Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange InstalledML20078A657 |
Person / Time |
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Site: |
Three Mile Island |
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Issue date: |
09/07/1983 |
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From: |
Hukill H, Stephenson C GENERAL PUBLIC UTILITIES CORP. |
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To: |
Murley T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
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References |
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RTR-NUREG-0737, RTR-NUREG-737, TASK-3.D.3.4, TASK-TM 5211-83-168, LER-82-001-01T, LER-82-1-1T, NUDOCS 8309230361 |
Download: ML20078A657 (4) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000289/LER-1984-007, Corrected LER 84-007-01:on 841116,once-through Steam Generator a Tubes Identified as Category C-3 Defective (More than 1% of Insp Tubes Defective).Further Manifestation of Problem Found During 1981 & 1982 Testing1985-05-31031 May 1985 Corrected LER 84-007-01:on 841116,once-through Steam Generator a Tubes Identified as Category C-3 Defective (More than 1% of Insp Tubes Defective).Further Manifestation of Problem Found During 1981 & 1982 Testing 05000289/LER-1983-046, Revised LER 83-046/01T-1:on 831214,nuclear safety-related Circuit for make-up Pump Lube Oil Pressure Trip Found Incorrectly Routed.Caused by Design Oversight.Circuits for make-up Pumps Rerouted in Raceways1984-01-31031 January 1984 Revised LER 83-046/01T-1:on 831214,nuclear safety-related Circuit for make-up Pump Lube Oil Pressure Trip Found Incorrectly Routed.Caused by Design Oversight.Circuits for make-up Pumps Rerouted in Raceways 05000289/LER-1982-001, Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange Installed1983-09-0707 September 1983 Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange Installed 05000289/LER-1983-003, Updated LER 83-003/01T-1:on 830211,PORV Special Insp Revealed Corrosion.Caused by Use of Acid Sulfur Compounds. PORV Internals Replaced & Leak Tested & Pressurizer Steam Space Inspected1983-06-0606 June 1983 Updated LER 83-003/01T-1:on 830211,PORV Special Insp Revealed Corrosion.Caused by Use of Acid Sulfur Compounds. PORV Internals Replaced & Leak Tested & Pressurizer Steam Space Inspected 05000320/LER-1979-015, Sanitized Version of LER 79-015/13L-1:on 790328,during Investigation of Radwaste & Makeup Sys,Three People Received Radiation Doses in Excess of Quarterly Limit.One Person Received Excess Dose to Skin.Investigation Suspended1982-06-10010 June 1982 Sanitized Version of LER 79-015/13L-1:on 790328,during Investigation of Radwaste & Makeup Sys,Three People Received Radiation Doses in Excess of Quarterly Limit.One Person Received Excess Dose to Skin.Investigation Suspended 05000289/LER-1982-0041982-04-14014 April 1982 LER 82-004:on 820413,EPRI Tests on Pressurizer Code Safety Valves Revealed Failure to Determine Ability of Valve to Perform Under Feed & Bleed Cooling If Pressurizer Power Operated Relief Valve Isolated.Investigation Underway 05000289/LER-1977-016, Supplemental LER 77-016/01T:on 770924,emergency Core Cooling Actuation Occurred.Caused by Full Open Pressurizer Power Relief Valve.Valve Closed1977-02-14014 February 1977 Supplemental LER 77-016/01T:on 770924,emergency Core Cooling Actuation Occurred.Caused by Full Open Pressurizer Power Relief Valve.Valve Closed 1985-05-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With ML20153A9941998-09-16016 September 1998 Safety Evaluation Denying Request to Remove Missile Shields from Plant Design ML20151U8821998-09-0808 September 1998 SER on Revised Emergency Action Levels for Gpu Nuclear,Inc, Three Mile Island Nuclear Plant Units 1 & 2 ML20151V2811998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Tmi,Unit 1.With ML20237A8331998-08-12012 August 1998 Safety Evaluation Accepting USI A-46 Program Implementation at Plant,Unit 1 ML20237C6411998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Tmi,Unit 1 ML20236R2201998-06-30030 June 1998 Monthly Operating Rept for June 1998 for TMI-1 ML20236W9961998-06-0909 June 1998 1998 Quadrennial Simulator Certification Rept ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20249A1061998-05-31031 May 1998 Monthly Operating Rept for May 1998 for TMI-1 ML20247G0761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Three Mile Island Nuclear Station,Unit 1 ML20212A2191998-04-22022 April 1998 Rev 3 to Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2 ML20248H6991998-04-0808 April 1998 Requests,By Negative Consent,Commission Approval of Intent to Inform Doe,Idaho Operations Ofc of Finding That Adequate Safety Basis Support Granting Exemption to 10CFR72 Seismic Design Requirement for ISFSI to Store TMI-2 Fuel Debris ML20216K1061998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Three Mile Island Nuclear Station,Unit 1 ML20217E0811998-03-24024 March 1998 Rev 0 to TR-121, TMI-1 Control Room Habitability for Max Hypothetical Accident ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216F0981998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Three Mile Island Nuclear Station,Unit 1 ML20202F8121998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for TMI Nuclear Station, Unit 1 ML20199G8371998-01-22022 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Three Mile Island Nuclear Station,Unit 1 ML20198N2901998-01-12012 January 1998 Form NIS-1 Owners' Data Rept for Isi ML20199J3251997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Three Mile Island Nuclear Station,Unit 1 1999-09-30
[Table view] |
LER-2082-001, Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange Installed |
Event date: |
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Report date: |
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2892082001R00 - NRC Website |
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EVENT DESCRIPTION AND PROS A8LE CONSEQUENCES h 1 o 121 l During ordered shutdown and while evaluatine contrn1 rnn- habitabilftv review off f7TTl i NUREG 0737 Item III.D'.3.4 an item reportable per T.S. 6.9.2.A(9) was identified. 1 i
4 lo 64 i l Computer room air conditioning unit duct work penetrates the wall to the fuel Iei5i L handling buildine. There is no radiation signal interlock to shutdown the unit.. I l o is j l There nnnenrm to be a notential for this to allow contaminated air to enter an ared ga;y; ; served by the control building ventilation system.
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,,,o,l Blind flange is installed on make-up duct to minimize the effect of an airborne Long term ;
g gcontamination problem in the fuel handling or auxiliary building.
g ; corrective action will be to implement administrative controls to close fire g Idampers FD-48 and 49 on seismic event alarm in the control room..
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ATTACHMENT I LICENSEE EVENT REPORT NARRATIVE REPORT TMI-1 LER 82-001 I. CURRENT ACTIVITIES AT THE TIME OF THE OCCURRENCE TMI Unit 1 was in a long term cold shutdown. Engineering was performing a design review on the Control Building Ventilation System.
II. LEADING CIRCUMSTANCES A preliminary safety concern which dealt with the potential of breaching an environmental barrier at the time of installation of an air conditioning unit to service the Control Building computer room has been evaluated.
The concern identified the possibility of introducing make-up air from the Auxiliary and Fuel Handling buildings, a potentially contaminated area (post accident), into the Control Building Ventilation System which serves the Control Room. The concern further identified the installation as having been made with no provision for automatic isolation on high airborne radioactivity to exclude che potencial contaminants from the Control Build-ing Ventilation System.
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III. DESCRIPTION In November 1975, criteria was developed for the installation of a " closed-loop" air conditioning unit to support the Modular Computer System in the Control Building. In early 1976, the installation was completed. During the 1979 Refueling' Outage the ductwork for this air conditioning system was modified with the installation of seismically qualified UL listed 3-hour rated fire dampers (FD-48 and FD-49) to isolate the Control Building side (computer room) from the Fuel Handling side where the air conditioner (AH-E-108) is mounted. The fire dampers trip closed and the air conditioner shuts down when a fire detection system actuated and not on high airborne radioactivity in the area. The fire detection system was installed in conjunction with a Halon 1301 fire suppression system for the computer room sub-floor area.
Although the fire dampers are seismically designed, the adjacent suction and discharge duct work are not. The concern is tnat if a seismic event were to suf ficiently damage this ductwork, in conjunction with a high airborne radioactivity condition in the fuel and auxiliary building ventilation system; the control room ventilation system could potentially become contaminated.
Also, should the air conditioning system make-up line let contaminated air into the mod comp room, it could potentially contaminate the control build-ing ventilation system.
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None V. PREVIOUS EVENTS OF A SIMILAR NATURE None VI. ROOT CAUSE Recen:~ design _ reviews have deter =ined tha: he " closed-loop" air conditioning syster was not built or designed in accc: dance with the standard review plan (SRP) and, therefore, :he syster does not mee:
the requirements of- NUPIG 0737 See:1on III.D.3.4 The application of the criteria contained in the SRP has resulted in a "new lock" at the purpose of the control roo: ventilarien envelope and has resulted in a reconsideration of the air conditiening system.
VII. I.WIDICE CORRECTIVE ACTION The installation of a- block off plate on the take-up air due: work -
has mini = iced the possibility of the introdue:io: cf centa=inated take-up air into the Control Building Envelope in the event of a radiation accident.
VIII. LONG TERM CORRECTIVE ACTION The procedure:for responding to a seistic even: has been codified c recuire that :ihe Control Building cc puter roc = air tendi:icner be i turned off and .he seistic fire da=pers FD-45 and FD-49 be manually l closed. This procedure is iniziated based en seis=ic even alarns in 1
- ne Con:rci noc=.
The closed fire da:pers would preclude significan: rigra:ic: cf centamination fro: the hallway area.in the eeen: cf centaninated air bei .; present in the Fuel Handling Suilding.
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GPU Nuclear Corporation L Nuclear =fme Bs48 S Middletown, Pennsylvania 17057 717 944 7621 TELEX 84-2386 Writer's Direct Dial Number:
September 7, 1983 5211-83-168 Dr. Thomas E. Murley Region I, Regional Administrator U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Sir:
Three Mile Island Nuclear Station, Unit 1 (TMI-1)
Operating License No. DPR-50 Docket No. 50-289 LER 82-01/0lT-2 Attached please find Update Licensee Event Report 82-01/0lT-2 which is a follow-up report concerning control building ventilation discrepancies.
This event was prompt reported per Technical Specifications 6.9.2. A(9) on February 25, 1982. The follow-up report was submitted March 17, 1982 (5211-83-070). This revision is simply corrections to Rev. 1 of the subject LER.
Sincerely, Pp L eek H. Hukill Director, TMI-l HDH:CJS:vj f Enclosures cc: R. Conte NRC Office of Management Information & Program Control 6
GPU Nuclear Corporation is a subsidiary of the General Pubhc Utilities Corporation
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05000289/LER-1982-001, Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange Installed | Updated LER 82-001/01T-2:on 820225,during Control Room Habitability Review of NUREG-0737,Item III.D.3.4,potential Discovered for Contaminated Air to Enter Area Served by Control Bldg Ventilation Sys.Flange Installed | | 05000289/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | 05000289/LER-1982-004 | LER 82-004:on 820413,EPRI Tests on Pressurizer Code Safety Valves Revealed Failure to Determine Ability of Valve to Perform Under Feed & Bleed Cooling If Pressurizer Power Operated Relief Valve Isolated.Investigation Underway | | 05000289/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | 05000289/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | 05000289/LER-1982-008, Forwards LER 82-008/01T-0 | Forwards LER 82-008/01T-0 | | 05000289/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | 05000289/LER-1982-010, Forwards LER 82-010/99X-0 | Forwards LER 82-010/99X-0 | | 05000289/LER-1982-011, Forwards LER 82-011/99X-0 | Forwards LER 82-011/99X-0 | | 05000289/LER-1982-013, Forwards LER 82-013/03L-0 | Forwards LER 82-013/03L-0 | | 05000289/LER-1982-014, Forwards LER 82-014/03L-0 | Forwards LER 82-014/03L-0 | | 05000289/LER-1982-015, Forwards LER 82-015/03L-0 | Forwards LER 82-015/03L-0 | | 05000320/LER-1982-015, Forwards LER 82-015/01L-0 | Forwards LER 82-015/01L-0 | | 05000289/LER-1982-016, Forwards LER 82-016/03L-0 | Forwards LER 82-016/03L-0 | | 05000320/LER-1982-016, Forwards LER 82-016/03L-0 | Forwards LER 82-016/03L-0 | | 05000320/LER-1982-017, Forwards LER 82-017/03L-0 | Forwards LER 82-017/03L-0 | | 05000320/LER-1982-018, Forwards LER 82-018/03L-0 | Forwards LER 82-018/03L-0 | | 05000320/LER-1982-019, Forwards LER 82-019/03L-0 | Forwards LER 82-019/03L-0 | | 05000320/LER-1982-020, Forwards LER 82-020/01L-0 | Forwards LER 82-020/01L-0 | | 05000320/LER-1982-022, Forwards LER 82-022/03L-0 | Forwards LER 82-022/03L-0 | | 05000320/LER-1982-023, Forwards LER 82-023/03L-0 | Forwards LER 82-023/03L-0 | |
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