Similar Documents at Salem |
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LER-1981-059, Supplemental LER 81-059/01X-01:on 810616,during Initial Testing,Auxiliary Feedwater Pump 23 Turbine Steam Supply Check Valves 21MS46 & 23MS46 Found Damaged Internally.Caused by Steam Flow Sys Oscillations |
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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l O l 2 l l On June 16, 1981, during initial testing of Unit 2, No. 23 Auxiliary Feedwater Pump l
turbine steam supply check valve (23MS46) was found to be damaged internally.
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notification was made to the Commission. All valves were repaired under the super-l 9, g lO l6 l l PSE&G to investigate and determine the cause. A monthly radiography program, for all l g,; g
,MS46 valves, was instituted until the cause was determined and corrected.
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8 9 to EE NAME OF PREPARER PHONE:
(5 jReport? Number:
81-059/01X-1
. Report ~Date:
02/24/84-Occurrence Date:
06/16/81 Facility:
_ Salem Generating Station Unit 1 Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 LIDENTIFICATION OF OCCURRENCE:
MainESteam System - 11MS46 and 13MS46 Checks Valves - Inoperable
' CONDITIONS PRIOR TO OCCURRENCE:
LMode 5 - Rx Power 000 5.- Unit Load 0000 MWe This report summarizes the events, subsequent investigations and corrective actions involving-the-inoperability of Unit 1 and Unit 2
' Turbine Steam Supply Check Valves (11MS46, 13MS46, 21MS46 and 23MS46)
- - ossociated with No. 13 and No. 23 steam driven Auxiliary Feedwater Pumps.
The ir.itial. reports were documented in Unit 1 LER 81-059/01T and. Unit'2 LER 81-035/01T.
11MS46 and 13MS46-(Unit 1) supply-steam from their respective main steam lines to No.'13 Auxiliary Feedwater Pump turbine, via 1MS132 and the. turbine governor valve.
Unit 2 is similar in design,'with 21MS46 and.23MS46 supplying ' steam: from their respective main steam lines to No. 231 Auxiliary Feewater Pump turbine, via 2MS132 and the turbine governor-valve.
DESCRIPTION OF OCCURRENCE:
On June 16, 1981,- during' initial testing of. Unit 2, while repairing a bonnet 11eak.on check valve 23MS46, the valve was.found to be damaged internally.- The' valve disc stud was broken and the valve disc was lying in the bottom of the. valve body.
Further inspection of the valve revealed. cracks in the. disc, cracked bushings, the hinge pin was twarped and the hinge pin holes were elongated.
An inspection of 21MS46 revealed similar. damage.
Due(to the' damage observed on these valves, Unit 1 check valves were also inspected.. Valve 11MS46 had a warped-hinge pin and elongated
~ hinge pin holes.. Valve 13MS46 had cracked bushings, a warped hinge pin, a broken disc stud and' elongated hinge pin holes.
Prompt
- notification of-these' events were madeLto the USNRC Regional Administrator in'accordance with Technical Specification 6.9 1.8.e.
'A vendor representative from Velan Valve Corporation assisted-in the inspection of.thefvalves.
Velan Field Service Report, by Jack W.
Kuhner, dated ' June '18,1981, documented the inspection results.
Velan aupplied the necessary1 parts; the valves =were refurbished and returned
.to an operable status.1 An inspection program was instituted that required ~the-valves to be radiographed once a month until the failure
.nechanism could be-determined and corrected.
r LER 81-05 9/01X-1 DESCRIPTION OF OCCURREECE: (cont'd)
Bolt Beranek and Newman Inc. was retained by PSE&G to investigate and determine the cause and to make recommendations for its solution.
Extensive testing was conducted with assistance from the Engineering Department and station personnel.
Their findings were documented in Report # 5401, by Bruce S. Murray, dated August 1983 APPARENT CAUSE OF_0CCURRENCE:
The investigation revealed that unstable operation of the turbine governor valves (at speeds of 3600 RPM and greater) resulted in pressure fluctuations in the path of the check valves.
These pressure fluctuations caused the check valve discs to repeatedly hammer themselves against their limit stops.
These violent oscillations ultimately led to the fracture and distortion of the valve internal components.
Pressure fluctuations also occur when the feed pumps are started.
The pressure pulses during the starting sequence are amplified by the natural oscillation (organ piping) of the steam flow in the system.
These fluctuations also cause the check valves to hammer; however, these events occur less frequently and are clearly less severe, in regards to check valve damage, than those caused by the governor.
CORRECTIVE ACTION
The governor valves were inspected, adjusted and lubricated.
The governor stability was corrected.
Subsequent testing has shown that the severity and number of check valve impacts has been substantially reduced.
Although check valve damage is still being experienced, the monthly radiography inspection of the MS46 valves has proven to be very offective in identifying potential problems with the valve internals.
This has afforded early detection and timely repairs to be effected, thus assuring a high degree of reliability.
This inspection program will continue until the check valve performance has been determined to be satisfactory.
Because some check valve hammer occurs due to natural oscillations of cystem flow, an investigation is still in progress for possible ways to minimize these oscillations.
In addition, Design Change Requests (1SC-0630 and 2SC-0631) are being formulated to replace the check valves with ones of a different design.
- - FAILURE DATA:
Velan Valve Corp.
6" Check Valves Type B14-2114 B-2TS Prepared By J._Runo 74ner%1 Mansger -
Salem Operations SORC Meeting No.89-154
E O PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station February 24, 1984 U.S. Nuclear' Regulatory Commission
- - Document Control Desk Washington,-DC 20555
~ Dear Sir:
LICENSE NO. DPR-70
- - DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-059/0lX-1 SUPPLEMENTAL REPORT Pursuant to'the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.8.e, we are submitting supplemental Licensee Event Report for Reportable Occurrence 81-059/0lX-1.
Sincerely yours, J. M.
Zupko, Jr.
General Manager -
Salem Operations JR:kilp6p CC:
Distribution V
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- - The Energy People
<am e.u, n ei
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| 05000311/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001-03, /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | | | 05000311/LER-1981-001-03, /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | | | 05000311/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-002-03, /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | | | 05000272/LER-1981-002-03, /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | | | 05000272/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000311/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-003-03, Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | | | 05000272/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000272/LER-1981-003-03, /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | | | 05000311/LER-1981-004-04, /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | | | 05000311/LER-1981-004, Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000272/LER-1981-004-03, /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | | | 05000311/LER-1981-005-03, /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | | | 05000311/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-005-03, /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. Defective Module Replaced | /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. Defective Module Replaced | | | 05000272/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000311/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-006-03, /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | | | 05000272/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000272/LER-1981-006-03, /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | | | 05000272/LER-1981-007-03, /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | | | 05000311/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-007, Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | | | 05000272/LER-1981-007-01, /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | | | 05000311/LER-1981-007-03, /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | | | 05000272/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000272/LER-1981-008-03, /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | | | 05000311/LER-1981-009-03, /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | | | 05000272/LER-1981-009-01, /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | | | 05000272/LER-1981-009, Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | | | 05000311/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000311/LER-1981-010-03, /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. Caused by Worn Main Shaft Packing.Packing Replaced | /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. Caused by Worn Main Shaft Packing.Packing Replaced | | | 05000311/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000272/LER-1981-010-03, /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | | | 05000272/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000311/LER-1981-011-03, /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | | | 05000311/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-011-03, /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | | | 05000272/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000272/LER-1981-012-03, /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | | | 05000311/LER-1981-012-03, /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | | | 05000311/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000311/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000311/LER-1981-013-03, /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | | | 05000272/LER-1981-013-03, /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | |
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