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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
05000289/LER-1998-009-01, :on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised1998-09-18018 September 1998
- on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised
05000289/LER-1998-008-01, :on 980818,RM RM-A-8G-High Was Noted Inoperable for More than 7 Days.Caused by Weaknesses in I&C Work Practices.Revised Data Collection Portion of Surveillance Procedures1998-09-14014 September 1998
- on 980818,RM RM-A-8G-High Was Noted Inoperable for More than 7 Days.Caused by Weaknesses in I&C Work Practices.Revised Data Collection Portion of Surveillance Procedures
05000289/LER-1998-007, :on 980720,inoperable Intake Screen & Pump House Floor Drain Check Valves Were Noted.Caused by Lack of Preventative Maint & Periodic Insp.Loose Scrap & Debris Was Cleaned Up from Floor1998-08-14014 August 1998
- on 980720,inoperable Intake Screen & Pump House Floor Drain Check Valves Were Noted.Caused by Lack of Preventative Maint & Periodic Insp.Loose Scrap & Debris Was Cleaned Up from Floor
05000289/LER-1998-006-01, :on 980617,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement,Was Identified.Caused by Personnel Error.Hourly Fire Watch Initiated1998-07-17017 July 1998
- on 980617,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement,Was Identified.Caused by Personnel Error.Hourly Fire Watch Initiated
05000289/LER-1998-005, :on 980416,inoperable Fire Dampers Were Noted. Caused by Improper re-installation of Link.Damper Trip Mechanism Was Properly Installed1998-07-14014 July 1998
- on 980416,inoperable Fire Dampers Were Noted. Caused by Improper re-installation of Link.Damper Trip Mechanism Was Properly Installed
05000320/LER-1998-001-02, :on 980604,flood Barriers Breached Between Turbine Bldg & Control Bldg Area.Caused by Work Planning Process for Dismantlement Work Failed to Include Adequate Controls.Openings Verified to Be Sealed1998-07-0202 July 1998
- on 980604,flood Barriers Breached Between Turbine Bldg & Control Bldg Area.Caused by Work Planning Process for Dismantlement Work Failed to Include Adequate Controls.Openings Verified to Be Sealed
05000289/LER-1998-002, :on 980204,missed SFP Sample Following Water Addition Was Determined.Caused by Unfamiliarity W/Sampling Requirements & Missing Operator Aid.New Operator Aid Posted at Valve Used to Fill SFP from Reclaimed Water Sys1998-04-0303 April 1998
- on 980204,missed SFP Sample Following Water Addition Was Determined.Caused by Unfamiliarity W/Sampling Requirements & Missing Operator Aid.New Operator Aid Posted at Valve Used to Fill SFP from Reclaimed Water Sys
05000289/LER-1998-004, :on 980218,loss of CS Capability Was Noted. Caused by Improper Assembly of RBS Pump Discharge Valve Control Switch Pushbutton.Pushbutton Switch Was Replaced W/New Properly Assembled Pushbutton Switch1998-03-20020 March 1998
- on 980218,loss of CS Capability Was Noted. Caused by Improper Assembly of RBS Pump Discharge Valve Control Switch Pushbutton.Pushbutton Switch Was Replaced W/New Properly Assembled Pushbutton Switch
05000289/LER-1998-003, :on 980218,discovered Installation of Thermo- Lag Fire Barrier on Incorrect Conduit Duct.Caused by Personnel Error.Revised Operating Procedure 1104-45 & Installed One Hour Fire Rated Barrier on Subject Cable Duct1998-03-19019 March 1998
- on 980218,discovered Installation of Thermo- Lag Fire Barrier on Incorrect Conduit Duct.Caused by Personnel Error.Revised Operating Procedure 1104-45 & Installed One Hour Fire Rated Barrier on Subject Cable Duct
05000289/LER-1998-002, :on 980204,missed SFP Sample Following Water Addition Occurred.Caused by Operator Aid Missing from Wall. New Operator Aid Posted at Valve Which Used to Fill Spent Fuel Pool from Reclaimed Water Sys1998-03-0303 March 1998
- on 980204,missed SFP Sample Following Water Addition Occurred.Caused by Operator Aid Missing from Wall. New Operator Aid Posted at Valve Which Used to Fill Spent Fuel Pool from Reclaimed Water Sys
05000289/LER-1997-006-02, Re Unqualified Cable Terminations.Ler 97-006-00 Retracted1997-11-26026 November 1997 Re Unqualified Cable Terminations.Ler 97-006-00 Retracted 05000289/LER-1997-010-01, :on 971012,PORV Inoperability Was Determined. Caused by mis-wiring & Failure to Perform post-maintenance Test Following Replacement During 11R Refueling Outage.Porv Replaced During 12R Refueling Outage Was Wired Correctly1997-11-12012 November 1997
- on 971012,PORV Inoperability Was Determined. Caused by mis-wiring & Failure to Perform post-maintenance Test Following Replacement During 11R Refueling Outage.Porv Replaced During 12R Refueling Outage Was Wired Correctly
05000289/LER-1997-009-01, :on 970725,engineering Analysis of Loss of a Train DC Power W/Loss of Offsite Power & LOCA Was Determined.Caused by Plant Designers Error.Trained Operators on Methodology to Regain Control of Es Equipment1997-08-25025 August 1997
- on 970725,engineering Analysis of Loss of a Train DC Power W/Loss of Offsite Power & LOCA Was Determined.Caused by Plant Designers Error.Trained Operators on Methodology to Regain Control of Es Equipment
05000289/LER-1997-005, Has Been Cancelled1997-08-20020 August 1997 Has Been Cancelled 05000289/LER-1997-006-01, :on 970424,reactor Bldg Fan Motors Unqualified Cable Termination Occurred Due to Incorrect Engineering Guidance.Caused by Personnel Error.Qualifiable Repair of AH-E-1A Fan Motor Termination Was Installed on 9703231997-05-23023 May 1997
- on 970424,reactor Bldg Fan Motors Unqualified Cable Termination Occurred Due to Incorrect Engineering Guidance.Caused by Personnel Error.Qualifiable Repair of AH-E-1A Fan Motor Termination Was Installed on 970323
05000289/LER-1997-005-01, :on 970410,declared motor-operated Reactor Bldg Purge Valves Inoperable Due to Inadequate Closing Torque. Caused by Deficient Design Analysis.Will Perform Evaluation of Valve Specific Seating Torque Test Data1997-05-12012 May 1997
- on 970410,declared motor-operated Reactor Bldg Purge Valves Inoperable Due to Inadequate Closing Torque. Caused by Deficient Design Analysis.Will Perform Evaluation of Valve Specific Seating Torque Test Data
05000289/LER-1996-001, :on 961112,investigation of Seismic Qualification of Class 1E 4160 W Breakers Was Conducted Due to Incident Caused by Personnel Error.Racked Out Breakers Were Removed from Associated Modules1997-03-31031 March 1997
- on 961112,investigation of Seismic Qualification of Class 1E 4160 W Breakers Was Conducted Due to Incident Caused by Personnel Error.Racked Out Breakers Were Removed from Associated Modules
05000289/LER-1997-003, :on 970224,potential Overpressurization of Makeup Pump Suction Piping Occurred Due to Inadequate Test & Operating Procedures.Procedure Changes Will Be Implemented Before Next Sys Testing Performed1997-03-26026 March 1997
- on 970224,potential Overpressurization of Makeup Pump Suction Piping Occurred Due to Inadequate Test & Operating Procedures.Procedure Changes Will Be Implemented Before Next Sys Testing Performed
05000289/LER-1997-002, :on 970129,potential Inability of Startup Feedwater Block Valves to Fully Close Following Main Steam Line Break Occurred Due to MOV Program Weakness.Increased Torque Switch Settings on Valve Operators1997-02-28028 February 1997
- on 970129,potential Inability of Startup Feedwater Block Valves to Fully Close Following Main Steam Line Break Occurred Due to MOV Program Weakness.Increased Torque Switch Settings on Valve Operators
05000289/LER-1997-001-02, :on 970117,potential Overpressurization of Piping Between Closed Reactor Building Containment Isolation Valves Occurred Due to Inadequate Design Code Guidance. Results of Review Will Be Documented.Pages 2 & 3 Corrected1997-02-17017 February 1997
- on 970117,potential Overpressurization of Piping Between Closed Reactor Building Containment Isolation Valves Occurred Due to Inadequate Design Code Guidance. Results of Review Will Be Documented.Pages 2 & 3 Corrected
05000289/LER-1997-001-01, :on 970117,potential Overpressurization of Piping Between Closed Reactor Building Isolation Valves Occurred Due to Inadequate Design Code Guidance.Results of This Review Will Be Documented1997-02-17017 February 1997
- on 970117,potential Overpressurization of Piping Between Closed Reactor Building Isolation Valves Occurred Due to Inadequate Design Code Guidance.Results of This Review Will Be Documented
05000289/LER-1996-002-01, :on 961221,discovered Use of non-conservative Setpoint May Result in Air Entrainment in ECCS Pumps.Caused by Personnel Error.Revised Procedures & Briefed Personnel on Air Entrainment Concerns1997-01-20020 January 1997
- on 961221,discovered Use of non-conservative Setpoint May Result in Air Entrainment in ECCS Pumps.Caused by Personnel Error.Revised Procedures & Briefed Personnel on Air Entrainment Concerns
05000289/LER-1996-001-02, :on 961112,Westinghouse Class IE 4160 Vac Switchgear W/Breakers Were Not Seismically Qualified.Caused by Personnel Error.Racked Out Breakers Were Removed from Modules & Seismically Restrained1996-12-12012 December 1996
- on 961112,Westinghouse Class IE 4160 Vac Switchgear W/Breakers Were Not Seismically Qualified.Caused by Personnel Error.Racked Out Breakers Were Removed from Modules & Seismically Restrained
05000289/LER-1996-001-01, :on 961112,determined That Westinghouse Class IE 4160 Vac Breakers Were Not Seismically Qualified.Caused by Personnel Error.Removed Racked Out Breakers from Modules & Seismically Restrained1996-12-12012 December 1996
- on 961112,determined That Westinghouse Class IE 4160 Vac Breakers Were Not Seismically Qualified.Caused by Personnel Error.Removed Racked Out Breakers from Modules & Seismically Restrained
05000289/LER-1995-005, :on 951012,invalid Heat Sink Protection Sys Actuation Occurred.Caused by Failure of Two Logic Modules. Continued Daily Inspections of Hsps Cabinet Lamps & Counseled Personnel Re Communication Technique1996-09-13013 September 1996
- on 951012,invalid Heat Sink Protection Sys Actuation Occurred.Caused by Failure of Two Logic Modules. Continued Daily Inspections of Hsps Cabinet Lamps & Counseled Personnel Re Communication Technique
05000289/LER-1995-005-01, :on 951012,invalid Heat Sink Protection Sys Actuation Occurred.Caused by Failure of Logic Modules.Logic Module Failure Analysis Will Continue in Order to Substantiate Suspected Failure Mode1995-11-0909 November 1995
- on 951012,invalid Heat Sink Protection Sys Actuation Occurred.Caused by Failure of Logic Modules.Logic Module Failure Analysis Will Continue in Order to Substantiate Suspected Failure Mode
05000289/LER-1995-003-01, :on 950909,reactor Coolant Leak Occurred Due to Crack Weld in Cold Leg Drain Line.Failed Line Replaced.W/1995-10-0909 October 1995
- on 950909,reactor Coolant Leak Occurred Due to Crack Weld in Cold Leg Drain Line.Failed Line Replaced.W/
05000289/LER-1995-004-01, :on 950912,short Term Interruption of DHR Flow Occurred Due to Inadvertent Operation of DH-V-1 During ESAS Relay Coil Replacement.Caused by Less than Adequate Procedural Guidance.Procedures Revised1995-10-0303 October 1995
- on 950912,short Term Interruption of DHR Flow Occurred Due to Inadvertent Operation of DH-V-1 During ESAS Relay Coil Replacement.Caused by Less than Adequate Procedural Guidance.Procedures Revised
05000289/LER-1995-002-01, :on 950908,control Rod Trip Insertion Times Exceeded TS 4.7.1.1 Limits.Caused by Accumulation of Corrosion Deposits in CRDM Thermal Barrier Call Check Valves & Lead Screw Guide Bushing1995-10-0303 October 1995
- on 950908,control Rod Trip Insertion Times Exceeded TS 4.7.1.1 Limits.Caused by Accumulation of Corrosion Deposits in CRDM Thermal Barrier Call Check Valves & Lead Screw Guide Bushing
05000289/LER-1995-001-01, :on 950307,RC Leak Caused by Failure of Parker Hannifin Compression Fitting Due to Insufficient Tightening During Installation.Shut Root Valves & Stopped Leak1995-04-0606 April 1995
- on 950307,RC Leak Caused by Failure of Parker Hannifin Compression Fitting Due to Insufficient Tightening During Installation.Shut Root Valves & Stopped Leak
05000289/LER-1994-006-01, :on 941002,inadvertent Actuation of EG-Y-1B Occurred Due to Personnel Error.Lead replaced,86B/E Relay Reset & EG-Y-1B Breaker Automatically Closed1994-10-30030 October 1994
- on 941002,inadvertent Actuation of EG-Y-1B Occurred Due to Personnel Error.Lead replaced,86B/E Relay Reset & EG-Y-1B Breaker Automatically Closed
05000289/LER-1994-005-01, :on 940609,noted Irregularity in Overlap Between Average Positions of Control Rod Groups 6 & 7 Due to Intermitent Failure of CRD Sys Programmer Motor.Group 7 Programmer Assembly Will Be Replaced1994-07-0808 July 1994
- on 940609,noted Irregularity in Overlap Between Average Positions of Control Rod Groups 6 & 7 Due to Intermitent Failure of CRD Sys Programmer Motor.Group 7 Programmer Assembly Will Be Replaced
05000289/LER-1994-004-01, :on 940601,discovered That Three Control Rods Exceeded Trip Insertion Time Limit of 1.666 Seconds Due to Postulated Deposits.Four Thermal Barriers Were Replaced W/New Thermal Barrier1994-06-24024 June 1994
- on 940601,discovered That Three Control Rods Exceeded Trip Insertion Time Limit of 1.666 Seconds Due to Postulated Deposits.Four Thermal Barriers Were Replaced W/New Thermal Barrier
05000289/LER-1994-003-01, :on 940523,level of Sodium Hydroxide Tank Incorrectly Reduced Due to Personnel Error.Applicable Administrative Requirements & Computer Alarms Will Be Reviewed to Determine Need for Changes1994-06-20020 June 1994
- on 940523,level of Sodium Hydroxide Tank Incorrectly Reduced Due to Personnel Error.Applicable Administrative Requirements & Computer Alarms Will Be Reviewed to Determine Need for Changes
05000289/LER-1994-002-01, :on 940317,twelve Control Rods Exceeded Trip Insertion Time Limit.Caused by Blockage of Thermal Barrier Check Valves.Corrective Action:Control Rods Were Restored to Drop Time1994-04-18018 April 1994
- on 940317,twelve Control Rods Exceeded Trip Insertion Time Limit.Caused by Blockage of Thermal Barrier Check Valves.Corrective Action:Control Rods Were Restored to Drop Time
05000289/LER-1994-001-01, :on 940307,RC-V1 Was Declared Inoperable Due to Leak from Pressurizer Spray Valve.Caused by Boric Acid Degradation.Corrective action:RC-V1 Was Repaired & Boric Acid Leakage Was Cleaned Up1994-04-0606 April 1994
- on 940307,RC-V1 Was Declared Inoperable Due to Leak from Pressurizer Spray Valve.Caused by Boric Acid Degradation.Corrective action:RC-V1 Was Repaired & Boric Acid Leakage Was Cleaned Up
05000289/LER-1993-009, :on 931112,motor Operator Failure Occurred Due to Improper Declutch Lever Installation.Eight Nuclear Safety Related Limitorque Size Smb 000 MOVs Modified W/New Balanced Declutch Levers1993-12-13013 December 1993
- on 931112,motor Operator Failure Occurred Due to Improper Declutch Lever Installation.Eight Nuclear Safety Related Limitorque Size Smb 000 MOVs Modified W/New Balanced Declutch Levers
05000289/LER-1993-008, :on 931103,disovered Pressurizer Code Safety Valve Setpoints Outside Required TS Tolerance During Plant Operation Due to Inadequate Test Procedure.Revised Test Procedure1993-12-0303 December 1993
- on 931103,disovered Pressurizer Code Safety Valve Setpoints Outside Required TS Tolerance During Plant Operation Due to Inadequate Test Procedure.Revised Test Procedure
05000289/LER-1993-007, :on 931008,pressure Isolation Valve Failed to Seat Tightly During Plant Operation Due to Loose Hinge Mechanism.Replaced Internals of Pressure Isolation Valve1993-11-0808 November 1993
- on 931008,pressure Isolation Valve Failed to Seat Tightly During Plant Operation Due to Loose Hinge Mechanism.Replaced Internals of Pressure Isolation Valve
1999-09-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
05000289/LER-1998-009-01, :on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised1998-09-18018 September 1998
- on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised
1999-09-30
[Table view] |
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j GPU Nuclear Corporation i
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Q Mf Post Office Box 460 Route 441 South Wddletown, Pennsylvania 1M67 0191 717 944 7621 i
TEl.EX 84 2386
" riter's Direct Dial Number:
(717) 948-8005 June 4, 1992 C311-92-2074 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
Dear Sir:
Three Mile Island Nuclear Station, Unit 1 (TMI-1)
Operating Licensing No. DPR-50 Docket No. 50-289 LER 92-001-01 This letter transmits Licensee Event Report (LER) No 92-001-01 regarding.in inadvertent Emergency Feedwater System (EFW) actuation which occurred on January 22, 1992 during planned maintenance due to an installation error.
Public health and safety were not affected. This revision is being submitted to clarify the root cause to include inadequate startup testing as a contributor to the event.
This LER is being submitted pursuant to 10 CFR 50.73.
The abstract provides a brief description of the event.
For a complete understanding of the event, refer to the text of the report.
Sincerely, 2Ki-u lh'-
T. G. Br ghton Vice President and Director, TMI-1 MriX Attachment cc:
Region.I Administrator THI-l Senior Project Manager TMI Senior Resident Inspector 9206110094' 9'20604
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PDR GPU Nucleaf Corporation is a subscary of General Pubirc Ubhbes Corporabon
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Inadvertent Emergency Feedwater (EFW) Actuation During Planned Maintenance Due to Installation Error TMl-1 was operating at 100% power. During a planned maintenance activity.
Emergency Feedwater (EFW) was inadvertently initiated for a short time.
This event is reportable in accordance with 10 CFR 50.73(a)(2)l,iv). The actuation occurred due to a construction wiring error resulting from n.odifications during a previous outage. This event was caused by lack of drawing clarity, inadequate supervisory oversight and failure of
.e test procedure to verify separation between HSPS channels and trains as required in the modification test program.
All equipment functioned as expected considering the wiring errors There was no adverse impact on nuclear safety.
Wiring errors which could affect system operation have now been corrected. A detailed walkdown will be performed and the applicable drawings will be revised to reflect the as built configuration. TMl-1 has in place sufficient procedural controls to preclude or identify wiring errors and as such this event is considered to be an isolated case.
The potential for single failures to cause an inadvertent EFW actuation had been previously evaluated and with the NRC's concurrence this wat deemed acceptable.
No additional action is considered necessary.
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,. uc %,u.. n n Inadvertent Emergency Feedwater (EFW) Actuation During Planned Maintenance Due to Installation Error I.
Plant Operating Conditions before Event:
TMI-l was operating at 100% rated power.
The ICS was in full automatic control. Work was planned to be performed on the "lB" Inverter.
11.
Status of Structures, Components, or Systems that were Inoperable at the Start of the Event and that Contributed to the Event
None III.
Event Description
This event occurred at approximately 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on January 22, 1992. The operating crew had performed the prerequisites for transferring the "B" 120 vac vital bus (VBB) (ED/BU]* from its normal source, the "lB" inverter (ED/lNV]*, to its alternate source (TPA), in accordance with Operating Procedure (0P) 1107-2, " Emergency Electrical System." During the transfer, it was necessary to temporarily deenergih vital bus kBB.
OP 1107-2 includes actions and precautions which identify the loads on the bus, the effect of loss of VBB and what precautionary actions are to be taken.
When VBB was deenergized in a aordance with the procedure, the follcwing events occurred in addition to those described in the procedure:
1.
Main Steam supply valve, MS-V13A (SB/V)', opened and the turbine-driven EFW Pump (EF-P1) developed discharge pressure sufficient to produce flow into the Once Through Steam Generators (OTSGs).
2.
Valve controllers asscciated with EFW control valves, EF-V30B/D [BA/V]*, switched to 50% operating level setpoints, an ope, ating range level input, and received a level signal less than the 50% sotpoint.
Both control valves opened and EFW flow was initiated te both OTSGs (AB/SG]*.
3.
Annunciator J-1-3/J-1-4 (IB/ ANN]* "EFW ACTVA'ED OTSG A/B" went into alarm.
The operator identified the improper system response, placed EF-V308/D in
" manual" and closed both valves.
This terminated flow to the OTSGs very shortly after it had been initiated.
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THRE: MILE ISLAND, UNIT 1 opo o ;o 2 l8 l9 9j2
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.-y,- -, w, The Control Room Operator (CRO) sent an Auxiliary Operator (AO) to EF-P1 (BA/P)*.
The CR0 attempted to close MS-V13A from console center.
MS-V13A did not close.
Within the first minute following the EFW actuation the overhead Annunciator J-1-3/J-1-4 cleared and the CR0 was able to close MS-V13A from the Control Room. These events occurred without any EFW functions being placed in " defeat."
EF-V30B/D continued to indicate that an actuation signal was present after the overhead annunciator was clear (the AUTO Light was "on' above each valva controller). The operators attempted to clear this signal by placing the Train "B" Loss of Reactor Coolant Pumps (RCPs) Defeat / Enable Switch to " defeat." This action had no apparent effect.
An operator verified that the Heat Sink Protection System (HSPS) Train "B" cabiret had swapped to the backup power source as designed and that there were no unexpected indications locally at the HSPS cabinets. With EfW flow terminated and without any cause of t'l actuation determined, the shiff supervisor and operations management decided to reduce the present vulnArability by restoring power to VBB from TRA.
When VBB was reenergized from TRA, EF-V30B/D transferred (without any operator action) into " Auto," with 0% setpoint and a good startup level input. This is the normal state for these controllers.
With power restored to VBB all indications for HSPS both locally and in the Control Room appeared normal.
a The actuation occurred due to a modification construction error during TMI-l's Cycle 8 Refueling Outage (8R) which had gone undetected until this time.
8R occurred between January and March, 1990.
Two train "B" nests had been powered from the Channel 11 DC distribution bus (located in HSPS Section A2, Rack 3) instead of the "B" Train DC distribution bus (located in Section A2, Rack 4) as required. The net effect was that deenergizing VBB caused a loss of power to a portion, but not all, of the Train "B"
nests.
The causes of this event were identified as follows:
1.
The 8R construction drawings were not clear and could easily be misinterpreted.
it was believed that all of the problems associated with drawing presentation and wiring errors had been identified and corrected prior to turnover. The subject installation error went undetected.
Problems with drawing clarity were addressed in the Post 8R critique of the HSPS modification to prevent a recurrence in future modifications, p._ _.,
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The Startup and Test (SV/T) group was not involved during tha init.ial phase of construction as has besa a practice in other outages including the most recent 9R outage which occurred between September and November, 1991. As a result, no THI-1 cognizant SU/T engineer was present during SR at the work site to provide technical guidance to the construction workers during the initial construction phase of the modification.
Inadequate supervisory oversight was identified as a probable contributor to construction errors described above during the BR critique and recommendations from the critique were implemented to increase SU/T involvement during construction of complex modifications with safety significance.
3.
Th0 generic electrical testing that verifies all construction wiring shous 3 have corrected this problem early in the test program, Functional testing requirements to verify power separation between HSPS channels and trains should have identified and resulted in correction of the wiring problems.
Inadequate implementation of the SU/T modification test program requirements allowed the power supply wiring error to go undetected during both generic an ' functional tests.
IV. Component Failure Data
There were no component failures associated with this event.
V.
Automatic or Manually Initiated Safety System Responses:
(
All equipment associated with a Train "B" EFW actuation functioned as expected considering the improper wiring configuration. MS-V13A opened after receiving an actuation signal caused by loss of power to modules (JB/lH0D]' within the actuation control logic, t
Based upon obsetlations during the event and subsequent testing it was
- oncluded that the actuation signal to MS-V13A and MS-V130 cleareu before MS-V13B received an "open" demand.
By design, MS-V13B is opened approximately 40 seconds after MS-V13A.
EF-P1 came up to speed and provided sufficient discharge pressure to deliver water to each OTSG. The motor-driven EFW Pump, EF-P2B, did not start because the HSPS actuation signal has an interposing relay powered from VBB which starts the pump.
With VBB deenergized, the relay did not energize to start EF-P28.
EF-V30B/D received invalid actuation signals and level inputs due to deenergized modules in the logic which provides the inputs to the controllers.
Given the faulty inputs, the valves functionad as expected.
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- VI. Assessment of the Safety Consequences and Implications of the Event:
A.
There is no adverse impv.t on nuclear safety from Train "B" modules being powered from Channel 11.
The Train "B" modules incorrectly powered from Channel 11 should receive power from Train "B" power supplies which are also powered from VBB. This condition would not resalt in a single failure which wculd have consequences worse than a failure of VBB which has been evaluated.
If power is lost to VBB, the HSPS System is still capable of performing its design function. With a loss of power to VBB, Channel 11 is actuated and Train "B" is incapable of performing its design function, but Train "A" is unaffected by loss of VBB.
B.
The design basis for EFW/HSPS considered system failures in which the EF-V30 valves would fail closed or open, t.oss of air or signal causes valve closure.
Under conditions of partial train power failure, the EF-V30 valves on nne train may fail open.
This does not impact nuclear safety because a reasonable time period (at least 15 minutes) is available for operator action to locally isolate the failed valve and the ability to terminate flow to one or both OTSGs is still available from the Control Room. This can be accomplished with EF-P2A and EF-P2B control switches and EFW discharge header crossconnect isolation valves, EF-V2A/B [BA/V]*, pushbuttons.
VII. Previous Events of a Similar Nature:
None.
Three previous EFW actuations nave occurred at TH1-1 since the HSPS was installed.
In the case of each previous EFW initiation, the system responded as designed when a valid actuation signal was sensed at the input to the system. The cause of previous events was external to the HSPS.
The cause of this event was an internal wiring error.
Therefore, the previous events were not similar.
Vill. C(rrective Actions Taken:
1.
Through entries in the night order book, the operating crews were advised of the events which h:d taken place and given instructions on
/
the actions to be taken if power were lost to VBB.
2.
The power cables from Train nests "A2-6-6" ana "A2-6-7" have been rewired to provide proper termination from the Train "B" power supply.
Functional testing, performed in accordance with a Special Test Procedure (STP-92-004), verified power separation between the HSPS channels and the "B" Train.
3.
A walkdown of Channels 1 & 11 and Trains *A"
& "B" was performed.
It was verified from the walkdown that the channel and train nests are povered from the proper train and channel powar supplies.
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additional testing of the "A" Train power supply was required.
Other discrepanciesbetweenthedrawingsandtheexistingconfigurationwerel noted during the walkdown. However, it was determinid that these discrepancies would have no effect on system operatic,1.
IX.
Corrective Actions Planned:
Wiring errors that could affect system operation have been corrected.
In order to correct the other noted discrepancies, a more detailed walkdown of the HSP5 povar supply wiring is required and will be performed at the next outage of opportunity.
The affected HSPS drawings will be revised to reflect the as built configuration.
X.
Conclusion The potential for single tallures, as occurred during this event, to cause an inadvertent EFW actuation were identified during THI-l's Cycle 8 Refueling Outage (BR).
Prior to startup from the 8R outage, modifications were performed to eliminate the potential for inadvertent MFW isolations resulting from a pari.ial or total loss of power to the HSPS.
However, evaluations during 8R confirmed that the consequences of an EFW actuation are acceptable. The prevention of inadvertent EFW initiation resulting from a single failure is not a regulatory requirement.
This was reported to the NRC in a letter dated July 5,1990
_ during THI-l's Cycle 8 Refueling Outage (8R). With NRC concurrence it was concluded-at that time that modifications to prevent EFW actuations on partial loss of power would not be required. Although, partial loss of power to the HSPS r" 4 not result in loss of safety function and does not result in a safety nard, this event was undesirable.
Having corrected the wiring errors that resulted in this event, GPU Nuclear continues to believe further modifications are not required.
The contributors to this event, which caused the wiring error, have been identified as a problem with drawing clarity and inadequate supervisory oversight by individuals knowledgeable of the HSPS design and the modification be 49 performed.
In addition, inadequate implementation of the SU/T modification test program allowcd the wiring errors to remain undetected. The involvement of the SU/T group during-the initial phase of construction, as in nther outages including the most recent 9R Outage, and. proper implementation of the SU/T modification test program requirements would have avoided the wiring error or identified its existence. Therefore, this ; vent fs considered to be an isolated case.
No additional ~ action is considered to be necessary.
- The Energy Industry Identification System (Ells), System Identification (SI) and Component Function Identification (CFI) Codes are included in brackets,
"[SI/CFI)", where applicable, as required by 10 CFR 50.73(b)(2)(ii)(F).
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