05000272/LER-1981-063, Forwards LER 81-063/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-063/03L-0.Detailed Event Analysis Encl
ML20030A831
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/21/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20030A832 List:
References
NUDOCS 8107290076
Download: ML20030A831 (3)


LER-1981-063, Forwards LER 81-063/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2721981063R00 - NRC Website

text

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n O PSEG Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 July 21, 1981 Mr. Boyce H.

Grier Director of USNRC Office of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-63/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-63/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours, 5

Ad edW R. A. Uderi.ti:

General Manager -

Nuclear Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies) i fh i

8107290076 810721 I(f PDR ADOCK 05000272 6

PDR The Energy People 95 2001 (400M) 181

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o Report Number:

81-63/03L Report Date:

July 21, 1981 Occurrence Date:

6-21-81 Facility:

Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Individual Rod Position Indicators - 2D1 and 2D5 - Inoperable.

This report was initiated by Incident Report 81-202.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 2 - Rx Power 0% - Unit Load 0 MWe DESCRIPTION OF OCCURRENCE:

During unit startup operations at 2318 hours0.0268 days <br />0.644 hours <br />0.00383 weeks <br />8.81999e-4 months <br />, June 21, 1981, action statement 3.1.3.2 was entered v. hen the control operator noticed the control rod bank demand indicator and the individual rod position indicators for control rods 2D1 and 2D5 were in disagreement by greater then + 12 steps.

Since with 2 individual rod position indicators inoperable per bank the limiting condition for operation was exceeded, the control rods were inserted and the unit was placed in mode 3 in accordance with the provisions of applicability state-ment 3.0.3 at 0016 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />, June 22, 1981.

This occurrence constituted operation in a degraded mode in accord-ance with technical specification 6.9.1.9b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment failure.

The individual rod position indicators had drifted out of calibration.

ANALYSIS OF OCCURRENCE:

Technical specification 3.0.3 requires that when a limiting condition for operation is not met, within one hour action shall be initiated to place the unit in a mode in which the specification does not apply.

s LER 81-63/03L July 21, 1981 C

i 4

CORRECTIVE ACTION

The Performance Department recalibrated the individual rod position indicators satisfactorily and they were returned to service.

FAILURE DATA:

2D1 and 2D5 Indicators Bailey Instrument Co. Inc.

Bailey Edgewise Indicators Model RY l

l Prepared By J. J.

Espey

'8# Lam, SORC Meeting No.

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