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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20217M4181998-04-30030 April 1998 Suppl Safety Evaluation Accepting Licensee RCS Pressure & Heat Removal by Containment Heat Removal Sys post-accident Monitoring Instrumentation ML20216G7921998-03-13013 March 1998 Safety Evaluation Authorizing Proposed Alternative to Check Valve Obturator Movement Requirements of OM-10 for SIL Accumulator Outlet for Listed Check Valves ML20203E8521998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(f) for Performing Required Inservice Testing of Certain Class 2 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E9341998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(g) for Performing Required Exams for Certain Class 1 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E2441998-02-0909 February 1998 Safety Evaluation Accepting Re Approval of Realistic,Median Centered Spectra Generated for Resolution of USI-A-46 ML20198R9941998-01-13013 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Millstone Nuclear Power Station,Unit 3 ML20202H7461997-12-10010 December 1997 Safety Evaluation Accepting Licensee Position That Correction of AC-11 Single Failure Vulnerability Unncessary ML20202J0911997-12-0202 December 1997 Safety Evaluation Accepting Proposed Exemption,Which Meets Special Circumstance Given in 10CFR50.12(a)(2)(ii) ML20198S2411997-10-31031 October 1997 SE Accepting Licensee Request for Deviations from Recommendations in Reg Guide 1.97,Rev 2 for Temp & Flow Monitoring Instrumentation for Cooling Water to ESF Sys Components & Containment Isolation Valve Position ML20212G5991997-10-27027 October 1997 Safety Evaluation Supporting Amend 103 to License DPR-21 ML20217K8801997-10-27027 October 1997 Correction to Safety Evaluation Supporting Amend 103 to License DPR-21.Phrase or Rod Block Protection Has Been Deleted from Listed Sentence in Staff Associated SE ML20212F1381997-10-22022 October 1997 Safety Evaluation Supporting Amend 102 to License DPR-21 ML20217M9301997-08-19019 August 1997 Safety Evaluation Accepting Continued Operation W/O High Startup Rate Trip by Nene for Millstone,Unit 2 ML20149J2661997-07-23023 July 1997 Safety Evaluation Accepting Changes & Reanalyses in ECCS Evaluation Models & Application of Models for Plant,Unit 2 ML20141L8821997-05-28028 May 1997 Safety Evaluation Supporting Amend 101 to License DPR-21 ML20138A0111997-04-23023 April 1997 Safety Evaluation Accepting Licensee Proposal,Not to Perform Type C Leakage Rate Testing on 14 Subject CIVs ML20137V5931997-04-15015 April 1997 Safety Evaluation Supporting Amend 100 to License DPR-21 ML20137U3121997-04-10010 April 1997 Safety Evaluation Supporting Amends 99,206 & 135 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20134A0331997-01-23023 January 1997 Safety Evaluation Accepting Util Proposed Alternatives to ASME Code Requirements ML20133N3401997-01-14014 January 1997 Safety Evaluation Supporting Amend 98 to License DPR-21 ML20135C4221996-12-0202 December 1996 Safety Evaluation Accepting Proposed Alternative Described in Relief Request R-1 Re Valve Inservice Testing Program at Facility ML20128P4381996-10-0909 October 1996 Safety Evaluation Accepting Review of Cracked Weld Operability Calculations & Staff Response to NRC Task Interference Agreement ML20128L7541996-10-0404 October 1996 Safety Evaluation Supporting Amend 97 to License DPR-21 ML20248C5451995-05-0202 May 1995 SER on Millstone Unit 3 Individual Plant Exam of External Events to Identify plant-specific Vulnerabilities,If Any,To Severe Accidents & Rept Results Together W/Any licensee-determined Improvements & C/A to Commission ML20248C5731994-07-19019 July 1994 SER Step 1 Review of Individual Plant Exam of External Fire Events for Millstone Unit 3 ML20059H4991994-01-24024 January 1994 Safety Evaluation Accepting Revised Responses to IEB-80-04 Re MSLB Reanalysis 1999-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
Text
i l
nog'o UNITED STATES i
,! g o NUCLEAR REGULATORY COMMISSION h ,$ WASHINGTON, D, C,20656
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SAFETY EVALUAT4ON BY THE OFFICE OF NUCLEAR REACTOR REGULATION !
1 RELATED TO AMENDM_ENT NO.19 TO FACILITY OPERATING LICENSE NO. DPR-_2_1 MRTHEASTNUCLEARENERGYCOMPANY l MILLSTONE NUCLEAR POWER STATI0h,. N .
UNIT NO. 1 DOCKET NO. 50-245 ,
l 1.0 I_NTR_0 DUCTION ,
By application for license amendnent dated December 22, 1986, Northeast Nuclear Energy Company, et al. (the licensec), requested a change to the Millstone Unit 1 Facility Operating License, DPR-21, to change the expiration date of the license from May 19, 2006 to October 6, 2010.
2.0 DISCUSSION
~
Section 103.c of the Atomic Energy Act of 1954 states that a license is to be issued for a specified period not to exceed 40 years. Title 10 CFR 50.51 specifies that each license will be issued for a fixed period of tinee not to exceed 40 years from the date of issuance. The currently licensed terin for M111 ster e Unit 1 is 40 years connencing with the issuance of the construction pemit which was on May 18, 1966. Accounting for the time that was required for plant construction, this repitsents an effective operating license term of !
approximately 36 years. Consistent with Section 103.c of the Atomic Energy :
Act and Section 50.51 of the Comission's regulations, the licensee, by the i December ??, 1986 application, seeks an extension of the operating license term for Millstone Unit I so the fixed period of the license would be from the date of the operating license issuance, i 3.0 EVALUATION The NRC staff has evaluated the safety issues associated with issuance of the proposed license anendinent which would allow approximately 4 additional years l of operation. The issues addressed consist of additional radiation exposure 1 to the licensee's operatin0 staff, impacts on t% off-site population, and the general aging of the plant structures and egr9mt. The impact of additional radiation exposure to the facility operating vf and the impact on the general population in the vicinity of Millstm Unit I are addressed in the NRC staff's Environnental Assesstent dated 8808240394 880818 i PDR ADOCK 05000245 P PDC
3.1 ,P_lant Structures and Systems The licensee's request for extension of the operating license is based in part, on the detennination that a 40-year service life was considered during the design and construction of the plant. This does not mean that sone components will not wear out during the plant lifetire. Rather, design features were incorporated which provide for inspectability of structures, systems and equipment. In addition structures, systents and components are required by the Technical Specifications to undergo routine surveillance to assure that there is a high degree of confidence that they will perfonn their safety functions when required.
Millstone Unit 1 Technical Specification (TS) 3.13 requires the licensee to raintain an inservice inspection (ISI) program for ASME Code Class 1, 2 and 3 con:ponents and an inservice test (IST) program for ASEE Code Class 1, 2 and 3 pun'ps and valves. These programs are necessary to assure the continued operability ard integrity of systems important to plant safety. The TS 3.13 requirerents further specify that the above programs comply with the applicable Code and addenda as required by 10 CFR Section 50.55a(g) except where the NRC staff provides written relief per 10 CFR 50.55a(g)(6)(1).
Required revisions to the ISI and IST programs will be issued throughout the lifetine of the facility and the reviews of the revisiens will be conducted independent of the issuance of this license amendrrent review.
Aging analyses have been performed for all safety
- elated electrical equiprent in accordance with 10 CFR 50.49, "Environmental quaiification of electrical equiper+nt inportant to safety for nuclear power plants," identifying qualified lifetimes for this equipaent. These lifetires are incorporated into plant equipnent maintenance and replacement practices to ensure that all safety-related electrieel equipnent remain qualified ard available to perfonn their safety functions regardless of the overall age of the plant. Our letter and Safety Evaluation dated March 20, 1985 provides our approval concerning the licensee's program for environmental cualifications of electrical equipnent.
3.2 Reactor Pressure Vessel The reactor pressure vessel (RFV) was designed for 40 years of operation at full power (2011 MW thertnal) with a plant capacity factor of 80%, which is equivalent to 32 Effective Full Power Years (EFPY). The RPV contains a nunber of in-vessel radiation capsules that are periodically withdrawn, and their contents tested, to assure that the RPV mhterials will continue to behave in a ductile fashion under expected operating conditions. The capsule withdrawal schedule is given in TS 4.6.B.5 and assures compliance with 10 CFR Part 50, Appendix H, over 32 EFPY. Thus far, a single capsule has been withdrawn and tested. License Amendment No. 9 contains the NRC staff's evaluation of the licensee's analysis of the capsule.
i /
Technical Specifications 3/4.6 contains temperature / pressure limits for the reactor coolant system in accordance with 10 CFR Part 50, Appendix G. The original limits in the TS were revised in License Amendment 9 issued on August 20, 1987. We expect that the licensee will continue to update the limits of TS 3/4.9 over the lifetime of the facility.
3.3 ALARA Measures In 1977, the licensee instituted a fomal ALARA program at Millstone Unit 1.
This program contains a number of reasures intended to minimize occupational doses consistent with ALARA considerations. One of these reasures is the use of decontamination prior to work on major components to reduce component dose rates. In 1984. Millstone Unit 1 perfomed a partial systeib decontaminaticn of the reactor recirculation system. This related in a net dose savings of 1300 person-rems on pipe repair and other drywell work perfonned following the system decontamination. Millstone Unit 1 perforned a second chemical decontamination on the recirculation system piping in 1987. Also in 1987, the licensee tested and implenented a zine injection process to reduce radionuclide retention on coolant component surfaces'. Other dose reduction ineasures used at Millstone Unit 1 include use of mockup training, remote tooling and inspection techniques, and use of special tooling and robotics. In order te keep track of occupatirnal radiation doses expended at Millstone Unit 1, the licensee began using a copputerized dese trackirg system in 1979. This system, which is used to track doses and man-hours by system / component / job, provides a good historical dose data base for trending job specific doses and for providing pre-job dose estimates. The reasures 1isted above, which will continue to the end of plant life, including the proposed extension, provide assurance that occupational doses will satisfy ALARA considerations throughout the period of operation.
In addition to the ALARA measures just described, the licensee is actively seeking new nethods to reduce total person-rem dose. The licensee's Exposure Reduction Initiative Program, which was implemented in 1986, consistt of several short-tern, initiatives which are part of this program are scheduled to be achieved in the 1987-1988 time frane, while the seven long-tem initiethes in this program have a completion date in early 1990's. Implementation of the Exposure Reduction Initiative Program should result in lower overall dose rates and lower collective doses at Millstone Unit 1.
As stated above, the licensee instituted an ALARA program in 1977 and an Exposure Reduction Initiative Program in 1986. The overall responsibility for the licensee's Corporate ALARA program lies with the Senior Vice President.
Nuclear Engineering and Operations (NEO). However, it is the responsibility of all NEO management and supervisors to ensure that their staff, their consultants, and their contractors are informed and comply with the licensae's Radiation Protection Program requirerents. There is routine managenent involve-ment in station ALARA concerns. Station ALARA goals are directly related to goals established by the corporate Radiological Assessment Branch. Corporate supplies health physics supervisors to the plant to' assist and oversee the
, station health physics staff during outages. Worker involvenent in minimizing deses is encouraged through worker initiatives and worker input to ALARA feedback reports. The licensee should continue to encourage worker and contractor awareness at the grass roots level of ALARA by making dose reducticn an integral part of design, installation, and maintenance at M'llstcne Unit 1.
3.4 Dos _e Assessment The staff has evaluated the occupational dose data from Millstone Unit 1 for the period from 1972 (startup) through 1987 and compared it with the BWR average for the same period. The cumulative average yearly dose for all U.S.
BWRs over this 16-year period has been approxinately 770 persons-rems. The everage yearly dose for Millstone Unit 1 over this same 16-year period has been approximately 1025 person-rems / year, or about 33 percent above the national average for BWRs. HoNever, since 1983, the yearly collective dose at Millstone Unit I has decreased markedly (the average yearly occupational dose for the five-year period from 1983-1987 for Millstone Unit No. I was 504 person-rems). In an attempt to ensure that this trend continues, the licensee, in 1986, established a three-year average dose goal of 570 person-rems / year to be realized at Millstone Unit 1 by 1990. This three-year averaged cunulative dose will be revitt d downwards on an annual basis as Villstone Unit 1 improves its perfonrance. Mraging the dose over a three-year period enables the licensee to more efrectively reduce person-rem by permitting nore up-front ident'fication of high person-rem jobs and allowing better planning. A plot of the three-year rolling dose averages for Millstone Unit 1, extrapolated to the 1988-1990 time period, shows the three-year averaged dose declining to the 570 person-rems / year dose goal by 1987. The three-year averaged dose for the most recent three-year period (1985-1987) of 481 person-reras/ year was, indeed, well below the three-year averaged dose goal of 570 person-rems / year set for Millstone Unit 1. The licensee plans to maintain the annual dose at Millstene Unit 1 at 570 person-rems / year or less through increased ALARA awareness, and successful inplementation of the Exposure Reduction Initiative Program.
3.5 Summary of Fjgn3s_
Based upon the above, we find that extension of the operating license for i Millstone Unit 1 to allcw a 40-year service life is consistent with the safety i analyses for Millstone Unit I and that the Contrissicn's previous safety !
findings are not changed. All issues associated with plant systems and '
equipnent, including aging and changes in RFV fracture toughness properties have been addressed and are acceptable for 40 years of operatien.
4.0 ENVIRONMENTAL CONSIDERATION
A Notice of Environmental Assessnent and Finding of No Significant Impact :
relating to the proposed extension of the Facility Operating License termination date for Millstone Unit 1 was published in the Federal Register l on August 4, 1988 (53 FR 29401).
5.0 CONCLUSION
We have concluded, based on the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will ,
1 be conducted in compliance with the Consnission's regulations, and the issuance of the anendrent will not be inimical to the common defense and security or to the health and safety of the public.
Dated: August 18, 1988 Principal Contributor:
M. Boyle and C. Hinson
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