07-13-2016 | On March 14, 2016, Watts Bar Nuclear Plant ( WBN) Unit 1 determined through engineering analysis that both trains of emergency gas treatment system ( EGTS) were inoperable for 8 minutes, 10 seconds during preoperational testing of Unit 2 EGTS. The inoperability of A and B trains of Unit 1 EGTS took place on October 22, 2015, while Unit 1 was in Mode 1 and two trains of EGTS were required to be operable in accordance with technical specification (TS) limiting condition for operation (LCO) 3.6.9, " Emergency Gas Treatment System ( EGTS)." At the time of the event, Unit 2 was in "no Mode," prior to initial fuel loading.
This condition is being reported pursuant to 10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), "Event or Condition That Could Have Prevented Fulfilment of a Safety Function. |
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Category:Letter
MONTHYEARML23319A2452024-01-29029 January 2024 Issuance of Amendment Nos. 366 and 360; 164 and 71 Regarding the Adoption of TSTF-567, Revision 1, Add Containment Sump TS to Address GSI-191 Issues ML24008A2462024-01-18018 January 2024 Revision to the Reactor Vessel Material Surveillance Capsule Withdrawal Schedule CNL-24-017, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions2024-01-17017 January 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions CNL-24-016, Supplement to Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14)2024-01-10010 January 2024 Supplement to Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14) CNL-23-052, Application to Adopt TSTF-427-A, Revision 2, Allowance for Non-Technical Specification Barrier Degradation on Supported System Operability2024-01-0909 January 2024 Application to Adopt TSTF-427-A, Revision 2, Allowance for Non-Technical Specification Barrier Degradation on Supported System Operability CNL-23-062, Application to Revise the Technical Specifications Section 3.8.2, AC Sources-Shutdown, to Remove Reference to the C-S Diesel Generator (WBN-TS-23-018)2024-01-0808 January 2024 Application to Revise the Technical Specifications Section 3.8.2, AC Sources-Shutdown, to Remove Reference to the C-S Diesel Generator (WBN-TS-23-018) ML23346A1382024-01-0303 January 2024 Regulatory Audit Summary Related to Request to Increase the Number of Tritium Producing Burnable Absorber Rods CNL-23-069, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-12-21021 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation IR 05000390/20234412023-12-21021 December 2023 Plantfinal Significance Determination for a Security-Related Greater than Green Finding, Nov, and Assessment Follow-up, 05000390-2023441 and 05000391-2023441-Public CNL-23-036, Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah Nuclear Plant and Watts Bar Nuclear Plant (SQN-TS-23-02 and WBN-TS-23-08)2023-12-18018 December 2023 Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah Nuclear Plant and Watts Bar Nuclear Plant (SQN-TS-23-02 and WBN-TS-23-08) IR 05000390/20234042023-12-14014 December 2023 Security Baseline Inspection Report 05000390/2023404 and 05000391/2023404 CNL-23-001, Rebaseline of Sections 3.1 and 3.2 of the Technical Specifications (WBN-TS-23-01)2023-12-13013 December 2023 Rebaseline of Sections 3.1 and 3.2 of the Technical Specifications (WBN-TS-23-01) ML23293A0572023-12-0606 December 2023 Issuance of Amendment Nos. 163 and 70 Regarding Adoption of TSTF-501-A, Revision 1, Relocate Stored Fuel Oil and Lube Oil Volume Values to Licensee Control IR 05000390/20230102023-11-30030 November 2023 RE-Issue Watts Bar Nuclear Plant - Biennial Problem Identification and Resolution Inspection Report 050000390/2023010 and 05000391/2023010 and Apparent Violation CNL-23-067, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-11-27027 November 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions IR 05000390/20230032023-11-13013 November 2023 Integrated Inspection Report 05000390/2023003 and 05000391/2023003 and Apparent Violation ML23312A1432023-11-0808 November 2023 Submittal of Dual Unit Updated Final Safety Analysis Report (UFSAR) Amendment 5 CNL-23-059, Supplement to Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2, Application to Revise Technical Specifications to Adopt TSTF-567-A, Revision 1, Add Containment Sump TS to Address GSI-191 Issues (SQN-TS-23-2023-09-20020 September 2023 Supplement to Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2, Application to Revise Technical Specifications to Adopt TSTF-567-A, Revision 1, Add Containment Sump TS to Address GSI-191 Issues (SQN-TS-23-03 CNL-23-061, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision2023-09-20020 September 2023 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML23251A2002023-09-11011 September 2023 Request for Withholding Information from Public Disclosure for Watts Bar Nuclear Plant, Units 1 and 2 CNL-23-057, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 642023-09-0505 September 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 64 IR 05000390/20230052023-08-30030 August 2023 Updated Inspection Plan for Watts Bar Nuclear Plant, Units 1 and 2 - Report 05000390/2023005 and 05000391/2023005 ML23233A0042023-08-28028 August 2023 Proposed Alternative to the Requirements of the ASME Boiler and Pressure Vessel Code for Upper Head Injection Dissimilar Metal Butt Welds IR 05000390/20230022023-08-16016 August 2023 Reissue - Watts Bar Nuclear Plant - Integrated Inspection Report 05000390/2023002 and 05000391/2023002 ML23220A1582023-08-0909 August 2023 Integrated Inspection Report 05000390/2023002 and 05000391/2023002 CNL-23-045, License Amendment Request to Revise Technical Specification Table 1.1-1 Regarding the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Bolts (WBN-TS-23-010)2023-08-0707 August 2023 License Amendment Request to Revise Technical Specification Table 1.1-1 Regarding the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Bolts (WBN-TS-23-010) CNL-23-028, Application to Revise Technical Specifications to Adopt TSTF-567-A, Revision 1, Add Containment Sump TS to Address GSI-191 Issues (SQN-TS-23-03 and WBN-TS-23-06)2023-08-0202 August 2023 Application to Revise Technical Specifications to Adopt TSTF-567-A, Revision 1, Add Containment Sump TS to Address GSI-191 Issues (SQN-TS-23-03 and WBN-TS-23-06) ML23192A4472023-07-31031 July 2023 Staff Assessment of Updated Seismic Hazards at TVA Sites Following the NRC Process for the Ongoing Assessment of Natural Hazards Information CNL-23-055, Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills2023-07-25025 July 2023 Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills IR 05000390/20230112023-07-24024 July 2023 Quadrennial Focused Engineering Inspection (FEI) Commercial Grade Dedication Report 05000390 2023011 and 05000391 2023011 CNL-23-053, Tennessee Valley Authority - Radiological Emergency Plan Revisions2023-07-18018 July 2023 Tennessee Valley Authority - Radiological Emergency Plan Revisions CNL-23-020, Application to Revise Technical Specifications to Adopt TSTF-501-A, Revision 1, Relocate Stored Fuel Oil and Lube Oil Volume Values to Licensee Control (WBN-TS-22-06)2023-06-28028 June 2023 Application to Revise Technical Specifications to Adopt TSTF-501-A, Revision 1, Relocate Stored Fuel Oil and Lube Oil Volume Values to Licensee Control (WBN-TS-22-06) CNL-23-049, Tennessee Valley Authority - Radiological Emergency Plan and Central Emergency Control Center Emergency Plan .2023-06-26026 June 2023 Tennessee Valley Authority - Radiological Emergency Plan and Central Emergency Control Center Emergency Plan . ML23122A2322023-06-0707 June 2023 Issuance of Amendment Nos. 162 and 69 Regarding Change to Date in Footnotes for Technical Specification 3.7.11, Control Room Emergency Air Temperature Control System (Creatcs) CNL-23-044, Transmittal of Revision 3 to WCAP-18774-P and WCAP-18774-NP, Addendum to the Rotterdam Dockyard Company Final Stress Report for 173 P.W.R. Vessels TVA III & IV (Report No. 30749-B-030, Rev. 3) - Evaluation of One Closure Stud Out2023-06-0101 June 2023 Transmittal of Revision 3 to WCAP-18774-P and WCAP-18774-NP, Addendum to the Rotterdam Dockyard Company Final Stress Report for 173 P.W.R. Vessels TVA III & IV (Report No. 30749-B-030, Rev. 3) - Evaluation of One Closure Stud Out IR 05000390/20234032023-05-30030 May 2023 Cyber Security Inspection Report 05000390/2023403 and 05000391/2023403 ML23131A1812023-05-23023 May 2023 Correction to Amendment No. 161 to Facility Operating License No. NPF-90 CNL-23-042, Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-05-16016 May 2023 Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revisions IR 05000390/20220032023-05-0909 May 2023 Reissue Watts Bar Nuclear Plant - Integrated Inspection Report 05000390/2022003 and 05000391/2022003 ML23125A2202023-05-0505 May 2023 Issuance of Amendment No. 161 Regarding a Change to Footnotes for Technical Specification Table 1.1-1 Modes (Emergency Circumstances) IR 05000390/20230012023-05-0404 May 2023 Integrated Inspection Report 05000390/2023001 and 05000391/2023001 CNL-23-043, Emergency License Amendment Request to Relax the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Studs in Technical Specification Table 1.1-1, Modes (WBN-TS-23-09)2023-05-0404 May 2023 Emergency License Amendment Request to Relax the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Studs in Technical Specification Table 1.1-1, Modes (WBN-TS-23-09) CNL-23-032, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 412023-04-27027 April 2023 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 41 CNL-23-030, Tennessee Valley Authority - Hydrologic Engineering Center River Analysis System Project Milestone Status Update2023-04-27027 April 2023 Tennessee Valley Authority - Hydrologic Engineering Center River Analysis System Project Milestone Status Update CNL-23-033, Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revision2023-04-24024 April 2023 Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revision CNL-23-029, Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-04-11011 April 2023 Radiological Emergency Plan and Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML23072A0652023-04-0505 April 2023 Units 1 and 2 Issuance of Amendment Nos. 364 and 358; 160 and 68 Regarding a Revision to Technical Specification 3.4.12 ML23073A2762023-04-0303 April 2023 Individual Notice of Consideration of Issuance of Amendments to Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, and Opportunity for a Hearing (EPID L-2023-LLA-0029) (Letter) CNL-23-023, Annual Insurance Status Report2023-03-30030 March 2023 Annual Insurance Status Report CNL-23-024, TVA Guarantee of Payment of Deferred Premiums - 2022 Annual Report2023-03-29029 March 2023 TVA Guarantee of Payment of Deferred Premiums - 2022 Annual Report 2024-01-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000391/LER-2017-0052018-01-25025 January 2018 Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error, LER 17-005-00 for Watts Bar, Unit 2, Regarding Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error 05000390/LER-2017-0152018-01-0808 January 2018 Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications, LER 17-015-00 for Watts Bar, Units 1 and 2, Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications 05000390/LER-2017-0142017-12-20020 December 2017 Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function, LER 17-014-00 for Watts Bar, Unit 1, Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function 05000390/LER-2017-0122017-10-23023 October 2017 Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications, LER 17-012-00 for Watts Bar, Unit 1, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0112017-10-23023 October 2017 Failure to Enter Technical Specification 3.6.3 for Containment Isolation Valve, LER 17-011-00 for Watts Bar, Unit 1, Regarding Failure to Enter Technical Specification 3.6.3 for Containment lsolation Valve 05000390/LER-2017-0102017-10-10010 October 2017 Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board, LER 17-010-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board 05000391/LER-2017-0042017-09-25025 September 2017 Manual Reactor Trip Due to Inoperable Rod Position Indication, LER 17-004-00 for Watts Bar Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication 05000390/LER-2017-0042017-08-31031 August 2017 Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup, LER 17-004-01 for Watts Bar, Unit 1, Regarding Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup 05000390/LER-2017-0082017-08-14014 August 2017 Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation, LER 17-008-00 for Watts Bar, Unit 1, Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation 05000390/LER-2017-0072017-08-0808 August 2017 Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance, LER 17-007-00 for Watts Bar, Unit 1, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance 05000390/LER-2017-0062017-07-31031 July 2017 Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications, LER 17-006-00 for Watts Bar, Unit 1, Regarding Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications 05000390/LER-2017-0052017-07-10010 July 2017 Isolation of the 1 B-B Safety Injection Pump Leads to Condition Prohibited by Technical Specifications, LER 17-005-00 for Watts Bar re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications 05000391/LER-2017-0032017-05-22022 May 2017 Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure, LER 17-003-00 for Watts Bar, Unit 2, Regarding Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure 05000391/LER-2017-0022017-05-12012 May 2017 Manual Reactor Trip as a Result of a Secondary Plant Transient, LER 17-002-00 for Watts Bar, Unit 2, Regarding Manual Reactor Trip as a Result of a Secondary Plant Transient 05000391/LER-2017-0012017-05-0303 May 2017 Containment Airlock Function Lost Due to Equalizing Valve Not Closing, LER 17-001-00 for Watts Bar, Unit 2, Regarding Containment Airlock Function Lost Due to Equalizing Valve Not Closing 05000390/LER-2017-0032017-03-0303 March 2017 Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications, LER 17-003-00 for Watts Bar, Unit 1, Regarding Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0022017-02-22022 February 2017 Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications, LER 17-002-00 for Watts Bar Nuclear Plant, Unit 1, Regarding: Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2016-0112016-12-0909 December 2016 Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler, LER 16-011-01 for Watts Bar Nuclear Plant, Unit 1 Regarding Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler 05000391/LER-2016-0082016-10-28028 October 2016 Reactor Trip Resulting from Failure of 2B Main Bank Transformer, LER 16-008-00 for Watts Bar, Unit 2, Regarding Reactor Trip Resulting from Failure of 2B Main Bank Transformer 05000391/LER-2016-0052016-08-19019 August 2016 Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip, LER 16-005-00 for Watts Bar, Unit 2, Regarding Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip 05000390/LER-2016-0102016-08-0808 August 2016 Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado, LER-16-010-00 for Watts Bar Nuclear Plant, Units 1 and 2 Regarding Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado 05000391/LER-2016-0042016-08-0404 August 2016 Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure, LER 16-004-00 for Watts Bar, Unit 2, Regarding Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure 05000391/LER-2016-0032016-07-27027 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Governor Valve Spring Over-Tensioning, LER 16-003-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump lnoperable for Longer Than Allowable Outage Time Due to Governor Valve Spring Over-Tensioning 05000390/LER-2016-0082016-07-15015 July 2016 Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B, LER 16-008-00 for Watts Bar, Unit 1, Regarding Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B 05000390/LER-2016-0092016-07-15015 July 2016 Failure to Complete Surveillance Requirements Causes a Condition Prohibited by the Technical Specifications, LER 16-009-00 for Watts Bar, Unit 1, Regarding Failure to Complete Surveillance Requirements Causes Conditions Prohibited by the Technical Specifications 05000391/LER-2016-0022016-07-11011 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Turbine Speed Control Failure, LER 16-002-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer Than Allowable Outage Time Due to Turbine Speed Control Failure 05000390/LER-2016-0062016-06-30030 June 2016 Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump, LER 16-006-00 for Watts Bar, Unit 1, Regarding Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump 05000390/LER-2016-0072016-06-20020 June 2016 Technical Specification Action Not Met for Rod Position Indication, LER 16-007-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Technical Specification Action Not Met for Rod Position Indication 05000391/LER-2016-0012016-06-13013 June 2016 Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines, LER 16-001-00 for Watts Bar, Unit 2, Regarding Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines 05000390/LER-2016-0042016-05-23023 May 2016 Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables, LER 16-004-00 for Watts Bar, Unit 1, Regarding Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables 05000390/LER-2016-0052016-05-13013 May 2016 Both Trains of Unit 1 Emergency Gas Treatment System Inoperable During Unit 2 Testing, LER 16-005-00 for Watts Bar, Unit 1, Regarding Both Trains of Unit 1, Emergency Gas Treatment System Inoperable During Unit 2, Testing 05000390/LER-2016-0032016-05-10010 May 2016 Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting, LER 16-003-00 for Watts Bar, Unit 1, Regarding Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting 05000390/LER-2016-0022016-05-0404 May 2016 Technical Specification Action Not Met for Inoperable Containment Isolation Valve, LER 16-002-00 for Watts Bar, Unit 1, Regarding Technical Specification Action Not Met for Inoperable Containment Isolation Valve 05000390/LER-2016-0012016-03-0909 March 2016 Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable, LER 16-001-00 for Watts Bar, Unit 1, Regarding Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable ML1134703432011-12-13013 December 2011 Withdrawal of License Event Report 390/2011-003, Mode Change Without Meeting Limiting Condition for Operation (LCO) 3.7.5 2018-01-08
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
I. PLANT OPERATING CONDITIONS BEFORE THE EVENT
Watts Bar Nuclear Plant (WBN) Unit 1 was in Mode 1 at 14 percent rated thermal power (RTP). WBN Unit 2 was in "no Mode" prior to initial fuel loading.
II. DESCRIPTION OF EVENT
A. Event
On March 14, 2016, Watts Bar Nuclear Plant (WBN) Unit 1 determined through engineering analysis that both trains of emergency gas treatment system (EGTS) [EMS: BH] were inoperable for 8 minutes, 10 seconds during preoperational testing of Unit 2 EGTS. The inoperability of A and B trains of Unit 1 EGTS took place on October 22, 2015, while Unit 1 was in Mode 1 and two trains of EGTS were required to be operable in accordance with technical specification (TS) limiting condition for operation (LCO) 3.6.9, "Emergency Gas Treatment System (EGTS)." At the time of the event, Unit 2 was in "no Mode," prior to initial fuel loading. This condition is being reported pursuant to 10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), "Event or Condition That Could Have Prevented Fulfilment of a Safety Function.
B. Inoperable Structures, Components, or Systems that Contributed to the Event Train A and train B EGTS were concurrently inoperable for 8 minutes, 10 seconds on October 22, 2015.
C. Dates and Approximate Times of Occurrences Date Time Event 10/17/15 1007 EDT WBN Unit 1 entered Mode 4 coming out of refueling outage 13 10/22/15 0118 EDT Both trains Unit 1 EGTS inoperable due to Unit 2 test configuration 10/22/15 0126 EDT Unit 2 EGTS train A suction dampers closed.
D. Manufacturer and Model Number of Components that Failed There were no failed components associated with this event.
E. Other Systems or Secondary Functions Affected
There were no systems or secondary functions affected by this event.
F. Method of discovery of each Component or System Failure or Procedural Error This issue was identified during the incorporation of Unit 2 EGTS system testing requirements into WBN engineering documents.
G. Failure Mode and Effect of Each Failed Component There were no component failures associated with this event.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc,gov, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 01
H. Operator Actions
There was no actual event requiring operator actions.
I. Automatically and Manually Initiated Safety System Responses There were no automatic or manual system responses associated with this event.
III. CAUSE OF THE EVENT
A. The cause of each component or system failure or personnel error, if known.
There was no component or system failure associated with this event.
B. The cause(s) and circumstances for each human performance related root cause.
The cause of this event was that engineers were assigned tasks without the requisite knowledge and experience to fully understand all issues that needed to be addressed for a first of a kind testing on a complex shared system. This resulted in inadequate special requirements to maintain Unit 1 EGTS operable during the Unit 2 preoperational testing.
IV. ANALYSIS OF THE EVENT
On October 22, 2015, both trains of Unit 1 EGTS were inoperable for 8 minutes, 10 seconds due to inadequate special requirements to maintain Unit 1 EGTS operable during Unit 2 EGTS testing. The specified safety functions of EGTS are:
1. To keep the air pressure within each Shield Building annulus below atmospheric pressure at all times in which the integrity of that particular containment is required.
2. To reduce the concentration of radioactive nuclides in annulus air that is released to the environs during a loss of coolant accident (LOCA) in either reactor unit to levels sufficiently low to keep the site boundary and low population zone (LPZ) dose rates below the 10 CFR 100 values.
3. To withstand the safe shutdown earthquake.
4. To provide for initial and periodic testing of the system capability to function as designed.
EGTS is a dual unit system. TS LCO 3.6.9 requires both trains of EGTS be Operable in Modes 1, 2, 3, and 4 and TS 3.6.15 requires that the Shield Building shall be Operable in Modes 1, 2, 3, and 4. The EGTS must be capable of producing the correct flow and pressure requirements relative to the annulus, which ensures that the EGTS is capable of performing Specified Safety Function 2 described above to keep annulus releases below the 10 CFR 100 limits. A single train of EGTS is capable of drawing suction on the annulus of the unit undergoing a LOCA such that the specified safety functions of EGTS are met.
Annulus in-leakage for the suction path in service is assumed to meet surveillance requirement (SR) 3.6.15.4 in-leakage limit of 5. 250 scfm.
Because in-leakage from the Unit 2 annulus was unknown, and both EGTS trains were aligned to the Unit 2 annulus for 8 minutes, 10 seconds, both trains should have been declared inoperable on Unit 1 which would have required that Unit 1 enter TS LCO 3.0.3.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
A demand for EGTS did not exist during this timeframe. During times where individual trains of EGTS were inoperable, the conditions existed for less than the TS LCO 3.6.9 required action completion times. In addition, LCO 3.0.3 required action completion times were not exceeded when both trains of EGTS were inoperable.
V. ASSESSMENT OF SAFETY CONSEQUENCES
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event The WBN probabilistic risk model does not consider EGTS in core damage and large early release frequencies. As a result, any risk increase associated with a short-duration misalignment of EGTS EGTS test for operators to close dampers to isolate Unit 2 from the suction path of EGTS, should it become necessary to prevent Unit 2 testing from adversely impacting Unit 1 operation.
See discussion below regarding safety system functional failure reporting in accordance with NEI 99-02.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident Not applicable. Watts Bar Unit 1 was in Mode 1 at the time of this event.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from the discovery of the failure until the train was returned to service There was not an actual failure associated with this event. In the engineering evaluation performed subsequent to the event, WBN demonstrated that both trains of Unit 1 EGTS were inoperable for 8 minutes, 10 seconds.
VI. CORRECTIVE ACTIONS
This event was entered into the Tennessee Valley Authority Corrective Action Program and is being tracked under condition report 1143076.
A. Immediate Corrective Actions
This issue was identified subsequent to the inoperability of both trains of Unit 1 EGTS. Condition report 1143076 was initiated, and a past operability evaluation performed.
B. Corrective Actions to Prevent Recurrence
Watts Bar Unit 2 EGTS has been turned over to plant operations, and is controlled under the WBN Unit 2 TS. Testing requirements for EGTS were revised to support dual unit operation, including appropriate controls to ensure that EGTS on the unit not undergoing testing will remain operable.
CONTINUATION SHEET
2016 - 01 APPROVED BY OMB: NO. 3150.0104 EXPIRES: 10131/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
VII. ADDITIONAL INFORMATION
A. Previous similar events at the same plant
None.
B. Additional Information
None.
C. Safety System Functional Failure Consideration
This event is considered a safety system functional failure in accordance with NEI 99-02.
The Emergency Gas Treatment System (EGTS) is a common system capable of drawing suction from the containment annulus of either Unit 1 or Unit 2 following an accident. While the system is capable of responding to an accident while testing the other unit, annulus in-leakage is assumed to meet Technical Specification 3.6.15, "Shield Building," requirements for both units.
During preoperational testing of the Unit 2 EGTS, Unit 2 annulus in-leakage did not meet Technical Specifications requirements during times when EGTS was required to be operable for Unit 1. Unit 2 EGTS was not required to be operable during this time. In order to compensate for the Unit 2 annulus in-leakage during Unit 2 preoperational testing, specific operator actions were developed to isolate the Unit 2 annulus and place the EGTS system into an alignment which would support the response to an accident on Unit 1.
In the 10 CFR 50.59 evaluation to support the Unit 2 EGTS testing, TVA concluded that the actions required to isolate Unit 2 EGTS in the event of a Unit 1 accident were reliable and achievable and could be implemented without prior NRC approval assuming only one train was tested at a time. For the period of concern, however, both trains of EGTS had been placed in the test configuration and were inoperable, and therefore outside the scope of the 10 CFR 50.59 evaluation. The actions required in the event of a Unit 1 loss of coolant accident were the closure of open Unit 2 EGTS dampers by a dedicated operator. The dampers met stroke time testing prior to the event described in LER 390/2016005 and were demonstrated to function properly from the main control room. In addition, TVA confirmed through review of testing documents and operator logs that the operator actions were in place during this event.
Given the above, there is high confidence that the EGTS safety functions were maintained.
D. Scrams with Complications Consideration None.
VIII. COMMITMENTS
None.
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