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LER-1981-081, Forwards LER 81-081/03L-0.Detailed Event Analysis Encl |
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O PSIEG Public Service Electric and Gas Company P.O. Box 168 Hancocks Bridge, New Jersey 08038 Salem Generating Station September 23, 1981 Mr.
R. C. Haynes i (h ;&
Director of USNRC
((' 0072 Office of Inspection and Enforcement u,
JgOIA *Sl Region 1 S
'b
'8'
'%f 5
631 Park Avenue King of Prussia, Pennsylvania 19406 O
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Dear Mr. Haynes:
4
..F LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-81/03L Pursuant to the requirements of Salem Generating Station Unit No.
1, Technical Specifications, Section 6.9.1.9 b, we'are submitting Licensee Event Report for Reportable Occurrence 81-81/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, ll..5 y
H.
J. Midura Manager - Salem Generating Station s
CC:
R. A Uderitz General Manager - Nuclear Production Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies)
(I 8110020326 G10923 PDR ADOCK 05000272 S
PDR The Energy People 9s 2189 02.sw iiso
1 Report Number:-
81-81/03L Report Date:
9-23-81 j
Occurrence Date:
8-27-81, 9-3-81, 9-9-81, 9-15-81 and 9-18-81 Facility:
Salem Generating Station, Unit 1 Public Service Electric & Gas _ Company Hancocks' Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Individual Rod Position Indications - 2Al, 1SC1, 1C2, 1D4 and 2D2 - Inoperable.
This report was initiated by Incident Reports81-346, 81-361,81-370, 81-375 and 81-384.
CONDITIONS PRIOR TO OCCURRENCE:
8-27-81 Mode 1 - Rx Power 97% - Unit Load 1030 MWe 9-03-81 Mode 1 - Rx Power 96% - Unit Load 990 MWe 9-09-81 Mode 1 - Rx Power 96% - Unit Load 1000 MWe 9-15-81 Mode 1 - Rx Power 91% - Unit Load 1010 MWe 9-18-81 Mode 1 - Rx Power 86% - Unit Load 870 MWe DESCRIPTION OF OCCURRENCE:
On five separate occasions, August 27 and' September 3, 9, 15 and 18, 1981, 1
the control operator noticed that individual rod position indicators (IRPI) for control rods 2A1, 1SCl, 1C2, 1D4 and 2D2, respectively, were-in disagreement with the demand position indicators bf greater than 12 steps.
The IRPIs were declared inoperable at 1845, 0910,.
0730, 0907 and 2240 hcurs, respectively, and action statement 3.1.3.2.a was entered.
These ocenrrences constituted operation in a_ degraded mode in accordance j
with technical specification 6.9.1.9.b.
i DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
l The causes of the IRPIs being in disagreement with the demand position j
indicators by greater than 12 steps are as follows:
2Al and 1C2 - These rods were verified at 228 steps by a series of. flux traces even though the indi -
i cators indicated a lower position.
i 1SCl - A malfunction in tha P-250 computer was loading.
l down the signal co-
,ning module.
1 I
1D4 - The signal conditioning module'and IRPI had drifted out of calibration.
2D2 - The'IRPI had drifted out of calibration.
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ANALYSIS OF OCCURRENCE:
Technical specification 3.1.3.2.a requires:
With a maximum of one rod position indicator channel per group inoperable either:
1.
Determine the position of the non-indicating rod (s) indirectly by the movable incore detectors at least once per eight hours and immediately after any motion of the non-indicating rod which exceeds 24 steps in ene direction since the last determination of the rod's position, or 2.
Reduce thermal power to < 50% of rated thermal power within eight hours.
CORRECTIVE ACTION
The corrective actions were as follows:
2Al and 1C2 - The signal conditioning module was recalibrated utilizing new input data to indicate 228 steps.
1SC1 - Circuit card serial No. 348 was replaced in.the P-250 computer.
1D4 - The signal conditioning module and IRPI were recalibrated.
2D2 - The IRPI was recalibrated.
The IRPIs and other affected units for all five control rods were tested satisfactorily and returned to service.
At 2240, 1115, 2000, 1150 and 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br /> on September 1, 3, 9, 15 and 18, 1981, respective to the occurrence dates, action statement 3.1.3.2.a was terminated.
FAILURE DATA:
Bailey Instrument Co., Inc.
Bailey Edgewise Indicator Model RY2 M&gnetics, Inc.
Signal Conditioning Module Type E2786 Westinghouse Electric Corporation P-250 Computer Circuit Card No. 348 Prepared By F.
Dickey
- - f.-
Managdr - Salem Generating Station SOPC Meeting No.
81-95
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| 05000311/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001-03, /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | | | 05000311/LER-1981-001-03, /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | | | 05000311/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-002-03, /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | | | 05000272/LER-1981-002-03, /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | | | 05000272/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000311/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-003-03, Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | | | 05000272/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000272/LER-1981-003-03, /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | | | 05000311/LER-1981-004-04, /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | | | 05000311/LER-1981-004, Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000272/LER-1981-004-03, /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | | | 05000311/LER-1981-005-03, /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | | | 05000311/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-005-03, /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. 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Defective Module Replaced | | | 05000272/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000311/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-006-03, /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | | | 05000272/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000272/LER-1981-006-03, /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | | | 05000272/LER-1981-007-03, /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | | | 05000311/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-007, Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | | | 05000272/LER-1981-007-01, /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | | | 05000311/LER-1981-007-03, /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | | | 05000272/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000272/LER-1981-008-03, /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | | | 05000311/LER-1981-009-03, /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | | | 05000272/LER-1981-009-01, /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | | | 05000272/LER-1981-009, Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | | | 05000311/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000311/LER-1981-010-03, /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. 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