07-06-2012 | On 05/09/12 a TMI-1 station review of Operating Experience ( OE) event # 0E30225 was provided to the NRC. The station recognized at that time that this response would need to be revised and entered an issue report (IR# 1364596) into the corrective action database. Subsequent review determined that in a condition in which one main feedwater pump had been reset but was not aligned and providing main feedwater flow to the steam generators, a trip of the other main feedwater pump while providing main feedwater flow to the steam generators, would not have resulted in an actuation to start the emergency feedwater system. It was concluded that the described condition occurred on six different occasions at TMI-1 in the past three years. This condition was not recognized as an entry condition into the TMI-1 Technical Specifications. Corrective actions include revising the 0E30225 response, revising applicable procedures, evaluating modifications, operator/technical training and improvements to the Technical Specifications. This event is considered to have no significance with respect to the health and safety of the public.
The submittal of this LER constitutes reporting to the NRC in accordance with 10 CFR 50.73 (a)(2)(vii)(A) and 10 CFR 50.73 (a)(2)(vii)(B). |
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There were no structures, systems, or components out of service that contributed to this event.
Event:
In response to the Nuclear Regulatory Commission's request to see Three Mile Island Nuclear Power Station's (TMI-1) original response to Oconee 0E30225, TMI-1 discovered that the original review would need to be revised and generated issue report IR# 1364596. TMI-1 provided the original response to the NRC on May 9, 2012.
TMI-1's original review of 0E30225 in 2009 assumed that operators would recognize and take action relative to the loss of main feedwater (FW). The original review recognized the applicability and similar vulnerability as described in 0E30225, however, there were no prescribed corrective actions.
TMI-1 main feedwater pump (MFWP) operating status is monitored by pressure switches that sense hydraulic oil pressure at the main feedwater pump turbine. The hydraulic oil pressure is an indication of main feedwater pump turbine operating status and inputs are provided to the Reactor Protection System (RPS) and Heat Sink Protection System (HSPS). With one main feedwater pump turbine operating (providing feedwater flow to the steam generators) and one main feedwater pump turbine in a `reset' condition (satisfactory hydraulic oil pressure is indiciated but is not providing feedwater flow to the steam generators), the Reactor Protection System (RPS) trip and a Heat Sink Protection System (HSPS) actuation associated with a loss of both main feedwater pumps is operationally bypassed.
In the past three years TMI has experienced the above operational condition six times as follows:
01/24/10, amount of time from second MFWP reset until FW flow established: 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, 42 min.
05/06/10, amount of time from second MFWP reset until FW flow established: 14 min.
05/31/10, amount of time from second MFWP reset until FW flow established: 39 min.
09/21/10, amount of time from second MFWP reset until FW flow established: 27 min.
11/26/11, amount of time from second MFWP reset until FW flow established: 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, 29 min.
05/26/12, amount of time from second MFWP reset until FW flow established: 25 min.
For all six of the above identified conditions the capability to remove residual heat was maintained although automatic actuation of emergency feedwater (EFW) on a trip of the operating main feedwater pump was lost. In all plant conditions, HSPS system would automatically initiate EFW based upon a low water level sensed in either steam generator and, manual actuation capability was maintained.
The six identified operational conditions were not recognized by the operating staff as an entry condition into a one hour technical specification action statement. On May 26, 2012, a planned down-power occurred which required one main feedwater pump to be secured. The Operating crew briefed the Oconee operating experience and discussed actions required to minimize time in this condition.
6 This condition is reportable under 10 CFR 50.73(a)(2)(vii)(B) since a single condition caused two independent trains to become inoperable in a system designed to remove residual heat because a single main feedwater pump in 'reset' bypassed the Emergency Feedwater pump auto start instrumentation for the Heat Sink Protection System.
The condition is also being reported under 10 CFR 50.73(a)(2)(vii)(A) because a single condition caused two independent trains or channels to become inoperable in a single system designed to shut down the reactor and maintain it in a safe shutdown condition. The single condition being when a single main feedwater pump is 'reset' with the other MFWP providing main feedwater flow while reactor power is greater than 7% power, a loss of the running MFWP would not result in an anticipatory reactor trip (ART).
B. CAUSE OF EVENT
The cause of the event was due to an inadequate review of pertinent and applicable operating experience that resulted in continuing station vulnerability to technical specification noncompliance.
The reviewer recognized the vulnerability but did not involve Operations licensed personnel to ensure Technical Specifications were complied with.
C. ANALYSIS / SAFETY SIGNIFICANCE
At no time was the allowed out of service time exceeded during the,six identified operating conditions when the Technical Specification was entered but not recognized.
The anticipatory reactor trip (ART) in the Reactor Protection System (RPS) for the event of loss of main feedwater when greater than 7% reactor power have been added to reduce the number of challenges to the safety valves and power operated relief valve. The ART feature is not credited in the plant safety analysis; it exists to reduce the probability of an overpressure event and challenge to the pressurizer code safety valves.
The Heat Sink Protection System (HSPS) detects low steam generator level and automatically initiates emergency feedwater. In the event that the reported condition in which one MFWP was running and providing main feedwater flow with the second MFWP in a reset condition (bypassing HSPS EFW actuation on loss of main feedwater), a low steam generator level in either steam generator would still actuate the start of emergency feedwater.
Therefore, in the main feedwater pump turbine 'reset' condition, with the RPS trip and a HSPS actuation associated with a loss of both main feedwater pumps operationally bypassed:
o The identified condition (bypass) does not initiate or result in a plant transient such that it could be viewed as a precursor to a significant event.
o There are alternate diverse parameters that sense the loss of feedwater and provide either a reactor trip or EFW actuation such that the identified condition would not lead to a more significant safety concern.
o TMI-1 has not had plant transients or complications to plant operations due to the identified condition such that the performance indicators were impacted let alone exceeded a threshold.
6 o The identified condition is associated with the NRC Reactor Safety cornerstone — mitigation systems by the attribute of configuration control as measured by the operating equipment lineup.
The associated cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage) is not adversely impacted as a result of the diverse parameters that sense loss of main feedwater and initiate emergency feedwater.
D. CORRECTIVE ACTIONS
1. Revise response to 0E30225 2. Revise operating procedures to recognize entry into TS condition (including declaring/logging LCO) 3. Evaluate possible modifications/design changes to preclude identified condition 4. Evaluate operator and technical training needs to correct deficiencies 5. Evaluate improvements to Technical Specifications and Bases 3.5.1.9 and Table 3.5-1 section D.
E. PREVIOUS OCCURENCES
TMI-1 recently performed a common cause analysis (CCA 1324039) due to several instances of either not properly identifying Technical Specification Limiting Conditions for Operation times or impacts on station risk during work preparation. From the CCA "Previous Events/OE Review section":
Institute of Nuclear Power Operation (INPO) Operating Experience (OE) database and Exelon's Corrective Action Program (CAP) Passport database were reviewed to find similar events associated with either inadequate LCO identification or understanding impacts of system availability. Several INPO OE items were identified relative to missed LCO and availability requirements due to failed equipment or untimely entry in LCO statements.
Two events associated with not properly identifying LCO action statements at TMI were identified.
Review of these analysis products was used to formulate corrective actions for this analysis.
Previous Events Previous Event Review Apparent Cause Evaluation (ACE) 1123004 Background:
(Late Containment Technical Specification In October 2010, TMI licensed personnelEntry during Reactor River Maintenance) failed to identify the applicability of entry into containment isolation Technical Specifications (TS) during performance of work on the Engineered Safeguards (ES) system Reactor Building Emergency Cooling (RBEC). NRC residents challenged the station approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> into a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown LCO statement on the missed entry.
Gap with senior reactor operators misapplying understanding of operability and design bases requirements relative to remotely controlled containment isolation valves associated with 6 5
Background:
On 2/21/08, Operations configured the plant such that only one train of Reactor Building Emergency Cooling (RBEC) was available.
TMI-1 TS allows this lineup for a seven day period, however, licensed operators failed to identify the nonconforming condition. During this event, electrical train separation did not exist between the two Reactor Building Air Handling Unit (AH-E-1) fans that were in service. This condition was identified approximately six and half days into a seven day shutdown LCO action statement.
ACE 742762 identified gaps with licensed operators improper interpretation of TS 3.3.3.c relative to three train systems and lack of TS procedural guidance when removing AH-E-1 fans from service.
Review:
Training solution actions and procedure revisions were implemented to ensure compliance with TS 3.3.3.c from ACE 742762.
Specifically, Licensed Operator Requalification Training (LORT) / Initial Licensed Operator Training (ILT) lesson plans were modified and procedure steps addressing RBEC TS requirements were added to procedures that remove AH-E-1 fans from service. Similar training and procedure change actions have been adopted for this analysis.
- Energy Industry Identification System (EllS), System Identification (SI) and Component Function Identification (CFI) Codes are included in brackets, [SI/CFI] where applicable, as required by 10 CFR 50.73 (b)(2)(ii)(F).
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05000413/LER-2012-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2012-001 | Unanalyzed Condition Affecting Essential Raw Cooling Water System due to External Flooding | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000388/LER-2012-001 | Two Control Room Floor Cooling Systems Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000395/LER-2012-001 | Vice President, Nuclear Operations 803.345.4342 August 3, 2012SCE~r .so A SCANA COMPANY Document Control Desk U. S. Nuclear Regulatory Commission
Washington, DC 20555
Dear Sir / Madam: Subject:VVIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50-395 OPERATING LICENSE NO. NPF-12 LICENSEE EVENT REPORT (LER 2012-001-01) CORE EXIT THERMOCOUPLES & REACTOR WATER LEVEL INDICATION SYSTEM INOPERABLE DUE TO AN INADEQUATE MAINTENANCE PROCEDURE Attached is Licensee Event Report (LER) No. 2012-001-01 for the Virgil C. Summer Nuclear Station Unit 1. This revised report describes a condition where Core Exit Thermocouples and Reactor Water Level Indication System would not be operable for accident monitoring. This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B). This letter and attached LER contain no new commitments and no revisions to existing
commitments.
Should you have any questions, please call Bruce Thompson at (803) 931-5042. Very truly yours, Dal Thomas D. Gatlin TS/TDG/jw
Attachment
c: K. B. Marsh P. Ledbetter S. A. Byrne J. C. Mellette J. B. Archie EPIX Coordinator N. S. Carps K. M. Sutton J. H. Hamilton INPO Records Center R. J. White Marsh USA, Inc. W. M. Cherry R. J. Schwartz V. M. McCree NSRC R. E. Martin RTS (CR-11-01807) NRC Resident Inspector FileV(818.07) M. N. Browne PRSF (RC-12-0116) V fALVirgil C. Summer Station • Post Office Box 88 .Jenkinsville, SC • 29065 • F (803) 345-5209 1 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours.0Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocollects.resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management andLICENSEE EVENT REPORT (LER) Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Virgil C. Summer Nuclear Station Unit 1 05000 395 1 OF 5 4. TITLE Core Exit Thermocouples & Reactor Water Level Indication System Inoperable due to Inadequate Maintenance Procedure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000397/LER-2012-001 | DG-3 Inoperable for Longer than Allowed by TS Due to Failed Governor 05000 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-001 | Forced Shutdown Due to an Increase in Drywell Leakage in Excess of Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000289/LER-2012-001 | Single Condition Making Independent Trains Inoperable | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2012-001 | Common Cause Inoperability of Both Trains of Motor Driven Auxiliary Feedwater (AFW) Pumps Due to Inability to Control AFW Regulating Valves After Isolation of Nitrogen Backup | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000265/LER-2012-001 | Main Steam Isolation Valve Local Leak Rate Test Exceeds Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2012-001 | Two Main Steam Safety Valves Failed Pre-outage Setpoint Testing Due to Abnormal Spring Geometry | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-001 | Technical Specification Required Plant Shutdown Due to Missed Surveillance and Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000483/LER-2012-001 | Modification Implementation Error Adversely Impacted the Containment Cooling System | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2012-001 | Containment Concrete Thickness At Spalled Patch Does Not Meet Technical Specification Design Value | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000414/LER-2012-001 | Carolinas Duke Energy Carolinas, LLC 4800 Concord Rd. York, SC 29745 803-701-4251 December 20, 2012 U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
Subject:�Duke Energy Carolinas, LLC (Duke Energy)
Catawba Nuclear Station, Units 1 and 2
Docket Nos. 50-413 and 50-414
Licensee Event Report 414/2012-001
Pursuant to 10 CFR 50.73(a)(1) and (d), attached is Licensee Event Report 414/2012-001,
Revision 0 entitled, "Diesel Generator (DG) 2B Was Unknowingly inoperable from 09/28/12 to
10/23/12 Due to Failed Tachometer Relay Power Supply".
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B), 10 CFR
50.73(a)(2)(ii)(B), and 10 CFR 50.73(a)(2)(v)(A)-(D).
There are no regulatory commitments contained in this letter or its attachment. This event is considered to be of no significance with respect to the health and safety of the
public.
If there are any questions on this report, please contact L.J. Rudy at (803) 701-3084. Kelvin Henderson LJR/s Attachment www. duke-energy. corn Document Control Desk Page 2 December 20, 2012 xc (with attachment): V.M. McCree Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, GA 30303-1257 J.H. Thompson (addressee only) NRC Project Manager U.S. Nuclear Regulatory Commission Mail Stop 8-G9A 11555 Rockville Pike Rockville, MD 20852-2738 G.A. Hutto, III NRC Senior Resident Inspector Catawba Nuclear Station INPO Records Center 700 Galleria Place Atlanta, GA 30339-5957 Document Control Desk Page 3 December 20, 2012 bxc (electronic copy)(with attachment): INPO L.E. Harmon C.S. Kamilaris R.D. Hart G.Y. Helton S.F. Hatley (ICES) M.K. Green R.T. Simril, Jr. B.C. Carroll M.C. Nolan W.J. Pritchett, Jr. T.L. Patterson K.R. Alter H.D. Brewer R.E. Abbott, Jr. B.J. Horsley S.L. Western bxc (hard copy)(with attachment): D.B. Alexander L.S. Nichols L.J. Rudy ELL Master File CN-801.01 LER File RGC Date File NCMPA-1 NCEMC PMPA ICES Lee.Harmon@NRC.gov NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013
(10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported
lessons learned are incorporated into the licensing process and fed back to industry. Send commentsLICENSEE EVENT REPORT (LER) regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.resource@nrclov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used(See reverse for required number of to impose an information collection does not display a currently valid OMB control number, the NRCdigits/characters for each block) may not conduct or sponsor, and a person is not required to respond to, the information collection. r1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 05000414 10OF •4. TITLE Diesel Generator (DG) 2B Was Unknowingly Inoperable from 09/28/12 to 10/23/12 Due to Failed Tachometer
Relay Power Supply | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000247/LER-2012-001 | Technical Specification (TS) Prohibited Condition Caused by an Inoperable 23 Emergency Diesel Generator Fuel Oil Storage Tank Due to Fuel Oil Below TS Limit | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2012-001 | Unanalyzed Conditions Exist for Standby Shutdown Facility Mitizated Events | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000445/LER-2012-002 | COMANCHE PEAK 05000445 10OF06 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000413/LER-2012-002 | Discovery of Inadequacy in Surveillance Testing of Solid State Protection System | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-002 | Unplanned LCO 3.5.4 Entry Due to RWST alignment to Purification | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-002 | Loss of Isolation Function on RHR Shutdown Cooling Suction Line due to Breaker Trip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000482/LER-2012-002 | . One Train of Automatic Safety Infection Blocked During Entry Into Mode 3 Due To Procedural Weakness | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2012-002 | Emergency Diesel Generator Vibration Trip Not Bypassed For Non-Accident Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000346/LER-2012-002 | Leak from Reactor Coolant Pump Seal Piping Socket Weld due to High Cycle Fatigue | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000333/LER-2012-002 | High Pressure Coolant Injection Pressure Control Valve Failure | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2012-002 | Unit 2 Emergency Diesel Generators Inoperable Due To Missing Flood Control Barrier Seal | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000250/LER-2012-002 | Non-compliance with TS 3.4.9.3 due to Manual Isolation Valve Found in Incorrect TS Configuration | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000278/LER-2012-002 | Failure of Primary Containment Isolation Valve due to Foreign Material Results in Condition Prohibited by TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2012-002 | Unit 2 Reactor Trip from Generator Trip Due to Incorrect Relay Setting | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2012-002 | Unplanned Actuation of 121 Motor Driven Cooling Water Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-002 | Improper Rotor Installation Causes Failure of Diesel Generator to Start | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2012-002 | Technical Specification (TS) Prohibited Condition Caused by New Fuel Assemblies Stored in a Configuration Prohibited by the TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2012-002 | Inlet Steam Drain Pot Drain Line Leaks Result in HPCI Inoperabilities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2012-003 | Reactor Building Doors Opened Simultaneously Causes Loss of Safety Function | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000410/LER-2012-003 | Suppression Pool Level Below Technical Specification Limit During Mode Change | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-003 | Plant Modification Interfered with the Operation of Containment Wide Range Level Indicator | | 05000298/LER-2012-004 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000410/LER-2012-004 | Manual Reactor Scram due to a Loss of Main Turbine Gland Sealing Steam Resulting in Lowering Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2012-004 | Essential Chiller Oil Leak Creates Unanalyzed Past Operability Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000265/LER-2012-004 | Drywell Radiation Monitor Failed Downscale | | 05000261/LER-2012-004 | Reactor Tripped Due to a Turbine Trip Caused by a Feedwater Isolation Signal from Steam Generator 'B' High Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000454/LER-2012-004 | Reactor Pressure Vessel Head Control Rod Drive Mechanism Penetration Nozzle Weld Repair Surface Indications | | 05000254/LER-2012-004 | Breech in Secondary Containment | | 05000482/LER-2012-004 | Two Charging Pumps Capable of Injecting into the RCS Due to Inadequate Definition of Centrifugal Charging Pump in LCO 3.4.12 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-005 | Automatic Diesel Actuation Due to the Loss of a 115 kV Offsite Power Source | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-005 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000298/LER-2012-006 | Missing Vent Plug Results in Technical Specifications Prohibited Condition | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2012-007 | High Pressure Coolant Injection System Logic Actuation Following an Automatic Turbine Trip Signal Due to High Reactor Water Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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