ML20148R979

From kanterella
Jump to navigation Jump to search
Insp Repts 50-317/97-03 & 50-318/97-03 on 970413-0531. Violation Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20148R979
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 07/01/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20148R934 List:
References
50-317-97-03, 50-317-97-3, 50-318-97-03, 50-318-97-3, NUDOCS 9707080062
Download: ML20148R979 (32)


See also: IR 05000317/1997003

Text

. _ . . _ ._

_ _

__

_ _ _ _ . _ . . _

___._._._._m

.._

.. _ _ _ _ _ _ _ _ . .

__

i

'

,.

.s

P

'

i,

t

U.S. NUCLEAR REGULATORY COMMISSION

i

REGION I

,

1

i

4

.;

License Nos.

DPR-53/DPR-69

.

.

,

Report Nos.

50-317/97-03; 50-318/97-03

-i

Licensee:

Baltimore Gas and Electric Company

l

Post Office Box 1475

.

Baltimore, Maryland 21203

l

'

i

Facility:

Calvert Cliffs Nuclear Power Plant, Units 1 and 2

i

Location:

. Lusby, Maryland

Dates:

April 13,1997 through May 31,1997

' ' '

Inspectors:

J. Scott Stewart, Senior Resident inspector

Fred L. Bower lli, Resident inspector

Henry K. Lathrop, Resident inspector

, ,

2

Leonard J. Prividy, Senior Engineer, DRS

Jason Jang, Senior Radiation Specialist, DRS

Lonnie Eckert, Radiation Specialist, DRS

-

i

Approved by:

Lawrence T. Doerflein, Chief

l

Projects Branch 1

Division of Reactor Projects

!~

l

i

I

'

I

'

?

i

l

l

l

'

9707080062 970701

PDR

ADOCK 05000317

G

PM

-

.

.

EXECUTIVE SUMMARY

Calvert Cliffs Nuclear Power Plant, Units 1 and 2

Inspection Report Nos. 50-317/97-03 and 50-318/97-03

This integrated inspection report includes aspects of BGE operations, maintenance,

engineering, and plant support. The report covers a seven week period of resident

inspection and the results of specialist inspections in radioactive effluents and engineering.

Plant Operations

BGE identified that the 12 HPSI pump handswitch had been misaligned following

troubleshooting. This event was the third control switch mispositioning in the last year

that was not identified during initial shift turnover control board walkdowns. BGE

management indicated that actions were being taken to improve problem identification

during control board walkdowns.

The inspectors observed that the startup from the Unit 2 refueling outage was conducted

with a strong regard for nuclear safety. Good management oversight, pre-evolution briefs,

and excellent communications were evident during the startup and testing programs.

During a plant walkthrough, the inspectors identified that a lock on the suction isolation

valve for 11 auxiliary feedwater pump was configured so that the lock and chain could be

easily removed without need of the key. In response, BGE documented the problem and

conducted walkdowns of locked components throughout the plant to verify there were no

additional problems. The inspectors considered the problem to be an isolated occurrence

and the BGE response appropriate to the circumstances.

The inspectors observed the BGE response to a Unit 1 reactor coolant leak and found the

activities effective in diagnosing and mitigating the event. The plant shutdown was well

controlled and the leak was quickly isolated. Support activities including engineering,

radiation protection, and maintenance were excellent and ensured that there were no

complications during the event.

4

Maintenance

The implementation of the warehouse management system contributed to the reduction in

the delivery of incorrect or defective parts to maintenance job sites. One practice of re-

issuing parts returned from the field without a thorough inspection was weak and had the

potential to introduce degraded or defective parts in safety-related applications.

Enaineerina

Changing conditions, such as the fouling factors and fouling rates have continued to

challenge the operability of the service water system. The inspectors concluded that BGE

continues to be proactive in testing and engineering work related to the service water

system reliability. Until the scheduled replacement of the service water heat exchangers in

ii

.

..

.

-

.-.. .

- _ _ , -

- .-

..

-

- - - .

--

- .

'

.

.

Executive Summary (cont'd)

1998 (Unit 1) and 1999 (Unit 2), this proactive approach appeared commensurate with the

'

safety significance of the system.

,

'

Plant Suonort

BGE maintained and implemented a very good radioactive liquid and gaseous effluent

control program. Also, BGE implemented a good routine surveillance test program for plant

-

effluents.

Safety Assessment

A BGE effluent control program quality assurance audit was sufficient to effectively assess

the program. BGE implemented a very good quality control program to validate

measurement results for effluent samples.

The inspector found that the radiation protection department did not generate issue reports

for some worker concerns. The BGE practice of using gold cards to document some

procedure compliance and personnel safety concerns was considered poor and could

prevent timely resolution of the concern.

i

)

a

lii

.

l

TABLE OF CONTENTS

EX ECUTI VE S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . il

i

TAB L E O F CO NT ENT S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

i

Summ a ry of Pla nt Statu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. O p e r a t i o n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01

Conduct of Operatio ns . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 General Comments

1

.................................

01.2 12 HPSI Pump Handswitch Mispositioning . . . . . . . . . . . . . . . . . 2

01.3 Reactor Coolant Leak on Unit 1

3

........................

02

Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 4

02.1 Engineered Safety Feature System Walkdown

4

..............

11. M a i nt e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1

Conduct of Maintenance

4

..................................

M 1.1 Routine Maintenance Observations . . . . . . . . . . . . . . . . . . . . . . 4

M1.2 Routine Surveillance Observations . . . . . . . . . . . . . . . . . -. . . . . . 4

M1.3 Worker injured During Maintenance . . . . . . . . . . . . . . . . . . . . . . 5

M 1.4 Procurem e nt Prog ram . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M8

Miscellaneous Maintenance issues

7

...........................

M8.1 (Closed) LER 50-317/9 6-04-00 . . . . . . . . . . . . . . . . . . . . . . . . . 7

M8.2 (Closed) LER 050-317/96-03

8

1

..........................

111. Engineering

8

...................................................

E2

Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . . 8

E2.1

(Update) URI 50-317 &318/9 6-06-03 . . . . . . . . . . . . . . . . . . . . . 8

E8

Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

E8.1

(Closed) Unresolved item 50-317&318/94-24-02 . . . . . . . . . . . 10

I V . Pl a n t S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

R1

Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 12

R1.1 Implementation of the Radioactive Liquid and Gaseous Effluent

Control Program s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

R1.2 Implementation of the Effluent ALARA Program . . . . . . . . . . . . 13

R1.3 High Radiation Area Control Problems . . . . . . . . . . . . . . . . . . . 14

R2

Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 14

R2.1 Calibration of Effluent / Process Radiation Monitoring Systems

14

..

R2.2 Air Cleaning Systems and Plant Air Balance . . . . . . . . . . . . . . . 16

R2.3 Radiologically Controlled Area Access Control and Electronic

Dosim eters (8 3 7 5 0) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

R3

RP&C Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . 18

R5

Staff Training and Qualification in RP&C . . . . . . . . . . . . . . . . . . . . . . 19

R6

RP&C Organization and Administration

20

.......................

R7

Quality Assurance (QA) in RP&C Activities . .

20

..................

R7.1

Effluents and Chemistry Ouality Assurance

20

...............

iv

.

.

Table of Contents (cont'd)

R7.2 Radiation Protection Department Problem Reporting . . . . . . . . . 21

V. M a nageme nt Mee ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

X1

Exit Meeting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

X2

Review of UFSAR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

ATTACHMENTS

Attachment 1:

Partial List of Persons Contacted

Inspection Procedures Used

items Opened, Closed, and Discussed

List of Acronyms Used

,

i

i

I

i

v

..

-

. . _ _ . . _ _ . _ _ _ _ _ . _ - . . _ _ . . . _ _ . . . _ _ .

_ _ . _ _ _ _ . _ _ _ . ,

i

.

.

I-

.

, . .

1

Report Details

,

i .

Summarv of Plant Status

'

4

.

'

_ Unit 1 started the inspection period at full power and remained at full power until May 17,

when power was briefly reduced for condenser water box cleaning and main turbine valve

!

j .

testing. On May 29, the unit was shut down to repair a primary leak (See Section 01.3).

.

l

Unit 1 remained shutdown at the end of the inspection period.

I

!

Unit 2 began the inspection period shutdown in a refueling outage. Power operation

resumed on May 23 and full power was achieved on May 31,1997.

1. Operation 1

01

Conduct of Operations '

01.1 General Comments (71707)

Overall, the plant was operated safely. During a plant walkthrough on April 15, the

inspectors identified that a lock on the suction isolation valve for 11 auxiliary

feedwater pump was configured so that the lock and chain could be easily removed

without need of the key. The inspector informed control room personnel of the

discrepancy. Plant operators promptly responded, confirmed the inspector's

observation, and restored the lock to a secured position. BGE documented the

problem on an issue report and plant security was informed. There was no

indication of tampering and the valve was in its designated position. BGE

completed formal walkdowns of locked components throughout the plant and

.

verified that alllocked valves were in the correct position. BGE considered the

auxiliary feedwater valve discrepancy was due to an open link type chain and

{

initiated action to employ closed link chain for valve locking. The inspectors

.

considered the problem to be an isolated occurrence and the BGE response

l

appropriate to the circumstances.

The inspector observed portions of the Unit 2 startup from the refueling outage in

addition to the normal operating crew complement, a dedicated reactor operator and

senior reactor operator were assigned to focus on the control of the primary plant

during startup and low power physics testing. The inspectors observed that the

I

dilution to initial criticality was well coordinated and safely conducted by operations

personnel through the use of a detailed pre-evolution brief, three-point

communications, self-checking techniques, and peer verifications of control

manipulations. After a portion of the low' power testing was completed, the reactor

i

was taken sub-critical to perform a normal startup. During this startup and prior to

reaching the upper bounds of the estimated critical position limit, operations and

nuclear fuels personnel identified that the estimated critical rod position was

miscalculated due to uncertainties in the critical boron concentration measured

j

' Topical headings such as 01, M1, etc., are used in accordance with the NRC standardized

I

reactor inspection report outline found in MC 0610. Individual reports are not expected to

address all outline topics.

.

_. ._

_ . _ _ . _ _ _ _ _ _ . _ - _ _

_ _ _ _ _ . _ - _

- _ . . . _ . .

i.

i

t

..

,

!

2

j

during initial criticality. A more precise crstical boron concentration, although

f

available, was not used in the estimated critical position. The reactor remained

subcritical while an evaluation of the occurrence was completed. The estimated -

l

critical rod position' was recalculated using the more accurate measure of critical

boron ' concentration, and the reactor was taken critical within the limits of the

,

re-estimated critical position. Operations l management performed supervisory

observations and provided management oversight for these evolutions. The

!L

inspector concluded that the startup from the Unit 2 refueling outage was

!

!

conducted well.

01 2 12 HPSI Pumo Handswitch Mispositionino

a.

Scope

!

The inspectors reviewed the circumstances surrounding the mispositioning of the

j

12 high pressure safety injection (HPSI) pump handswitch.

~

b.

Findinas and Observations

-

~

On May 8, a BGE senior licensed operator identified that the standby 12 HPSI pump

i

'

was in the " auto" position versus its required " pull-to-lock" (PTL) position.' This

condition rendered the redundant 13 HPSl pump inoperable because the 13 pump

would not have automatically started on a safety injection actuation signal (SIAS).

Once discovered, the 12 HPSI pump handswitch was immediately restored to the

correct position. BGE also took corrective action to: perform breaker and valve

position verification surveillances; add additional switches, such as those that do

not alarm when taken out of their normal position to the turnover checklist; install

notes on the main control board concerning the required position on the 12 and

22 HPSI handswitches; and initiate a root cause analysis to fully evaluate.this

event.

Investigations by BGE personnel identified ;that the 12 HPSI handswitch had been

misaligned for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />, since the conclusion of troubleshooting that

placed the handswitch in the auto position. - At the time, the 13 HPSI pump was not

'~

declared inoperable, and Technical Specificttion Action Statement 3.5.2 had not

been entered. The 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed outage time for the Technical Specification

action statement was not exceeded.

The inspectors noted that this misalignment was not identified for approximately

14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />, including a shift turnover control board.walkdown. The misalignment

- was identified by an oncoming senior reactor operator during the control board

walkdown for the subsequent day shift (i.e., the second shift turnover after the

mispositioning occurred).

~ The inspectors were concerned that this event was the third control switch

mispositioning event within the past year that was missed during the shift

turnover control board walkdowns. The first mispositioning occurred in August

1996, when the 11 header emergency core cooling system (ECCS) room cooler fan

.

. - .

.-

. - . - .

_

,.

..

_

.

-

.

.

3

control handswitch was mispositioned after the 11 saltwater header was retumed

to service. This condition went undetected for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />. See

NRC Inspection Report 50 317&318/96-06. The second event occurred on

,

November 5,1996, when a loss of power to the flow instrumentation for service

>

l

water to the containment air coolers was identified during a control board walkdown

by an operations support person. This condition was undetected by control room

operators for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

c.

Conclusions

BGE identified that the 12 HPSI pump handswitch had been misaligned following

troubleshooting. The troubleshooting control form restoration directed the

handswitch be placed in the incorrect " auto" position. The inspectors were

concemed that this event was the third control switch mispositioning in the last

year that was not identified during the control board walkdowns conducted for

licensed operator shift tumover. The inspectors considered the missed opportunity

to identify the misposition handswitch a weakness in the tumover process.

01.3 Reactor Coolant Leak on Unit 1

a.

insoection Scoce

The inspectors assessed BGE response to a smallloss of reactor coolant event on

Unit 1.

b.

Findinas and Observations

On May 29, at 4:27 p.m. a thermal margin low pressure pretrip occurred and

reactor operators observed that one of four channels of pressurizer pressure had

failed low. Subsequently, pressurizer and volume control tank levels dropped

slightly, and containment humidity and radiation levels went up. Plant operators

quickly and correctly diagnosed the event as a loss of coolant event and entered

Abnormal Operating Procedure 2A, " Excessive Reactor Coolant Leskage," which

directed actions to isolate the leak.

BGE declared an Unusual Event at 4:50 p.m. due to reactor coolant leakage that

required unit shutdown. The estimated leak rate was approximately 10 gallons per

minute. The operators determined, using control room indications, that the leak

was on a 3/4 inch stainless steelinstrument line that supplied the pressurizer

pressure instrument. As the reactor was shutdown, a containment entry was made

and the leak was isolated. The Unusual Event was then term'nated at 8:05 p.m.

The NRC inspectors responded to the control room and observed the reactor

shutdown and BGE activities to control and mitigate the event. Procedures were

appropriately used and an ample contingent of operators and support personnel

,

were available to effectively complete the shutdown and leak isolation. There were

no complications to the event.

l

,

.

4

BGE determined the leak was due to a failed compression fitting on the pressurizer

pressure instrument sensing line. While a root cause determination was being

conducted, BGE inspected other compression fittings used on both units. At the

end of the inspection period, no leaking compression fittings were found, although a

number of fittings were tightened,

i

c.

Conclusions

The inspectors observed the BGE response to the Unit 1 reactor coolant leak and

found the activities effective in diagnosing and mitigating the event. The plant

shutdown was well controlled and the leak was quickly isolated. Support activities

including engineering, radiation protection, and maintenance were excellent and

ensured that there were no complications during the event.

O2

Operational Status of Facilities and Equipment

02.1 Enaineered Safetv Feature System Walkdown (71707)

The inspectors walked down accessible portions of the spent fuel pool cooling

system and determined that the system was properly aligned in accordance with the

operating procedures. Material condition 2nd housekeeping were good. Licensee

identified minor discrepancies were properly tagged. Several minor discrepancies

that were identified to the system engineer were promptly entered into the issue i

reporting system. The inspectors identified no substantive problems during the

system walkdown.

II. Maintenance

M1

Conduct of Maintenance

M 1.1 Routine Maintenance Observations (62707)

The inspector observed the conduct of maintenance and surveillance testing on

systems and components important to safety. The inspectors also reviewed

selected maintenance activities to assure that the work was performed safely and in

accordance with procedures. The inspectors noted that an appropriate level of

supervisory attention was given to the work depending on its priority and difficulty.

Maintenance activities reviewed included:

MO2199702954

Adjustment of Gain of Linear Range Nuclear instruments

MO2199604120

Replace 22A Reactor Coolant Pump Rotating Assembly

MO2199604119

Replace 21 A Reactor Coolant Pump Rotating Assembly

MOO 199701138

Replace OC Diesel Engine-Driven Fuel Oil Pump

M1.2 Routine Surveillance Observations (61726)

The inspector witnessed and reviewed selected surveillance tests to determine

whether approved procedures were in use, details were adequate, test

_.

.

.

_

..

_

_. _ _ _ _ _ .

__.

, _ .

.

.

.

5

,

instrumentation was calibrated and used, technical specifications were satisfied,

testing was performed by qualified personnel, and test results met acceptance

criteria or were appropriately dispositioned.

i

The surveillance testing was performed safely and in accordance with proper

)

procedures. The inspectors noted that an appropriate level of supervisory attention

was given to the testing depending on its sensitivity and difficulty. Surveillance

testing activities that were observed and reviewed included:

STP-047A

MSIV Partial Stroke Test

STP-M-212A

Channel A Reactor Protection System Functional Test

STP-M-571 C-2

Local Leak Rate Test, Penetrations 2A

(Letdown to Purif Demin),2B (RC Charging)

STP-M-471-2

Air Lock Operability and Local Leak Rate Test

,

STP-M-213-2 '

Calibration of Power Range Nuclear instruments by

Comparison with incore Nuclear Instruments

STP-O-5A-2

Auxiliary Feedwater System Quarterly Surveillance Test

M1.3 Worker Iniured Durina Maintenance

On May 7, a contracted worker was injured when an electric motor and gearbox

assembly weighing approximately 75 pounds, fell from its support and struck the

worker in the hard hat and shoulder. At the time, the individual was completing

repairs to an overhead rollup door serviced by the motor and gearbox. The

individual remained conscious following the accident and was transported to Calvert

Memorial Hospital by ambulance. Although the work was done in a radiologically

controlled area, no contamination was found on the worker in preparation for offsite

transport. BGE initiated an investigation of the occurrence.

M1.4 Procurement Proaram

a.

Inspection Scope (38701)

The inspector reviewed aspects of BGE's procurement program for the iscuence,

return and inspection of spare parts, and equipment staged for field implementation.

The inspection was in part the result of an apparent increasing trend in the delivery

to the field of incorrect or defective parts. Procurement management and

engineering personnel were interviewed to assess their knowledge of the issues, as

well as implemented or anticipated corrective actions.

b.

_ Observations and Findinas

in early 1996, BGE implemented a warehouse management system (WMS) to better

track the receipt storage, and disbursement of spare parts and material for plant

modifications. At that time, the inspectors were given a tour of the warehouse

facility and a demonstration of WMS performance. Based on a review of issue

reports generated in the latter part of 1996, the inspectors noted that there were

fewer reports describing the delivery of defective or incorrect parts than had

___

_

_

_

. .

__ _ . _ _ _

. .

_ _ _ _ . .

_.

..

-

.

'

6

historically been the case,-indicating that the WMS had been effective in improving

'

parts and material control performance. However, in the first quarter of 1997, and

particularly after the Unit 2 refueling outage began in mid-March, the inspectors

j

noticed a pronounced increase in the number of issue reports detailing the delivery

)

to the job site of incorrect or defective parts. in addition, several issue reports

indicated that in some instances, parts and material returned to the warehouse did

not conform to the original procurement documentation.

The inspector discussed the incorrect parts issue with procurement management,

who stated that there had been a site-wide program in 1996 to return both safety

and non safety-related parts and equipment to the warehouse. Returned items were

receipt inspected prior to being placed in stock. However, the inspectors noted that

the inspection was not always of sufficient rigM to identify deficiencies which might

not be immediately visible. In some cases, re'.urned items were then the first items

issued when needed in the field. The inspectors considered this practice to have

been weak with the potential to introduce degraded or defective components in

)

safety-related applications and whose condition might not be apparent during post-

maintenance or implementation testing. While root cause analyses for several of

j

the recent issue reports dealing with defective parts delivered to the jobsite were

pending, BGE stated that preliminary indications were that these parts had been

returned to the warehouse in 1996, but had not been noted as being degraded or

defective.

i

The inspector found several other apparent causes for delivery of incorrect parts,

i

Recently, BGE implemented a corporate-wide business information system (BIS)

which was to integrate allinformation-based data systems used at various BGE

locations. However, BIS did not interface effectively with the WMS in use at

Calvert Cliffs. In the meantime, several data bases used to control inventories had

been eliminated, causing a degradation in parts and material control. The inspectors

considered the length of time expended on resolving the BIS /WMS interface

compatibility problems to be excessive and was reflective of poor change

management by BGE.

The inspector reviewed a recently completed BGE audit (97-01) covering

.

procurement and materials management. The audit was of sufficient scope to

support the conclusion that the procurement program was generally effective in

procuring and controlling items and services. The audit did not reveal any safety-

significant weaknesses, although the effectiveness and timeliness of corrective

actions for some shelf-life and storage issues were noted to be unsatisfactory. The

inspectors discussed the results of the audit with procurement management, who

indicated that not all of the thirteen recommendations had been accepted,

specifically recommendations dealing with increased inspections and checks of

equipment where problems had not been identified to date. The inspectors

concluded that the rationale behind the rejection of several such recommendations

appeared reasonable.

,

__

. _ _ _ _ _ .

__

__

_

_ _ _ . _ _ . _ _ . .

m_

_ _ _ _ .

-.

i

.

i

!

7

l

-

. BGE procurement management outlined several initiatives undertaken in the last

l

fifteen months to strengthen the procurement process, including:

L

i

e

implementation'of the warehouse management system

_

i

l

Procedure enhancements to streamline and simplify procurement and

i

procurement engineering procet.ses

e

Procurement process training for interfacing engineers and planners

e

Enhancements to the commercial grade dedication program

,

The inspector considered these initiatives to reflect BGE's efforts to improve the

procurement process and address several long-standing deficiencies. An audit by

independent engineering personnel conducted in June 1997, indicated that some

improvements have resulted from these efforts with regard to safety-related parts

and equipment. However, the inspectors noted that neither the June 1997 audit

nor internal BGE procurement assessments addressed how effectively BGE managed

j

issues with non safety-related parts whose failure could affect safety-related

equipment. This was a weakness in BGE's procurement program which requires

additional management attention.

I

c.

Conclusions

.

The implementation of the warehouse management system contributed to the

reduction in the delivery of incorrect or defective parts to work sites. However, the

,

return of many spare parts from the field in 1996 may not have included adequate

'

receipt inspection prior to being replaced in stock. This problem may have

'

contributed to an increasing trend of improper deliveries noted in 1997. The

l

practice of re-issuing these parts was weak and had the potential to introduce

degraded or defective parts in safety-related applications where testing might not

,

reveal problems. The BIS /WMS interface difficulty was a problem with change

management.

M8

Miscelleneous Maintenance issues

!

M8.1 (Closed) LER 50-317/96-04-00 Two ASI Channels OOS Due to Reversed Nuclear

Instrumentation Leads

The Licensee Event Report (LER) described the discovery that the axial shape index

for Unit 1 Reactor Protective System Channels B and C were out of service due to

_ !

'

the reversal of the associated upper and lower linear range nuclear instrument

detector leads. The causes of this event were personnel error in not recognizing

j

changes to or the importance of detector labeling, and inadequate procedure

guidance to ensure proper cable connection. An opportunity to find the problem

,

was missed during the post-installation test. The leads were correctly reconnected

on August 2,1996. The inspectors verified the corrective actions stated in the LER

including: performance of root cause analyses, enhancement of the installation and

test procedure, and strengthening of related procurement documentation and receipt

inspection procedures. The LER was closed as a Non-Cited Violation in accordance

with Section Vll.B.1 of NUREG 1600, NRC Enforcement Policy. A related item

.

_

_

_

_

~

,

_ ,

.

.

8

(URI 50-317&318/96-06-02) that was unresolved pending completion of the BGE

root cause analyses was also closed.

M8.2 (Closed) LER 050-317/96-03: Discoverv of Holes in the Containment Sumo Screen

to Facilitate Field Run Tubina

The Licensee Event Report described the discovery of two approximately three inch

by six inch holes in the containment sump screens for Units 1 and 2. BGE stated

that the holes were likely field installed during initial plant construction and were

made to allow instrument tubing to pass into the sumps. Upon discovery, BGE

closed the holes by welding stainless steel plates over the openings. The inspectors

observed that the penetrations had been closed. After observing the holes and their

orientation, the inspectors concluded that the threat to the sump from material

passing through the holes was negligible. The BGE actions to identify and correct

,

the penetrations was appropriate. The LER is closed.

'

ill. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1

(Uodate) URI 50-317&318/96-06-03: Salt Water and Service Water Systems

1

Continued Ooerability

a.

Insoection Scone (37550)

The inspectors reviewed the BGE efforts to ensure service water system reliability

during summer Chesapeake Bay water temperatures.

1

b.

Findinos and Observations

In January 1996, while reviewing data collected to quantify the tube side (or micro-)

fouling factor, BGE determined that the equilibrium micro-fouling factor assumed in

the service water heat exchanger (SRWHX) thermal performance calculations was

too small. This issue was documented in NRC Inspection Report (IR)

50-317&318/96-01 and in Licensee Event Report (LER) 50-317/96-01.

'

Prior to this discovery, BGE design calculations had established the maximum

allowed Chesapeake Bay water temperature for service water subsystem operability

l

at 87.4 degrees Fahrenheit ( F). The fouling factor data indicated that to

continue to use the same rnicro-fouling factor and retain the same maximum

temperature limit, BGE would be required to clean the individual tubes in the

SRWHX every 14 days. BGE sought additional means to increase the design margin

of the SW and SRW systems and completed a 1996 bi-weekly cleaning schedule for

the SRWHX as bay temperatures rose above 70 F.

1

BGE sought to restore the lost design margin by replacing the fixed flow stops on

the containment air cooler (CAC) SRW inlet control valve actuators with flow

control devices. The intended finer control of SRW flow would remove uncertainty

J

__

_ - _ _ _ _ _ _ __ ... _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ . ..

1

i

-

1

,

l

!;: *

i

9

from the design calculations and therefore increase margin lost to the increase in

[

the micro-fouling factor. Since this modification involved an unreviewed safety

l

question, a license amendment was obtained from the NRC, and the modification

j

was installed in both units in 1996.

During surveillance testing in December 1996, the containment air cooler-service

,

water inlet control valves demonstrated unstable behavior. A temporary

l

modification was installed to disable the flow controllers and reinstall the

4

mechanical stops in the control valves until the instability of the flow controllers

could be resolved. The return to the mechanical stops was expected to reduce the

i

maximum allowable Chesapeake Bay water temperature by 2*F.

i.

BGE continued to collect additional fouling factor data using a single tube model of

the SRWHX called a side stream monitor. BGE reviewed this data and determined

,

l

that, although .the equilibrium micro-fouling factor remained the same, the time to

j

reach a' limiting micro-fouling factor was reduced from approximately 14 to

j

approximately 9 days,

j

'

'BGE determined that cleaning the SRWHXs on a frequency of every 9 days would

j

_

not be prudent. The related thermal performance calculations were being

j

recalculated using the equilibrium micro-fouling factor. Using the equilibrium micro-

fouling factor would provide an extended period of time between cleanings for

,

micro-fouling. Bay water inlet temperature, SRWHX differential pressure, and flow

]

,

through the SRWHX would continue to be monitored to determine when cleaning

-

was required for macro-fouling.

BGE considered several additional measures to increase the maximum allowable

inlet water temperature. Among the measures, BGE planned to quantify the

capacity of each of the normal service water pumps. Using the information

i

obtained from these tests in the thermal performance calculations was expected to

{

reduce the uncertainty in the calculations and increase the design margin. BGE's

preliminary estimate of the increase in margin is l'F.

BGE also considered throttling the SRW flow to the EDGs and making it a safety-

related function by the installation of a safety-related backup supply (nitrogen

accumulator) to the air operator for the EDG SRW control valve operator. Once

completed the maximum saltwater inlet temperature limits will be 88*F for 11 train

and 86*F for the 12,21, and 22 trains of cooling water. This modification is

j

scheduled for completion in July 1997.

'

Another option was to take one of the four containment air coolers out-of-service

and enter the related technical specification action statement when the salt water

maximum temperature limits were approached. Taking a containment air cooler out--

of-service was to reduce the amount of post-accident heat rejected to the SRW

I

header, and therefore, reduce the peak SRW header temperature below the EDG-

design limit of 105'F. BGE estimated that implementing this option could raise the

maximum inlet saltwater temperature for each train to as high as 90*F. BGE

continued to review the potential safety and regulatory impacts of this option.

'

.

10

BGE also stated that the final actions for increasing bay water temperature would be

included in a procedure upgrado and would receive review by the plant operational

safety review committee. The action plan would receive a 10 CFR 50.59 screen to

ensure that an unreviewed safety question was not involved.

l

c.

Conclusions

Changing conditions, such as the fouling factors and fouling rates on operability of

the service water system has continued to challenge BGE. The inspectors

concluded that BGE has continued to be proactive in testing and engineering work

related to the service water system reliability. Until the scheduled replacement of

the SRWHXs in 1998 (Unit 1) and 1999 (Unit 2), this proactive approach appears

commensurate with the safety significance of the system. However, NRC review of

the BGE action plan and operating procedures for high Chesapeake bay

temperatures will be necessary to close the unresolved item.

E8

Miscellaneous Engineering issues

.

E8.1

(Closed) Unresolved Item 50-317&318/94-24-02: Reactor Coolant Code Safety

Valve Performance issues

a.

Inspection Scone (92903)

The inspector reviewed the unresolved item which involved BGE's investigation into

the causes behind the seat leakage from the reactor coolant system (RCS) safety

valves (SRVs) 1-RV-200 and 1-RV-201, as well as potential discrepancies in the

procedures and facilities used to set / adjust the safety valve lift setpoint.

b.

Observations and Findinas

BGE determined that the seat leakage from the two safety relief valves in 1994 was

caused by unrelated circumstances. In the first case,1-RV-201 had been shipped

to a vendor for disassembly and inspection. The vendor found that the valve had

lifted prematurely in 1994 because the disc holder had been improperly staked,

allowing it to contact the lower adjusting ring. Steam leaking past the seat then

effectively worked against the seating force of the SRV spring, resulting in a lower

lifting point. Misalignment of the disc holder also caused internal damage to the

SRV such that it did not fully reseat following the original lift, resulting in the high

leak rate observed after the transient. The vendor concluded that the internal

damage would not have prevented the SRV from lifting again should pressure have

increased beyond the lift setpoint. BGE also performed an extensive root cause

analysis (RCA) and developed a number of corrective actions, including an

inspection of 1-RV-201 during the 1996 refueling outage which validated the

assumptions and corrective actions of the root cause analysis.

BGE also evaluated whether the deferral of the replacement of 1-RV-201 during the

1994 refueling outage contributed to the valve's leakage. BGE system engineering

concluded that the reasons for the deferral were sound, given the excellent

_._

-

.

11

!

performance of 1-RV-201 up to that point. Several SRVs had been in service for

fifteen years without notable problems prior to BGE's implementation of a routine

l

preventive maintenance program in 1991.

'

in the case of relief valve,1-RV-200 seat leakage, BGE engineering personnel noted

i

that several different SRVs in this position had leaked previously in .1984,1986 and

1992. Following extensive walkdowns and evaluations,' BGE engineers determined

that several SRV discharge piping supports (sway struts and spring hangers) were

either misaligned or improperly loaded, which, as the pressurizer expanded during

plant heatup, imparted a bending force to the SRV discharge nozzle, which distorted

the valve seat, allowing leakage to occur. BGE could not determine exactly when

the supports became misaligned, but suspected it may have occurred when the

pressurizer spray valves were relocated to the top of the pressurizer " dog house" in

the early 1980s. The piping supports were returned to their original configuration in

1

1994. Relief valve,1-RV-200 was inspected during the 1996 refueling outage and

,

there was no indication of seat leakage or piping stresses beyond design limits.

. BGE evaluated the causes behind the consistent setpoint difference between the as-

f

left at the laboratory and what was found after the valve was re-installed in the

'

plant. BGE determined that almost all of the difference was attributable to the use

of differing ternperature profiles BGE's profile used data gathered over the previous-

!

three years, while the laboratory profile used original construction data which had

not been updated. Some minor enhancements to the Hydroset test procedure

accounted for the remaining difference. The laboratory profiles were updated and

BGE engineers validated these conclusions during the Unit 2 refueling outage in-

1995.

c.

Conclusions

BGE's root cause analyses for the problems with 1-RV-200 and -201 in 1994 were

comprehensive and very thorough. Given that in both cases there were significant

raw data lapses due to unrelated equipment performance issues, the inspectors-

noted that BGE engineering personnel paid special attention to the validation of their

assumptions and the effectiveness of their corrective actions. The inspectors

concluded that BGE's actions were effective, as demonstrated by satisfactory SRV

performance since July 1994, including no recurrence of seat leakage. This item is

therefore closed.

. ..

.

. -

___

-

- _ =

. -

- . - . .

._

__

- . _ .

.

i

-12

IV. Plant Support

4

R1

Radiological Protection and Chemistry (RP&C) Controls

R1.1 Imolementation of the Radioactive Liould and Gaseous Effluent Control Proarams

)

a.

Insoection Scope (84750)

The inspection consisted of: a tour of radioactive liquid and gaseous effluent

pathways and the BGE process facilities, and control room; a review of radioactive

liquid and gaseous effluent release permits; a review of unplanned or unmonitored

i

release pathways; and review of the quantification technique for the airborne tritium

i

release.

b.

Ohservations and Findinos

The inspector toured the control room radiation monitoring station and selected

radioactive liquid and gas processing facilities and equipr.1ent, including effluent

radiation monitors and air cleaning systems. All equipment was operable at the

time of the tour. Effluent / process / area radiation monitors were also operable with

the exception of Unit 2 main steam line monitors which were being calibrated.

During review of selected radioactive liquid and gaseous effluent discharge permits,

the inspector determined that discharge permits were complete and met the

Technical Specification /Offsite Dose Calculation Manual (TS/ODCM) requirements

for sampling and analyses at the frequencies and lower limits of detection

established in the TS/ODCM.

The inspector also noted that there were no unplanned /unmonitored radioactive

liquid and gas releases since the previous inspection conducted in February 1996.

The inspectors noted that BGE had reviewed the effluent control programs relative

to IE Bulletin No. 80-10, " Contamination of Nonradioactive System and Resulting

Potential for Unmonitored, Uncontrolled Release of Radioactivity to Environment."

The inspector requested BGE demonstrate the capability for monitoring and

quantifying airborne tritium. BGE calculated the total amount of water loss from

the spent fuel pool (SFP). BGE assumed that water loss was due to evaporation

from the SFP released to the environment via the plant vent. BGE calculated the

airborne tritium released using SFP tritium measurement results. Calculated

airborne tritium released through the plant vent during the second half of 1996

was 1.16 curies. BGE reported, in the second half of 1996, " Semiannual Effluent

Report," that 1.49 curies of airborne tritium was released. The inspector

determined that BGE's assumptions and calculation methodologies were effective in

monitoring and quantifying airborne tritium releases.

__

_

_

.

.

13

c.

Conclusions

Based on the above reviews, the inspector determined that BGE maintained and

implemented very good radioactive liquid and gaseous effluent control programs.

i

R1.2 Imolementation of the Effluent ALARA Proaram

a.

Insoection Scone (84750-01)

The chemistry department implemented the Chemistry Business Plan in February

1996 and the effluent ALARA program was a major part of this plan. During this

inspection, the inspector reviewed: (1) comparisons between projected radioactive

liquid and gaseous releases and actual releases during 1996; (2) participation of

other supporting groups (e.g., HP, l&C, system engineers, and operations) to the

program; (3) communicstion; and (4) safety focus.

j

b.

Observations and Findinas

i

The projected tota! smount of radioactive liquid and gaseous effluents released

during 1996 were 214 millicuries and 80 curies, respectively. The 1996 actual

'

releases of liquid and gaseous effluents were 220 millicuries and 77.4 curies,

respectively, indicating that BGE was effective in monitoring and controlling effluent

releases.

Participation of other supporting groups (i.e., staff from operations, maintenance,

engineering, and radiation control departments) to support the effluent ALARA

program was good. For example, chemistry and engineering / technical staff made .

efforts to optimize system performance to reduce the radioactive liquid and gaseous

effluent releases to the environment. The inspector also noted that management

supported the effluent ALARA program and efforts to minimize radiological releases

to the environment.

Good communications between the chemistry staff and other supporting groups

(operations, maintenance, engineering, and radiation control) were noted. The

chemistry organization also provided technical training to other organizations. For

example, training topics for the control room operators were: (1) secondary

chemistry, including S/G corrosion; (2) implementation of the ODCM; (3) outage

chemistry, including reactor coolant system degasification, and liquid and gaseous

waste controls; and (4) primary chemistry principles. A similar training program

was developed by the chemistry staff for engineering / technical initial training and

system engineering training,

c.

Conclusions

Based on the above reviews, the inspector determined that BGE maintained and

implemented a very good effluent ALARA program.

.

.

14

R1.3 Hiah Radiation Area Control Problems

On May 1,1997, BGE identified that an electrician had entered the Unit 2

containment and had worked for over one hour m a locked high radiation area

without the required dosimetry. The individual had entered the radiologically

controlled area with the proper dosimetry for the job, but had removed the

dosimetry during dressout for the containment entry. Subsequently, the individual

entered the containment with no dosimetry. About an hour later, another BGE

employee saw the dosimetry and reported the finding to radiation controls

personnel. The electrician was informed and immediately directed out of the

radiation area.

On May 4,1997, BGE identified that during the construction of scaffolding in

the radiologically controlled area, a high radiation area was inadvertently

entered. As individuals constructed the third tier of the scaffolding, the worker's

electronic personnel dosimeters alarmed. The individuals irnmediately informed

radiation controls personnel, a survey was performed, and a maximum dose rate of

300 mrem per hour was found. The area had not been previously surveyed. Work

was stopped until an evaluation was completed.

BGE discussed these events with NRC personnel on May 1 and May 5,1997.

Subsequently, BGE documented the occurrences and corrective actions taken in a

letter to NRC Region I, dated May 9,1997. These events were also discussed at a

predecisional enforcement conference held on June 12,1997. Since the two

events involved non-compliance with BGE procedures for control of high radiation

area access, and were additional examples of recent high radiation area control

problems, they were considered apparent violations of NRC requirements.

Enforcement action for the two events will be addressed in a separate

correspondence.

R2

Status of RP&C Facilities and Equipment

R2.1 Calibration of Effluent / Process Radiation Monitorina Systems

a.

insoection Scone (84750)

The inspector reviewed: (1) the most recent calibration results for the following

selected effluent / process / area radiation monitoring systems and their system flow

rates; (2) an RMS self-assessment; and (3) the quarterly trending reports.

Liquid Radwaste Effluent Monitor (Common)

Liquid Radwaste Effluent Line Flow Rate Measuring Device

Steam Generator Blowdown Radiation Monitors (Units 1 and 2)

Steam Generator Blowdown Line Flow Rate Measuring Device

Main Steam Line Monitors (Units 1 and 2)

Main / Plant Vents Noble Gas Monitors (Units 1 and 2)

Wide Range Noble Gas Monitors (Units 1 and 2)

Waste Gas Discharge Noble Gas Monitor (Common)

-

-

- ..- - _ .. . - . . . - - _ - - . - - - - . . - - - .

_ . . - .

I

.

I

,i

..

.

4 '*

,

15

!-

]

e

Waste Gas Effluent System Flow Rate Measuring Device

o

. Containment Purge Radiation Monitors (Units 1 and 2)

Condenser Air Evacuators Discharge Monitors (Units 1 and 2)

..

{

e

Containment Area High Range Monitors (Units 1 and 2)

!

Spent Fuel Pool Platform Area Monitor (Common)

e

Access Control Area Vent Monitor (Common)

e

Control Room Vent Gaseous Monitor (Common)

i

l

b.

Observations and Findinas

!

.

[

The instrumentation and controls department had the responsibility to perform

i

electronic and radiological calibrations for the above radiation monitors. The

i

!

system engineer had the responsibility to trend and track the above RMS. All

.

reviewed calibration results were within BGE's acceptance criteria, with the

!

!

exception of Unit 2 main steam line monitors which were_ newly installed and were

j

.being calibrated. Calibration results will be reviewed during a subsequent

'

inspection.

l

' During the review of the above RMS calibration documentation, the inspector

)

.

independently calculated and compared several calibration results, including linearity

j

-

"

tests and conversion factors. The inspector determined that BGE's results were

comparable to the independent calculations.

)

BGE applied very good calibration methodologies for the above area radiation

i

monitoring systems, including radiological and electronic calibrations. Alarm -

setpoint calculation methodologies were good. Calibration procedures were detailed

and easy to follow.

The inspector also reviewed RMS assessment and quarterly trending reports that

were prepared by the RMS system manager. The RMS system manager assessed

the system availability using a tracking system (e.g.,99.5% availability of the

Unit.2 wide range gas monitor during 1996). The inspectors determined that the

RMS . system manager and engineer provided focus and attention in the areas of:

)

(1) RMS upgrade project; (2) RMS system improvement project; (3) trending

analyses for conversion factors and linearities; and (4) follow-up'on the progress of

modifications.

i

c.

Conclusions

Based on the above reviews, the inspector determined that BGE maintained and

implemented good calibration and assessment / trending programs for

effluent / process / area radiation monitoring systems.

)

-

--

. - -

- . - . - .

-.

. .

.

.,

-

- -.,

-

,

- .,

.

.

16

R2.2 Air Cleanina Systems and Plant Air Balance

a.

Insoection Scope (84750)

The inspector reviewed BGE's most recent surveillance test results (visual

inspection, in-place HEPA and charcoal filter leak tests, air capacity / pressure drop

tests, and laboratory tests for the iodine collection efficiencies) for the following

systems:

Control Room Emergency Air Supply Systems,

Spent Fuel Handling Building,

Penetration Room Exhaust System,

Containment Building, and

ECCS Pump Room Exhaust System.

The inspectors reviewed the plant air balance for the following facilities as described

in Section 9.8.2.3 of the UFSAR:

Positive pressure for the Control Room,

Negative pressure for the Waste Processing Area, and

Negative pressure for the Spent Fuel Pool Ventilation.

b.

Observations and Findinas

All reviewed surneillance test results were within Calvert Cliffs technical

specification acceptance criteria. During discussions with the responsible individual,

the inspector noted that the individual had very good knowledge not only for

technical specification requirements, but also for standard industry practices. As

noted in inspection report no. 50-317/96-02 and 50-318/96-02, BGE previously

identified a weakness concerning the test temperature (130*C) for the iodine

collection efficiency test as specified by the TS As a result, BGE tests the charcoal

filter system at both 130 C and 30 C. The inspector determined that BGE

maintained and implemented a good routine surveillance test program.

Maintaining positive and negative pressures for the above systems appeared to be

acceptable, however, there were no pressure differences in the measurement

devices for the above f acilities. BGE verified appropriate positive / negative pressures

by periodic smoke testing. The inspector noted that periodic smoke testing to verify

positive / negative pressures for the above facilities was difficult because there were

different ventilation system configurations. BGE was considering the installation of

differential pressure gauges for the above systems.

)

!

BGE submitted a Licensee Event Report (50-318/97-001) to the NRC regarding the

air balance between the Spent Fuel Pool (SFP) area and the auxiliary building while

fuel was being moved in the SFP. There were no differential pressure measurement

!

devices for the SFP and auxiliary building, and BGE did not identify air flow

direction. Pressure of the auxiliary building was more strongly negative than that of

the SFP, therefore, the air from the SFP leaked into the auxiliary building. The

)

.

'

,

17

inspector noted that air in the SFP was required to pass through the SFP ventilation

system (charcoal and HEPA filters) in the event of a fuel handling accident.

BGE stated in the LER that procedures were being revised to ensure that the SFP

ventilation remained operable when auxiliary building ventilation lineup changes

were made,

c.

Conclusions

Based on the above reviews, the inspector determined that BGE maintained and

implemented a good routine surveillance test program. The responsible individual

for ventilation had very good knowledge not only for technical specification

requirements, but also for standard industry practices. BGE implemented action to

ensure that ventilation system configuration changes did not affect ventilation

design.

R2.3 Radioloaically Controlled Area Access Control and Electronic Dosimeters (83750)

a.

Inspection Scope

The BGE Radiologically Controlled Area (RCA) access control and electronic

personal dosimeter (EPD) system was evaluated through discussions with radiation

protection staff and the following documents:

Enhanced Radiation Worker Training, General Orientation Training (GOT)

Lesson Plan GOT-337-9, Revision 1, January 15,1997

GOT Annual Requalification, Lesson Plan GOT-337-27R, Revision 5

GOT Initial Training, Lesson Plan GOT-337-27, Revision 11

IR1 -019-441, Issue Report, Improper RCA Entry, April 29,1997

First Quarter 1997 Exposure Evaluation Reports

First Quarter Thermoluminescent Dosimeters (TLDs)/EPD Error Evaluation

Reports

Second Quarter 1997 Exposure Evaluation Reports

First Quarter 1997 EPD Loss / Failure Reports

Second Quarter 1997 EPD Loss / Failure Reports

b.

Observations and Findinas

The inspector found that GOT training emphasized how to properly use the

EPD/ access control system. The GOT initial test evaluated worker knowledge on

EPD access control. GOT requalification tests asked several questions regarding

RCA access control.

BGE informed the inspector that TLDs were the device of record used to measure

dose. BGE stated that EPDs were used as a control device only. NRC regulation

10 CFR 20.1501(c)(1) required that processed dosimeters used to comply with

10 CFR 20.1201 were required to be National Voluntary Laboratory Accreditation

Program (NVLAP) accredited. The BGE TLD program was accredited by NVLAP.

.

.

18

The inspector noted that TLD results demonstrated that worker exposures have

been well within the federal regulatory limit of five rem in a year.

The inspector found that BGE programmed the EPD/ access control system to

'

provide both visual (CRT monitor) and audio (computer soundboard) warnings if the

EPD was removed prior to completing the log-in access transaction. While it was

possible for an individual to remove an EPD prior to the completion of the access

transaction, visual and audible alarms sounded. An individual would have to ignore

these wamings that RCA access had not been granted.

l

Several cases were identified by BGE in which a worker received an error message

upon exiting the RCA. BGE investigation into these cases indicated that the worker

had failed to check the EPD for the HPID# (a self-check to insure that the electronic

transaction was succest.ful). The inspector reviewed one issue Report detailing an

.

'

event in which a worker entered the RCA without having properly completed the

Real Time Exposure Management System (REMS) log-in. The issue Report was

generated on April 29,1997, and the accompanying REMS transaction log indicated

that the EPD had been removed prior to completion of the sign-in.

The inspector reviewed several EPD failure reports. The inspector assessed that the

actions ar.d assumptions taken by BGE to evaluate worker doses in these cases of

lost or failed EPDs were reasonable (worker doses were evaluated and tracked as a

temporary control measure until TLD results were acquired). The inspector found

that individuals who failed to make proper RCA entries had received disciplinary

action.

c.

Conclusions

No issues other than some human performance problems were noted regarding the

electronic access control and electronic dosimeter system. BGE reviewed cases in

which EPDs were lost, failed, or provided anomalous readings. The actions taken

and the assumptions made in these cases were reasonable.

R3

RP&C Procedures and Documentation

a.

Inspection Scope (845'70)

The inspection consisted of: (1) review of selected chemistry procedures to

determine whether BGE could implement the routine radioactive liquid and gaseous

effluent control programs and the emergency operations; (2) review of 1995 and

1996 Semiannual Radioactive Effluent Reports to verify the implementation of TS

requirements; and (3) review of the contents of the ODCM for performing the

effluent control programs, including methodologies for calculating projected dose to

the public.

.

19

b.

Observations and Findinas

The inspector noted that effluent control procedures were detailed, easy to follow,

and ODCM requirements were incorporated into the appropriate procedures. BGE

had good procedures to satisfy the TS/ODCM requirements for routine and

emergency operations.

The inspector reviewed the 1995 and 1996 Semiannual Radioactive Effluent

Release Reports. These reports provided data indicating total radioactivity released

for liquid and gaseous effluents. The annual reports also summarized the

assessment of the projected maximum individual and population doses resulting

from routine radioactive airborne and liquid effluents. Projected doses to the public

were well below the Technical Specification (TS) limits. The inspector determined

that there were no anomalous measurements, omissions, or adverse trends in the

reports.

The ODCM provided descriptions of the sampling and analysis programs, which are

established for quantifying radioactive liquid and gaseous effluent concentrations,

ar;d for calculating projected doses to the public. Methods for establishing effluent

radiation monitor setpoints were listed in the ODCM. BGE adopted other necessary

parameters from Regulatory Guide 1.109.

c.

Conclusions

Based on the above reviews, the inspector made the following deterrninations:

e

effluent control procedures were sufficiently detailed to facilitate

performance of all necessary steps for routine and emergency operations,

e

BGE effectively implemented the TS/ODCM requirements for reporting

effluent releases and projected doses to the public, and

BGE's ODCM contained sufficient specification, information, and instruction

to acceptably implement and maintain the radioactive liquid and gaseous

effluent control programs.

R5

Staff Training and Qualification in RP&C

The inspection consisted of: (1) discussions with a chemistry training instructor,

(2) a review of the training manuals, and (3) a review of chemistry technicians

training records,

The inspector reviewed a selected portion of the chemistry training manual for the

chemistry technicians. The training manual contained good information about

chemistry laboratory techniques and appropriate learning objectives and training

sequences. The chemistry training instructor stated that the expectation was that

the trainees were to clearly understand the importance of each laboratory analytical

step and effectively perform the requirement. The annual training and as-needed

-~.

---

!

j

-

i

'

j

r ..

1

a

20

a

training (on-the-job) were required as part of the training. The passing grade was

80%. The inspector also reviewed the training records for chemistry technicians

,

l

and verified that the training requirements were met.

'

!

Based on the above review and discussions, the inspector determined that the

training department implemented an effective training program for chem!Mry

"

technicians.

R8

RP&C Organization and Administration

,

The inspector reviewed the organization and administration of the radioactive liquid

and gaseous effluent control programs and discussed changes made since the last

inspection, conducted in February 1996.'

There were no program changes since the last inspection. The chemistry

department had the major responsibility to conduct the effluent control programs.-

Other groups (i.e., radiation controls, operations, l&C, and system engineers) had

supporting responsibilities to the program. Staffing levels appeared to be

appropriate for the conduct of routine and emergency operations.

R7.

Quality Assurance (QA)in RP&C Activities

R7.1

Effluents and Chemistry Quality Assurance

a.

Inspection Scope (84750)

The inspection consisted of: (1) review of the 1996 audit and its responses; (2) QA

'

policy of the measurement laboratory; and (3) implementation of the measurement

laboratory QC program for radioactive liquid and gaseous effluent samples.

b.

Observations and Findinas

The inspector reviewed QA audit report No. 96-16, " Chemistry." The inspector

q

noted that the audit team also included other technical personnel. The 1996 audit

'

team identified one finding. The finding was not safety-related, but rather

recommended an enhancement to the effluent control programs. The response to

this finding was completed in a timely manner. The inspector noted that the scope

and technical depth of the audit was sufficient to assess the quality of the.

radioactive liquid and gaseous effluent control programs.

BGE maintained a good QA policy and implemented the policy throughout the

chemistry department, including analytical measurement laboratory. The inspector

reviewed the QC data for intra /interlaboratory comparisons. When discrepancies

'

were found, effective resolutions were determined and implemented.

i

.

i

i

!

.

l

21

i

c.

Conclusions

i

Based on the above reviews, the inspector determined that BGE's OA audit was

sufficient to effectively assess the radioactive liquid and gaseous effluent control

j

programs. BGE implemented a very good QA/QC program to validate measurement

results for effluent samples.

R7.2 Radiation Protection Department Problem Reportina

a.

Inspection Scooe

The inspector reviewed problem reporting activities in the Calvert Cliffs radiation

protection department,

b.

Findinas and Observations

i

'

A number of BGE and contractor radiation protection technicians were asked how

problems were reported and the receptiveness of BGE management to problem

reports. All of the selected individuals stated that issues were documented on gold

cards, which were available at the radiation protection control desk. Issue reports

were typically only initiated by supervisors after reviewing the gold cards. Of the

individuals interviewed, some stated that supervision was generally receptive to

worker concerns and would take appropriate action to resolve concerns when

identified. However, some workers stated that concerns sometimes were not

promptly answered.

Ar, followup to the worker concerns, the inspector reviewed gold cards collected

during the Unit 2 outage to determine if identified deficiencies were being

dispositioned in accordance with BGE policy and procedures. Approximately

200 gold cards were reviewed. The inspector found that most issues were

appropriate for gold card documentation, such as good performance by technicians

in the field or suggestions for process improvements. All of the gold cards had

been reviewed by supervisory and management personnel in the radiation protec'. ion

department. Most of the gold cards had not been entered into radiation protection

'

department computer based trending system. The filing and entering into the

tracking system was in progress at the time of the inspection. A number of gold

cards identified procedure or process deficiencies and these were upgraded to issue

reports by the reviewing supervisor. Issues in this group included:

-

On April 5, a small spill of potentially contaminated water from a tank truck

occurred due to an improper valve lineup.

-

On April 10, an air sampler was found out-of-calibration. The sampler had

been used four times prior to identification of the problem.

The inspector found one gold card that identified a personnel safety issues that had

i

not been upgraded to an issue report. Although the issue was entered in the

j

t

!

1

j

i

-

-

-

-

,

.

-

-

-

-

.

i

i

"

1

22

radiation controls tracking system, resolution of the concerns was not apparent.

The issue was as follows:

-

On March 22, an individual observed personnel attaching safety tethers

improperly, doubling tethers, and working without tethers on the edge of the

refuel pool.

No investigation had been conducted into the observations even though the

3

observations of working without tethers and doubling tethers were contrary to both

BGE and United States Occupational Safety and Health Administration Guidelines.

Maintenance and radiation protection department management informed the

inspector that they did not believe that work was conducted without tethers and

that the observer was likely in error; however, no investigation had been conducted

at the time of the observation and the concerns were unanswered until questions

j

were raised by the inspector.

j

The inspector found four additional gold cards that involved procedure compliance

issues. None of these issues were documented as issue reports and corrective

l

actions were not documented:

On March 15, technicians respor.ded to a personnel contamination. The

-

decontamination effort was not dane in accordance with BGE procedure

RSP-1-107.

On April 4, an unused ty-wrap wai, found floating in the refuel pool. (The

-

refuel pool was a foreign materialt exclusion zone.)

On April 8, BGE identified that personnel were changing alarming dosimeter

-

calibration setpoints in the field. One reason was that the radiation safety

procedure RSP-1-129 was not being followed.

j

i

On April 13, three Cobalt-60 sources were returned to Calvert Cliffs by a

-

vendor as a limited quantity shipment. The receipt survey showed up to

1 millirem per hour on contact, which is greater than limited quantity. The

package may not have considered Department of Transportation regulations.

The inspector reviewed these issues and found that some corrective actions had

been implemented for each of the concerns. For example, for the April 8 issue, field

personnel were re-trained on setting SAIC dosimeter setpoints. However, the

inspector considered the BGE practice of using gold cards to document procedure

compliance issues to be a poor practice because interdisciplinary review and station

wide trending were not done. Also none of the issues received review by

management outside of the radiation protection department.

The inspector discussed these concerns with BGE management. The radiation

protection department manager stated that the radiation protection staff would be

retrained on Calvert Cliffs problem reporting and this training was completed for all

radiation protection supervisors and managers. Also issue reports were written for

.

.

23

i

all procedure compliance issues, including past issues identified during the outage

using the gold card system. Additionally, the radiation protection department

weekly staff meeting began to include a review of allissue reports and gold cards

written for the week, and gold cards were to be evaluated by management to

determine if an issue report was appropriate.

BGE procedure OL-2-100, " Issue Reporting and Assessment," stated that "All

personnel at CCNPP are responsible for identifying and promptly documenting

deficiencies and nonconformances on issue reports." Further, QL-2-100 specified

j

an issue report for an actual or suspected process or program deficiency or

j

nonconformance. The issue resolution sponsor for the issue report shall be

responsible for evaluating the issue, initiating corrective actions, and verifying

completion of all actions necessary to fully resolve the issue described on the issue

report. Upon completion of all required actions, the sponsor shall provide a

resolution document to describe actions taken to resolve the issue. The document

shall provide sufficient detail to ensure a reasonable understanding of the issue, its

cause, and its resolution. For the March 15, April 8 and 13 problems, issue reports

were not written and corrective actions were not documented as specified by

Calvert Cliffs procedure OL-2-100. These failures were considered a violation of

NRC requirements, (VIO 50 317&318/97-03-01)

c.

Conclusions

The inspector found that the radiation protection department did not generate issue

reports for some worker concerns and some concerns were not promptly resolved.

Among the unresolved concerns were personnel safety and procedure compliance

issues. The BGE practice of using gold cards to document some procedure

compliance and personnel safety concerns was considered poor and could prevent

proper resolution and tracking of the concern.

V. Manaaement Meetinos

X1

Exit Meeting Summary

During this inspection, periodic meetings were held with station management to

discuss inspection observations and findings. On June 19,1997, an exit meeting

was held to summarize the conclusions of the inspection. BGE management in

attendance acknowledged the findings presented.

.

.

24

X2

Review of UFSAR Commitments

4

A recent discovery of a licensee operating its facility in a manner contrary to the

'

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a

,

special focused review that compares plant practices, procedures and/or parameters

to the UFSAR description While performing the inspections discussed in this

,

report, the inspectors reviewed the applicable portions of the UFSAR that related to

,

the areas inspected to verify that the UFSAR wording was consistent with the

'

observed plant practices, procedures and/or parameters. No discrepancies were

identified.

.

U

l

_. -- .

..

- -

- - . - - -

. . . .

.-

-

.. -

-. .

-

- - - ~ . .

.

-j

.

. ..

2

ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

y

H.CtE

.

F

P. Katz, Plant General Manager

K. Cellers, Superintendent, Nuclear Maintenance

.

K. Neitmann, Superintendent, Nuclear Operations

i

P. Chabot, Manager, Nuclear Engineering -

T. Pritchett, Director, Nuclear Regulatory Matters

1

B. Watson, General Supervisor, Radiation Safety

)

,

C. Earls, General Supervisor, Chemistry

l

L. Gibbs, Director, Nuclear Security

.I

j

T. Sydnor, General Supervisor, Plant Engineering

i

T. Forgette, Director - Emergency Preparedness

G. Detter, Design Engineer

j

-NB.G

]

S. Adams, Reactor Engineer, Region l

)'

INSPECTION PROCEDURES USED

IP 62707: Maintenance Observation

)

IP 71707: Plant Operations

.

IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

IP 61726: Surveillance Observations

!

IP 37550: Engineering

l

'

IP 37551: Onsite Engineering

IP 71750: Plant Support Activities

IP 84750: Radioactive Waste Treatment, and Effluent and Environmental Monitoring

j

!

i

!

t

i

l

~i

r

I

l

!

-

.

- -

.

,:

i

Attachment 1

2

.

ITEMS OPENED, CLOSED, AND DISCUSSED

,

OR2014

50-317&3i8/97-03-01

VIO

Multiple examples of failure to document and

report to management significant conditions

adverse to quality

Q!gsg_4

50-317/96-04-00

LER

Two ASI Channels OOS Due to Reversed Nuclear

Instrumentation Leads

50-317&318/96-06-02

URI

Two ASI Channels OOS Due to Reversed Nuclear

instrumentation Leads

50-317/96-03

LER

Discovery of Holes in the Containment Sump

Screen to Field Run Tubing

Updated

50-317&318/96-06-03

URI

Salt Water and Service Water Systems

Continued Operability

LIST OF ACRONYMS USED

ASI

Axial Symmetry Index

ALARA

As Low As Reasonably Achievable

RCA

Root Cause Analysis

UFSAR

Updated Safety Analysis Report

EDG

Emergency Diesel Generator

IR

issue Report

ASME

American Society of Mechanical Engineers

PASS

Post-Accident Sample System

URI

Unresolved item

ALARA

As Low As is Reasonably Achievable

,

HEPA

High Efficiency Particulate

i

HPSI

High Pressure Safety injection

MSIV

Main Steam Isolation Valve

ODCM

Offsite Dose Calculation Manual

QA

Quality Assurance

QC

Quality Control

RMS

Radiation Monitoring System

RP&C

Radiological Protection and Chemistry

!

'

SFP

Spent Fuel Pool

UFSAR

Updated Final Safety Analysis Report

TS

Technical Specifications

OOS

Out of Service

EPD

Electronic Personal Dosimeter

.

Attachment 1

3

GOT

General Orientation Training

-NVLAP

National Voluntary Laboratory Accreditation Program

RCA

Radiologically Controlled Area

RP

Radiclogical Protection

REMS

Real Time Exposure Management System

TLD

Thermoluminescent Dosimeter

WMS

Warehouse Management System

BIS

Business Information System

SRW

Service Water

SRWHX

Service Water Heat Exchanger

CAC

Containment Air Cooler

SRV

Safety Relief Valve