR-43 05000305/LER-1996-007, :on 961023,identified Design Deficiency in Containment Isolation Function.Caused by Oversight During Plant Design.Implemented Administrative Controls to Preclude Subject Condition Prior to Plant start-up1996-11-22022 November 1996
- on 961023,identified Design Deficiency in Containment Isolation Function.Caused by Oversight During Plant Design.Implemented Administrative Controls to Preclude Subject Condition Prior to Plant start-up
ML20115J3981996-07-22022 July 1996 Interim Part 21 Rept Re 3/4 Schedule 80 Pipe Furnished to Consolidated Power Supply.Investigation Revealed Only One Nuclear Customer Involved in Sale of Matl 05000305/LER-1995-003, :on 950516,failed to Adequately Assess Consequences During Recovery from Switch Misposition Resulted in Turbine/Rt.Reminded Nco of Importance of Self Checking1995-06-14014 June 1995
- on 950516,failed to Adequately Assess Consequences During Recovery from Switch Misposition Resulted in Turbine/Rt.Reminded Nco of Importance of Self Checking
ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20113H4871992-07-30030 July 1992 Part 21 Rept Re Surge Line Flooding Which May Occur When Large Pressurizer Vent Used to Support Reduced Rc Inventory Operations.Notification Received from Westinghouse on 920312.Item Not Reportable Per 10CFR21 ML20086U0311991-11-30030 November 1991 SG Tube Plugging Criteria for Outside Diameter Stress Corrosion Cracking (ODSCC) at Tube Support Plates ML20077K0831991-06-30030 June 1991 Nonproprietary Technical Justification for Eliminating Pressurizer Surge Line Rupture as Structural Design Basis for Kewaunee Nuclear Plant ML1118102861991-05-31031 May 1991 Handbook on Flaw Evaluation Kewaunee,Unit 1 Steam Generators Upper Shell to Cone Weld. ML20091E3441991-03-31031 March 1991 Nonproprietary Structural Evaluation of Kewaunee Pressurizer Surge Line,Considering Effects of Thermal Stratification ML20066B2101990-12-31031 December 1990 Generator Mid-Cycle Rept,Dec 1990 ML20062A4641990-09-30030 September 1990 Nonproprietary, Reevaluation of U-Bend Tube Fatique for Kewaunee Plant Steam Generators 05000305/LER-1990-005, :on 900404,intergranular Attack & IGSCC Results in Both Steam Generators a & B Being Categorized as C-3.All Defective Tubes Plugged & Sludge Lancing & Crevice Flushing Conducted1990-05-0404 May 1990
- on 900404,intergranular Attack & IGSCC Results in Both Steam Generators a & B Being Categorized as C-3.All Defective Tubes Plugged & Sludge Lancing & Crevice Flushing Conducted
ML1117803551990-04-30030 April 1990 Generator Tubesheet Crevice Indications Return to Power Rept. ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML19354D8351989-11-0808 November 1989 Presentation to NRC Re Kewaunee (Wps) SECY-83-472 LOCA Analysis Effort. ML20247D3011989-07-12012 July 1989 Part 21 Rept 10CFR21-0047 Re Control Wiring Insulation of Inner Jacket Used on General Motors Diesel Generator Sets Identified as 999 or MP Series.Encl List of Owners of Units Notified 05000305/LER-1989-009, :on 890401,during Repositioning of Ventilation Dampers,Jumper Inadvertently Detached from Terminal Block Contact,Causing Damper Actuation.Caused by Procedural Inadequacies.Weidmuller Blocks Installed1989-05-0101 May 1989
- on 890401,during Repositioning of Ventilation Dampers,Jumper Inadvertently Detached from Terminal Block Contact,Causing Damper Actuation.Caused by Procedural Inadequacies.Weidmuller Blocks Installed
05000305/LER-1989-006, :on 890315,audit Identified Failure to Implement Tech Spec Re Testing of Fan Coil Emergency Discharge Dampers & Backfit Dampers.Caused by Procedural Inadequacy.Procedure Updated1989-04-14014 April 1989
- on 890315,audit Identified Failure to Implement Tech Spec Re Testing of Fan Coil Emergency Discharge Dampers & Backfit Dampers.Caused by Procedural Inadequacy.Procedure Updated
05000305/LER-1989-005, :on 890310,insp of Diesel Generator Start Up Air Sys Finds Deficiencies That Could Render Both Diesel Generators Inoperable Due to Inadequate Design.Cause Unknown.Generic Implications Will Be Examined1989-04-10010 April 1989
- on 890310,insp of Diesel Generator Start Up Air Sys Finds Deficiencies That Could Render Both Diesel Generators Inoperable Due to Inadequate Design.Cause Unknown.Generic Implications Will Be Examined
ML20235J1941988-11-30030 November 1988 Analysis of Capsule P from Wisconsin Public Svc Corp Kewaunee Nuclear Plant Reactor Vessel Radiation Surveillance Program ML20207N4641988-10-12012 October 1988 Part 21 Rept Re Potential Problem W/Emd 20-645E4,Type 999 Excitation Sys Circuit Breaker & Wiring.Potential for Field Circuit Breaker to Trip Due to Combined Air Temps & Field Current Exists at All Plants W/Model 999 Sys ML20206E9801988-06-30030 June 1988 Rev 2 to Handbook on Flaw Evaluation,Kewaunee Unit 1 Steam Generators Upper Shell to Cone Weld ML20196G5251988-06-15015 June 1988 Technical Review Rept T809, Blocked Thimble Tubes/Stuck Incore Detector ML20154H0391988-04-30030 April 1988 Slide Presentation Matl,Nrc Meeting 880331,Kewaunee Nuclear Power Plant Steam Generator Tube Sleeve Installation ML20196G8881988-03-0303 March 1988 Headquarters Daily Rept for 880303 ML20147B2921987-12-31031 December 1987 Annual Operating Rept for 1987 ML20149J0261987-12-21021 December 1987 Part 21 Rept Re Installation of Relay Part B8002DN in Foxboro 62H Controllers in Facilities.Subj Relay Must Be Replaced by Relay Part N0196ZN.Relay B8002DN Not Used in Any Other Plants ML20236W7341987-11-30030 November 1987 Nonproprietary Kewaunee Steam Generator Sleeving Rept (Mechanical Sleeves) ML20236N3451987-10-31031 October 1987 Monthly Operating Rept for Oct 1987 ML20236F3101987-10-31031 October 1987 Nonproprietary WCAP-11620, Addl Technical Bases for Eliminating Large Primary Loop Pipe Rupture as Structural Design Basis for Kewaunee ML20235V1161987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20238F7541987-08-31031 August 1987 Monthly Operating Rept for Aug 1987 ML20237H6861987-07-31031 July 1987 Monthly Operating Rept for Jul 1987 ML20235J3101987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML17261A5301987-06-18018 June 1987 Part 21 Rept Re Potential Util Failure to Comply W/Component Containment Isolation Licensing Commitment If Proposed Mods to Component Cooling Water Sys Instituted.Utils Advised to Evaluate Containment Isolation Sys ML20215A3211987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20215L8061987-04-30030 April 1987 Nonproprietary Rev 1 to Technical Bases for Eliminating Large Pipe Rupture as Structural Design Basis for Kewaunee ML20213G4341987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20206H4301987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 05000305/LER-1987-002, :on 870224,reactor Tripped When Source Range Nuclear Flux Detectors 1 & 2 Erroneously Reached Nominal Reactor Trip Setpoint of 1.0E05 Counts/S.Caused by Seepage of Borated Refueling Water Into Instrument1987-03-26026 March 1987
- on 870224,reactor Tripped When Source Range Nuclear Flux Detectors 1 & 2 Erroneously Reached Nominal Reactor Trip Setpoint of 1.0E05 Counts/S.Caused by Seepage of Borated Refueling Water Into Instrument
05000305/LER-1987-001, :on 870223 & 24,series of High Radiation Alarms Received in Control Room.Caused by Primary to Secondary Leak in Steam Generator 1A.Results of Eddy Current Testing Will Be Submitted1987-03-25025 March 1987
- on 870223 & 24,series of High Radiation Alarms Received in Control Room.Caused by Primary to Secondary Leak in Steam Generator 1A.Results of Eddy Current Testing Will Be Submitted
05000305/LER-1985-015, :on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 211987-03-0606 March 1987
- on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 21
ML20207R6091987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20211P7211987-02-23023 February 1987 Part 21 Rept Re Rockbestos Coaxial Cable Used in Sorrento Electronics Digital & Analog high-range Radiation Monitor. Insulation Resistance at High Temp Not High Enough for Ion Chamber & Associated Electronics to Operate Properly ML20211A1761987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 05000305/LER-1986-015, :on 861229,svc Water Inlet Valve for Radiation Monitor R-16 Found Closed.Caused by Personnel Error.Sight Flow Meter Cleaned & Operating Procedure Used to Perform Flushing Process Reviewed1987-01-28028 January 1987
- on 861229,svc Water Inlet Valve for Radiation Monitor R-16 Found Closed.Caused by Personnel Error.Sight Flow Meter Cleaned & Operating Procedure Used to Perform Flushing Process Reviewed
ML20212B9451986-12-31031 December 1986 Reload Safety Evaluation,Kewaunee Cycle 13 ML20212F6581986-12-31031 December 1986 Technical Review Rept, Degradation of Safety Sys Due to Component Misalignment &/Or Mispositioned Control/Selector Switches 1998-03-05
[Table view] |
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l l'l Ae871ACT (Omst so 7400 apsres, ie seeresamerswy Mvsea omgwe spece typewertsoa poet Het At 1437 on January 22, 1985, during full power oper.ition, there was an inadvertent actuation of the IB Internal Containment Spray Systim. The IB pump ran for 1 minute and 40 seconds discharging an estimated 2500 gallons of borated water into the containment building before being secured. The pump start occurred during the per-fonnance of SP55-155, " Engineered Safeguards Logic Test".
When the pump start occurred, the operator verified that it was inadvertent, secured the system and reset containment spray. The operators received various battery ground alarms as a result of instrument malfunctions in containment.
At 1525 it was discovered that the RWST level was below technical specification limits, refilling was started and preparations were made to begin a-plant power reduction.
The TWST level was above TS setpoint at 1555 hence no reduction in power was initiated.
Immediate actions were taken to assess the situation and identify the cause. Long term actions planned are to clean the containment interior, and perform an evaluation
' to identify potential hardware modifications which would prevent reoccurrence.
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UCENSEE FVENT REPORT (LER) TEXT CONTINUATION areaovto cwe =o uso-mu E MPIRES' 8/31/06 PactLeiv NAME W DoCati NvustR m LIR NUMetR 161 PAGE438 Kewaunee Nuclear Power Plant rnr,-.
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.,im o 1510 lo lo l l l 8l5 0 l 0l1 0 10 0 12 0F 0h At 1437 on January 22, 1985, during full power operation, there was an inadvertent actuation of the IB Internal Containment Spray System [ICS] (BE).
The 1B pump (P) ran for 1 minute and 40 seconds discharging an estimated 2500 gallons of borated water into the containment building before being secured. The pump start occurred during the performance of SP55-155 " Engineered Safeguards Logic Test". This test is perfomed monthly to satisfy plant Technical Specification requirements.
Each safeguards logic train is tested individually. A contact is opened to prevent the slave relay on the train in test from being energized by the master relay.
By procedure the I & C personnel are to monitor the computer printout, the sequence of events recorder points, annunciators and/or trip status lights and the test lamps or permissive status lights actuated by the procedure.
When the pump start occurred the operator verified that it was inadvertent, secured the system and reset containment spray. The operators received battery ground alarms (ALM) as a result of instrument malfunctions in containment. Among the alarms received were 1A RCP fire protection, 1B RCP upper bearing temperature, and rod deviation alarms.
At 1525 it was discovered that the Refueling Water Storage Tank (BQ) level was below Technical Specification limits. Refilling was started and preparations were made to begin a plant power reduction. The RWST was above TS setpoint at 1555 hence no reduction in power was initiated.
AT 1610 a containment entry was made by Operations personnel and plant electricians.
They found pools of water at all elevations of containment that were evaporating and leaving boric acid residue.
Everything else appeared normal with no visible evidence of ground faults.
At 1742 the operators completed SP87-125 " Shift Turnover Channel Checks". All of the parameters were normal and within specification. The only abnormal conditions at that time were battery grounds of 60 volts negative on "B" battery,120 volts positiva on "A" battery, a 1A RCP fire alam which was shown to be invalid during the visual inspection, a high containment humidity indication, a mid-position indication of the emergency airlock inner door switch, and an abnormal RCP upper Radial BRG temperature indication. The last two abnormal conditions were due to water intrusion.
At 2040, indication for control rod (AA).K-7 in Bank D began behaving erratically. All~
cther core conditions showed normal behavior and the rod position indication;for rod K-7 was declared out of service.
A review of the surveillance procedure perfomance was initiated to identify the cause of the actuation. From the Sequence of Events Recorder printout, it was discovered that during the performance of the containment Hi pressure logic testing, the Hi-Hi containment pressure alarm actuated twice. This Hi-Hi containment pressure bistable (IS) actuation durin~g the test on the Hi containment pressure ligic is attributed to an interaction between the-two bistables, referred to as cross-talk. This is possible because the Hi and the Hi-Hi containment pressure actuation circuitry are contained in the same duplex bistable unit. The problem of cross-talk has been detected before and Na Fomu 3esa
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,,.m Kewaunee Nuclear Power Plant o ls lo lo lo j i l 8 ]5 0l0l1 0l0 0l3 OF 0 14 has been the subject of letters between WPS and the bistable manufacturer, Foxboro.
This cross-talk may have resulted in energizing the Containment Spray Master Relay (RLY).
At the end of the procedure, when safety injection was reset, the slave relay was energized and the IB ICS pump actuated.
A retest was perfomed two days after the event in an attempt to reproduce the occurrence.
In two of seventeen attempts Hi-Hi containment pressure alarmed during testing of the Hi containment pressure channel.
In addition, recorders were set up to monitor the coils on the bistable outputs.
Fluttering of the de-energized bistable was otserved. This evidence indicates that cross-talk may have occurred, but is not conclusive as to the cause of the pump start. Additional testing is planned during the in-progress 1985 refueling outage.
A related event occurred on February 10, with the plant in cold shutdown and RCS pressure at approximately 320 psig. The control room operator noticed that the 1B Reactor Coolant Pump (AB) had started without swtich action. Upon discovery the operator secured the pump and started the associated oil lift pump. Residual water (believed to be from the-ICS actuation) discovered in the pump pressure switch housing had grounded the RCP 4160V breaker SCR circuitry sending a close signal to the breaker and starting the pump.
(ReferenceLER85-04).
CORRECTIVE ACTIONS
The following actions were taken:
- 1) The NSSS vendor (Westinghouse) and the A/E (Fluor Engineers) were contacted immediately to aid in the evaluation of the incident. The effects of the spray on equipment operability and potential for Boric Acid and Na0H corrosion of metal components was considered. The decision was made to remain at full power.
- 2) Chemistry samples were taken to determine the amount of caustic discharged to containment. The results were a PH of 6.8 in the spray discharge line and a PH of 5.9 in the Refueling Water Storage Tank.
- 3) The Operations Superintendent routed a letter to the operating crews alerting them to potential problem areas based on conversations with Westinghouse. These areas are:
the reactor coolant pumps, nuclear instrumentation, individual rod position indication and limit switch indication.
- 4) A valve timing test was performed on the air operated containment isolation valves within containment. All:were within specification.
- 6) k. following day the IB ICS piping was flushed to remove caustic in the system and the lines were sampled to ensure the caustic was flushed.
- 6) A core flux map was performed which confimed that control rod K-7 was at its normal bank position.
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- 7) On January 24, the Safeguards Logic Test was repeated to aid in identifying the cause of the pump start. The results were not conclusive.
- 8) Our initial review of the RCP start (breakaway measurements, vibration measurements, and thrust bearing temperatures) indicated that no damage occurred. (Reference LER85-04).
Long term actions planned are:
- 1) Cleanup the residual boric acid crystals.
- 2) Perfonn further testing on the safeguards actuation logic during refueling.
- 3) Monitor reactor coolant pump performance during startup.
4)
Inysstigate replacing the duplex bistables used in the energize to actuate applications.
- 5) Perfonn a random check on insulated carbon steel lines inside containment to ensure no boric acid is on the piping.
SAFETY CONSEQUENCES
The immediate concerns following this event were proper operation of equipment. The containment tour verified that there was no major problems and abnormal instrument indications could be attributed to water instrusion.
The other concernwas possible corrosion of carbon steel co;nponents covered by mineral based insulation material when exposed to boric acid solution. According to infonnation received from Westinghouse, when the solution evaporates boric acid crystals are left; as long as the crystals remain unwetted there should be no short nr medium term corrosion concern. However, because of the design of the insulation and the high operating temperature of the carbon steel components it is unlikely that the solution came in contact with the components.
Containment humidity returned to normal conditions, (the 15-20 percent range) by 1937
- n January 22 indicating that the water inside containment looked dry, with boric acid crystals coating exposed surfaces.
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NRC-85-29 WISCONSIN PUBLIC SERVICE CORPORATION P.O. Box 1200, Green Bay, WI 54305 February 21, 1935 U. S. Nuclear Regulatory Comission Document Control Desk Washington, D.C.
20555 Gentlemen:
Docket 50-305 Operating License DPR-43 Kewaunee Nuclear Power Plant Reportable Occurrence 85-001-00 In accordance with the requirements of 10 CFR 50.73 " Licensee Event Report System",
the attached Licensee Event Report for reportable occurrence 85-001-00 is being submitted.
Very truly yours,
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D. C. Hintz Manager - Nuclear Power JGT/js Attach.
cc - INP0 Records Center Suite 1500,1100 Circle 75 Parkway Atlanta, GA 30339 Mr. Robert Nelson,' NRC Resident Inspector Mr S k.
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US NRC, Washington, DC 20555 Mr. J. G. Keppler, Regional Administrator
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05000305/LER-1985-001, :on 850122,inadvertent Actuation of Internal Containment Spray Sys 1B Occurred,Discharging Approx 2,500 Gallons Borated Water Into Containment Bldg.Operator Secured Sys & Reset Containment Spray |
- on 850122,inadvertent Actuation of Internal Containment Spray Sys 1B Occurred,Discharging Approx 2,500 Gallons Borated Water Into Containment Bldg.Operator Secured Sys & Reset Containment Spray
| | 05000305/LER-1985-002, :on 850125,seismic Analysis for nonsafety- Related Piping Section of Containment Integrated Leak Rate Test Penetration Could Not Be Located.Design Change Will Be Completed During 1985 Refueling Shutdown |
- on 850125,seismic Analysis for nonsafety- Related Piping Section of Containment Integrated Leak Rate Test Penetration Could Not Be Located.Design Change Will Be Completed During 1985 Refueling Shutdown
| | 05000305/LER-1985-003, :on 850208,reactor Tripped.Caused by Decrease in Steam Generator Vol to Low Level Alarm Setpoints. Corrective Action Being Investigated |
- on 850208,reactor Tripped.Caused by Decrease in Steam Generator Vol to Low Level Alarm Setpoints. Corrective Action Being Investigated
| | 05000305/LER-1985-004, :on 850210,control Room Operator Noticed Reactor Coolant Pump 1B Running.Caused by Grounded Condition in Actuation Circuitry Due to Water Accumulation in Pressure Switch.Hardware Mod Being Evaluated |
- on 850210,control Room Operator Noticed Reactor Coolant Pump 1B Running.Caused by Grounded Condition in Actuation Circuitry Due to Water Accumulation in Pressure Switch.Hardware Mod Being Evaluated
| | 05000305/LER-1985-005, :on 850211,exhaust Fan 1A of Auxiliary Bldg Special Ventilation Sys Found Running.Caused by Burnt Out Coil in Solenoid Valve Controlling Air to Zone SV Exhaust Filter 1A Inlet Damper.Valve Replaced |
- on 850211,exhaust Fan 1A of Auxiliary Bldg Special Ventilation Sys Found Running.Caused by Burnt Out Coil in Solenoid Valve Controlling Air to Zone SV Exhaust Filter 1A Inlet Damper.Valve Replaced
| | 05000305/LER-1985-006, :on 850220,steam Generator Tube Found Incorrectly Plugged.Possibly Caused by Mismarked Tube Sheet. Template Marked to Identify Tubes to Be Plugged |
- on 850220,steam Generator Tube Found Incorrectly Plugged.Possibly Caused by Mismarked Tube Sheet. Template Marked to Identify Tubes to Be Plugged
| | 05000305/LER-1985-007, :on 850225,w/red Pressurizer Channel Tripped & White Channel Calibr,Safety Injection Signal Occurred. Caused by Technician Requesting Wrong Channel Be Tripped. Surveillance Procedure Revised |
- on 850225,w/red Pressurizer Channel Tripped & White Channel Calibr,Safety Injection Signal Occurred. Caused by Technician Requesting Wrong Channel Be Tripped. Surveillance Procedure Revised
| | 05000305/LER-1985-008, :on 850225,alarm 47001-34 for Condenser Low Vacuum Turbine Trip,Cleared & Alarmed Again & Both Diesel Generators Started.Caused by Maint to Turbine Trip Mechanism.Start Signal Will Be Removed |
- on 850225,alarm 47001-34 for Condenser Low Vacuum Turbine Trip,Cleared & Alarmed Again & Both Diesel Generators Started.Caused by Maint to Turbine Trip Mechanism.Start Signal Will Be Removed
| | 05000305/LER-1985-010, :on 850405,reactor Trip Occurred Due to Steam Flow Greater than Feed Flow Signal Coincident W/Lo Steam Generator Level Signal.Caused by One Feed Flow & One Steam Low Transmitter Out of Calibr |
- on 850405,reactor Trip Occurred Due to Steam Flow Greater than Feed Flow Signal Coincident W/Lo Steam Generator Level Signal.Caused by One Feed Flow & One Steam Low Transmitter Out of Calibr
| | 05000305/LER-1985-011, :on 850407,auxiliary Bldg Special Ventilation Sys Actuated from Steam Exclusion Signal.Caused by Steam Issuing Through Blown Rupture Disk on Boric Acid Evaporator Condenser.Ventilation Sys Reset |
- on 850407,auxiliary Bldg Special Ventilation Sys Actuated from Steam Exclusion Signal.Caused by Steam Issuing Through Blown Rupture Disk on Boric Acid Evaporator Condenser.Ventilation Sys Reset
| | 05000305/LER-1985-012, :on 850410,reactor Tripped.Caused by Differences in Ground Potential Between Ni & Test Equipment. Purchase of New Portable Picoammeter Being Considered |
- on 850410,reactor Tripped.Caused by Differences in Ground Potential Between Ni & Test Equipment. Purchase of New Portable Picoammeter Being Considered
| | 05000305/LER-1985-013, :on 850404 & 0505,heat Tracing Circuit on Suction Line to Containment Hydrogen Analyzer 1A Discovered Inoperable.Caused by Failed Amphenol Connector.Spare Parts Ordered & Failed Connector Bypassed |
- on 850404 & 0505,heat Tracing Circuit on Suction Line to Containment Hydrogen Analyzer 1A Discovered Inoperable.Caused by Failed Amphenol Connector.Spare Parts Ordered & Failed Connector Bypassed
| | 05000305/LER-1985-014, :on 850615,concrete Block Preventing Access to Spent Resin Storage Tank Room Found Removed.Caused by Design Change & Maint Work on Tank.Requirements for Securing High Radiation Areas Discussed |
- on 850615,concrete Block Preventing Access to Spent Resin Storage Tank Room Found Removed.Caused by Design Change & Maint Work on Tank.Requirements for Securing High Radiation Areas Discussed
| | 05000305/LER-1985-015, :on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 21 |
- on 850617,Fluor Engineers,Inc Notified Util of Inadequate Documentation to Support Seismic Qualification of Diesel Generator Differential Relays.Relays Replaced W/Ge Seismically Qualified Relays on 870120 & 21
| | 05000305/LER-1985-015, :on 850617,Fluor Engineers Notified Util That Seismic Qualification of Emergency Diesel Generator Differential Relays Could Not Be Conclusively Determined. Resolution Under Review |
- on 850617,Fluor Engineers Notified Util That Seismic Qualification of Emergency Diesel Generator Differential Relays Could Not Be Conclusively Determined. Resolution Under Review
| | 05000305/LER-1985-016, :on 850725,control Operator Observed That Position Indication for Containment Isolation Valves & Steam Exclusion Dampers Changed Position.Caused by Power Interruption & Loss of Sys Redundancy |
- on 850725,control Operator Observed That Position Indication for Containment Isolation Valves & Steam Exclusion Dampers Changed Position.Caused by Power Interruption & Loss of Sys Redundancy
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000305/LER-1985-017, :on 850808,reactor Tripped Manually to Isolate Ruptured Excess Steam Vent Line.Caused by Carbon Steel Piping Erosion.Ruptured Vent Lines Replaced.Program Implemented to Examine Steam Line Piping |
- on 850808,reactor Tripped Manually to Isolate Ruptured Excess Steam Vent Line.Caused by Carbon Steel Piping Erosion.Ruptured Vent Lines Replaced.Program Implemented to Examine Steam Line Piping
| | 05000305/LER-1985-018, :on 850820,discovered That Fire Hose Insp Required by Tech Spec 4.15.2 Performed Outside Required 18-month (Plus or Minus 25%) Time Interval.Caused by Mgt Oversight When Procedure Modified |
- on 850820,discovered That Fire Hose Insp Required by Tech Spec 4.15.2 Performed Outside Required 18-month (Plus or Minus 25%) Time Interval.Caused by Mgt Oversight When Procedure Modified
| | 05000305/LER-1985-019, :on 851107,at 100% Power,Test of Undervoltage Trip Attachment Conducted for Each Reactor Trip Breaker to Verify Existence of 20 Oz of Force Margin,Per IE Bulletin 85-002.Two Breakers Failed |
- on 851107,at 100% Power,Test of Undervoltage Trip Attachment Conducted for Each Reactor Trip Breaker to Verify Existence of 20 Oz of Force Margin,Per IE Bulletin 85-002.Two Breakers Failed
| | 05000305/LER-1985-020, :on 851113,failure of Train a Main Feedwater Control Valve Caused lo-lo Water Level in Steam Generator 1A & Reactor Trip.Caused by Two of Four Cap Screws Holding Valve Actuator to Yoke Shearing |
- on 851113,failure of Train a Main Feedwater Control Valve Caused lo-lo Water Level in Steam Generator 1A & Reactor Trip.Caused by Two of Four Cap Screws Holding Valve Actuator to Yoke Shearing
| | 05000305/LER-1985-021, :on 851114,high Flux Shutdown Bistable Trip Value Recorded in Place of High Flux Level Trip Setpoint on Both Source Range Channels.Caused by Personnel Error. Individuals Counseled on Procedure Performance |
- on 851114,high Flux Shutdown Bistable Trip Value Recorded in Place of High Flux Level Trip Setpoint on Both Source Range Channels.Caused by Personnel Error. Individuals Counseled on Procedure Performance
| 10 CFR 50.73(a)(2)(1) | 05000305/LER-1985-022, :on 851203,discovered That Surveillance Procedure Sp 48-046,conducted on 851127,performed Outside of Required Time Interval.Caused by Calibr of Nuclear Instrumentation Due to 851113 Trip |
- on 851203,discovered That Surveillance Procedure Sp 48-046,conducted on 851127,performed Outside of Required Time Interval.Caused by Calibr of Nuclear Instrumentation Due to 851113 Trip
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | 05000305/LER-1985-023, :on 851212,loss of Power to Instrument Bus I Occurred.Caused by Failure of Constant Voltage Transformer. Constant Voltage Transformer Replaced & Instrument Bus Returned to Normal Power Supply |
- on 851212,loss of Power to Instrument Bus I Occurred.Caused by Failure of Constant Voltage Transformer. Constant Voltage Transformer Replaced & Instrument Bus Returned to Normal Power Supply
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