Letter Sequence Other |
|---|
|
Results
Other: 05000206/LER-1980-031, Forwards LER 80-031/03L-0, 05000206/LER-1980-031-03, /03L-0:on 800728,during Routine Equipment Rotation,South Saltwater Cooling Pump Discharge Valve Failed to Open Automatically.Caused by Installation of Solenoid Valve Operator W/Wrong Size Spring.Valve Replaced, 05000206/LER-1980-032, Forwards LER 80-032/03L-0, 05000206/LER-1980-032-03, /03L-0:on 800717,during Cold Shutdown Conditions, Isolation Valve for Svc Water to Containment Failed to Close Upon Demand.Caused by Small Amount of Desiccant Which Entered Solenoid During Removal of Air Dryer Desiccant, 05000206/LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted, 05000206/LER-1981-018-01, /01T-0:on 810717,hydrogen-air Mixture Ignited in North Radwaste Gas Decay Tank Resulting in Manway Damage & Gaseous Release.Caused by check-valve Back Leakage of Volatile Gas Mix at Dinitrogen Instrument Air Interface, 05000206/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted, 05000206/LER-1982-007-03, /03L-0:on 820208,south Saltwater Cooling Pump (G13B) Declared Inoperable.Caused by Random Failure of Discharge Pressure switch,PS-39.Pressure Switch Replaced, ML13310A232, ML13310B052, ML13311A417, ML13317B073, ML13317B074, ML13322A850, ML13323A784, ML13323A889, ML13330A058, ML13330A076, ML13330B182, ML13330B400, ML13333A925, ML13333B765, ML13333B984, ML13333B987, ML20004F191, ML20079R245
|
MONTHYEARML13316B7251980-04-0404 April 1980 Discusses Licensee Actions Re 800310 Failure of Saltwater Cooling Sys.Auxiliary Salt Water Cooling Pump Will Not Be Considered in Determining Operability of Sys.Requests Review of All Emergency Procedures & Revision Prior to Operation Project stage: Approval ML13330A0581980-04-16016 April 1980 Notice of Violation from Insp on 800301-0404 Project stage: Other ML13323A7841980-05-13013 May 1980 Responds to NRC Re Violations Noted in IE Insp Rept 50-206/80-09.Corrective Actions:Emergency Operating Instruction S-3-5.34 Revised & Training for Operators Conducted Project stage: Other IR 05000206/19800151980-06-20020 June 1980 IE Insp Rept 50-206/80-15 on 800528-30.No Noncompliance Noted.Major Areas Inspected:Insp Activities Per IE Bulletin 79-13 Re Cracking in Feedwater Sys Piping Project stage: Request ML13330A0761980-06-20020 June 1980 Requests Addl Info Re Failure of Saltwater Cooling Sys on 800310.Info About Events Where Multiple Equipment Failures Occur & Contributing Factors Would Be Beneficial Project stage: Other ML13322A8501980-07-24024 July 1980 Submits Responses to Items 1,2 & 3 of NRC Re Failure of Saltwater Cooling Sys.Response to Item 4 Will Be Submitted by 800804 Project stage: Other ML13330A0771980-08-0808 August 1980 Responds to NRC 800620 Request for Info Re Failure of Salt Water Cooling Sys.Provides Analysis of Loss of Salt Water Cooling Sys Effect on Design Basis LOCA & Main Steam Line Break Inside Containment Project stage: Request 05000206/LER-1980-032, Forwards LER 80-032/03L-01980-08-18018 August 1980 Forwards LER 80-032/03L-0 Project stage: Other 05000206/LER-1980-032-03, /03L-0:on 800717,during Cold Shutdown Conditions, Isolation Valve for Svc Water to Containment Failed to Close Upon Demand.Caused by Small Amount of Desiccant Which Entered Solenoid During Removal of Air Dryer Desiccant1980-08-18018 August 1980 /03L-0:on 800717,during Cold Shutdown Conditions, Isolation Valve for Svc Water to Containment Failed to Close Upon Demand.Caused by Small Amount of Desiccant Which Entered Solenoid During Removal of Air Dryer Desiccant Project stage: Other 05000206/LER-1980-031-03, /03L-0:on 800728,during Routine Equipment Rotation,South Saltwater Cooling Pump Discharge Valve Failed to Open Automatically.Caused by Installation of Solenoid Valve Operator W/Wrong Size Spring.Valve Replaced1980-08-19019 August 1980 /03L-0:on 800728,during Routine Equipment Rotation,South Saltwater Cooling Pump Discharge Valve Failed to Open Automatically.Caused by Installation of Solenoid Valve Operator W/Wrong Size Spring.Valve Replaced Project stage: Other 05000206/LER-1980-031, Forwards LER 80-031/03L-01980-08-21021 August 1980 Forwards LER 80-031/03L-0 Project stage: Other ML13330A1201980-09-24024 September 1980 Ack Receipt of 800829 Request for Addl Info Re Failure of Salt Water Cooling Sys.Input from Several Engineers & Operating Entities Required to Complete Request.Response Will Be Submitted 801008 Project stage: Request ML13302A8381980-10-0808 October 1980 Notification of 801020 Meeting W/Util,Orange County,San Diego County & State of CA OES in El Segundo,Ca to Discuss Completion Dates & Review Matters for State & Local Emergency Plans for Facility & Vicinity Project stage: Request ML13330B0811980-10-28028 October 1980 Notification of 801030 Meeting W/Util in Bethesda,Md to Discuss Loss of Saltwater Cooling Event & Procedures in Place for Loss of Saltwater Cooling & Dessicate in Air Sys Project stage: Meeting ML13330B1031980-12-0808 December 1980 Notification of 801218 Meeting W/Util in Bethesda,Md to Discuss Util Comments Re NRC Case Study of Loss of Salt Water Cooling Sys Project stage: Meeting ML13323A8891980-12-26026 December 1980 Provides Justification for Util Corrective Actions Re Notice of Violation from 800310 Loss of Saltwater Cooling Incident. Proposed Hot Shutdown Time Limit Is Consistent W/Emergency Operating Instruction SO1-3-5.34 Project stage: Other ML13331A0361981-01-0606 January 1981 Summary of 801030 Meeting W/Util in Bethesda,Md Re Loss of Saltwater Cooling Event at Facility & Effects of Desiccant in Compressed Air Sys.W/List of Attendees Project stage: Meeting ML13330A1771981-01-12012 January 1981 Submits Comments on NRC Draft Rept on 800310 Loss of Saltwater Cooling.Forwards Addl Info Requested in 801223 Meeting & Interpretation of Tech Specs Re Saltwater Cooling Sys.Encls Available in Central Files Only ML13333A9251981-02-23023 February 1981 Provides Status Rept on Corrective Actions Taken to Ensure Continued Operability of safety-related air-using Equipment. Blowdown of Header Performed to Remove Dessicant.Preventive Maint Program Is Under Development Project stage: Other ML20004F1911981-06-0404 June 1981 Responds to IE Bulletin 81-03, Flow Blockage of Cooling Water to Safety Sys Components by Corbicula Sp (Asiatic Clam) & Mytilus Sp (Mussel). Periodic Insp & Daily Checks of Heat Exchangers Assure Proper Flow Project stage: Other 05000206/LER-1981-018-01, /01T-0:on 810717,hydrogen-air Mixture Ignited in North Radwaste Gas Decay Tank Resulting in Manway Damage & Gaseous Release.Caused by check-valve Back Leakage of Volatile Gas Mix at Dinitrogen Instrument Air Interface1981-07-31031 July 1981 /01T-0:on 810717,hydrogen-air Mixture Ignited in North Radwaste Gas Decay Tank Resulting in Manway Damage & Gaseous Release.Caused by check-valve Back Leakage of Volatile Gas Mix at Dinitrogen Instrument Air Interface Project stage: Other 05000206/LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted1981-07-31031 July 1981 Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted Project stage: Other ML13317A7181981-11-0202 November 1981 Forwards Draft Assessment for SEP Topic IX-3 Re Station Svc & Cooling Water Sys Project stage: Draft Other ML13310A2321982-02-28028 February 1982 Preliminary Rept, Loss of Salt Water Cooling Event on 800310 Project stage: Other ML13317B0741982-03-0404 March 1982 Forwards Preliminary Rept Re Loss of Salt Water Cooling Event of 800310 for Comment on Accuracy & Completeness of Technical Details Project stage: Other ML13317B0191982-03-0404 March 1982 Forwards Page 5,inadvertently Omitted from 820224 Submittal, Re Environ Qualification of Electrical Equipment Project stage: Request 05000206/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted1982-03-0505 March 1982 Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted Project stage: Other 05000206/LER-1982-007-03, /03L-0:on 820208,south Saltwater Cooling Pump (G13B) Declared Inoperable.Caused by Random Failure of Discharge Pressure switch,PS-39.Pressure Switch Replaced1982-03-0505 March 1982 /03L-0:on 820208,south Saltwater Cooling Pump (G13B) Declared Inoperable.Caused by Random Failure of Discharge Pressure switch,PS-39.Pressure Switch Replaced Project stage: Other ML13317B0731982-04-0707 April 1982 Forwards Comments on San Onofre Unit 1 Loss of Salt Water Cooling Event of 800310, Per 820403 Request Project stage: Other ML13333B7651982-08-12012 August 1982 Forwards Case Study Rept Containing Detailed Description, Findings,Conclusions & Recommendations Re 800310 Loss of Salt Water Cooling Event Project stage: Other ML20079R2451983-06-18018 June 1983 Comments on H Dieckamp 830527 & 0610 Ltrs Re Immediate Effectiveness of Restart.Dieckamp Concealment of Info Detrimental to Mgt Evidences Util Policy of Expediency. Certificate of Svc Encl Project stage: Other ML13310B0551983-10-28028 October 1983 Safety Evaluation Concluding That Proposed Change 98 Re Auxiliary Salt Water Cooling Pump Unacceptable.Deficiencies Identified.Alternatives Presented Project stage: Approval ML13310B0521983-10-28028 October 1983 Advises That 800827 Proposed Change 98 Re Auxiliary Salt Water Cooling Pump,Unacceptable.Revised Proposed Tech Spec Change Addressing Both Auxiliary Salt Water & Screen Wash Pumps as Backup Sources of Cooling Requested Project stage: Other ML13333B9871983-10-31031 October 1983 Degradation of Salt Water Cooling Sys Caused by Loss of Instrument Air, Technical Review Rept Project stage: Other ML13333B9841983-10-31031 October 1983 Forwards Degradation of Salt Water Cooling Sys Caused by Loss of Instrument Air, Technical Review Rept Project stage: Other ML13330B1821987-04-0101 April 1987 Forwards Erin Engineering & Research,Inc Rept, Reliability Assessment of San Onofre Unit 1 Saltwater Cooling Sys, Per NUREG-0829.Study Concludes That Sys as Designed Provides Very Reliable Means of Removing Decay Heat Project stage: Other ML13311A4171987-04-30030 April 1987 Reliability Assessment of San Onofre Unit 1 Saltwater Cooling Sys Project stage: Other ML13331B0021987-11-24024 November 1987 Forwards Request for Addl Info Re Plant Salt Water Cooling Sys Reliability Study Project stage: RAI ML13333A6031987-12-0202 December 1987 Forwards Safety Evaluation Accepting Util 871016 Single Failures Analysis for Esf,Per 871009 Meeting.Justification for Interim Plant Operation Acceptable Until 871214,pending Further Analysis Project stage: Approval ML13311A7291988-07-22022 July 1988 Forwards Responses to 871124 Request for Addl Info Re Salt Water Cooling Sys Reliability Study.Initiating Events Affecting Saltwater Cooling Sys or Vital Support Sys Can Affect Overall Sys Reliability Project stage: Request ML13330B4001988-10-0303 October 1988 Agrees W/Licensee That No Actions Required to Improve Reliability of Salt Water Cooling Sys Per SEP Topic IX-3, Item 4.32.7.If Complete Loss of Salt Water Cooling Occurs, Backup Pumps Can Provide Interim Cooling Project stage: Other 1981-11-02
[Table View] |
LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2061981018R00 - NRC Website |
|
text
_-
4 h5 Southern California Edison Company q
P, O. BOX 8 00 22 44 WALNUT GROVE AVENUE f gg -
ROSE M E AD. CALIFORNI A 91770 i
0 agou v re..,~o~r 4.c.wavurs July 31, 1981 Wosc/$8 C '"""""'
8
- ~... o, ~ u c u.. o,.....o ~,
T1 U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region V 1990 North California Boulevard Suite 202, Walnut Creek Plaza A
Walnut Craek, California 94596 l
Attention: Mr. R. H. Engelken, Director e
7 412198k TL DOCKET No. 50-206 A
SAN ONOFRE - UNIT 1
\\(g WY
Dear Sir:
By letter dated July 20, 1981 we provided prompt notification of a reportable occurrence involving the Radioactive Waste Gas System. This letter constitutes the two week follow-up report.
Subm1ttal is in accordance with the reporting requirements stipulated in Section 5.6.3 of Appendix B to our Provisional Operating License DPR-13.
At 2125 on July 17, 1980 a venting process was underway for the' north radwaste gas decay tank C-6A (located in the Reactor Auxiliary Building) through the cryogenic waste gas treatment system. The system had been placed in service in accordance with approved procedures.
It is noted that just prior to processing the north decay tank the set th decay tank had been processed without incident. As processing began on the north decay tank difficulty was experienced in adjusting the flow rate through the system.
Investigation of the problem determined that a reducing valve which controls dcwnstream gas pressure into the gas treatment system was cycling. While attempting to alleviate this problem an operator noted " popping" noises, apparently originating in the piping downstream of the reducing valve.
Sometime thereafter an ignition of the gas mixture in tank C-6A occurred.
Fire alanns were observed in the control room, and operating personnel within the gas treatment system area were notified. These personnel reported a loud noise, apparently from the gas decay tank area. Operating personnel entered the Reactor Auxiliary Building and reported the presence of smoke. Local pressure indication on tank C-6A was observed to read 0-psig. The operating-personnel exited the area and requested a radinlogical survey. While the survey was in progress, operating personnel re-entered the area in Scott-Air-Packs and inspected the north waste gas decay tank.
At this time the area was observed cleared of smoke and no fire was prdsent.
The tank manway cover bolts were found loose and minor damage around the tank manway noted.
(=)108130250 810731 DR ADOCK 05000 3g
4 U. S. Nuclear Regulatory Commission LER 81-018 Page # 2 Post investigation of this event found that damage to the tank is apparently limited to the manway area and the manway bolting.
It appears that the source of the ignition was the oxygen recombiner located in the cryogenic waste gas treatment system. At oxygen concentrations greater than 3% the chemical reaction in the recombiner can generate temperatures above the ignition temperature for an oxygen-hydrogen combination. The manufacturer provides an oxygen analyzer with this system to detect oxygen levels exceeding this value. However, at the time of the event this meter was inoperable and its use was not required by the operating procedure. Local ignition of the hydrogen-oxygen atmosphere evidently created pressure spikes that caused the control valve, CV-M2, to cycle resulting in the popping noise observed by the operators. During one of the local ignitions the flame front propagated upstream of CV-M2 and ignited the gas mixture in the tank.
An analysis of the plant stack monitoring system subsequent to the event indicated that the activity release due to the man-way cover failure (8.8 curies) occurred during an 18 minute period.
Utilizing an extrapolated peak for the most limiting isotope involved (Xe-133), the dilution "clume through the stack and meteorological dilution factors, the calculated plant boundary activity concentration was determined to be a factor of ten below the maximJm permissible Concentration delineated in Appendi.' B, Part 20 of CFR Title 10. Additionally, onsite personnel exposure associated with this event was well within limits.
Subsequent investigation into the cause of high oxygen concentrations within the waste gas system revealed high oxygen concentrations in the station's Nitrogen System. This had been discovered the day prior to the event and had led to sampling of the flash tank gas space (completed just prior to the ignition). This sample showed the presence of oxygen in the tank.
It has been determined that instrument air (maintained 10 to 20 psig above the Nitrogen System pressure) was ente.ing the Nitrogen System at locations where nitrogen serves as a backup to instrument air. The backup function is for the following safety related valves: Pressurizer relief and pressurizer relief block valves, isolation valve on the nitrogen supply to the pressurizer, Auxiliary Feedwater System control valves and the auxiliary feedwater turbine driven pump, steam control valve.
The primary source of leakage was confined tn those valves associated with the auxiliary feedwater system (insignificant leakage was found at the other locations).
The check valves isolating the two systems had not been installed in accordance with manufacturer's recommendations during the recent TMI backfit modifications.
As a result of this installation the valves failed to seat properly providing a direct and rather large communication path between the two systems.
S
U. S. Nuclear Regulatory Commissicr.
LER 81-018 Page # 3 The following action will be taken in regard to this incident:
(1 )
The Instrument Air System and the Station's Nitrogen System will be physically separated from each other and bottled gas used in lieu of _
the station Nitrogen System.
t (2)
The procedure used to operate the waste gas treatment system will be revised to prohibit system use if oxygen concentrations above 3% are present (manufacturer's upper limit on oxygen concentration). Sampling for oxygen prior to rel(ise will be required.
(3)
Tank C-6A shall be examined with liquid penetrant, repaired and pressure tested in accordance with the ASME Boiler and Pressure Yessel Code,Section VIII.
(4)
The pressure boundary components in the immediaw vicinity of tank C-6A shall b uamined for indications of damage and action taken accordingly.
(5)
In the cryogenic waste gas treatment system, the oxygen recombiner and system filter will be replaced, and the oxygen analyzer repaired.
Items (1) and (2) will be complete prior to return to power.
Items (3), (4) and (5) are currently in progress.
It is our intent to complete these activities prior to return to power subject to material lead times and the results of inspections t:nderway.
Should you have any questions on the above, please call me.
Sincerel,
fynt/$-
J. G. Haynes Manager of' Nuclear Operations JTR:dh:900
Enclosures:
Licensee Event Report 80-018 cc:
U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Office of Management Infonnation & Program Control Nuclear Safety Analysis Center L. F. Miller (USNRC Resident Inspector) a
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000206/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000206/LER-1981-001-01, /01T-0:on 810116,design Problem Noted Re Safeguard Load Sequencing Sys.Caused by Possible Resequencing of Safety Injection Sys Loads Due to Oscillation of Safety Injection Parameters About Setpoints | /01T-0:on 810116,design Problem Noted Re Safeguard Load Sequencing Sys.Caused by Possible Resequencing of Safety Injection Sys Loads Due to Oscillation of Safety Injection Parameters About Setpoints | | | 05000206/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | | | 05000206/LER-1981-002-01, /01T-0:on 810202,during IE Bulletin 79-14 Insp, Bolts Discovered Missing on Feedwater Line 392-10 Eg.Cause Not Stated.Bolts Will Be Replaced Prior to Return to Svc from Current Outage | /01T-0:on 810202,during IE Bulletin 79-14 Insp, Bolts Discovered Missing on Feedwater Line 392-10 Eg.Cause Not Stated.Bolts Will Be Replaced Prior to Return to Svc from Current Outage | | | 05000206/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-003/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-003-03, /03L-0:on 810417,snubbers PSA-3 & 10 Could Not Be Manually Stroked in Tension or Compression Direction Per IE Bulletin 81-01.Caused by Internal Corrosion on One & Improper Installation of Other.Snubbers Returned to Mfg | /03L-0:on 810417,snubbers PSA-3 & 10 Could Not Be Manually Stroked in Tension or Compression Direction Per IE Bulletin 81-01.Caused by Internal Corrosion on One & Improper Installation of Other.Snubbers Returned to Mfg | | | 05000206/LER-1981-004-01, /01T-0:on 810416,consultants Determined That non- Metallic Internals of Actuators,Regulators & Solenoid Valves of Recirculation Flow Control Valves 1115 D,E & F Required Replacement.Caused by Aging.Internals Being Replaced | /01T-0:on 810416,consultants Determined That non- Metallic Internals of Actuators,Regulators & Solenoid Valves of Recirculation Flow Control Valves 1115 D,E & F Required Replacement.Caused by Aging.Internals Being Replaced | | | 05000206/LER-1981-004, Forwards LER 81-004/01T-0.Detailed Event Analysis Encl | Forwards LER 81-004/01T-0.Detailed Event Analysis Encl | | | 05000206/LER-1981-005-04, /04L-0:on 810331,during Preparation for Annual Radiological Environ Monitoring Rept,Discovered Only One Local Crop Sampling Was Conducted During 1980.Caused by Personnel Oversight | /04L-0:on 810331,during Preparation for Annual Radiological Environ Monitoring Rept,Discovered Only One Local Crop Sampling Was Conducted During 1980.Caused by Personnel Oversight | | | 05000206/LER-1981-005, Forwards LER 81-005/04L-0.Detailed Event Analysis Encl | Forwards LER 81-005/04L-0.Detailed Event Analysis Encl | | | 05000206/LER-1981-006-01, /01T-0:on 810428,determined That Terminal Blocks Could Not Be Guaranteed to Function in post-accident Environ.Qualified in-line Splices in safety-related Circuits Will Be Installed on Terminal Blocks | /01T-0:on 810428,determined That Terminal Blocks Could Not Be Guaranteed to Function in post-accident Environ.Qualified in-line Splices in safety-related Circuits Will Be Installed on Terminal Blocks | | | 05000206/LER-1981-006, Forwards LER 81-006/01T-0.Detailed Event Analysis Also Submitted | Forwards LER 81-006/01T-0.Detailed Event Analysis Also Submitted | | | 05000206/LER-1981-007, Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | | | 05000206/LER-1981-007-01, /01T-0:on 810515,pump to Motor Coupling Failed During Qualification Testing of RHR Pump Motors.Caused by Corrosive Effects of Environ & Unnatural Stresses to Coupling Due to Test Setup.Couplings Will Be Replaced | /01T-0:on 810515,pump to Motor Coupling Failed During Qualification Testing of RHR Pump Motors.Caused by Corrosive Effects of Environ & Unnatural Stresses to Coupling Due to Test Setup.Couplings Will Be Replaced | | | 05000206/LER-1981-008, Forwards LER 81-008/03X-0.Detailed Event Analysis Also Submitted | Forwards LER 81-008/03X-0.Detailed Event Analysis Also Submitted | | | 05000206/LER-1981-008-03, /03X-0:on 810504,insp of Thermal Sleeve & Feedring Assembly on Steam Generator B Found Thermal Sleeve Deformation in Feed Nozzle Area,Radial Indications at Several Feedring Distribution Holes & Other Defects | /03X-0:on 810504,insp of Thermal Sleeve & Feedring Assembly on Steam Generator B Found Thermal Sleeve Deformation in Feed Nozzle Area,Radial Indications at Several Feedring Distribution Holes & Other Defects | | | 05000206/LER-1981-009-01, /01T-0:on 810609,low Coolant Flow Rate & Butterfly Valve Malfunctions Occurred on Saltwater Discharge Side of Component Cooling Heat Exchanger.Caused by Impeded Valve Movement Due to Gooseneck Barnacle Growth | /01T-0:on 810609,low Coolant Flow Rate & Butterfly Valve Malfunctions Occurred on Saltwater Discharge Side of Component Cooling Heat Exchanger.Caused by Impeded Valve Movement Due to Gooseneck Barnacle Growth | | | 05000206/LER-1981-009, Forwards LER 81-009/01T-0.Detailed Event Analysis Also Submitted | Forwards LER 81-009/01T-0.Detailed Event Analysis Also Submitted | | | 05000206/LER-1981-010, Forwards LER 81-010/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-010/03L-0.Detailed Event Analysis Also Submitted | | | 05000206/LER-1981-010-03, /03L-0:on 810603 & 05,inadvertent Breach of Primary Containment Occurred When Both Main Containment Personnel Airlock Doors Were Open.Caused by Three Worn Cam Followers & Misaligned Operating Shaft | /03L-0:on 810603 & 05,inadvertent Breach of Primary Containment Occurred When Both Main Containment Personnel Airlock Doors Were Open.Caused by Three Worn Cam Followers & Misaligned Operating Shaft | | | 05000206/LER-1981-011-04, /04T-0:on 810510,contamination Discovered in Beach Sand Adjacent to out-of-svc Yard Drainline Uncovered in Excavation.Caused by Either Runoff or Leakage from Radioactive Sys That Interface W/Drain Sys | /04T-0:on 810510,contamination Discovered in Beach Sand Adjacent to out-of-svc Yard Drainline Uncovered in Excavation.Caused by Either Runoff or Leakage from Radioactive Sys That Interface W/Drain Sys | | | 05000206/LER-1981-011, Submits Detailed Rept as Followup to LER 81-011/04T-0 Addressing Environ Impact of Beach Contamination | Submits Detailed Rept as Followup to LER 81-011/04T-0 Addressing Environ Impact of Beach Contamination | | | 05000206/LER-1981-012-03, /03L-0:on 810623,during Reactor Startup,Trip Bistables in Variable Low Pressure Trip Sys Were Set Low. Caused by Error in Biweekly Reactor Plant Instrumentation Test Procedure.Procedure Corrected | /03L-0:on 810623,during Reactor Startup,Trip Bistables in Variable Low Pressure Trip Sys Were Set Low. Caused by Error in Biweekly Reactor Plant Instrumentation Test Procedure.Procedure Corrected | | | 05000206/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000206/LER-1981-013, Forwards LER 81-013/99X-0.Detailed Event Analysis Submitted | Forwards LER 81-013/99X-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-013-99, /99X-0:on 810618,power Operated Relief Valve Controller Opened Twice During Normal Pressure Transient Following Reactor Trip.Caused by Setting Time Constant to Off to Satisfy NUREG-0737,Item II.K.3.9 | /99X-0:on 810618,power Operated Relief Valve Controller Opened Twice During Normal Pressure Transient Following Reactor Trip.Caused by Setting Time Constant to Off to Satisfy NUREG-0737,Item II.K.3.9 | | | 05000206/LER-1981-014-03, /03L-0:on 810630,erroneous Feedwater Flow Indications Produced Indicated Power Levels Below Actual Levels.Caused by Feedwater Flow Orifice Installed Backwards on One Line & Excessive Vibration on Other | /03L-0:on 810630,erroneous Feedwater Flow Indications Produced Indicated Power Levels Below Actual Levels.Caused by Feedwater Flow Orifice Installed Backwards on One Line & Excessive Vibration on Other | | | 05000206/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-014/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-015/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-015-03, /03L-0:on 810630,during Monthly Operability Test Number 2 Diesel Generator Tripped.Caused by Lube Oil Draining Through Tygon Tubing.Installation of Tubing Was Design Deficiency.Tubing Removed & Lube Oil Added to Tank | /03L-0:on 810630,during Monthly Operability Test Number 2 Diesel Generator Tripped.Caused by Lube Oil Draining Through Tygon Tubing.Installation of Tubing Was Design Deficiency.Tubing Removed & Lube Oil Added to Tank | | | 05000206/LER-1981-016-01, /01T-0:on 810711,immediately Following Unit Shutdown,Both Personnel Airlock Doors Were Simultaneously Open 12 Minutes.Caused by Misaligned Locking Mechanism Due to Damaged Cam Followers.Damaged or Worn Parts Replaced | /01T-0:on 810711,immediately Following Unit Shutdown,Both Personnel Airlock Doors Were Simultaneously Open 12 Minutes.Caused by Misaligned Locking Mechanism Due to Damaged Cam Followers.Damaged or Worn Parts Replaced | | | 05000206/LER-1981-016, Forwards LER 81-016/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-016/01T-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-017/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-017-03, /03L-0:on 810714,lube Oil Spraying from Cracked Instrument Line Ignited by Hot Exhaust Piping Above Diesel Engine.Caused by Instrument Line Cracking Due to Postulated Fatigue Failure Due to Vibrating Pressure Gauge | /03L-0:on 810714,lube Oil Spraying from Cracked Instrument Line Ignited by Hot Exhaust Piping Above Diesel Engine.Caused by Instrument Line Cracking Due to Postulated Fatigue Failure Due to Vibrating Pressure Gauge | | | 05000206/LER-1981-018-01, /01T-0:on 810717,hydrogen-air Mixture Ignited in North Radwaste Gas Decay Tank Resulting in Manway Damage & Gaseous Release.Caused by check-valve Back Leakage of Volatile Gas Mix at Dinitrogen Instrument Air Interface | /01T-0:on 810717,hydrogen-air Mixture Ignited in North Radwaste Gas Decay Tank Resulting in Manway Damage & Gaseous Release.Caused by check-valve Back Leakage of Volatile Gas Mix at Dinitrogen Instrument Air Interface | | | 05000206/LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-018/01T-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-019-03, /03L-0:on 810816 & 25,seal Water Line to North Charging Pump Outboard Seal Found Leaking in Excess of Tech Spec Limits.Caused by Svc Induced Wear on Threaded Joint of Seal Water Line.Joint Tightened | /03L-0:on 810816 & 25,seal Water Line to North Charging Pump Outboard Seal Found Leaking in Excess of Tech Spec Limits.Caused by Svc Induced Wear on Threaded Joint of Seal Water Line.Joint Tightened | | | 05000206/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-020-01, /01T-0:on 810903,following Manual Reactor Trip, Two Safety Injection Valves HV 851 Failed to Open Upon Valid Safety Injection Sys Signal.Caused by Inadequate as-built Design.Design Changes Being Considered | /01T-0:on 810903,following Manual Reactor Trip, Two Safety Injection Valves HV 851 Failed to Open Upon Valid Safety Injection Sys Signal.Caused by Inadequate as-built Design.Design Changes Being Considered | | | 05000206/LER-1981-021-01, /01T-0:on 810903,feedwater & Steam Generator Level Control Was Erratic.Caused by Twinco Voltage Regulator Filter Choke 1 Failure to Ground W/Resulting Degradation of 115-volt Ac Power.Regulator Repaired | /01T-0:on 810903,feedwater & Steam Generator Level Control Was Erratic.Caused by Twinco Voltage Regulator Filter Choke 1 Failure to Ground W/Resulting Degradation of 115-volt Ac Power.Regulator Repaired | | | 05000206/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | | | 05000206/LER-1981-022-03, /03L-0:on 811003,during Performance of Visual Surveillance Insp of Hydraulic Snubbers Installed on safety- Related Sys,Hydraulic Fluid Reservoir in One Snubber Found Empty.Caused by Failed Reservoir Seal Gasket | /03L-0:on 811003,during Performance of Visual Surveillance Insp of Hydraulic Snubbers Installed on safety- Related Sys,Hydraulic Fluid Reservoir in One Snubber Found Empty.Caused by Failed Reservoir Seal Gasket | | | 05000206/LER-1981-023, /00X-0:on 810925,loss of Power to Train a of Containment Spray Actuation Sys Caused Max of 400 Gallons of Borated Water to Be Sprayed Inside Containment.Caused by Blown Fuse Combined W/Inadvertent Breaker Tripping | /00X-0:on 810925,loss of Power to Train a of Containment Spray Actuation Sys Caused Max of 400 Gallons of Borated Water to Be Sprayed Inside Containment.Caused by Blown Fuse Combined W/Inadvertent Breaker Tripping | | | 05000206/LER-1981-024-01, /01T-0:on 811025,two Containment Isolation Valves CV-526 & CV-528 Did Not Immediately Operate on Demand.On 811013,isolation Valve CV-516 Did Not Immediately Operate. Caused by Blocking Lever Not Dropping Sufficiently | /01T-0:on 811025,two Containment Isolation Valves CV-526 & CV-528 Did Not Immediately Operate on Demand.On 811013,isolation Valve CV-516 Did Not Immediately Operate. Caused by Blocking Lever Not Dropping Sufficiently | | | 05000206/LER-1981-024, Submits Followup to LER 81-024 Re Failure of Energy Products Group Ball Valves W/Efcomatic Actuators to Trip Initially Per Commitment Made in Design Change 78-34.Actuators Will Be Replaced W/Different Design | Submits Followup to LER 81-024 Re Failure of Energy Products Group Ball Valves W/Efcomatic Actuators to Trip Initially Per Commitment Made in Design Change 78-34.Actuators Will Be Replaced W/Different Design | | | 05000206/LER-1981-025, Forwards LER 81-025/01X-1.Detailed Event Analysis Submitted | Forwards LER 81-025/01X-1.Detailed Event Analysis Submitted | | | 05000206/LER-1981-025-01, /01T-0:on 811025,ball Valve CV-534 Did Not Close Automatically on Initiation of Containment Isolation Signal.On 811101,containment Isolation Valve CV-102 Did Not Close.Caused by Sticking Relays in Closing Circuits | /01T-0:on 811025,ball Valve CV-534 Did Not Close Automatically on Initiation of Containment Isolation Signal.On 811101,containment Isolation Valve CV-102 Did Not Close.Caused by Sticking Relays in Closing Circuits | | | 05000206/LER-1981-026-01, /01T-0:on 811102 Vol of Water in Refueling Water Storage Tank Fell Below Tech Spec When recirculation-to- Condenser Valve Water CV-36 Failed to Close,Allowing 15,000 Gallons of Refueling to Be Pumped Into Condenser | /01T-0:on 811102 Vol of Water in Refueling Water Storage Tank Fell Below Tech Spec When recirculation-to- Condenser Valve Water CV-36 Failed to Close,Allowing 15,000 Gallons of Refueling to Be Pumped Into Condenser | | | 05000206/LER-1981-026, Forwards LER 81-026/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-026/01T-0.Detailed Event Analysis Submitted | | | 05000206/LER-1981-027, Forwards LER 81-027/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-027/01T-0.Detailed Event Analysis Submitted | |
|