ML20203F436

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Insp Repts 50-317/97-06 & 50-318/97-06 on 970914-1101. Violations Noted.Major Areas Inspected:Integrated Insp Rept Includes Aspects of Util Operations,Maint,Engineering & Plant Support
ML20203F436
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 12/05/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20203F390 List:
References
50-317-97-06, 50-317-97-6, 50-318-97-06, 50-318-97-6, NUDOCS 9712170379
Download: ML20203F436 (38)


See also: IR 05000317/1997006

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U.S. NUCLEAR REGULATORY COMMISSION

REGION 1

License Nos. DPR 53/DPR 69

Report Nos. 50 317/97-06:50-318/97 06

Licensee: Baltimore Gas and Electric Company

Post Office Box 1475

Baltimore, Maryland 21203

Facility: Calvert Cliffs Nuclear Power Plant

Units 1 and 2

Location: Lusby, Maryland

Dates: September 14,1997 through November 1,1997

Inspectors: J. Scott Stewart, Senior Resident inspector

Fred L. Bower Ill, Resident inspector

Henry K. Lathrop, Resident inspector

James Noggle, Senior Radiation Specialist, DRS

Paul H. Bissett, Senior Operations Engineer, DRS

Laurie A. Peluso, Radiation Physicist, DRS

Approved by: Lawrence T. Doerflein, Chief

Projects Branch 1

Division of Fieactor Projects

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PDR ADOCK 05000317

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EXECUTIVE SUMMARY

Calvert Cliffs Nuclear Power Plant, Units 1 and 2

Inspection Report Nos. 50 317/97-06and 50 318/97-06

This integrated inspection report includes aspects of BGE operations, maintenance,

engineering, and plant support. The report covers a seven week period of resident

inspection and includes the results of announced inspections by radiation safety and

operator licensing personnel.

Plant Operations

BGE actions to minimize risk during a reactor coolant pump seal replacement were notable.

During the seal replacement, a number of control room deficiencies were corrected. The

plant was recovered and returned to full power without complication.

The inspectors observed the BGE response to an automatic trip of Unit 1. Operator actions

were very good and included completion of the appropriate emergency operating

procedures, periodic status briefings, and detailed evaluation of plant conditions. BGE did

a thorough review of the transient and after the cause of the trip was understood and

corrected, a plant startup was authorized by management. The plant was restarted and

returned to full power without complication.

The conduct of operations was professional and safety-conscious. The operations and

engineering departments implemented multiple and detailed safety risk assessments for

planned safety related equipment outages. The applicable system Technical Specification

(TS) limiting conditions for operation (LCO) were entered and exited correctly for the

equipment outage times.

The inspectors found that while BGE had not met their established goals for the number of

control room deficiencies; efforts to reduce the total number of deficiencies had been

aggressive. No existing deficiency represented an immediate safety concern.

The inspectorr determined _that operator preparedness for use of self-contained

breathing apparatus was weak. A number of operators did not know the location of the

j equipment, some operators wors f acial hair that would inhibit SCBA use, and some

operators had not trained with the equipment for five years. BGE responded to

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inspector concerns by requiring that operators be clean shaven and establishing a

practical training plan for SCBAs.

! The inspectors reviewed the licensed operator requalification program and found it was

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implemented acceptably. Operator performance during the annual operating test was

i good. The operations and training departments worked effectively to maintain operator

knowledge and skills at desired levels of performance. Licensed operator exams were

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administered appropriately; however, the inspectors noted some concerns in the areas of

l simulator and JPM debriefs, JPM critical task identification, and evaluator cuing.

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Executive Summary (cont'dl

Maintenu 3

In general, maintenance was conducted safely and in accordance with approved

procedures. The inspectors observed during maintenance inspections, that workers

were knowledgeable and performed work effectively.

A leak repair activity on the high pressure main turbine was initiated without normal

engineering assessment. The effort was stopped by the BGE nuclear assessment

department af ter identification that fire protection, injection pressure, and injection

volume had not been assessed. The NRC inspectors considered the efforts of the BGE

nuclear assessment department to be aggressive and prudent, initial mainwnance

department preparations for the higt. pressure turbine leak repair were poor.

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in 1980, BGE increased the toxic material hazard from the on sita storage of liquid

ammonia from 55 gallon drums to a 5600 gallon storage tank without completing a

written safety evaluation. Further, BGE had approved the replacement of the 5600

gallon tank with an 8500 gallon tank without a written safety evaluation providing the

basis that the change did not involve an unreviewed safety question. Safety evaluation

screening reports completed for the tank installations, had not considered UFSAR

Section 1.8, or UFSAR Figure 1-2.

The inspectors found that BGE had stored ammonium hy6 oxide solution within the

protected area boundary without ensuring that the plant was fully prepared for a

potential spill of the storage tank contents. The need to place control room ventilation

in the recirculation mode or have the licensed operators don respiratory protection had

not been fully considered and procedures for response to an ammonia spill had not been

developed.

The inspectors concluded that BGE was takin0 appropriate actions to address industry

identified concerns 'with the f atigue of welds on the 18,2A, and 2B emergency diesel

generator lube-oil and jacket water piping systems, o

On infrequent occasions, aircraf t have been observed flying at low altitudes over the

Calvert Cliffs site, BGE had assessed airplane flyovers and concluded that flights over

the plant did not represent a significant safety hazard.

Plant Supp_qrt

The programs for radiologicel environmental monitoring (REMP) and meteorological

monitoring (MMP) continued to be effective. Management oversight of the REMP and

MMP was effective. The quality assurance audits were of sufficient technical depth

to identify and assess program strengths and weaknesses. BGE audits evaluated the

technical adequacy of implomenting procedures, technical specification and of fsite

dose calculation manualimplementation, and practices,

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Executive Summsry (cont'd)

The inspectors found that BGE had not developed and implemented a procedure to

prevent personnel contaminations from occurring as a result of contaminated Anti-C

clothing. Although no significant skin contaminations had been observed, Anti C

articles that had been returned to Calvert Cliffs from the laundry vendor, were at

times contaminated above the limits specified in tne Calvert Cliffs procedure for

laundering of Anti C clothing. However no proceduro existed ' J.ich specified actions

to be taken when articles were found above the monitoring limits, including criteria

for sample expansion, assessment of the contamination in excess of the limits, and

actions to ensure that laundered clothing contaminated above acceptable limits was

not made available for general use.

Communication deficiencies were observed in a radiation safety technician turnover

and in prejob briefing for a reactor coolant pump seal replacement.

Radiation safety technician performance weaknesses were observed during high

radiation area coverage of a reactor )lant pump seal replacement that included:

poor placement of an air sampler, lace of knowledge of radiation levels of a canister ,

that was located in the work area, and inadequate control of a worker who was not

wearing the required water resistant protective clothing and was observed spraying

down a highly contaminated seal cartridge.

Good control and oversight to prevent foreign material from entering the reactor

coolant system during reactor coolant pump seal replacement was observed.

During the initial containment entry following a reactor trip, two radiation safety

technicians were observed by the NRC inspector making a high radiation entry

without following the Special Work Permit requirement to wear the TLD on the

outside of the Anti-C clothing, with the beta window exposed.

The inspectots conducted walkdowns of various fire protection equipment, including

fire hydrants, sprinkler piping, hose and nozzle storage boxes, and emergency fire

pumps. All of the equipment was in good materiai condition and no problems were

identified,

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TABLE OF CONTENTS

EXECUTIVE SUM M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . Il

TA BLE O F CO NT ENT S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v

Report D e t a il s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. O pe r a ti on s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . *

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1  :

01.1 General Comments (71707) ...................... 1

- 01.2 Unit 1 Re actor Trip . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

02 Operational Status of Facilities and Equipment .............. 3

02.1 Engineerod Safety Feature System Walkdowns . . . . . . . . . 3 7

02.2 Control Hoom Deficiencies . . . . . . , . . . , , . . . . . . . . . 3  !

02.3 Use of Self Contained Breathing Apparatus . , . . . . . . . . . 4

05 Operator Training and Qualification . . . . . . . . . . . . . . . . . . . . . . 5

05.1 General Sc ope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

05.2 Ex am Cont e nt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

05.3 Exam Administration and Evaluation . . . . . . . . . . . . . . . . . 6

05.4 Continuing Training ............................ 8

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05.5 Remedial Training . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

05.6 License Reactivation .................-........9

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08 Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . 9

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08.1 (Closed) Unresolved item 50 317&318/95 10-01 ....... 9

08.2 (Closed) Unresolved item 50 317&318/95 10 02....... 10

11. M a i n i e n a nc e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

< M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

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M1.1 General Comments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

M1.2 - Routine Surveillance Observations . . . . . . . . . . . . . . . . . 11

Ill . Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . , . . . . . . . . . . . . . 12

El Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

E1.1 Onsite Storage of Ammonia and other Toxic Chemicals . . 12

E2 Engineering Support of Facilities and Equipment ............ 15

E2.1 Emergency Diesel Generator Piping Operability . . . . . . . . 15

E 8 .- Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . 16

E8.1 Aircraf t Flight Hazards . . . . . . . . . . . . . . . . . . . . . . . . . 16

IV - Pl a nt Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17  !

R1 Radiological Protection and Chemiury (RP&C) Controls . . , . . . . 17

RI .1 The Radiological Environmental Monitoring Program . . . . . 17

H1.2 Meteorological Monitoring Program . . . . . . . . . . . . . . . . 19  !

R1.3 Secondary Chemistry Controliniplementat;on Chang . . . 20

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Table of Contents (cont'd)

! R2 Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . 21

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' R3 RP&C Procedures and Documentation . . . . . . . . . . . . . . . . . . . 22 -

R3.1 Laundering of Contaminated Clothing . . . . . . . . . . . . . . . 22

R4 Staff Knowledge and Performance in RP&C . . . . . . . . . . . . . . . . 24-

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R6 RP&C Organization and Administration . . . . . . . . . . . . . . . . . . . 26

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R6.1 Organization Changes and Responsibilities . . . . . . . . . . . 26- i

i R7 Quality Assurance in RP&C Activities . . . . . . . . . . . . . . . . . . . . 27 .

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R7.1 Quality Assurance Audit Program ' . . . . . . . . . . . . . . . . . 27 - i

R7.2 Quality Assurance of Analytical Measurements . . . . . . . . . 27

S8- Miscellaneous Security and Safeguards Activities . . . . . . . . . . . 28

F8 Miscellaneous Fire Protection issues . . . . . . . . . . . ... . . . . . . . . 28 3

} V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 9 7

. X1 Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 9 i

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ATTACHMENTS

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Attachment 1: Partial List of Persons Contacted

Inspection Procedures Used

items Opened,. Closed and Discussed

List of Acronyms Used  !

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Summarv of Plant Status

The inspection period began with Unit 1 shutdown to support replacement of a

reactor coolant pump seal. The reactor returned to full power on September 22,

1997. Unit 1 tripped from full power on October 24 due to a loss of condenser

vacuum (section 01.2) and was returned to full power on October 26,1997.

Unit 2 remained at full power during the inspection period.

l. Onorations

01 Conduct of Operations -

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01.1 Gentf el Comments (71707)

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Overall plant operations were conducted safely with a proper focus on

continued nuclear safety. At the beginning of the inspection period, Unit 1

was shutdown in Mode 5 to replace the 118 reactor coolant pump seal. The '

replacement required that the reactor coolant system (RCS) be placed in the

hQher risk, reduced inventory condition. In preparation, the operations

department conducted briefings and established a reduced inventory plan that

specified tra ning requirements, actions to minimize time in the reduced

inventory condition, compensatory actions to ensure inventory control, and

contingency actions should there be a loss of RCS inventory. Operators and

other key personnel were trained on the plan and briefings for critical work in

the containment included discussions of containrnent evacuation procedures. ,

The focus of training was personnel and nuclear safety during the higher riek

condition. The inspectors reviraved the BGE plan and observed its

implementation, BGE actions to minimize the risk of the reduced inventory

condition were very good and the seal was replaced without problems. During

the seal replacement outage, a number of control room deficiencies were

worked and cleared. The plant was recovered and returned to full power on

September 22,1997, without complication.

The inspectors reviewed the June 1997 World Association of Nuclear

Operators (WANO) evaluation of Calvert Cliffs. The report was based on a

two week team review of Calvert Cliffs activities in operations, maintenance,

radiation protection, t.nd other areas. The report discussed a number of

strengths and areas for iraprovement. No significant operability issues were

identified and the inspectors were generally aware of issues ra!3ed in the

evaluation.

Using inspection Procedure 71707," Plant Operatior.3," the inspectors

conducted frequent reviews of ongoing plant operations. In general, the

conduct of operations was professional and safety conscious. The operations,

maintenance, and engineering departments implemented roultiple detailed on-

line safety risk assessments for planned safety related equipment cutages that

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included safety risk and trip risk assessments. Maintenance was sequenced to

minimize the risk factors. The applicable system Technical Specification (TS)

limiting conditione for operation (LCO) were entered and exited correctly for

the equipment outago times.

01.2 Unit 1 Reactor Trio

a. Insoectios. Scooe

The inspectors observed and assessed a reactor trip on Unit 1.

b. Observations _ and Findinos

On October 24, at approximately 9:17 a.m., Unit 1 automatically tripped from

full power. In the control room, operators had observed a main condenser low

vacuum alarm followed within ten seconds by the automatic trip. The plant

responded to the trip as designed and there were no complications. The

inspectors responded to the control room and observed the performance of

Emergency Operating Procedure, EOP-0, " Post Trip Immediate Actions," and

EOP 1, " Reactor Trip." Following the trip, the operators observed that a main

condenser vacuum breaker had fully opened, causing a loss of main condenser

vacuum. Because the main condenser was not available, the reactor was

stabilized in Hot Standby using auxiliary feedwater and steam generator

atmospheric dump valves. The control room supervisor appropriately assumed

an oversight position and followed control of the transient and execution the

emergency operating procedures. Periodic status briefings were held with the

operators with a notable briefing during the transition between EOP-0 and

EOP 1. Prior to exiting the emergency procedures, the vacuum breaker was

shut, vacuum was restored, and main feedwater was restored to supply water

to the steam generators. The inspector considered the operator actions in

response to the trip and to implement the emergency operating procedures to

be very good. BGE reported the trip to the NRC in accordance with 10 CFR

50.72(b)(2)(ii).

A Significant incident Findings Team was assembled to review the trip, to

determine the root cause, and to recommend appropriate corrective actions.

The root cause was determined to be a poorly completed wire termination for

the vacuum breaker handswitch in the control room. A loose strand of wire

extemal to the termination had contacted an adjacent powered contact

causing a seal-in contact to close in the vacuum breaker control circuit,

opening of the vacuum breaker. As corrective action, BGE initiated a

100 percent inspection of the type of electrical connection that had caused the

problem, initiated a procedure upgrade to ensure wire terminations were done

correctly, and implemented training on the cause and corrective actions for the

problem.

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On October 25, when the cause of the reactor trip was known and corrected,

a plant startup was initiated. Full power was reached on October 26, and

there were no complications to the startup,

c. Conclusions

The inspectors observed the BGE response to an automatic trip of Unit 1.

Operator actions were very good and included completion of the appropriate

emergency operating procedures, periodic status briefings, and detailed

evaluation of plant conditions. BGE did a thorough review of the transient and >

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af ter the csuse of the trip was understood and corrected, a plant startup was

authorized by management. The plant was restarted and returned to full

power without complication.

02 Operational Status of Facilities and Equipment

02.1 Enaineered Safety Feature Systern.Wr;kdowns (71707)

The inspectors performed walkdowns of accessible portions of the Unit 2

emergency diesel generators and the combined control room heating,

ventilating, and air conditioning (HVAC) system. Equipment configuration was

consistent with plant drawings. Equipment material condition and

housekeeping in the areas were good. Several minor discrepancies were

brought to BGE's attention and were corrected. The inspectors identified no

safety concerns as a result of these walkdowns.

02.2 Control Room DeficiencJgg

a. Scoon

Tha inspectors reviewed BGE Operations Administrative Policy 93-7," Control

Room Deficiency Reduction Program," and its implementation. ,

b. Observations and Findinos

The operations department had assigned a senior reactor operator the

collateral duty of coordinating the control room deficiencies program. One

program goal was to have the control room deficiencies planned and scheduled

to work within three weeks of identification. The control room deficiency

coordinator trended the deficiencies and issued monthly status reports which

were reviewed by operations management. BGE management specified that

issues affecting safety be repaired on an expedited schedule.

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The inspectors reviewed the trend for the previous 18 months and compared the

current trend to 1996 results. The inspectors observed that, as expected, the

number of control room deficiencies were reduced during outages and trended

upward between outages. In September 1996, BGE had approximately

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40 control room deficiencies and met their goal of less that 55 deficiencies, in

rarly 1997, BGE established a more aggressive goal of less than 35 total control i

room deficiencies. The inspectors noted that the September 1997 total of

55 control room deficiencies was higher than the September 1996 total. Most of

the deficiencies required unit shutdown for repair. However, the inspectors ,

noted that the September 1997 total reflected BGE's recent efforts to reduce the '

deficiencies from a recer,t peak of 72 and included the correction of 17 control

room doficiencies during the Unit 1 reactor coolant pump seal replacement

outage.

The inspectors reviewed the outstanding r ontrol room deficiencies and

determined that no single item in the backlog represented an immediate safety

concern. The inspectors noted that those items with higher safety significance

were repaired in an expedited manner.

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c. Conclusions

The inspectors found that while BGE had not met their established goals for

number of control room deficiencies, efforts to reduce the total number of

deficiencies had been aggressive. No existing deficiency represented an

immediate safety concern. BGE had focused management attention to ensure

that control room deficiencies when considered in ' heir aggregate did not become

a safety concern.

02.3 Use of Self Contained Breathino Aooaratus ISCBAs)

a. Insoection Scooe

The operational readiness of plant operators to use self contained breathing

apparatus was assessed,

b. Findinos and Observations

Self contained breathing apparatus were provided near the control room to be

used in event of a radiological emergency. BGE told the inspectors that in some

scenarios, breathing apparatus would be necessary to protect operations

personnel 45 minutes following an accident that included a significant ,

radiological release. On questioning by the inspectors on the readiness vf the

control room for hazardous material spills, BGE reviewed the engineering

assessments that had been completed for ammonia storage and responded that

the SCBAs could be used during hazardous material spills or fires; however, BGE

told the inspectors that no amount of hazardous material that would require

SCBA use was stored in the Calvert Cliffs protected area.

The inspectors observed that most operators were clean shaven; however, a

number of operators wore beards or other facial hair that would inhibit

immediate respirator use. The inspectors were informed that razors were

available for personnel to allow shaving if needed for respirator use. On

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questioning, some operators did not know the location of the self contained

breathing apparatus. Also, instructions on how to effectively don and use the

breathing apparatus were not provided with the kits.

Based on inspector questioning, a senior reactor operator demonstrated donning

an SCBA. The operator, from memory, successfully used the apparatus in four

minutes; however, the operator did not check the leak tightness of the mask and

did not check t'ne low pressure alarm prior to activating the SCBA. These

checks were specified in BGE training manual for SCBA use. The senior reactor

operator stated that although annual written examinations on SCBA use had

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been completed, practical SCBA training had not been offered for five years.

Plant operators that were members of the fire brigade regularly used SCBAs in ,

training.

Following questioning by the inspectors, BGE specified operators to be clean $

shaven and to have practical training on SCBA use. BGE also initiated a review

to determine if the need for SCBAs could be eliminated.

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c. Conclusions

The inspectors determined that licensed operator preparedness for use of self-

contained breathing apparatus was weak. A number of operators did not know

the location of the equipment, some operators wore facial hair that would inhibit

SCBA use, and some operators had not traineel with the equipment for up to five

years. BGE responded to inspector concerns by establishing a practical training

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plan for SCBAs and initiated a review to eliminate the need for SCBAs for

licensed operators.

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05 Operator Training and Qualification

05.1 General Scoce (71001)

A scheduled inspection of the Calvert Cliffs' licensed operators' requalification

program was conducted from October 20 24,1997, using NRC inspection

procedure 71001. The scope of the inspection included the observation of the

annual operating exams administered to one operating and one staff crew of

, licensed operators, the review of previously completed annual exams, remedial

actions taken for exam failures, and reactivation of inact!ve licenses. The annual

examination consisted of a static simulator and classroom written examination,

simulator scenarios and job performance measures (JPMs), which were -

performed both in the siraulator and in the plant.

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05.2 Exam Contant

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a. insoection Scoos ,

The inspectors reviewed the annual written and operating examinations for the '[

licensed operators being examined during the inspection. Also reviewed were r

previously administered exams and weekly training quizzes. l

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b. Observations and Findinas

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The inspectors reviewed the written exams administered during the week and

found the questions to be of good quality with an appropriate mix of high and  ;

low cognitive level questions. Both Parts A and B written exams were -;

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i adequately constructed, and the distribution of questions was appropriate  :

between different examinations.

The inspectors reviewed and witnessed the performance of several simulator and i

in-plant JPMs. The JPMs were relevant to operator tasks, were consistently

administered by different evaluators, were technically sufficient to discriminate i

operator abilities, and were apprupriately evaluated to identify weaknesses in

l performance. However, there were some NRC identified concerns regarding JPM  !

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construction that were brought to the attention of BGE management. These i

concerns included
1) not identifying all critical tasks, 2) designating some JPM - i
  • steps as critical that should not have been, and 3) not including evaluator cues in

many instances for inplant JPMs.

l The inspectors reviewed several simulator scenarios that were given to one

operating and one staff crew.. The scenarit,s were challenging and met the ,

criteria set forth in the examiner standards. The scenarios were diverse and

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utilized variously abnormal and emergency operating procedures.

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c. Conclusions

4 The f acility had developed annual licensed operator requalification exams that  !

effectively tested the knowledge and abilities of alllicensed operators.

05.3 Exam Administration and Evaluation

a. Inspection Scooe

The inspector observed one operating and one staff crew complete two sections i

of the. written examination, perform at least two simulator scenarios, and perform

five job performance measures (JPM). The inspector also reviewed the facility

evaluation of both crew and individual operator performance,

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b. Observations and Findinas

The crews ard individuals passed their operating and written examinations.

Crew and individual operator performance during the conduct of the simulator

scenarios was good Communication, for the most part, was very good. Peer

checks were conducted frequently in an effort to ensure that all control board

manipulations were carried out correctly. Crew briefings were also held

frequently. Individual and crew performance was appropriately evaluated by

operations and training evaluators.

During one scenario, the senior shif t supervisor displayed such a dominant role

throughout the scenario that the f acility evaluators were unable to effectively

evaluate the performance of the control room supervisor or the reactor operator.

The decision was made to delay final performance evaluations for these two

operators pending their participation in another scenario during the next week's

annual exam. The inspectors agreed with this decision.

During a previous NRC annual requalification inspection, as detailed in inspection

Report 317 & 318/9510,it was noted by the inspectors that a management

representative from operations was not present during the simulator exams and

that f acility evaluators did not provide detailed results of the simulator exam until

alllicensed operators had been examined and the results reviewed by

management. The NRC stated that this long delay could reduce the effectiveness

of the evaluations. The inspectors noted during this inspection that operations

management was present during the conduct of the simulator exams for the

operating crew. An operations representative was scheduled to observe the

performance of the staff crew, but was unable to be present due to a schedJIing

conflict. Operations management stated that it is now common policy for

operations management to be present during all simulator examinations.

In an effort to address the inspectors' concern regarding simulator debriefs, the

facility instituted a policy to perform debriefs immediately following the

completion of each scenario. These debriefs consisted of not only informing

each individual and crew of pass /f ail results, but also pointed out what they did

incorrectly and what the correct actions should have been, The inspectors stated

that the timing of this debrief was inappropriate because it transferred the setting

from an examination mode to a training mode. Providing training in the middle of

an exam could inadvertently provide the knowledge needed by certain individuals

necessary for successful completion of subsequent scenarios, or other segments

of the exam, and thus distort the evaluation of skills and abilities. The inspectors

stated that debriefs should be provided as soon as possible after an individual's

entire exam has been administered, but not anytime prior to completion of the

entire examination phase for each individual. Facility management stated that

they had misinterpreted the pievious inspector's concern and that they would

again address the area of debriefs and make the appropr! ate changes to correct

this area of concern.

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Overall performance of JPMs was acceptable. As noted above concerning

scenario debriefs, the same occurred during the performance of JPMs. JPM

debriefs, including incorrect actions were discussed with the operators following

the completion of each JPM. Again, the inspectors stated that this was

inappropriate because it provided training during an examination phase. The

inspectors also noted that each JPM task standard, an essential element to a

systematic approach to training (SAT) based training program, was provided to

each c serator prior to their performing a JPM. This information is appropriate for

JPM construction; however, it is inappropriate information to be given to the

operator. Knowledge of the task standard can be utilized by any individual to

indicate the success path necessary to satisf act 3rily complete a JPM, an

inappropriate cue. Facility management acknowledged the inspectors' concern

and stated that appropriate ections would be taken to address this concern

during future examinations.

,

During the administration of the static written exam, which is administered in the

'

simulator,it was noted that seven opcrators participated in the first session, and

eight operators participated in the second session. The inspectors also noted

that there was only one proctor present to monitor and address questions during

both test sessions. The inspectors questioned the ability of one proctor to

maintain an awareness of allindividuals in this type of test environment, in an

effort to maintain examination integrity, the inspectors stated that for this large

of a class, there should be at least two proctors. Again, the facility agreed to

make the necessary adjustments based upon further evaluation. The inspectors

did not identify any indication of examination compromise.

The evaluations by training and operations department evaluators were effective

for those portions of the exam observed by the inspector. The inspectors agreed

with the 4cility evaluations. Documentation of test results appeared adequate in

all instances,

c. Conclusions

The annuallicensed operator requalification exams were administered and

evaluated acceptably; however, program enhancements were warranted in the

areas of test result debriefs, JPM information provided to the operators, and

static exam administration.

05.4 Continuina Trainina

The inspectors reviewed several Calvert Cliffs licensee event reports (LERs) that

occurred in 1996 and 1997 in an effort to determine if any of the events were a

result of inadequate training. The LERs reviewed did not indicate any

deficiencies in the knowledge level of individuals or inadequate training provided

by the training department. The facility recently developed and has been using

performance indicator graphs for crew and individual performance during

examinations and evaluations. Each crew was evaluated against various

performance categories similar to competencies listed in the NRC examiner

.

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9

standards. Each crew shift rating was compared to the average of all crew shifts

and each individual crew member was compared to the overall crew average.

Should an average for a crew or individual be lower than the overall average to

which the results are compared, operations or training management can initiate

remedial training as they deem necessary to enhance the knowledge level of a

crew or individual to bring them in I;ne with the average. The Calvert Cliffs

training department had implemented a continuing licensed operator training

program that met administrative and regulatory requirements.

05.5 Remedial Trainino

The inspectors reviewed remedial actions taken for those licensed individuals

who had f ailed any portion of their weekly training evaluations or their annual

toqualification exam. In this instance, the inspectors reviewed the remediation

documentation for five individual f ailures of a weekly written quiz, one individual

f ailure of a weekly simulator scenario evaluation, and two individual f ailures

during the annual simulator exam scenarios. Documentation of remediatior'

included a review of areas of weakness with the individuals and a retake of

another exam. In allinstances, the individuals passed their retake examinations.

The inspector concluded that the Calvert Cliffs' training department had taken

appropriato action in regard to those individuals who had f ailed any portion of

their annuallicensed operator exam. For those failures reviewed by the

inspector, appropriate remedial action had been taken, and documentation was

acceptable.

05.6 License Reactivation

The inspector reviewed the f acility's program for restoration of active operator

license status following inactivation and found the program to be acceptably

documented and administered. The records of three licensed operators, whose

licenses had been recently reactivated, were reviewed. The inspector noted that

the records were complete and reactivation requircments had been met in

accordance with administrative and 10 CFR 55.53(f) requirements. The

inspectors determined that the f acility had appropriately implemented the

program and regulatory requirements for reactivation of licenses for operators at

Calvert Cliffs Unit 1 and 2.

08 Miscellaneous Operations issues

08.1 (Closed) Unresolved item 50-317&318/95-10-01: Training facility did not

document individual operator evaluations except when a failure occurred. The

inspectors reviewed current and past simulator evaluations and determined that

the f acility evaluators were performing and documenting individual evaluations in

additir,n to crew evaluations. Based upon this review, the item is eh.

. _ _ _ _ _ . .

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08.2 (Closed) Unresolved item 50 317&318/95-10-02: Not requiring attendance at all

requalification training and individuals missing training. The inspectors reviewed

records of participation (by attendance)in the licensed operator requalification

training program and discussed this area with facility management. In

accordance with f acility procedures and management expectations, alllicensed

operators were required to attend all continuing training sessions. The inspectors

reviswed the tracking process for five individuals who had missed occasional

training sessions the past year, it was determined that the facility adequately

tracked and followed up on the missed training sessions. Missed classes were

made up by attending either subsequent shift training classes or viewing video

sessions of previously conducted training. The inspectors determined that the

training department had adequately tracked missed training classes and that

individuals routinely made up training that they had missed. Through a review of

quarterly operations and training interface meetings, the inspectors noted that

continued emphasis was being placed on the importance of attending all

scheduled classes. Based upon this review, this item is closed,

ll< Maintenance

M1 Conduct of Maintenance

M 1.1 General Comments

a. inspection Scope (62707)

The inspectors reviewed maintenance activities and focused on the status of

work that involved systems and components important to safety. Component

f ailures or system problems that affected systems included in the BGE

maintenance rule program were assessed to determine if the maintenance was

effective. Also, the inspectors directly observed all of portions of the following

work activities:

MO2199700634 23 Saltwater Pump Motor, Breaker, and Controls

MO2199602803 Repair Expansion Joints for Unit 2 Diesel Rooms

M01199700292 Replace Seals and Boarings on 1 A EDG Prelube Pump

M01199704163 Boroscope 1 A EDG Cylinders

b. Observations and Findinns

The inspectors found that the selected maintenance activities were performed

safely and in accordance with approved procedures. Technicians were

experienced and knowledgeable of the assigned duties. Pre-job briefings were

effective in ensuring that the work was conducted in accordance with BGE work

protocols and plans. The inspectors noted that an appropriate level of

supervisory attention was given to the work. The BGE system engineering report

cards discusud problems, maintenance rule status, action plans for systems with

lower ratings, and problem trending.

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The inspectors were informed by BGE that a leak repair activity for the Unit 1

high pressure turbine casing had been stopped by the quality assurance

department on September 30. A Calvert Liffs Nuclear Perforrnance Assessment

Department inspector had identified during the pre job briefing that Calvert Cliffs

Maintenance Procedure LR 1,"On-line Leak Repair to Pressure Retaining

Components," had not been used in developing the leak repair work order. Also,

some considerations in procedure LR 1, such as a fire protection assessment, the

volume of sealant allowed, and the rpecified injection pressure for the sealant

had not been evaluated by BGE engineering. Instead, a vendor procedure had

been used to plan the work and the involvement of BGE engineering was

minimal. Following the work stoppage, plans for the leak repair were assessed

by Oalvert Cliffs engineering, appropriate procedurcs were imptomented, and the

job was completed on October 7,1997, without problems.

A reactor trip was caused by an improper termination on a ma.n condenser

vacuum breaker control switch. As corrective action, BGE inspected similar

electrical terminations and some additional problems were found and corrected.

A procedure change was made and training was conducted to prevent

recurrence. (See 01.2)

c. ConclusioD1

in general, maintenance was conducted safely and in accordance with approved

procedures. Workers were knowledgeable and pe-formed work effectively. A

leak repair activity on the high pressure main turbine was initiated without normal

engineering assessment. The effort was stopped by the BGE nuclear plant

assessment department af tor identification that fire protection, injection pressure,

and injection volume had not been assessed. The NRC inspectors considered the

efforts of the BGE nuclear performance assessment department to be aggressive

and prudent. Initial maintenance department preparations for the high pressure

turbine leak repair were poor.

M1.2 Routine Surveillance Observations

The inspectors observed and reviewed selected surveillance tests to determine

whether approved procedures were in use, details were adequate, test

instrumentation was properly calibrated and used, technical specifications were

satisfied, testing was performed by qualified personnel, and test results satisfied

acceptance criteria or were properly dispositioned. Tests that were inspected

included:

STP O 88-2 Test of 2B DG and No. 24 4Kv Bus LOCl Sequencer

0130 Nuciear instrument - Daily Survel: lance / Calibration

STP-0 73A-1 Saltwater Pump and Check Valve Quarterly Test

STP-F-490 Fire Detection Functional Test (Smoke)

STP-F-76 Staggered Test of Electric Fire Pump

STP-F-696 Diesol Pump Flow Test

. _ _ _ _ _ . m._ _ _ _ _ _ _ _ _ m._ _ . _ _ _ _ . . _ _ _ _ _ _

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The observed surveillance testing was performed safely and in accordance with

approved procedures. Pre test briefings included means of communication, test

- control details, and contingency actions. The inspectors noted that an j

appropriate level of supervisory attention was given to the testing depending on  !

, its censitivity and difficulty. For fire protection system testing, the fire and safety i

'

personnel were well organized and knowledgeable about the fire protection i

system. The procedures were clear and easily implemented. The fire protection

equipment was found in good material condition,

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lil. Ennineedna

E1 Conduct of Engineering

i i

E1.1_ Onsite Storaae of Ammonia and other Toxic Chemicals {

1

a. insoection Scope

The inspectors reviewed the Calvert Cliffs on site storage of liquid ammonia.

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b. Findinas z7d Observations ,

'

The inspectors reviewed the Calvert Cliffs Updated Final Safety Analysis Report

(UFSAR), concerning the onsite storage of toxic chemicals. UFSAR Section

1.8, Generic issues, Subsection Ill.D.3.4, stated that the control room r

operators would be adeauately protected against the effects of accidental

release of toxic gases. The subsection referenced an evaluation of control 3

room habitability that was reported to the NRC in a BGE letter dated

December 30,1980.

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The December 30 letter to the NRC provided a control room habitability study

L as an attachment. The study stated in Section 2.8 that liquid ammonia was s

'

stored in 55 gallon drums,550 feet from the control r.,om intake. Further in

i Section 3.3 of the submittal, BGE stated that in the event of a drum f ailure, the

concentration of ammonia at the control room intake would be "30.0 ppm,

. much less that the ammonia toxicity limit of 50 ppm." BGE concluded in the -

i

evaluation that on site ammonia storage posed no hazard to control room

personnel.

The inspectors observed that ammonia was stored in a 5600 gallon container

outside of the north end of the Unit 1 turbine building, in the vicinity of the tank

storage area. The inspectors noted that UFSAR Figure 12,"Calvert Cliffs Site

. Plan " showed that morpholine was stored at the location where the inspectors

observed ammonia storage. BGE informed the inspectors that the 5600 gallon

polyethylene tank had been installed in the tank f arm in 1986. At that time,-

BGE did not complete an unreviewed safety question evaluation in accordance

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with 10 CFR 50.59. The inspectors observed that a BGE design checklist

accompanying the modification which installed the tank had been checked *Not

Applicable" for a review of the Final Safety Analysis Report. .

In 1996, because the existing storage tank had degraded from ultra violet

<

exposure, DGE initiated the replacement of the ammonia storage tank with an

upgraded 8500 gallon ammonia storage system. The new system included a

secondary spill containment, a localleak detection monitor, and a manifold for j

filling and venting the tank,

in preparation for the installation of the 8500 gallon system, BGE reviewed the

effects of onsite storage of ammonia for the 5600 gallon tank in June 1996. A .

BGE calculation completed at that time showed that the peak concentration of l

ammonia in the control room following a worst case spill of a 5000 gallon tank

containing 11 percent ammonia would be 137 pprn. A BGE engineer f amillar

with the calculation told the inspectors that the peak level of ammonia would

persist for about 30 minutes until the ammonia dissipated and that a number of

conservatisms remained in the evaluation. BGE reconclied the difference

between the 5000 0allon calculation and the actual 5600 gallon tank capacity

by stating that the existing tank was never filled above 3500 gallons.

The GGE control room habitability evaluation provided toxicity limits from the

Hazardous Chemicals Data Book (Weiss) of 100 ppm for 30 minutes exposures

and 500 ppm for 10 minute exposures. The Material Safety Data Sheet

provided by the ammonia supplier st sted that the immediate Danger to Life and

Health limit (IDLH) was 500 ppm 8"d specified respiratory protection using self-

contained breathing apparatus 'or longer term exposures at 250 ppm

concentration. Another reference, the Johnson Matthey Data Book, stated that

brief expuures to concentrations of 5000 ppm ammonia could be lethal. The

June 1996 BGE review concluded that ammonia at 137 ppm peak

concentration in the control room would not pose a toxic hazard following a

worst case spill.

1

The engineering service package for installation of the 8500 gallon tank had

been appro red for installation. However, the 10 CFR 50,59 screening report

that accompanied the service package did not evaluate applicability to UFSAR

Section 1.8 or Figure 12. Also, the engineering service package did not

provide for an ammonia tank leak detection alarm or ammonia concentration

readout instrumentation in the control room. The screening report answered

"No" to the question, "Will the proposed activity result in a change to the

safety analysis report description of the design, function, or method of

performing the function of any other structure, system, or component described

in the SAR?". The negative answer was based, in part, on the October 1996

control room habitability calculation, which concluded that a toxic hazard was

not created by the new tank. The screening report did not state that the

increase in the volume of the storage tank did not involve an unreviewed safety

question. The screening toport restated the conclusion of the June 1996

engineering calculation that the ammonium hydroxide solution would not

_ _ _ _ _ _ , _ , _ _ _ _ _ _ _ _ _ _ _ .

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constitute a toxicological hazard to the control room.

The inspector considered that the October 1996 review for installation of the

8500 gallon ammonia storage tank circumvented the 10 CFR 50.59 process.

'

Specifically, the December 30,1980 BGE letter to the NRC, described the

storage of 55 gallon drums of ammonia inside the Calvert Cliffs protected area.

The letter stated a control room peak concentration of 30.0 ppm ammonia and

stated a toxicity limit of 50 ppm. BGE justified not completing 10 CFR 50.59

reviews for the storage of increasing amounts of a hazardous material onsite

using the habitability calculations done in 19961n the screening reports. The

inspectors considered that the increasing amounts of ammonia introduced an

increasing hazard to contret room personnel, and that this hazard should have

been assessed in accordance with 10 CFR 50.59. Although the BGE

determination that the control room habitability remained viable, no specific

written safety evaluation had been completed to justify increasing amounts of

>

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ammonia in the storage location and UFSAR Figure 12 was never updated.

The failure to document a safety evaluation which provided the basis for

determining that the increasing amounts of ammonia stored within the Calvert

Cliffs protected area was not an unreviewed safety question, was a violation of

NRC requirements (VIO 50 317&318/97 06 01).

The inspector also reviewed preparations for an ammonia spill onsite. The

inspector noted there was no emergency procedure that specified actions for

prots ction of control room or other personnel in event of a toxic chemical spill.

No pli.ns had been specified for personnel evacuation or use of the breathing

apparat is for ammonia spills. BGE informed the inspector that a procedure for

i

combatir 1 a toxic chemical spill on site was under development. Failure to

have a procedure to combat a spill of toxic chemicals onsite, including

ammonia, was a violation of NRC requirements (VIO 50 317&318/97 06 02),

c. Conclusions

The inspectors found ' hat BGE had stored liquid ammonia since 1986 within

the protected area boundary without ensuring that the plant was fully prepared

for a potential spill of the storage tank contents. An evaluation of the need to

place control room ventilation in the recirculation mode and the need to have

the operators don respiratory protection had not been considered and

procedures for response to an ammonia spill had not been developed.

BGE had in 1986, increased the toxic material hazard from the on site storage

of ammonium hydroxide from 55 gallon drums to a 5600 gallon storage tank,

without completing a written safety evaluation. Further, BGE had approved

the replacement of the 5600 gallon tar'k with an 8500 gallon tank without a

written safety evaluation providing the basis that the change did not involve an

unreviewed safety question. Safety evaluation screening reports completed for

the tank installations, had not considered UFSAR Section 1.8, or UFSAR Figure

1 2. As a result, the UFSAR had not been updated.

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E2 Engineering Support of Facilities and Equipment

'

E2.1 Emeraency Diesel Generator Pioina Ooerability

a. Scope

The inspector reviewed BGE's actions and response to vendor identified

- concerns with welds on the emergency diesel generator lube oil and Jacket

water piping systems,

b. Findinas and Observations

in a preliminary 10 CFR Part 21 report, dated September 30,1997, the vendor ,

for the Calvert Cliffs 18,2A, and 2B emergency diesel generators (EDGs)

identified that a weld associated with the lube oil piping on a similar engine had

'

f ailed. The piping cracked at a partial penetration weld on piping that

experienced high vibration when the engine was running. The vendor noted

I that the root cause of this failure was undetermined and the analysis was

ongoing; however, the quality of the welds had been questioned.

, BGE had visually inspected the piping for evidence of leakage or cracking in

August 1997. Af ter the vendor notification was received, BGE personnel from

engineering and analntenance conducted additional visualinspections of each of

suspected welds on each of the engines. Vibration measurements were also

recorded.

Engineering developed an operability determination to support continued

operation of the EDGs. The operability evaluation noted that the available

industry and vendor information suggested that the weld f ailures were due to

high cycle fatigue. Based on the measured frequency of the piping and the

number of hours on the three opposed piston engines at Calvert Cliffs, BGE

engineering determined that a high cycle fatigue failure was unlikely. ,

'

Instructions have been issued for operations personnel to monitor the suspect

weld joints during engine operation. BGE planned to develop additional actions

in early 1998, based on recommendations from the EDG vendors' ongoing

investigation of this issue.

The inspectors noted that the vendor letter also identified that the jacket water

piping could be of concern and questioned why the operability determination

only addressed the lube oil piping. BGE stated that although there had been no

industry experience with failures in the jacket water cooling piping, the

operability determination would be revised to include this piping that was

addressed by the vendor preliminary report to the NRC.

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c. Conclusions

The inspectors concluded that BGE was taking appropriate actions to address

industry identified concerns with the f atigue of welds on the 18,2A, and 2B

emergency diesel generator lube oil and jacket water piping systems.

E8 Miscellaneous Engineering issues

E8.1 Aircraf t Fliaht Hazards

a. insoection Scoco

Recently, the inspectors noted two occasions of low flying aircraf t flights over

the Calvert Cliffs site. The inspectors also reviewed the applicable updated

final safety analysis report (UFSAR) and individual plant examination of external

events (IPEEE) sections related to the hazards from aircraft and discussed the

hazards with BGE personnel.

b. Findinas and Observations

The inspectors observed a large aircraft flying on a northwesterly course over

both containments at heights estimated to be less than 1000 feet on

September 17 and again on September 24. The inspectors notified BGE

management and this concern was entered into BGE's issue reporting system.

BGE personnelinformed the inspectors that the airspace over the plant was not

restricted. However, BGE contacted Patuxent River Naval Air Station (NAS).

The NAS personnel confirmed that pilots are trained to avoid flight directly over

the plant and indicated that they would reinforce these instructions in training

sessions.

UFSAR section 2.2.5.1 indicates that there are three airports within 11 miles of

the plant. The airport with the largest aircraf t and most flights is the Patuxent

River NAS. The UFSAR indicated that, during approach and departure using

instrument flight rules (IFR), the closest flight path would be seven miles from

the plant. During a review of the UFSAR in 1995, BGE identified that the flight

pattern data in the FSAR was outdated and current IFR flight paths would allow

flights over Calvert Cliffs ander certain circumstances. BGE initiated an issue

report into their corrective actions system that identified that a potential

unreviewed safety question had been identified as a result of the possible

increased probtbility of an accident. This issue report remained under BGE

review while the IPEEE was completed.

The IPEEE noted that flights over the plant were rare. The United States Navy

Airman's Information Manual directed pilots to avoid flyovers of the plant site

- and pilots from Patumt River were generally sent on three mile bypass loops

around the plant to avoid flyovers. However, three possible routes that fly over

the plant were iden4fied. An air traffic count provided by Patuxent River Naval

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17  ;

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Air Station identified that 214 flights used these routes within the past year. ]

This information was used to calculate a total frequency of an aircraf t crash ,

I

from Patuxent River NAS of 4.65x10E-9. BGE found that 74% of the total

probability of an air crash impacting vital structures comes from helicopter

operations which serve the Calvert Cliffs site. Subsequently, BGE established a

limit of six helicopter flights per year and has enforced this limit in their

contract with the vendor providing BGE helicopter services. Consequently, the

total aircraft crash and the related core damage frequene was determined to

be less than 1x10E 6. BGE personnelidentified that by .ie guidance in

NUREG 1407, Procedural and Submittal Guidance for 9 Individual Plant

Examination of external Events (IPEEE) for Severe * . ant Vulnerab iities, the

low probability of thit hazard did not warrant ca cu. ing a resulting core

damage frequency.

c. Conclusions

On infrequent occasions, aircraf t have been observed flying at low altitudes

over the Calvert Cliffs site. Based on the information provided by the

Calvert Cliffs IPEEE, the inspectors concluded that the recent flights over the

plant did not represent a significant safety hazard.

IV Plant SuDDort

R1 Radiological Protection and Chemistry (RP&C) Controls

R 1.1 The Radioloaical Environmental Monitorina Proaram

o. Insoection Scone (84750 2)

The following components of the radiological environmental monitoring program

(REMP) were inspected against technical specifications (TS) and the ODCM

(TS/ODCM) and NRC Regulatory Guide 4.1, " Programs for Monitoring

Radioactivity in the Environs of Nuclear Power Plants" to assess BGE

performance of the program:

- Sample collection from selected sampling locations;

- REMP procedures, the TS/ODCM, and UFSAR, including any changes

which pertained to REMP

- Revisions to the program implemented in 1997;

- Annual Reports of the REMP;

- Material condition of air sampling equipment t . automatic water

compositors relative to function, operability, and calibration;

- Thermoluminescent dosimeter (TLD) processing and handling;

- The land use census results; and

- Wind roses from the previous five years to asse:: any significant

changes since pre-operation to the present.

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b. Observations and Findinas

4

The inspector, accompanied by a BGE chemist responsible for implementation

and oversight of the REMP, visited selected sites where air samplerc, water

compositors, gardens, and TLDs were located. The inspector observed the

responsible personnel from BGE's contractor laboratory (Fort Smallwood)

exchange air particulate filters and charcoal canisters from the air samplers. The

inspector also discussed sampling techniques not observed, such as collection of

broad leaf vegetation, fish, soil and sediment. The observed air sampling '

equipment was well maintained and calibrated and the water compositor was

well maintained.

'

The intrector compared the sample locations in the ODCM with those in the

UFSAR and noted that the UFSAR, Section 2.9, Table 2 47 had not been

updatt J to reflect a footnote in the ODCM Table 3.121. The footnote *

, explained that cueln sample locations are not "in the general area of", "close

to", or "near the sita bi. 'ndary" for a direct radiation sample (DR1), an air

satapler (A1), and a food voduct location (Ib4, Ib5, Ib6), respectively. The

licensee was in the process if an UFSAR update and completed the 50.59

safety analysis during 'he I ,spection. The change appropriate to the REMP

program will be submitted to the NRC in November 1997. The inspector will

verify the change during a subsequent inspection. This is an inspection follow-

up item (IFl 50 317&318/97 08 03).

The inspector reviewed BGE Chemistry Procedure, CP 234, " Specification and

Surveillance for the Radiological Environmental Monitoring Program". The REMP

procedure contained appropriate steps for sampling, analysis, program

responsibilities and reporting requirements. The responsible personnel reviewed

the procedures for technical content, current practices, and requalification.

Procedure revisions were consistent with the current REMP changes.

The analytical results of samples from 1995 and 1996 (documented in the

annual reports) and from January through October 1997 were reviewed. The

inspector noted that the types and frequencies of analyses were performed as

required and the results showed no radiologicalincreases as a result of effluents

from the plant.

BGE replaced the TLD system for environmental monitoring with a more modern

system (Panasonic UD 814ASI)in September 1996. BGE performed the

. . comparison analysis of the previous and current dosimeter types for six months,

as required by ANSI N545 and Regulatory Guide 4.13. The inspector reviewed

the results and noted the results demonstrated no significant differences in the

two dosimeter types and met the ANSI criteria. The handling and processing of

the environmental TLDs were reviewed. The TLDs were analyzed by the

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chemistry unit of BGE's contractor laboratory, Fort Smallwood. The inspector

discussed with responsible personnel handling, processing, calibrating, and

maintaining the TLD reader and irradiator. Tiic inspector reviewed the

' associated procedures. The level of detail in the handling, processing, and

calibration of TLDs, provided assurance in the ambient radiation measurements

around the site.

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Tlio 1995 and 1996 annual reports of the REMP were reviewed to verify the

implementation of TS Section 6.6.2. The 1995 and 1996 annual reports

provided a comprehensive summary of the resu!!a of the REMP around the site i

and met the TS reporting requirements. No omissions, mistakes, or obvious

anomalous results and trends were noted.

The 1995,1996, and 1997 land use census were performed during August of

1995 and 1996, and June 1997 as required by the TS/ODCM. Performance of

the land use census was thorough and complete. No program changes (e.g.,

changes in sample locations) were required as a result of the census.

The inspector reviewed the wind direction assessments (wind roses) from the

past 10 years and compared them to the pre-operational wind roses to detect

changes,if any,in the prevailing wind directions. No significant changes were

evident. The environmental monitoring control station locations were reviewed

against the prevalent directions and the inspector noted that the control

locations remained valid in areas that are minimally impacted by the f acility,

c. Conclusion

Based on the above review, observation, and discussions, the inspector

determined the BGE performance in implementing the REMP continued to be

very good. The BGE sampling procedures contained appropriate information and

methods compared to industry standards and good practices. BGE

demonstrated a good working knowledge and understanding of the intent of the

REMP. Sampies were collected from the locations and frequencies specified by

the TS/ODCM.

R1.2 _Meteorotonical Monitorina Progu!m

a. Inspection Scope (84730 2)

The fohowing components of the meteorological monitoring program (MMP)

were inspected against TS, the UFSAR, and Regulatory Guide 1.23

commitmunts to assess the BGE performance of the program:

- Calibration procedures and methods;

- Calibration results of wind speed, wind direction and temperature sensors

and any related components;

- Operability and maintenance of instruments and equipment; and

- Modifications to the tower or associated instrumentation,

b. Observations and Findinns

The BGE Secondary System Engineering Department had responsibility to

calibrate and maintain the meteorological mmitoring instrumentation.

Calibrations of the wind speed, wind directio and temperature sensors were

conducted using the appropriate procedures. The inspector reviewed the

calibration results from 1995 through 1997. Calibration methods were

acceptable and the results were within the required equipment tolerances in the

-.- .- .. - - . - - - _ _ _ - - . _ . _ - - - -.. ----. . -- . -

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1

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20

procedures. The meteorologicalinstrumentation was calibrated at the  ;

semlannual frequency, as required by the TS. The physical condition of the

equipment appeared to be good. BGE maintained a preventive maintenance  ;

program to ensure equipment operability. Modifications to the tower and

associated instrumentation had been made since the previous inspection. The

modifications made included the addition of metal oxide varistors (varying

resistors) and surge protectors to reduce the effects of lightning strikes on the l

'

tower and instrumentation,

c. Conclusions

"

The inspector determined that overall, the BGE performance of maintaining and

.!

calibrating the meteorological m;,nitoring instrumentation was very good.

R1.3 Secondary Chemistry Control Imolementation Chanae j

a. lamection.Sagan

The inspectors reviewed changes to the BGE secondary chemistry control

program,

,

b. Findinas and Observations

'

'

On October 2, BGE implemented a change to the chemicals used in the

condensate and feedwater systems with the introduction of dimethylamine

(DMA) into these process streams (in Unit 1 only) to enhance corrosion control.

DMA is a low molecular weight organic amine which is highly volatile and has

been used successfully at several other nuclear plants for secondary chemistry

control. At a recent plant safety review committee meeting observed by the

inspectors, BGE engineers indicated that the primary benefits of DMA use would

be a further reduction in iron transport to the steam generators (S/G) and

lessened fouling of the secondary side of the S/G tubes. The engineers also

,

pointed out that DMA's reaction with copper alloys could result in an increase of

copper transport to the S/Gs, and copper is an aggressive corrosive towards S/G

'

tubes. The insoectors noted that committee members displayed a conservative

and questionir.g attitude, particularly regarding the safety aspects of DMA's

potentially deleterious effects.

The inspectors questioned whether personnel safety, including control room

operators, had been evaluated should a spill of DMA occur. BGE indicated that

,

a calculation (Calculation CA03489)had been performed which damonstrated

that the dilute concentration to be used (2%) was not a fire or toxicological

hazardi To further reduce the risk, only one 335 gallon container would be

permitted in the turbine building at any given time. The inspectors reviewed the

test procedure (ETP 97-067," Introduction of DMA mto Unit 1 Feedwater") and

'

the controlling chemistry procedure (CP 217, " Specifications and Surveillance:

Secondary Chemistry") and concluded that they contained, as appropriate,-

personnel safety precautions and warnings.

. _

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21

c. . Conclusions

The inspectors found that BGE had taken adequate precautions for a change in '

the chemical agents added to the Unit 1 secondary system.

R2 Status of RP&C Facilities and Equipment

a. Insoection Scopo

The inspectors reviewed the BGE programs for monitoring for personnel

contamination at the protected area boundary,

b. Observations and Findinas

BGE used portal monitors at both the entrance and exit to the protected area.

BGE told the inspector that the purpose of the monitoring was to ensure that

stray contamination was neither brought onto or taken from the site. The

inspectors were informed that contamination control for individuals working in

radiation areas in the plant was maintained either at the specific job site

boundary, at the exit to the auxiliary building, or both. BGE personnel stated

that the exit monitors at the protected area boundary served only as a backup

and not as a control point. The exit monitoring required a 10 second pause to

ensure effective dete: tion of radioactive material.

In 1997, BGE identified that some individuals were not pausing at the entrance

monitors in the Nuclear Office Facility (NOF). BGE conducted an assessment of

the effectiveness of the entrance and exit monitors and determined that a pause

should be required to monitor for contamination. To ensure that personnel acted

appropriately, BGE stationed radiation controls or security personnel at the

monitors until a high assurance of personnel compliance with the pause was

established. Additionally, both the entrance and exit monitors were posted that

a pause was required and the pause times were extended to ensure that a valid

count was completed. The inspectors observed that individuals entering the

plant properly paused until the radiation scan was complete. The inspectors

also observed that BGE posted a guard at the monitors during outage periods to

ensure that contractor personnel were aware of the pause requirements.

c. Conclusions

The inspectors concluded that the BGE monitoring and control of radioactive

material at both the entrence and exit to the plant protective areas was effective

for the intended purpose.

.

22

R3 RP&C Procedures and Docurnentation

R3.1 Launderina of Contaminated Clothina

a. Insoection Scope

The inspectors reviewed the BGE handling and re use of Anti Contamination

clothing (Anti Cs).

b. Findinos and Observations

in the 1996 Personnel Contamination Report, BGE identified that 21 personnel

contamination events had been attributed to contaminated re used Anti C

clothing. The report stated that this was an increase from 15 similar

occurrences in 1995. As a result, BGE specified that a self assessment of

contaminations from Anti C clothing would be conducted. The assessment,

which was completed in April 1997, identified a number of weaknesses in the

control of laundered anti-Cs, and recommended corrective actions. The

assessment concluded that the laundering process was adequate to prevent

significant skin contaminations from occurring (above the levelin which BGE

procedures required completion of a dose assessment). BGE changed the

vendor that provided laundry services et the end of March 1997. BGE informed

the inspector that no significant skin contaminations had occurred in 1995,

1996, or 1997.

The inspectors reviewed a BGE, August 1997 personnel contamination

summary, completed by radiation controls personnel. The report stated that 80

personnel contaminations had occurred in 1997 with 16 events attributed to

contaminated, re used anti Cs.

A personnel contamination was defined as greater than 100 counts per minute

above background on an individuals skin or clothing. A contamination was

normally detected during personnel monitoring at frisker stations on each level in

the auxiliary building or at the personnel contamination monitors at the exit to

the auxiliary building.

The inspector was informed that most used Anti C clothing was shipped to an

'

offsite vendor for cleaning. Upon return, five percent of the Anti-C clothis was

removed for contamination monitoring by BGE personnel. The remaining 95

percent were sont directly to the auxiliary building for use by plant personnel.

BGE stated that the monitoring was used to evaluate the effectiveness of the

vendor.

The inspector reviewed the results of laundry monitoring by BGE. An automated

detector system, with a limit of 25,000 decays per minute (dpm) or less to pass

the cloth!ng, was used to monitor individual pieces of clothing. Il levels above

25,000 dpm were observed, an alarm would sound and the pieces would be

- - - _ - _. .. .- - - - - - . - - - . - - . - - _ _ . - - _

.

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identified as contaminated. Pieces with contamination less that 25,000 dpm  !

were returned to the plant for general use. BGE informed the inspector that  !

25,000 dpm was equivalent to 5000 counts per minutes per 100 square j

.

l centimeters, which was equivalent to five times the BGE free release criteria of j

100 counts per minute with a 20 square centimeter hand held probe. BGE  ;

J considered less than 25,000 dpm of contamination on used clothing an i

acceptable risk for rt,diation workers wearing anti C clothing in the conduct of

radiation work.

I

A sample of monitoring results were reviewed by the inspector. On April 29,

'i

1997,84 hoods were tested and 2 failed, 563 cloth shoe covers were tested r

and 2 failed, and 78 coveralls were tested and 8 f ailed. On April 30,209 l

Jumbo rubber gloves were monitored and 59 gloves f ailed, and 189 extra large

totes were sampled and 113 failed. On May 17,20 large personnel clothing  ;

(PCS) were sampled, and 11 f ailed,73 red gloves were tested and 23 fnited, j

and 254 Kevlar gloves were tested and 4 failed. Oli August 26,130 hoods

were tested and 8 f ailed,60 green boots were tested and 7 failed, and 122  ;

!

cloth booties were tested and 2 f ailed. ,

The inspector found th:st BGE did not have criteria for increasing the sample size

or dispostioning laundry when a high failure rate of monitored clothing was

i observed. BGE informally used the data to assess the vendor. As seen in the

some shipments, a large fraction of clothing sampled was above the monitoring

limits. Therefore, some shipments would result in a higher likelihood that a

personnel contamination would result from contaminated anti C clothing. ,

,

Additionally, the amount of contamination observed on articles that failed the

'

monitoring was not assessed to determine if a personnel hazard existed or if the

'

BGE acceptance criteria for laundering of Anti Cs (no significant skin

contaminations) could be exceeded.

,

Although no significant skin contaminations had been observed, Anti C articles

that had been returned to Calvert Cliffs from the laundry vendor were at times

!. contaminated above the limits specified in the Calvert Cliffs procedure for

laundering of Anti C clothing. No procedure existed which specified actions to

i be taken when articles were found auove the monitoring limits, including criteria

i

'

for sample expansion, assessment of the contamination in excess of the limits,

and actions to ensure that laundered clothing contaminated above acceptable

limits was not made available for general use. The f ailure to develop and

implement a procedure for control of laundered contaminated clothing was a ,

violation of NRC requirements (VIO 50 317&318/97 06 04). ,

'

During the review of contamination events from Anti C clothing, the inspector

.

learned of an event that occurred on April 7,1997. The event was documented

l in an issue report and involved an individual with detectable skin contamination,

L - but at a level below the 100 counts per minute definition of a personnel

' contamination incides.t. BGE generated the issue report after determining that

'

the comamination was greater than 50 cpm but less that 100 cpm and had not

been documented in the personnel monitor alarm log.' The inspector was

l

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L

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. , . _ _ _ . _ . _ _ _ , _ _ . _ _ _ , . _ -_

.

.

24

successfully decontaminated. For this event, the inspector was informed that

because the auxilisry building monitors were 10 percent ef ficient for detection of

contamination, the individual may have indicated an uncorrected count of about

1640 decays per minute, that when divided by 10 for counter efficiency and

when the nominal outage background of 70 counts was subtracted, resulted in a

corrected count rate of about 94 cpm. Since the corrected count rate was less

than 100 creunts, it would not be a recordable personnel contamination event at

Calvert Chtfs. As a result, the inspector was concerned that the actual number

of problems resulting from poorly laundered anti-C clothing could be greater than

stated on the personnel contamination summary report. As noted above, an

issue report was written and BGE initiated changes to the personnel

contamination procedure to ensure that contamination events were properly

documented.

c. Conclusiong

BGE had not developed and implemented a procedure to prevent personnel

contaminations from occurring as a result of contaminated Anti C clothing.

Although no significant skin contaminations had been observed, Anti C articles

that had been returned to Calvert Cliffs from the laundry vendor, were at times

contaminated above the limits specified in the Calvert Cliffs procedure for

laundering of Anti C clothing. However no procedure existed which specified

actions to be taken when articles were found above the monitoring limits,

including criteria for sample expansion, assessment of the contamination in

excess of the limits, and actions to ensure that laundered clothing contaminated

above acceptable limits was not made available for general use.

The inspector found that some contamination events below the 100 count level

wete not documented in the personnel rnonitor log. Not documenting and

tracking these events was a poor practice and as a result, ths actual number of

problems resulting from poorly laundered anti C clothi 9 could be greater that

stated on the personnel contamination summary report.

R4 Staff Knowledge and Performance in RP&C

a. Srang (83729)

The inspectors performed a tour of Unit 1 containment and observed 118

raactor coolant pump seal replacement activities on September 16,1997. Also,

the inspector observed the initial containment entry following the reactor trip on

October 24,1997.

b. Qhiervations and Fip_ dings

Dui  : tour of the Unit 1 containment, high radiation area barriers were

revL sd and evaluated. These barriers consirted of ladder locks and locked

stairway door barricades that were substantial. In addition, during entry to

containment and also prior to entering the high radiation area locked door

_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ -

.

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25

leading to the reactor coolant pump area, radiation safety personnel verified

special work permit (SWP) authodzation, electronic dosimeter setpoints, and

worker knowledge of these setpoints prior to authorizing entry.

Af ter the old reactor coolant pump seal cartridge had been removed and placed

inside a storage canister, the radiation safety technicians (RSTs) conducted a

turnover. The on-coming RST received some information from the outgoing

RST. The on-coming RST was generally aware of the seal dose rates although

the beta radiation levels were not correctly passed along in the turnover. In

addition, the configuration of the seal stored inside a canister in the work area at

the time of the turnover had not been surveyed by the c r coming RST and no

turnover had been given on the canister dose rates. No instruction was provided

that this survey should be psrformed. Later, surveys revealed dose rates of 200

miem/hr on contact and 60 mrem /hr at 30 centimeters. This was a significant

radiation sourca on the work platform area (35 mrem /hr) which had not been

surveyed by tho responsible RST covering the workers. The oversight in

monitoring radiation levels at the work site was a significant weakness in high

radiation monitoring coverage of this job.

The inspectors observed good control and oversight to prevent foreign material

from entering the reactor coo: ant system during the pump seal replacement.

After the highly contaminated seal had been removed and placed inside the

storage canister, the work supervisor was observed handling the open canister

and spraying down the highly contaminated seal with water. This worker was

not wearing a set of water resistant protective clothing or a f ace shield as

required by Special Work Permit Number 802, task C. This doviation from the

SWP requirements was not stopped or corrected by the RST controlling the job.

Non-compliance with the SWP was a violation of the Calvert Cliffs Radiation

Safety Manual, Section 6.2.3.e (VIO 50-317&318/97-06-05).

During seal replacement activities, stationary low volume air samples were taken

at two different platform elevations. The air sample location on the pump seal ,

platform area was placed at the shroud circumference nearest to the platform

access ladder. The seal had been removed and rigged out from the opposite

  • le of the shroud from the air sample location. In addition, a small 250 CFM

. EPA unit was located on the opposite side from the air sample location

drawing the seal area air flow away from the air sample. No personallapel air

samplers had been provided for the workers on this job. The air sample results

indicated 2.124 derived air cencentration (DAC) and 0.04 DAC during seal

removal and inspection activit:es, respectively. Due to the air sample location

and questioning by the .nspectors, BGE determined that the sample location did

not represent the highest airborne radinctivity hazard in the work area. The

inspectors considered that the sampling location representec an inadequate

survey and was a violation of 10 CFR 20.1501 pursuant to 10 CFR 20.1204

(VIO 50-317&318/97-03-06).

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. _ _ . . . . _ _ . _ _ __. . -__ __ _

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26

Following the reactor trip that occurred on October 24, the inspectors observed

two RSTs making an initial entry into the Unit 1 containment for air sampling.

, - The inspectors observed that the RSTs wore no respiratory protection anrf had -

- their thermoluminescent detectors (TLDs) and other dosimetry inside of their

protective clothing (Anti Cs). The RSTs informed the inspector that they were

entering containment using Special Work Permit (SWP) Number 11C. Toe

inspector observed that the S'NP stated that "In the absence of Respiratory

Protection or Facial Anti Cs, the TLD is to be worn on the outside of the Anti-

Cs." The discrepancy was pointed out to the Radiation Controls Shift

'

Supervisor and the Radiation Controls Superintendent. Following the event in a

typed statement, the RSTs stated + hat they had not entered the Unit 1

containment because lighting was not available when the inner containment

door was opened. For this reason, BGE informed the inspector that a skin dose

assessment was not necessary. However, the SWP was applicable when the

workers crossed the boundary that leads into the containment building. Non-

compliance with the SWP was a violation of the Calvert Cliffs Radiation Safety

Manual, Section 6.2.3.e (VIO 50 317&318/97-06-07).

c. Conclusions

'Although the licensee has tightened the controls for access into high radiation

i areas, control of work within high radiation areas was weak. Several problems

were observed in work performance during reactor coolant pump seal

replacement activities. Specifically, insufficient radiation safety technician

turnover of radiological information, an improperly positioned air sampler, and an

improperly dress worker was not stopped or controlled by the job coverage

radiation safety technician. Two violations were cited involving failure to take-

suitable measurements of airborne radioactivity and failure to comply with the

requirements of the applicable SWP.

During the initial containment entry following the reactor trip on October 24,

two radiation safety technicians were observed by the NRC inspector making a

high radiation entry without fo: lowing the Special Work Permit requirement to

wear the TLD on the outside of the Anti-C clothing, with the beta window

exposed. This was an additional violation of NRC requirements.

R6 RP&C Organization and Administration

R6.1 Oraanization Chanaes and Responsibilities

.The inspector reviewed organization changes and the responsibilities relative

to oversight of the REMP and MMP. No changes in the organ!:ation regarding

the oversight of the REMP or MMP were made since the previous inspection

in this area. The responsibilities relative to oversight of the REMP and MMP

have essentially remained the same. The BGE Chemical Technical Services

Department has primary responsibility for conducting the radiological

environmental monitoring program aad the Secondary Systems Engineering

_

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27

Department has primary responsibility for maintaining the meteorological

monitoring tower. The Fossil Engineering and Maintenance Department

Chemistry Unit of BGE's contractor laboratory (Fort Smallwood) were

responsible for the sampling and analysis of environmental samples.

R7 Quality Assurance in RP&C Activities

R 7.1 Quality Assurance Audit Prooram

a, 'Insoection Scoce (84750 2)

The following quality assurance audits of the BGE radiological environmental

monitoring program were reviewed:

- 1995 QA Audit Report (Report No. 95 3); and

- 1996 QA Audit Report (Report No. 96-16).

b .- Observations and Findings

The audits were conducted by the Nuclear Performance Assessment

Department (NPAD), formerly the Nuclear Quality Assurance Department

(NOAD). The audits covered the radiological environmental monitoring

program and were conducted by the BGE NPAD staff with assistance from

other technical specialists, including a specialist from another utility. Both

audits concluded that the Chemistry Department implemented a very good

environmental monitoring program. Both audits identified findings. These

findings were of minor safety significance and were closed. The next audit

in this area will be performed in 1998.

c. Conclusions

Based on the review of the BGE audits and discussions with an auditor, the

inspector concluded that BGE effectively identified and assessed the

radiological monitoring program strengths and weaknesses. The audits

evaluated the technical adequacy of implementing procedures and TS and

ODCM requirements. Performance of the audits was thorough, objective,

and of very good quality.

R7.2 Quality Assurance of Analvtical Measurements

a, insoection Scoce (84750-2)

The inspector reviewed the quality assurance (QA) and quality control (OC)

programs of the licensee's Fort Smallwood analytical laboratory.

_-_ _

. . . .. . . . .

... .. . . .

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28

b. Observations and Findinos

The inspector reviewed the programs for QA and OC of analytical

measurements for radiological environmental samples to determine whether

the licensee had adequate control with respect to sampling, analyzing, and

evaluating data for the implementation of the REMP. The Fossil Engineering

and Maintenance Department (FF.MD) Chemistry Unit implemented an

interlaboratory comparison program, required by technical speciiscations, .

through continued participation with the Environmental Protection Agency

(EPA) drinking water program and a program prnvided by Analytics,

incorporated. The inspector reviewed the analytical results. The inspector

noted that the results of the quality control and interlaboratory programs

were within the established acceptance criteria. The RGE quality control

program consisted of measurements of duplicato and split samples. The

inspector reviewed the analytical results and ..oted that the results were

generally within the acceptance criteria. When discrepancies were found,

reasons for the discrepancies were investigated and resolved,

c. Conclusior

Based on the above observations, the inspector determined that the

performance of the laboratory analyses was excellent and the interlaboratory

comparisor, programs were effective. BGE had a good quality control

program with respect to sampling, analyzing, and evaluating data for

implementation of the REMP.

S8 Miscellaneous Security and Safeguards Activities

The inspector reviewed a BGE investigation concerning fitness for duty of a

small number of workers at the site. The NRC inspection included review of

documents and discussions with BGE personnel. None of the workers

involved in the investigation conducted work on safety systems. The

inspectors found that BGE had conducted a thorough review and had

properly dispositioned all concerns raised during the investigation.

,

F8 Miscellaneous Fire Protection issues

During the period, the inspectors conducted walkdowns of varicus fire

protection equipment, including fire hydrants, sprinkler piping, hose and

nozzle storage boxes, and emergency fire pumps. All of the equipment was

in good material condition and no problems were identified. The fire and

iafety personnel were well organized and knowledgeable about the fire

protection system (See M1.2), the fire protection procedures were clear and

easily implemented. The fire protection equipment was found in good

material condition.

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29

V. M_a.Lrm9emtqt Meetinas

X1 Exit Meeting Summary

During this intpection, periodic meetings were held with the plant general

manager and other station management to discuss inspection observations

and findings. Ori November 25,1997, are exit meeting was held to

summarize the conclusions of the inspection. BGE management in

'

attendance acknowledged the findings presented.

.

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ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

l E

P. Katz, Plant General Manager

K. Cellers, Superintendent, Nuclear Maintenance

K. Neitmann, Superintendent, Nuclear Operations

P. Chabot, Manager, Nuclear Engineering

T. Pritchett, Director, Nuclear Regulatory Matters

B. Watson, General Supervisor, Radiation Safety

C. Earls, General Supervisor, Chemistry

L. Gibbs, Director, Nuclear Security

T. Sydnor, General Supervisor, Plant Engineering

T. Forgette, Director - Emergency Preparednecs

M. Tonacci, Chemistry Supervisor

G. Barley, Senior Chemist

J. Carroll, PGM Alternate

B. Putman, NPAD Lead Assesscr

Fort Smahypod Laboratory

A. Kaupa, Senior Chemist

L. Bartol, Senior Chemist

R. Lassahn, Supervisor

NRQ

J. White, Chief, Radiation Safety Branch, DRS

INSPECTION PROCEDURES USED

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

IP 61726: Surveillance Observations

IP 37550: Engineering

IP 37551: Onsite Engineering

IP 71750: Plant Support Activities

IP 83750: Occupational Exposure

IP 92700: Followup of Written Reports of Events at Power Reactor Facilities

IP 92902: Followup - Engineering

IP 82701: Operational Status of the Emergency Preparedness Program

IP 83729: Occupational Exposures During Extended Outages

IP 84750: Radioactive Waste Treatment, and Environmental Monitoring

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- Attachment 1 2

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened.

50 317&318/97-06-01 VIO The failure to document a safety evaluation for

increasing amounts of ammonia in the protected

area

50-317&318/97-06-02 VIO Failure to have a procedure to combat a spill of

toxic chemicals onsite, including ammonia

50-317&318/97-06-03 IFl UFSAR not consistent with the ODCM, REMP

program to be changed.

50 317&318/97-06 04 V!O Failure to develop and implement a procedure for

control of laundered contaminated clothing.

-50 317&318/97-06-05 V.O Failure to follow SWP requirements during RCP

work.

50 317&318/97 06-06 VIO Sampling location represented an inadequate

i survey during RCP work.

50-317&318/97-06-07 VIO Failure to follow SWP requirements during

containment entry.

. Closed

50 317&318/95 10-01 URI - Training did not document individual operator

evaluations during requalification exam.

50-317&318/95-10-02 URI Training did not require attendance at all

requalification training se::sions. *

LIST OF ACRONYMS USED

CFR Code of Federal Regulations

DAC Derived Air Concentration (radiation limit)

dpm decays per minute (radiation)-

EOP-O Emergency Operating Procedure for Post Trip immediate Actions

EOP-1 Emergency Operating Procedure for Reactor Trip

EDG Emergancy Diesel Generator

IPEEE Individual Plant Examination for External Events

LCO Limiting Condition for Operation (Technical Specification)

-

mrem /hr rnillirem per hour

NAS Naval Air Station (Patauxent)

RCS, ~ Reactor Coolant System

RP&C 9adiation Protection and Chemistry

RST Radiation Safety Technician

SCBA Self-Contained Breathing Apparatus

a u aEa eA-

+

[*, l

1: ,

-

Attachment 1 3

SWP Special (radiation) Work Permit

UFSAR Updated Final Safety Analysis Report

MOV Motor Operated Valve <

LPSI - Low Pressure Safety injection

IR BGE issue Report

GA Quality Assurance

TLD Thermoluminescent Dosimeter

MMP . BGE Meteorological Monitoring Program

NPAD BGE Nuclear Performance Assessment Department

ODCM Offsite Dose Calculation Manual

REMP Radiological Environmental Monitoring Program

TS . Technical Specifications

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