ML20126C839

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SALP Repts 50-277/85-99 & 50-278/85-99 for Jan 1984 - Mar 1985
ML20126C839
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 05/13/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20126C612 List:
References
50-277-85-99, 50-278-85-99, NUDOCS 8506140541
Download: ML20126C839 (58)


See also: IR 05000277/1985099

Text

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Philadelphia Electric Company

PEACH BOTTOM ATOMIC POWER STATION

May 13, 1985

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TABLE OF CONTENTS

Page

I. INTRODUCTION...............................................

1.1 Purpose and 0verview.................................. I

1.2 SALP Board and Attendees.............................. 1

4 1.3 Background............................................ 1

II. CRITERIA................................................... 8

III. SUMMARY OF RESULTS......................................... 10

IV. PERFORMANCE ANALYSIS....................................... 13

4.1 Plant Operations...................................... 13

4.2 Radiological Controls................................. 17

4.3 Maintenance........................................... 21

4.4 Surveillance.......................................... 24

4.5 Fire Protection / Housekeeping ...... .................. 26

4.6 Emergency Preparedness................................ 28

4.7 Security and Safeguards............................... 30

4.8 Refueling / Outage Activities........................... 32

4.9 Licensing Activities.................................. 35

V. _ SUPPORTING DATA AND SUMMARIES.............................. 37

5.1 Investigations and Allegations Review................. 37

5.2 Escalated Enforcement Action.......................... 37-

5.3 Management Conferences................................ 38

5.4 Li cen s ee Eve n t Repo rt s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 38

5.5 Forced Outages and Unplanned Scrams. ................ 39

TABLES

Table 1 Licensee Event Reports T1-1

Table 2 Violations T2-1

Table 3 Inspection Report Activities T3-1

Table 4 Inspection Hours Summary T4-1

Table 5 Forced Outages and Unplanned Scrams T5-1

Table 6 NRR Supporting Data and Summary T6-1

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.I. INTRODUCTION

1.1 Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an inte-

grated NRC staff effort to collect the available observations and

data on a periodic basis and to evaluate licensee performance based

upon this information. SALP is supplemental to normal regulatory

processes used to ensure compliance to NRC rules and regulations.

.SALP is intended to be sufficiently diagnostic to provide a rational

basis for allocating NRC resources and to provide meaningful

guidance to the licensee's management to promote quality and safety

of plant construction and operation.

An NRC SALP Board, composed of the statf members listed below, met

on May 13, 1985, to review the collection of performance

observations and data and to assess the licensee performance in

accordance with the guidance in NRC Manual Chapter 0516, " Systematic

Assessment of Licensee Performance." A summary of the guidance and

evaluation criteria is provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's per-

formance at the Peach Bottom Atomic Power Station for the period

January 1, 1984 through March 31, 1985.

1.2 SALP Board:

R. W. Starostecki, Director, Division of Reactor Projects (DRP)

W. F. Kane, Deputy Director, Division of Reactor Project < (DRP)

T. T. Martin, Director, Division of Radiation Safety and Safeguards

(DRSS)

S. D. Ebneter, Director, Division of Reactor Safety (DRS)

S. J. Collins, Chief, Projects Branch No. 2, DRP

R. M. Gallo, Chief, Reactor Projects Section 2A, DRP

J. F. Stolz, Chief, Operating Reactors Branch 4, NRR

G. Gears, Licensing Project Manager, NRR

T. P. Johnson, Senior Resident Inspector, Peach Bottom Atomic Power

Station, Units 2 and 3

Other NRC Attendees:

J. E. Beall,-Project Engineer, RPS 2A, DRP

J. H. Williams, Resident Inspector, Peach Bottom Atomic Power

Station, Units 2 and 3

1.3 Backaround

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. Peach Bottom Units 2 and 3 were issued operating licenses on

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October 25,1973 (DPR-44) and July 2,1974 (DPR-56), respectively.

Unit 2 began commercial operation during July, 1974, and Unit 3

began commercial operation during December, 1974.

Presently, Unit 2 is recovering from its sixth refueling / outage and

Unit 3 is in power coast down from its sixth cycle. Major items of

interest which occurred during the assessment period are depicted

below.

(1) Licensee Activities

Unit 2

The unit operated at or near full power from January 1 through

January 28, 1984. On January 28, 1984, a controlled shutdown

was initiated to repair a leak on the RCIC testable check valve.

The unit returned to power on February 2, 1984, and on February

18, 1984, the unit was removed from service for Main Steam

Isolation Valve (MSIV) and Feedwater Check Valve leak testing.

During this outage, an inspection of the' Torus Vent Header was

conducted in response to generic BWR concerns. An isolated

defect in the workmanship, associated with previous torus modifi-

cations, was identified and repaired. The unit returned to

service on February 25, 1984.

Power reductions occurred on February 27, 1984, and again on

March 2,1984, for control rod pattern adjustments and r

condenser water box inspection and repair. At 2:19 a.m., on

April 28, 1984, the unit was shutdown for refueling and

a recirculation and RHR pipe replacement outage.

During May,1984, the vessel head, steam dryer, and moisture

separator were removed and all fuel was transferred from the

reactor core to the spent fuel pool in preparation for pipe

replacements. The new piping material is type 316 austenitic

stainless steel (controlled chemistry) and is less susceptible

to intergranular stress corrosion cracking.

In June, 1984, the core spray sparger inspection, repair of

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fuel pool gate cracks, Source Range Monitor and Intermediate

Range Monitor instrument dry tube inspections, installation and

testing of the jet pump diffuser plugs and installation of.

vessel annulus shielding in front of the suction nozzles of the

recirculation loops were completed.

Installation of recirculation discharge nozzle caps was com-

pleted, measurements for head spray piping replacement were

taken, all recirculation suction nozzles were cut, and pre-

operational tests for chemical decontamination of the pipe to be

removed were completed during July,1984.

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During August, 1984, after completion of the cutting and

capping of the recirculation and RHR piping, the reactor vessel

was flooded to the head flange and chemical decontamination of

the piping started. The jet pump plugs were removed and jet

beams were replaced. The recirculation and RHR piping was

drained following completion of chemical decontamination, and

the jet pump plugs were replaced and the vessel was flooded.

In September, 1984, control blade relocation and replace-

ment, removal of the jet pump nozzle plugs, and radiography on

the recirculation N-2 (safe end) nozzles were completed. The

"A" and "B" recirculation suction and discharge valves were

3_ disassembled and removed from the drywell, and temporary reactor

water cleanup pumps were installed in the reactor-vessel.

During October,1984, replacement of the nuclear instrument dry

tubes in the reactor, head spray piping installation, and

removal of the recirculation and Residual Heat Removal piping

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were completed. The "B" recirculation pump motor was removed

from the drywell.

Both recirculation pump motors were uncoupled and removed from

the drywell during November, 1984. Decontamination and inspec-

tion of both recirculation pump shafts and impellers, fitting of

both the "A" and "B" recirculation loop ring headers, decontamin-

. ation of the "A" and "B" loop recirculation, loop. valve bodies

and pump bowls, removal of the recirculation pump flow splitters,

replacement of two recirculation inlet safe ends, removal of two

additional recirculation inlet safe ends, ard replacement of the

3A feedwater heater were completed.

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In December,1984, January and February 1985, the major activity,

was pipe replacement and welding operations. Also, both "A" and

"B" recirculation pump motors were returned to the drywell.

Ddring March,1985, all small bore pipe welds needed to support

vessel fill were complete. The "A" and "B" recirculation pump

seals were installed; the main steam drain valves were

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replaced; the four recirculation motor operated valves were

reassembled; and the Residual Heat Removal valve which leaked

during the primary recirculation pipe flush was repaired.

Unit 2 remained shut down for the refueling / pipe replacement

outage at the end of the assessment period. Current plans

project startup during June,1985. In addition to replacing all

the reactor recirculation piping, RHR (drywell portions), piping

head spray and reactor water cleanup (drywell portions) piping,

the ten recirculation inlet safe-ends and two jet pump penetra-

tion seals, a number of major modifications were performed.

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Unit 3

The unit began the assessment period at full power. On

' January 14, 1984, the unit was removed from service due to

flooding of the condensate pump pit which was caused by an

open vent valve on a main condenser water box. The flooding

of the condensate pump room resulted in damage to the

condensate pump thrust bearings. During the manual scram on

January 14, 1984, control rod (34-27) failed to insert within

the prescribed time due to sticking of a scram pilot solenoid

valve. The unit was returned to power on January 27, 1984.

On February 9,1984, the unit shutdown on an automatic scram

high neutron flux signal. The scram occurred following a

trip of the "B" reactor feedwater pump due to high vibration.

Loss of the feedpump initiated runback of recirculation pumps

and main turbine. Turbine runback did not automatically

terminate as designed, resulting in a reactor pressure

transient that caused the high flux spike. Following repairs,

the unit returned to service on February 10, 1984.

During March and April, 1984, load was reduced several times

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for inspection and tube plugging of the main condenser waterbox

along with control rod pattern adjustments.

The unit was removed from service for a feedwater heater repair

on June 2, 1984. The RCIC steam supply isolation valve was also

repaired and tested during this outage. Since cracking had been

found on the Unit 2 jet pump instrumentation nozzles, the Unit 3

nozzles were also checked during this outage and indications

were found on both the A and B instrumentation nozzles. Weld

overlay repairs were performed on both welds.

On July 11, 1984, the unit tripped when a lightning strike near

the substation initiated a sequence of electrical breaker

openings culminating in an automatic reactor scram. While the

unit was shut down, a reactor water cleanup system isolation

valve failed to open during a functional test. The valve

operator was replaced to correct the problem. Also, an

external leak on the condensate-system drain cooler was

repaired. The unit returned to service on July 15, 1984.

Unit 3 automatically scrammed due to a feedwater controller

failure which resulted in a low reactor water level on August

21, 1984. Reactor startup commenced following completion of the

work required to return an emergency diesel generator to service.

The diesel generator had been out-of-service for a scheduled

annual inspection. Unit startup was initiated August 24, 1984.

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-Load was reduced on September 29, 1984 for control rod

pattern adjustment, condenser circulation pump repair, and

condensate pump work.

On October 25, 1984, load was reduced to 80% power to reduce

the high off gas radiation levels of approximately 45,000

uCi/second and mitigate. future fuel failures. After the

power reduction, the off gas radiation level was 24,000

uCi/second with the unit at 80% power.

The unit was shut down to repair the Traversing Incore Probe

(TIP) machine and correct a 4 gpm unidentified leak inside the

drywell on November 6,1984. The unit returned to service on

November 12, 1984. On November 14, the "B" recirculation pump

tripped when water, leaking into a pressure switch, shorted its

contact thus energizing the trip circuit of the pump motor.

During the. restart of the pump, the reactor scrammed on an

Average P4er Range Monitor (APRM) high flux signal caused by a

small scram margin. The unit was returned to service on

November 16, 1984. On November 24, 1984, load was reduced to

.repairicondenser water box leaks.

The dnit reduced power on December 1, 1984, to 65% power to

repair condenser waterbox leaks. On December 10, 1984, the

unit was removed from service for repair of offgas recombiner

condenser tubes. While in~ hot standby, the "B" recirculation

pump tripped on motor overcurrent. This was caused by the

motor generator set hydraulic coupling experiencing a scoop

tube linkage failure. Following repairs to the recombiner

condenser and the recirculation motor generator set scoop

tube positioner, and checkout of the MG set, pump motor and

associated controls, the unit was returned to power. Load was

reduced on December 15, 1984, for a control rod pattern

. adjustment. A special hydrogen water chemistry test was

performed on December 17-20, 1984. The purpose of the test was

to obtain data to evaluate the results of injecting hydrogen

into the feedwater to reduce the oxygen concentration in the

primary coolant as a pipe crack mitigation measure. The unit

was operated at 90 to 100% power during the test. Load was

reduced on December 20, 1984 to 85% power due to offgas

radiation levels.

On January 5,1985, load was reduced to 66% power to repair

a broken test tap on the 3A condensate pump. The unit

returned to 80% power on January 6, 1984. On January 7,1984,

the "A" loop torus cooling valve would not stroke and was

declared inoperable. An Unusual Event was declared and

shutdown was initiated on January 15, 1985, when the E-4

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diesel generator and the "A" loop torus cooling valve were

declared inoperable. The valve was returned to service by

the time the unit reached 25%. The E-4 diesel generator was

returned to service on January 21, 1985.

The unit was shut down on January 23, 1985, to clean the

main generator exciter brushes. (An oil leak was causing a

ground fault alarm.) On January 24, 1985, the unit returned to

service and reached 90% power the next day.

The unit was taken out of service to perform required surveil-

lance tests on February 1, 1985. Three of the eight Main Steam

Isolation Valves (MSIV's) tested failed local; leak rate testing

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and required repair prior to restart. Startup was begun on

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February 25, 1985. The unit was returned to service following

repair to the 71L relief valve bellows and replacement'of a

solenoid valve which prevented closure of a reactor head vent

valve (AO-17). Following repair of a drywell airlock door seal,

the unit was returned to service on March 1, 1985.

Later on March 1, a scram was caused by condenser low vacuum

resulting from a missing plug in a relief valve on the 2A fned-

water heater. A metal plug was installed, several minor vacuum

leaks were repaired and the unit was returned to service that

same day. On March 9, 1985, load was reduced to 55% power.for

43 hours4.976852e-4 days <br />0.0119 hours <br />7.109788e-5 weeks <br />1.63615e-5 months <br /> to accommodate control rod pattern adjtttment and

helium leak testing of condenser waterboxes. Two small leaks

were located and repaired. Unit operation (during power coast

down prior to refueling) was limited to 90% power throughout the

remainder of the assessment period due to high offgas activity.

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(2) Inspection Activities

~Two NRC resident inspectors were assigned to the site during the

assessment period. The total NRC inspection hours for the assessment

period was 5422 hours0.0628 days <br />1.506 hours <br />0.00896 weeks <br />0.00206 months <br /> (resident and region-based) for the 15 month

assessment period. The total inspection hours when normalized to a

12 month (1 year) period are equivalent to 4338 hours0.0502 days <br />1.205 hours <br />0.00717 weeks <br />0.00165 months <br />. Distribution

of these hours for each functional area is depicted in Table 4.

Details of inspection report activities is presented in Table 3.

Emergency plan team inspections were conducted on October 16-18,

1984 (annual emergency exercise) and on January 8-11, 1985.

An Operations Assessment Team Inspection to assess the Unit 2 pipe

replacement outage was performed on July 16-20 and 23-27, 1984.

Special inspections were conducted as follows:

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To review individual rod scramming on January 5-20, 1984.

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To review security and safeguards on June 25-July 1,1984.

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To review inoperability of one diesel generator and one loop

of containment cooling on January 15-18, 1985.

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To review the contamination of several radiation workers on

February 13-15, 1985.

The NRC Region I NDE Mobile Van was onsite for an inspection

associated with Unit 2 pipe replacement on January 14-25, 1985.

The NRC Region I Mobile Radiological Measurements Laboratory was

onsite for an inspection on January 28 thru February 1, 1985.

Major enforcement issues occurring during the assessment period are

discussed.in report Section 5.2. Table 2 lists specific enforcement

data.

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II. CRITERIA

The following criteria were used where arpropriate in evaluating each

functional area:

1. Management involvement in assuring quality.

2. Approach to resolution of technical issues from a safety standpoint.

3. Responsiveness to NRC initiatives.

4. --Enforcement history.

5. Reporting and analysis of Licensee Event Reports, 50.55(e) reports

and Part 21 items.

6. Staffing (including management).

7. Training effectiveness and qualification.

To provide a consistent evaluation of licensee performance, attributes

associated with each criterion and describing the characteristics

applicable to Category -1, 2 and 3 performance were applied as

described in NRC Manual Chapter 0516, Part II and. Table 1.

The SALP Board conclusions were categorized as follows:

Category 1: Reduced NRC attention may be appropriate. Licensee

management attention and involvement are aggressive and oriented

toward nuclear safety; licensee resources are ample and effectively

used such that a high level of performance with respect to operational

safety or construction is being achieved.

Category 2: NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and are

reasonably effective such that satisfactory performance with respect to

operational safety or construction is being achieved.

Category 3: Both NRC and licensee attention should be increased. Licen-

see management attention or involvement is acceptable and considers nuc-

lear safety, but weaknesses are evident; licensee resources appeared

strained or not effectively used such that minimally satisfactory per-

formance with respect to operational safety or construction is being

achieved.

The SALP Board has also categorized the performance trend over the last

quarter of the SALP assessment period. The categorization describes

the general or prevailing tendency (the performance gradient) during the

.last quarter (January 1,1985 to March 31,1985) of the SALP period. The

performance trends are defined as follows:

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Improving: Licensee performance has generally improved over the

last quarter of the SALP assessment period.

Consistent: Licensee performance has remained essentially constant over

the last quarter of the SALP assessment period.

Declining: Licensee performance has generally declined over the

last quarter of the SALP assessment period.

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III. SUMMARY OF RESULTS

A. Overall Facility Evaluation

During this assessment period, Peach Bottom has demonstrated that they

have a staff and managers who are technically knowedgeable and are

involved in station activities affecting safety. The conduct of

plant operations, maintenance activities and surveillance testing is

sound and conservative. Licensee performance and response to NRC

licensing issues and actions was generally timely and technically

sound. Major weaknesses were identified in the functional areas of

radiological controls and security / safeguards. The summary ratings

of overall facility performance for each functional area, both during

the current and previous assessment period, and trends, are depicted

in Section III.D of this report.

The plant is generally operated conservatively and plant transients

are handled well. Plant operators are well trained, technically

knowledgeable, have demonstrated ability and are experienced. Improve-

ment in adherence to procedures is evident and must continue.

The performance in the area of radiological controls has degraded

during the current assessment period. A major contributing factor

was the heavy radiological work load during the Unit 2 outage. A

significant deficiency exists with regard to the ability to take

effective corrective action to prevent recurrence of identified

radiation protection problems. Also, the performance of security and

safeguards has degraded markedly. Deficiencies exist in the perfor-

mance of ouards in carrying out their duties as required by the

Security t'lan, and in licensee oversight of the contractor guard

force. Management involvement and development of improvement pro-

grams are warranted for these two areas.

Fire prctection and housekeeping controls have improved somewhat

during the current assessment period. Management continues to be

involved in this area, in particular during the lengthy outage

period during the assessment. Site QC remains involved in

identification of housekeeping deficiencies. Continued management

involvement in fire protection and housekeeping area is warranted.

B. Training Evaluation

The licensed operator training program (replacement and requalifi-

cation) functions well. Training of QA personnel was observed in the

area of QC inspectors and was evaluated as good. Mockup training for

specific maintenance activities is good. Inadequate training in the

area of radiological controls was identified in two areas: specific

training of chemistry technicians who perform radwaste surveillances

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and training of the Radioactive Material Coordinator.

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Training deficiencies were also identified for emergency plan person-

nel.

C. Quality Assurance Evaluation

Overall the QA organization is a itcensee strength. The licensee has

staffed the on site Electric Production Department (EPD) QC organt-

zation during the assessment period. Although, the QA organization

is somewhat fragmented, it functions well. Weaknesses were identified

in the Engineering and Research Department (E&R) QA system that tracks,

corrective action for audit findings. Also, deficiencies were identi-

fied in the radiological controls problem identification and correc-

tive actions. QA is evident in day-to-day plant operations as evi-

denced by QA personnel presence in the control room and in daily

plant operations meetings. QC is also evident in the performance of

plant housekeeping inspections.

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D. Facility Performance

Category Category Recent

Functional Area Last Period This Period Trend

{ March 1,1983 (January 1, 1984 to

to December 31,1983) March 31, 1985)

1. Plant Operations 2 2 Consistent

2. Radiological

Controls' 2 3 Consistent

3. Maintenance 2 1 Consistent

4. Surveillance 2 2 Consistent

5. Fire Protection &

Housekeeping 2 2 Improving

6. Emergency ,

Preparedness 2 2 Improving

7. Security and

Safeguards 1 3 Consistent.

8. Refueling /0utage

Activities 2 1 Consistent

9. Licensing Activities 1 1 Declining

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IV. FUNCTIONAL AREA ASSESSMENTS

4.1 Plant Operations (34%)

During this SALP period, resident inspections routinely reviewed

plant operations; specialist inspections reviewed QA and QC programs,

procurement, modifications, contractor controls, and response to

gener-ic issues.

Corporate and station management presence and involvement in plant

operations provides appreciation for plant technical problems. Review

of control room and plant activities and control room logs by on site

management is frequent. Corporate management is on site often as evi-

denced by attendance at meetings and discussions with on site manage-

ment personnel. Communications between groups in the plant appears

to be effective. No significant problems were noted with respect to

the level of decision making. Electric Production Department has

issued a " Requirement and Guidelines" manual to provide policy gui-

dance and clarify policy issues. Plant management has begun to issue

newsletters to keep all plant workers informed of significant hap-

penings and provide additional information which may be of interest

to workers.

As noted in previous SALP assessments, control room operators

response to plant transients was a strength and continues to be so.

Operators use the symptom-based emergency operating procedures

effectively. During a low probability event such as the earthquake

of April 22, 1984, the operator took the proper actions. Establish-

ment of the "Inside Supervisor" position, an SR0 in the control room

at all times has provided additional depth to the control room

capability. The STAS function well with the other shift members.

The operators work well with and respect the function of the STA.

The licensed operators take pride in their control room and related

activities. They are knowledgeable of overall plant status as exhibited

by documentation in the shift turnover checklists and personal inter-

views. There is no evidence of control room distractions. Noise

level is generally controlled so as not to interfere with control

room activities; however, there have been a few observed occasions of

shouting in the control room (not related to duties). Access to the

general control room area is restricted only by the vital area doors.

However, there are control room floor boundary tape markings where

access to the control room panels and c]ntrols is limited to autho-

rized personnel only. The overall control room appearance is good

with no evidence of inappropriate material. General area cleanliness

is also good.

Adherence to procedures and attention to detail in safety-related

equipment lineups have been generally adequate. However, there were

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several instances where lapses. occurred in following procedures, such

as exceeding heatup rate limits (Units 2 and 3), pressurizing the

reactor vessel above limits (Unit 3), mode switch in improper posi-

tion (Unit 3), and exceeding the torus water level limit (Unit 3). A

civil penalty was assessed for pressurizing the reactor vessel above

limits and exceeding the heatup rate. Another example of lack of

operator attention to procedural details occurred when the Unit 3

operators took a redundant safety system (HPCI) out of service before

permitted by technical specifications. The licensee took appropriate

corrective actions regarding safety system operability including

reinstruction of operators.

The licensee's return to power operations following outage periods is

generally smooth and well controlled. However, following the Unit 3

shutdown in February,1985, for maintenance and testing the return to

power operations was hindered due to problems associated with a main

steam safety relief valve, leakage from the drywell air lock and a

scram on loss of vacuum. The operators handled these problems profes-

sionally. At the time of the SALP board, Unit 2 continues to be shut

down in a refueling / outage period and related items for refueling /

outage activities are addressed in Section 4.8.

During June, 1984, an NRC Order Modifying License (see Section 5.2)

was issued. This Order resulted from the establishment of a licensee

practice of individually scramming control rods during controlled

shutdowns without adequate safety reviews as required by 10 CFR 50.59.

The individual rod scramming resulted in effectively bypassing the

functions of Rod Worth Minimizer (RWM) and the Rod Sequence Control

System (RSCS). The Order requires the licensee to perform an assess-

ment of the safety review process, to conduct a review of station

procedures and to ensure personnel involved in the procedure review

and approval process are aware of the licensing bases. The Operations

Analysis Corporation, the contractor who performed the safety review

process appraisal, concluded that the licensee's process for safety

evaluations was adequate. However, the existing controls for safety

reviews of procedure changes were determined to be ineffective. The

licensee's review of station procedures is currently ongoing with a

-scheduled completion date of September 1985. The licensee's review

of personnel qualifications associated with the procedure change

process was completed on February 25, 1985.

The on site review committee (PORC) appears to be functioning well

based upon observation by inspectors at PORC meetings. The Station

Superintendent appears to be utilizing the PORC in an effective

manner, as evidenced by the frequency of meetings and scope of

questioning of items brought before PORC. As an example, although

! plant procedures did not require PORC to review and approve the modi-

fication test results, PORC chose to review the completed Modifica-

tion Acceptance Tests as well as the test procedures for Unit 2. The

l PORC takes an active part in contributing to operational safety.

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Several strengths were noted in the licensee's overall QA programs.

These include the following: positive welder identification through

the use of photographs, more conservative requirements for the evalua-

tion of ASME NDE results, and independent audits of vendors previously

audited and accepted by a contractor. In response to the last SALP

assessment, the licensee has staffed the EPD site QC organization

with well qualified contractor personnel. Licensee personnel have

been selected for on-the-job training to fill the QC positions per-

manently. These personnel are currently one-on-one training with the

contractor personnel in order to qualify the licensee personnel for

the QC positions.

EPD QA routinely monitors shift turnover and control room activities.

Management involvement in QA is evident, staffing is adequate,'and

audit activities by the licensee are generally effective. However,

the E&R QA system for tracking corrective actions was noted to be

weak in that audit findings remained open for a long time. The multi-

departmental organization results in a somewhat fragmented QA program

whereby QA activities are divided among those departments. Despite

the fragmentation, the QA program is effective, but some implemen-

tation problems have been observed. For example, problems with the

storage of safety grade pipe, control over access to the storage

area, and mixing Q and non-Q items were identified. The licensee has

initiated corrective actions in this area, and this item will be

reviewed during future NRC inspections.

A well organized system is in place for tracking IE Bulletins which

results in adequate documentation regarding each item. The system

results in technically justified closeout when the reqd red actions

are completed. Implementation of the system indicates a large degree

of involvement and control by management. However, response to NRC

inspection issues is not always timely and limited management atten-

tion has been paid to this area. Additional management attention is

required to closeout open NRC inspection findings.

The LER process is adequate as demonstrated by NRC review of licensee

submittals. LERs are further discussed in Section 5.4.

No difficulty has been observed in obtaining the necessary records to

complete NRC reviews. Minor administrative errors were found in

the control of piping and instrument drawings (P& ids) and the main-

tenance of controlled copies of procedures. These problems identi-

fied were not of any major significance, however, it was determined

that Quality Assurance had identified similar problems in three pre-

vious audits (October 1982, November 1983, and February 1984), thus

indicating that in*tial licensee corrective actions were inadequate.

Subsequent corrective action in these deficient areas resulted in

overall improvements in document control.

r

16

The previous SALP assessment recommended that the licensee move for-

ward with the independent safety assessment activities. The licensee

has established a functional onsite Independent Safety Engineering

Group (ISEG). A concern with the simultaneous inoperability of the

containment cooling subsystem and one diesel generator resulted in

the licensee initiating a daily review by the ISEG of safety equip- '

ment out of service and the effect on plant operations. Further

licensee review of ISEG activities appears warranted to move clearly

' define its functions and responsibilities.

The licensee's training program has resulted in four operators and

three senior operators being licensed with only one operator

candidate failing an NRC written examination. In addition, three

candidates passed the senior operators examination as part of

intructor qualifications. No significant areas of weakness were

noted during the examinations and no suggestions for improvement

in training programs were made as a result of the examinations.

Overall, the licensee's replacement operator training program

appears to be satisfactory as evidenced by performance on NRC

administered examinations.

Conclusion:

Rating: Category 2

Trend: Consistent

Recommendations:

Licensee

Evalute the causes of the forced outages and unplanned scrams with

respect to plant operations, maintenance and testing activities.

NRC

Review licensee's actions from the appraisal plan recommendations

resulting from the NRC Order. Observe the offsite review committee

activities.

_ . - . _ . _ _ _

. __

, _ _ - _ .

17

4.2 Radiological Controls (9%)

Inspection efforts in this area included 10 inspections by Radiation

Specialists in the program areas detailed below. Day-to-day review

of ongoing activities was provided by the resident inspectors.

The overall area of radiological controls has degraded primarily due

to poor performance in radiation protection. Problems were noted in

several of the program areas reviewed. The Unit 2 pipe replacement

outage placed a strain on the radiological controls area. During the

previous assessment period, improvement frem Category 3 to Category 2

performance was noted. During this a m ssment period, programmatic

weaknesses were noted in radiat 6 protection and transportation.

Radiation Protection

Eight inspections, incitding six special inspections relating to the

piping replacement radittion protection program, identified problems

in the areas of training and qualification of personnel, in

procedural adherence and 10 assessment and control of radiological

conditions.

The licensee's radiation prctection supervisory personnel and quality

assurance activities were at times ineffective in problem identifica-

tion and correction. Responsibility for assessing the radiological

practices associated with on going radiological operations appeared

fragmented.

The apparent inability on the part of the licensee to take effective

corre tive action to prevent recurrence of radiation protection prob-

lems .3 of concern. In June and August 1984, the licensee did not

provide specific radiological exposure controls in radiation work

permits nor did they thoroughly evaluate radiological conditions

during the Unit 2 drywell work. In February'1985, the licensee again

did not provide specific radiological exposure controls in radiation

work permits nor did they evaluate the radiological conditions asso-

ciated with work on the "81A" valve of the RHR system. The corrective

action system did not recognize nor address a problem in radiological

controls involving valve "81A" on February 3, 1985. As a result, a

similar problem occurred on February 10, 1985 at the same valve with

a significant potential for serious radiation exposures to drywell

workers. At the March 4, 1985, Enforcement Conference, the licensee

presented additional management controls to address this concern for

recurring radiation protection problems. A number of immediate cor-

rective actions were implemented by the licensee, and reviewed as

being satisfactory by the NRC. Further improvements in this area

remain to be completed.

Occasional poor understanding of and adherence to radiation protection

procedures were noted. Examples include: correction factors were

not developed and applied to personnel mpnitoring devices; Health

<

'

18

Physics technicians, assigned to the piping replacement, were not

trained in four radiation protection procedures defining their duties

and responsibilities; dosimetry personnel did not receive formal

training and determination of their competency in the tasks assigned

to them; a radiation worker failed to exit the drywell promptly when

his audible-alarming dosimeter indicated his administrative dose

limit had been reached; several radiation workers entered valve "81A"

without adequate knowledge of the radiological status of their work

area; procedures for operation of the whole body counting system were

not provided; guidance for the issuance and use of extremity and

other supplementary personnel monitoring devices was not provided;

and, source checks for operability of audible-alarming dosimeters

used to control exposures in high radiation areas were not required.

Licensee corrective actions were implemented for each deficient con-

'ition. Corrective action for most of these items have been com-

p.eted and the review of the remaining items is pending.

The licensee's exposure control program is good as evidenced by main-

taining personnel radiation exposure within the estimates for the

Unit 2 refueling / outage. No personnel overexposures occurred during

the period.

-

'

The licensee's facilities and equipment were reviewed during the asses-

sment period and were found to be generally adcquate to support normal

and outage operations.

Management attention was directed to providing a defined ALARA program

to support Unit 2 piping replacement. During the planning and pre-

paration for the piping replacement, th piping replacement contractor

developed instructions for the pre-job planning to control radiation

exposures, mockup training for piping replacement personnel and radia-

tion exposure tracking throughout the operation. The licensee kept

abreast of other ALARA programs for BWR pipe replacement outages and

considered their experiences in Peach Bottom ALARA planning. The

licensee adopted the ALARA instructions and implemented them into

controlled station procedures. However, the licensee did not ade-

quately review the interface between the ALARA instructions and

existing station procedures. Two procedures, with differing require-

ments, were used to identify, report and correct radiological defi-

ciencies. When identified by the NRC, the licensee promptly took

action to make the procedures comparable.

Radioactive Waste Management and Effluent Monitoring

s

The review of the radwaste organizational structure indicated that it

was consistent with Section 6 of the licensee's Technical Specifica-

tions.

19

Two inspections, including the Operations Assessment Team Inspection,

identified several problems and weaknesses in the licensee's radwaste

program primarily due to an occasional lack of management attention

to detail to assure quality. No effluent release limits were exceeded.

The review of the licensee's selection, training and qualification

of personnel indicated a weakness in the training program to

maintain proficiency of the radwaste staff. The licensee did not

have a periodic retraining program for chemistry technicians

performing'sufveillance tests on liquid radwaste equipment.

Actions to ensure that safety evaluations were completed for con-

~

tractor-op'erated temporary radioactive. waste disposal operations to

support UnTt'2 pipe replacement were not taken by the licensee prior

to their arrival and setup for operation. When the lack of safety

evaluations"was identified by the NRC, the licensee took prompt

action to prevent waste disposal operations before the safety evalua-

tions were completed.

The review of the licensee's radwaste quality assurance program

indicated that audits of the radwaste program were performed in accor-

dance with licensee requirements. However, a problem with assuring

compliance with 10 CFR 61.56 was noted. In December, 1984, a cask

containing solidified resins from the Unit 2 pipe decontamination

released a flammable gas and a radioactive aerosol which resulted in

measurable contamination and intake of radioactive materials by two

workers. The Ticensee did not properly evaluate the generation of

the gas and its potential release during handling preparatory to ship-

ment. The licensee added precautionary measures for future radwaste

processes and has initiated a formal evaluation of the radwaste pro-

gram at Peach Bottom.

One Licen'ees Event Report (LER) was issued by the licensee in this

area (LER 2-84-06). In March, 1984, a leak in the "2B" RHR heat ex-

changer was discovered which resulted in a discharge of approximately

65 microcuries per day, and an estimated total release of 1,170 to

2,150 microcuries to the environment. The "2B" RHR heat exchanger

was repaired and returned to service.

'The licensee' implemented a program to reduce the amount of solid rad-

waste at the station. This program is referred to as " green is clean".

'(The clean' trash receptacles are painted green.) This program has

reduced the amount of solid radwaste generated on site.

~

Transportation

,

- An inspectio,n of the transportation program identified several

'p.oblems primarily due to an ineffective training program for the

lice,nsee's staff. The training program in transportation did not

.

!

[:

20

- properly train the Radioactive Material Coordinator.and non-licensed

operations personnel in NRC or DOT Regulations to assure that suit-

able proficiency was achieved and maintained. Non-licensed opera-

tions personnel were not trained in NRC and DOT Regulations and

appropriate procedures during-1981, 1982 and 1983 as committed to the

NRC-by the licensee in response to Bulletin No. 79-19. By December

1984, the Radioactive Material Coordinator, Shift Supervisors and the

non-licensed operations personnel had received training.

-The lack:of an effective training and qualification program in

transportation req'uirements and procedures was a major contributing

factor to an inade

tions and led to p'quate

roblemsunderstanding of theand

in classification transportation

certificationregula-

of ship-

ments. Three waste _ shipments identified were improperly classified.

The. Shift Supervisor certified that the shipments were properly

classified when they were not. The licensee revised the appropriate

procedures and counseled the individual involved.

Although the licensee's quality assurance audit program identified

the' lack of training, the audit-program for transport packages

did'not address the applicable criteria of a quality assurance

program for' transport packages as defined in Appendix B, 10 CFR 50.

This weakness suggests a lack of technical expertise in transport

package reviews conducted by the quality assurance organization.

Conclusion:

Licensee performance in radiological controls has degraded since the

last assessment period. Increased management attention is required

in work planning, training, procedures and corrective action.

Rating: Category 3

Trend: Consistent

Recommendations:

Licensee

Conside'r a third party audit and assessment of corporate and onsite

radiological controls and related activities.

'

NRC

Within six months, conduct a team inspection and perform an NRC

assessment of radiological controls. Conduct a licensee management

~

meetirig~ to discuss licensee actions and current status of the Peach

Bottom radiological control program.

,

21

4.3 Maintenance (8%)

Maintenance activities were reviewed during each resident

inspection. Various specialist inspections reviewed maintenance

and related activities during reviews of plant modifications,

responses to IE Bulletins, reviews of corrective and preventive

maintenance programs, and reviews of maintenance associated with

the Unit 2 pipe replacement outage.

Last assessment period maintenance was evaluated as Category 2.

Deficient areas included lack'of aggressiveness with respect to

minor maintenance items, maintenance performed using measuring and

test equipment that was out of tolerance, and inadequate overview of

vendor activities engaged in maintenance.

Overall, improvement was noted during the current assessment

period. Management is appropriately involved in the maintenance

programs and associated activities. The maintenance organizations

are well staffed with knowledgeable and experienced supervisors and

craft. Managem nt and engineering personnel are directly

involved in support of maintenance activities. Large maintenance

tasks are well planned and executed. Training and pre-job briefings

are conducted adequately in order to minimize the maintenance

activities' impact on overall schedule and to ensure that the

maintenance tasks proceed smoothly. This is evidenced by the

recent control rod drive (CRD) changeout at Unit 2. The maintenance

was well planned, training was given (including mockup training) to

individuals involved, pre-job-briefings occurred, the ALARA program

for the changeout was excellent, and problems were handled

adequately as they occurred. In all, the CRD changeout activity

and associated maintenance tasks went well and on schedule.

Maintenance is adequately conducted in accordance with administrative

procedures and specific maintenance procedures. Maintenance proce-

dures are detailed step by step and provide the maintenance techni-

cians adequate guidance. Administrative controls associated with the

Maintenance Request Form (MRF) are adequate. A problem was noted

however, regarding maintenance procedures directly referencing

drawings (i.e., part No.) that were not attached as required. Also

several maintenance division administrative procedures were identi-

,

'

fied as overdue for their periodic review. The licensee reviewed

these procedures,'and initiated revisions as necessary. NRC review

of licenseo action is pending.

An inspection was conducted to ensure that maintenance activities

are given proper review for the identification of equipment

failures, trends and root causes, and that the documentation systems

are organized to support evaluations. A computerized system for

maintenance management and documentation is now being used to

22

l

provide a better capability for researching equipment history and

for trending equipment failures. The licensee is adequately

addressing repetitive equipment problems and searching for the root

causes of failures.

Major equipment deficiencies continue to receive prompt and

appropriate attention consistent with safety and technical speci-

fication requirements. Examples during the assessment period

include safety relief valve failures, ECCS pump and valve mal-

functions, main steam isolation valve (MSIV) leakage and safety-

related instrument failures. Corrective maintenance is at times not

successful in repairing the deficient condition. However, problems

are detected during post-maintenance checkout and testing, and

repairs are initiated again. For example, additional repair of MSIV

seat leakage was required after initial repairs did not correct the

leakage.

During the assessment period, the licensee completed the development

of an upgraded preventive maintenance (PM) program and began its

implementation. This PM system has the capability to provide

feedback information for maintenance procedure revision.

Control of major modifications by the use of a Construction Job Memo

is effective for simple modifications. The Construction Job Memo

details the scope of work and references drawings, specifications and

construction procedures and appears to be implemented effectively.

More complicated modifications are controlled by the use of work

instructions for each item of the modification.

Personnel are well qualified and familiar with the work

demonstrating an effective training program. QA/QC training

regarding applicable procedures is provided. Strong management

involvement and control is demonstrated by continuing surveillance

and coordination by licensee personnel. An example of this was the

torus modification requirements and work procedures which were

clearly established and well organized. Hold points for QC and ANI

inspection were clearly identified.

Management involvement was further demonstrated by the issuance of

general and special instructions which controlled the work. Doc-

umentation for completed work was readily available and complete.

Changes are closely controlled, approved by engineering and

independently reviewed.

1 The long delays associated with the documentation of change approval

'

points out a need for increased management attention in this area.

Further evidence of the need for increased attention was identified

in the case of electrical modifications where installation drawings

were found to lack sufficient detail for their intended use and

~

inexperienced personnel reviewed those drawings.

_ _

23

Evidence of strong management involvement was identified in the

areas of post maintenance testing. Test requirements are reviewed

by management,-testing is completed in a timely manner and the

licensee's tracking system assures that testing is completed prior

to system startup.

-In summary, maintenance is well planned and performed in accordance

with procedures. Management is involved in all aspects of

maintenance activities.

Conclusion:

Rating: Category.1

Trend: Consistent-

Recommendations:

Licensee

None

NRC

None

24

4.4 Surveillance (3%)

In the current assessment period, one region-based inspector

conducted an inspection of the containment local leak rate test

program. Specialist inspections by region-based inspectors also

reviewed surveillances applicable to health physics, fire

protection, refueling equipment, maintenance activities, snubbers,

emergency preparedness, and environmental monitoring. Resident

inspectors reviewed selected program areas each month.

The previous assessment period noted the following problems

regarding surveillance test activities: improper restoration from a

calibration procedure resulting in primary containment integrity

degradation, use of incorrect revisions of surveillance test

procedures, and programmatic weakness with the control of measuring

and test equipment.

Inspections during this period confirmed that the surveillance

testing programs are technically sound and generally well planned.

Staffing of the various groups responsible for conducting sur-

veillance testing appears adequate. Surveillance test procedures

continue to be systematically upgraded to provide for better

control, improved documentation, and independent verification as an

integral part of the procedure. Management involvement is evident

in ensuring that changes to surveillance requirements, such as those

resulting from Technical Specification Amendments, are properly

implemented.

Some !mplementation problems associated with the surveillance test

program occurred during this assessment period. These problem areas

were associated with the escalated enforcement action early in

assessment period, and are as follows: surveillance tests not

completed after the tests had begun, specific steps required by TS

not denoted as such, inadequate review of r rveillance results by

technical personnel and failure to follow a surveillance test

procedure. These deficiencies, along with other problem areas, are

currently being addressed in the licensee's response to the NRC

Order of June 18, 1984. Surveillance procedures are being reviewed

by an appraisal team as required by NRC Order (Section 4.1).

Quality Assurance (QA) involvement in surveillance is generally

appropriate. QA audits include a broad scope review of completed

surveillances. Surveillances are observed during audits of indi-

vidual functional areas.

Containment local leak rate testing (LLRT) for Unit 3 was reviewed

in detail during the assessment period. LLRT is generally per-

formed in accordance with appropriate test procedures, with

calibrated instrumentation, by qualified test personnel and with

adequate QC monitoring. One area of concern was identified with

regards to the licensee's method of tracking and computing as found

leak rate value at time of plant shutdown.

__

25

The existing method does not adequately demonstrate compliance with

10 CFR 50, Appendix J, combined local leak rate test acceptance

criteria. License review of this calculational method is in

progress.

In summary, although problems were identified early in the

assessment period, the surveillance program has improved, with

further-improvement attainable through the following: continued

management, supervisory, and QC attention _ to upgrading of attention

to detail, especially with respect to equipment lineups; and

supervisory and management attention to the thorough review and

evaluation of test data, as well as to identification and

correction of deficiencies in the approved procedures.

Conclusion:

Rating: Category 2

Trend: Consistent

Recommendations:

Licensee

Increase management, supervisory and QC involvement in surveillance

test conduct, test review, system restoration and procedure upgrades.

NRC

None

[.

i

I

'

_

26

4.5 Fire Protection / Housekeeping (1%)

In the current assessment period, fire protection and housekeeping

was reviewed during one specialist inspection and as part of each

resident inspection.

During the previous assessment period the licensee made significant

improvement in the areas of housekeeping and in plant fire

protection. Fire brigade training, fire barrier integrity,

maintenance and coordination of the fire protection program were

identified as areas requiring improvement and increased management

attention.

During the current assessment period continued efforts of manage-

ment to maintain good housekeeping and fire protection controls were

apparent. Management administrative controls were strengthened and

changes were incorporated to increase monitoring activities

regarding fire brigade personnel training which resulted in

maintaining the required level of training. Additionally,

procedures were revised to reflect the requirements of current

regulations and the present site organization. The site position of

Fire Protection Coordinator which had been vacant for sometime, has

been filled.

A continuing weakness that is evident is the maintenance of fire

barriers. This is attributed to a lack of management attention in

the pursuit of resolutions to related issues. This is evidenced

by the following conditions noted regarding fire doors: door

closer not working properly, doors found open and unlisted doors (UL

label missing).

Access to fire fighting equipment stations was identified as a

problem area during previous assessment periods. One instance

of blocking fire extinguisher access was noted during this assess-

ment period on the Unit 2 refueling floor. The licensee subsequently

installed fire equipment location signs on both units' refueling

floors.

During the annual emergency exercise, the scenario included a fire

in the auxiliary boiler building. This required activation and

response of the on-site fire brigade, and assistance of the off-site

fire organization. The fire brigade responded promptly to the fire

scene and there were excellent coordination and strategy discussions

between the fire brigade leader and the off-site fire chief. Minor

exercise deficiencies were noted and were corrected by the licensee.

With Unit 2 in a pipe replacement / refueling outage during 11 months

of the assessment period and during other outages associated with

Unit 3, housekeeping conditions were monitored closely. A few small

fires occurred that were associated with poor housekeeping activities.

_

27

The site QC group was given responsibility for evaluating house-

keeping and they appeared to be effective in early identification

and resolution of housekeeping discrepancies. Housekeeping

.

conditions, noted problem areas and corrective actions were

routinely discussed at the daily and weekly outage meetings.

During the special Operations Assessment Team Inspection for Unit 2,

noted deficiencies in the drywell regarding housekeeping and tool

-

control were observed. Specific problems included: small tools

scattered about, metal machining chips not collected, removed

mirror insulation left laying around, and hoses strewn about.

These conditions increased the possibility.of the instrusion of small

items into piping systems, contaminated injury to workers and other

unwarranted conditions. When these items were brought to the atten-

tion of the licensee, drywell work was stopped and a general area

cleanup was immediately conducted. Subsequently, the drywell con-

ditions were monitored periodically and found to be acceptable.

Overall, fire protection and housekeeping has improved. Continued

management attention to the identified weak areas will lead to

further improvements.

Conclusion:

Rating: Category 2

Trend: Improving

Recommendations:

Licensee

Maintain senior corporate and station management attention toward

good housekeeping and fire protection habits at the station and seek

methods for further improvements in this area.

NRC

None

__ . _ . _ _. . _ _ _ ___ _ ._ _ __

. _

$

28

4.6 Emergency Preparedness (10%)

Two region-based inspections were conducted during the assessment

period, including the annual emergency exercise. The resident

inspectors monitored the licensees' performance throughout the

period.

During the previous assessment period, inadequacies were identified

in the management review and administrative followup of emergency

preparedness training programs. Significant weaknesses were '

. identified in the Health Physics area during the June 1983 exercise.

A confirmatory letter was issued outlining the corrective action

commitments. A successful remedial in plant Health Physics drill was

observed by the NRC in August 1983.

During this assessment period, an annual full participation emergency

exercise was conducted in October, 1984. The area of Health Physics

control improved significantly compared to the previous exercise. A

weakness with the review of procedures for compatibility with pla'nt

equipment was identified during the exercise. The emergency

procedure which identified emergency action levels based on the

reactor building and main stack radiation monitors specified

emergency action levels that were above the full scale capabilities

-

of the associated radiation monitoring instrumentation. The licensee

modified the appropriate emergency procedure and the NRC found the

procedure acceptable.

A subsequent inspection in January 1985 identified problems in 3

areas. Personnel were identified who did act have all of the

' required training for the positions in the emergency organization to

which they were assigned. Appendices to the emergency plan, which

contain the names and telephone numbers of personnel to be contacted

in an emergency, were 17 months overdue for updating. Some names and

numbers were incorrect. The third weakness was the licensees audit

program which did not follow up on previously identified deficiencies

in the emergency preparedness area. Licensee corrective actions and

NRC review of the actions, are pending.

The licensee.is currently revising and updating the emergency plan

procedures and training program. A permanent site Emergency

Preparedness Coordinator position has been established rather than a

rotating 1 year assignment. A strengthened corporate management

involvement has been apparent in recent activities.

Conclusion:

.

Rating: Category 2

Trend: Improving

. __ _ _. . . - . _ . _ _ __ _ _ - . _ _ _

. . . . . -_ ..... .. .. . . .... - . , -- . - . .

,

.

29

.

Recommendations:

-

-

Licensee

,

~

~

Continue current level of. corporate management' involvement to further

m improve.this area.

. NRC'

None

,

t

'

?

4 ,

d

-

1

%

i

1-

.

t

4

e

$

&

e -,.e , - - - . ,.e,, . - - . - ..e-- , , ,,,-,..,.w-,4-,,r.w.,--, , ,_,en,,. . _ , .- - awr,,, , . , ,,, , . ,, -,,,_,.g.,,,,_,.m, , - ,

_

30

4.7 Security and Safeguards (4%)

Three unannounced physical protection inspections were performed

during the assessment period by region-based inspectors. Routine

resident inspections continued throughout the assessment period.

During June 1984, with Unit 2-in a major outage, a physical security

inspection noted. numerous problems and an enforcement conference

resulted. NRC inspection findings were addressed by the licensee

during the enforcement conference and actions to prevent recurrence

for several issues were provided at that time. More complex issues

required additional review and actions by the licensee in order to

develop appropriate corrective actions. The security problems were

cumulatively cited at the Level III severity for the licensee's

failure to exercise proper supervision and oversight of the contract

guard force.

In reviewing the security deficiencies that were observed during the

outage, of particular concern was the fact that members of the

security force did not respond to alarms in vital areas of the

plant. The failure to respond to alarms was compounded by the fact

that the capacity of the security computer to monitor alarms had

been reached. Security force members apparently did not recognize

the seriousness of the problems nor did they escalate their

awareness that the problems existed. Neither the contract security

supervisors nor licensee management were providing sufficient

oversight of the guard force; and, they were either unaware of or

did not recognize these events as a serious security system

breakdown. Further, the contractor's security supervisors and

licensee security management were aware of the potential for the

computer overload problem, but did not provide for this

contingency'and take the appropriate corrective action.

The need for an assistant site security supervisor position was

recognized by the licensee prior to the outage. However, the

licensee management failed to give adequate priority to the filling

of this position. As a result, a position essential to maintaining

licensee oversight of the contract guard force, particularly

important during a major maintenance outage, was not filled. This

vacancy, along with the resulting poor corporate and site security

management oversight during the outage, are considered to be the

major contributors to the security program problems identifed during

a June, 1984 inspection. However, security program implementation

during periods of routine plant operation was considered adequate.

The security contractor's general performance level decreased

considerably since the last assessment period, as evidenced by the

problems involving ineffective supervision, personnel not

following procedures and inadequate response to alarms. Also, the

quality of security force training appeared to have decreased or

-

N

31

was less effective during this period, as evidenced by an increase

in personnel errors. This may have been exacerbated by inadequate

management attention.

Seven security event reports were submitted pursuant to the

requirements of 10 CFR 73.71. Three reports pertained to computer

failure, three described security personnel errors (two involving

placement of vital area doors in access, and the other, a guard

intentionally alarming a zone), and one involved evacuating the

Central Alarm Station because of a fire protection system alarm.

Although all events were adequately handled, the three events

involving personnel errors could have resulted in undetected

access to vital areas. Further, the report describing the CAS

evacuation was inaccurate as initially submitted. NRC review of

the incident revealed that the inaccurate report was the result of

_ poor communication between the site security supervisor and contract

security management and inadequate follow-up of the incident by

security management. A corrected report was subsequently submitted.

The licensee was responsive to regional concerns and to questions

regarding 3 revisions to ths Security Plan and 1 revision to the

. Training and Qualification Plan. The format and content of these

revisions were considered satisfactory.

Conclusion:

Rating: Category 3

Trend: Consistent

Recommendations:

Licensee

Increase licensee management oversight and control of the contractor

security force on a day-to-day basis. Provide for periodic assessment

of the adequacy of program implementation.

NRC

Resident Inspectors provide monitoring of improvements for licensee

actions. Region I perform a programmatic review of security and safe-

guards within 6 months to assess licensee performance.

32

4.8 Refueling /0utage Activities (31%)

In the current assessment period, both units experienced outages.

Unit 2 was shutdown on April 28, 1984, to replace recirculation

system and RHR system pipe inside the drywell and to refuel. A large

number of other modifications were done while Unit 2 was down. The

unit has been out-of-service from April 28, 1984, through the rest of

the SALP report period. Unit 3 was shut down in February 1985, for

about three weeks to conduct required maintenance and surveillance

testing. This assessment focuses on the Unit 2 activities which have

been extensive. The outage required large numbers of support per-

sonnel, both licensee and contractor. During this time staffing

appeared adequate except for isolated security and radiation protec-

tion areas discussed in Sections 4.2 and 4.7, respectively. Inspec-

tions did not reveal any problems with lack of adequate staffing

during the outage.

Aspects of outage activities assessed during this period included QA

and QC, modification control, modification acceptance testing, ALARA

activities, welding, purchasing, ISI, NDE, control of contractors,

committee (PORC) activities, management control and involvement,

procedural adequacy and adherence, planning, audits, and response to

generic issues. The inspections found that the technical aspect of

the pipe replacement activities is a strength.

Pipe replacement management personnel were actively involved in the

project. Daily outage meetings and biweekly Project Review Meetings

were held to keep all management knowledgeable of the project.

Contractor site management was intimately involved in day-to-day

program activities. The licensee's project engineers were found to

be knowledgeable of day to day activities of the contractors and

interfaced well with corporate, site and contractor personnel. Early

in the project it was determined that contractor specifications were

used for procurement prior to obtaining licensee approval and this

caused some problems. The licensee indicated that he had reviewed a

draft of the specification to assure compliance with the ASME code

and later made changes which were enhancements beyond the Code re-

quirements. The prior approval of draft specifications caused the

problem with the weld buildup, since the specification enhancement

prchibited buildup, on pipe pieces received by the licensee. The

licensee initiated corrective action to evaluate each pipe piece for

conformance to code and specification requirements.

Management involvement and control in assuring quality was demons-

trated by the decisions regarding surface conditioning of the replace-

ment pipes to aid in ultrasonic examination results interpretation.

Further control was evidenced by the establishment of plans and sche-

dules to assure an orderly progression of the work activity and to

assure that ASME code requirements were met regarding preservice

inspection. In the area of nondestructive examination management

!

33

control was demonstrated by the thoroughness and effectiveness of the

licensee audits which in two separate instances, identified vendor

errors regarding radiographic film interpretation.

The licensee shows strength in the resolution of technical issues

from a safety standpoint. The licensee implemented Quality Assurance

provisions that exceeded requirements in a number of instances. For

example, they added more conservative requirements to the contractors

ASME approved QA program in that they required the contractor to

include safety related nonpressure retaining parts in the ASME program.

The licensee also places a strong emphasis on QA observations, at

random times, of on going activities.

During this assessment period, the licensee has been responsive to

NRC initiatives. The staff had identified a concern regarding the

lack of provisions taken to assure that all plant systems and com-

ponents that could be impacted by the pipe replacement program were

in acceptable condition prior to restart. The licensee formed an

experienced team (Major Outage Recovery Effort - MORE Team) of

engineers to be responsible for the activities associated with re-

storing to service drywell components and systems affected by the

outage. The MORE Team has developed a comprehensive set of tests to

cover all drywell activities and systems. In addition, the MORE

Team verified that components and systems were satisfactory and indi-

cated that CBI, PECo construction and PEco Electric Production were

all planning drywell walkdowns to check out components. The MORE

Team activities adequately addressed the NRC concern.

During the core alteration phase of the outage, operators were not

aware of a procecural requirement to verify refueling interlocks but

when the licensee was informed, he issued a comprehensive " shift-

meeting notice" dealing with responsibilities of operators during

core alterations. When concerns were identified regarding the ALARA

aspects.of replacement work on the N-2 nozzles the licensee stopped

all work on the nozzles until a decision was made on nozzle replace-

ment. The ALARA concerns were adequately addressed and nozzle work

resumed.

Training and personnel qualifications of outage workers were in

general good, because of the high standards set by the licensee.

Welders and NDE personnel were normally qualified to higher levels

than called for by the specifications. In addition, the licensee

E made extensive use of mockups for training and qualification which

helped keep radiation exposure within the outage specific ALARA

guidelines.

_ _ - . _ _ . ._- ____ __-_ _ ____ . ____.. . _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

34

Maintenance of industrial and fire safety during the outage has been

adequate. There have been relatively few accidents during the

outage. Fires have been minor and handled effectively by the

licensee.

Conclusion:

,

Rating: Category 1

, Trend: Consistent

Recommendations:

Licensee

None

NRC

Continue routine inspection of recovery activites and provide

specialist inspectors for Unit 2 restart activities.

.

i

- . , --, ,. -

-e- 9. - , ,- , ,-,-,-,.,e , - - , , - , . . - , . . - . , , - - . . - - . , . . . , - - , . , , - - - - , - - , .

- ~.

r.-

-

35

4.9 Licensing Activities

The approach used for this evaluation was to select a number of

licensing issues which involved a significant amount of staff effort

or which related to important safety or regulatory issues for the

period from January 1, 1984 to March 31, 1985. In most cases the

staff applied the evaluation criterion for the performance

attributes based on their first hand experience with the licensee

or with the licensee's submittals. This areas was rated as Category

1 during the previous assessment.

Actions during this period included licensee requests for license

amendments, responses to generic letters, and various submittals of

information for multi plant and NUREG-0737 actions. Active actions

during this period are classified below. A total of 74 licensing

actions were completed as noted in Table 6. In addition to these

specific issues, the licensee was evaluated for overall general per-

formance in the many day-to-day issues which arise.

In general, the licensee's management participated in licensing

activities in a manner appropriate for the significance of the

issue. There has been strong management involvement concerning

licensing activities pertaining to Unit 2 pipe replacement and

continued oversight of the Appendix R Fire Protection Program.

A trend developed in this period where management involvement

and control did not appear to be fully functional. One

such example was a TS change request pertaining to an exemption

from local leak rate testing of MSIVs which appeared to indicate

poor planning and assignment of priorities. Another area where

management involvement appeared to be lacking is the overall plan

and design of the Safety Parameter Display System (SPDS) where the

proposed SPDS has not met the minimum guidance of NUREG-

0737, Supplement 1.

The licensee's approach to issues has been both technically sound

and thorough in almost all cases. Resolutions are timely in almost

all cases and conservatism is routinely exhibited when a potential

for safety significance exists. The licensee's approach to

equipment qualification, post-accident sampling, and increased core

flow TS changes all showed above average, technical approach and

resolutions during this period.

However, in the last 6 months of the assessment period, there has

been a noticeable decline in the licensee's usually timely response

and resolution of licensing issues. This decline apparently coincided

with the increased activity in licensing activities at Limerick. The

licensee should give more attention to the structuring of its licensing

staff in order to accommodate the addition of the Limerick facility as

an operating plant.

g-

'

l

36

Also, the licensee should give more attention to the significant ,

hazards consideration determination that are submitted with each TS

change request. Specifically, the licensee should prepare more

explicit arguments for each of the criteria that must be addressed

.in reaching a significant hazards determination and thereby reduce

L

the time required to publish the Federal Register pre-notice.

- The licensee has continued to show a highly effective tracking

system for responding to NRC requests and almost always alerts

the staff in a timely fashion when an extension to a particular

submittal is needed. Generally, issues are resolved in a timely

'

fashion with acceptable resolutions proposed initially in most

cases.

Conclusion:

Rating: Category 1

Trend: Declining

Recommendations:

'

Licensee

, None.

NRC

None.

l

l

l

i

l

'

!

i.

, _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ . _ _ _ _ _ _ _ _ _

37

V. -SUPPORTING DATA AND SUMMARIES

5.1 Investigations and Allegations Review

NRC Region I received and evaluated four allegations during . e

assessment period. The allegations are summarized as follows:

--

CAS attendant overloaded with administrative duties and impact on

security job.

--

Contractor and licensee not meeting ALARA requirements.

--

Poor security practices effecting HP programs.

--

Deliberate misuse of emergency sirens.

5.2 Escalated Enforcement Actions

1. Civil Penalties

--

Notice of Violation and Civil Penalty of $30,000.00 dated

June 18, 1984 associated with violations (Enforcement Action

84-39) regarding excessive heatup rates, an unplanned reactor

pressurization, and excessive rod scram times.

2. Orders

--

Order dated June 14, 1984, confirming commitments to

implement Suaolement 1 to NUREG-0737, " Requirements for

Emergency Re:,ponse Capability" based on commitments to NRC

Generic Letter 82-33 dated December 17, 1982.

--

Order modifying license dated June 18, 1984, regarding

violations associated with Enforcement Action 84-39 requiring

the licensee to submit and implement a plan for an appraisal

of: (1) the process for performing safety evaluations and

reviews of procedures pursuant to 10 CFR 50.59 to determine

if the process is currently effective, or if improvements are

needed; (2) plant and system operating procedures to verify

that existing procedures are consistent with technical

specification bases, and those sections of the FSAR

concerning systems necessary to mitigate Design Basis

Accidents, and do not involve unreviewed safety questions;

and (3) the program for ensuring that employees

involved in the review and approval of operating procedures

remain cognizant of the licensing bases.

3. Confirmatory Action Letters

None.

-- - - . - - - - - - - - - - - - - - - - - - - - _ - - - - - - - - - _ - - -

,

38

4. Enforcement Conferences

-

An Enforcement Conference was held to discuss the findings of

Inspections 50-278/83-32, 50-277/84-01, 50-278/84-01, 50-

277/84-03 and 50-278/84-03 relative to individual rod

scramming and LCO violations on April 12, 1984.

-

An Enforcement Conference was held to discuss the findings of

Inspection 50-277/84-19 and 50-278/84-10 relative to security

plan violations on July 31, 1984.

-

An Enforcement Conference was held to discuss the findings of

Inspection 50-278/85-07, a Unit 3 event regarding simultaneous

diesel generator inoperability and containment cooling on

February 8, 1985.

-

An Enforcement Conference was held to discuss findings of a

radiological event during the Unit 2 outage from Inspection

50-277/85-11 on March 4, 1985.

5.3 Management Conferences Held During the Assessment Period

1. SALP Management Meeting at Peach Bottom Atomic Power Station

on March 2, 1984.

2. Management meoting to discuss licensee plans and controls for the

Unit 2 piping replacement outage on April 5, 1984.

5.4 Licensee Event Rrnorts (LERs)

Forty-one LERs were submitted during the assessment period. The 17

LERs for Unit 2 and 24 for Unit 3 are characterized by cause in Table

1. LERs reviewed include 84-01 through 84-16 and 85-01 for Unit 2;

and, 84-01 through 84-16 and 85-01 through 85-08 for Unit 3. Four

causally-linked event sets were identified:

-

Five LERs (3-85-01, 3-84-13, 3-84-15, 3-84-16, 3-85-04) all

involved inoperability of the HPCI turbine due to the inner

rupture disc (PSD-3-23-6) failure for Unit 3.

!

-

Three LERs (2-84-10, 2-84-16, 3-84-08) involved pipe cracking

indications for Units 2 and 3.

-

Eleven LERs (2-84-03, 2-84-07, 2-84-09, 2-84-15, 3-84-02, 3-84-06,

3-84-07,3-84-10,3-85-02,3-85-06,3-85-08) involved events

caused by personnel error. The errors were due to operating,

maintenance and test personnel.

-

Five LERs (2-84-01, 3-84-03, 2-85-01, 3-85-05, 3-85-03) involved

equipment failures encountered during surveillance testing.

I

39

The Office for Analysis and Evaluation of Operational Data (AE00)

assessed the Licensee Event Reports (LERs). The review covered a

majority of the LERs submitted during the assessment period. The

LERs submitted were adequate in each important respect with few

exceptions. All the LERs provided an abstract followed by:

(1)' description of the event, (2) consequence of the event, (3) cause

of the event and (4) corrective actions. The LERs provided clear

descriptions of the cause and nature of the events as well as-

adequate explanations of the effects on both system function and

public safety. The described corrective actions taken or planned by

the licensee were considered to be commensurate with the nature,

seriousness and frequency of the problems found. Table 1

provides additional observation from the AE00 review of the LERs.

In summary, the LERs indicates that the licensee provided adequate

descriptions of the events . None of the LERs reviewed involved

a significant event or serious challenge to plant safety.

5.5 Forced Outages and Unplanned Scrams

1. During the assessment period, Unit 3 experienced five unplanned

automatic scrams. As Unit 2 was in a refueling / pipe replacement

outage for the majority of the time, no unplanned automatic scrams occurred. Table 5 summarizes these scrams.

2. During the assessment period, the following unit forced outages

occurred:

--

Unit 2 - 5 forced outages, including 2 power reductions and

I shutdown for refueling.

--

Unit 3 - 19 forced outages, including 14 power

reductions / load level drops.

Table 5 summarizes these outages.

.

_ -- _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .____ _

_

'

l

T1-1

TABLE 1

TABULAR LISTING OF LERs BY FUNCTIONAL AREA

PEACH BOTTOM ATOMIC POWER STATION

Area Number /Cause Code Total

'1. Plant Operations 7/A, 2/B, 1/0, 7/X 17

2. Radiological

, Controls IX 1

-v 3. Maintenance 2/A, 2/X 4

4. Surveillance 4/B, 2/E, 4/X 10

5. Fire Protection 1/A, 1/B, 1/D, 2/X 5

, 6. Emergency

Preparedness 0

7. Security and

Safeguards 0

8. Refueling / Outage

Activities 1/A, 3/X 4

9. Licensing Activities 0

TOTAL 41

Cause Codes:

A - Personnel Error

B - Design, Manufacturing, Construction, or

Installation Error

C - External Cause

D - Defective Procedure

E - Component Failure

X - Other

AE00 Review of LERs

.The AEOD review of LERs included the following:

For Peach Bottom 2: 84-001 through 84-016 and 85-001

For Peach Bottom 3: 84-001 through 84-014 and 85-001 through 85-005

The LER review covered the following subjects and the general instructions of

~NUREG-016. The SALP review is presented with the topic review followed by

comments on that topic.

1. Review of LER for completeness

(a) Is the information sufficient to provide a good understanding of the

event?

The LERs provided sufficient data to give clear and

adequate descriptions of the occurrences, their direct consequences,

_ _ _. _ _ _ __ _ _ _ _ _ _ _ . _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ -

,.

T1-2

, Table 1 (continued)

root causes, and where known, corrective actions needed to prevent

recurrence.

-(b) Were the LERs coded correctly?

All coded entries reviewed appeared to be correct. However, there

were six LERs which did not specify the. failed component and

component manufacturer. These LERs were: 84-007,84-009,

84-013 and 84-014 for Peach Bottom 2; and 84-004 and 84-014

for Peach Bottom 3.

(c) Was supplementary information provided when needed?

Most of the LERs reviewed contained supplementary information.

The supplementary information provided was clear, concise and

adequate.

(d) Were follow-up reports promised and submitted?

The licensee submitted a follow-up report in every case reviewed

where such a commitment was made.

(e) Were similar occurrences properly referenced?

The licensee appropriately referenced similar prior occurrences

as necessary.

2. Multiple Event Reporting in a Single LER.

The licensee did not report any multiple events in a single LER.

3. Prompt Notification Follow-up Reports.

The region issued one PN for Peach Bottom 2 and three PNs for Peach

Bottom 3 during this review period. Two of the PNs issued should be

followed by an LER. Our review indicates that the licensee did issue

LERs84-008 and 84-011 for these two PNs. Both of these LERs were for

Peach Bottom 2.

In summary, the review indicates that based on the stated criteria, the

licensee.provided clear and adequate event reports during the assessment

period. No significant deficiencies were found in the LERs reviewed.

p

T2-1

' TABLE 2

VIOLATION SUMMARY (1/1/84 3/31/85)

PEACH BOTTOM ATOMIC POWER STATION

A. NUMBER AN0 SEVERITY LEVEL OF VIOLATIONS

Violations

Severity Level I O

Severity Level II O

Severity Level III 2

Severity Level IV 19

Severity Level V 7

B. - VIOLATION VS FUNCTIONAL AREA

Severity Level

Functional Area

III IV V

1 -Plant Operations 1 6 2

2 Radiological Controls * 0 7 3

3 Maintenance 0 1 1

4 Surveillance 0 0 1

5 Fire Protection / Housekeeping 0 3 0

6 Emergency Preparedness ** 0 1 0

7 Security and Safeguards 1 1 0

8 Refueling / Outage Activities 0 0 0

,

9 Licensing Activities 0 0 0

  • Inspection Report 85-11 issued, enforcement action pending as of May 13, 1985.
    • Inspection Report 85-03 not issued as of May 13, 1985.

= _ _ - - _ _ _ _ _ - _ - _ - - _ _ - _ _ _ _ _ _ - _ _ _ . - _ _ . _ . - . _ _ - _ . _ _ - .

. - -

.

T2-2

-Table ~2(continued)

C. SUMMARY

Inspection ~ Inspection . Severity Functional

' Report No. Date Level Area Violation

Unit 2 Unit 3

84-01 84-01 -1/5-20/84 III-CP* 1 Excessive heatup

rate, reactor

vessel pressuriza-

tion and excessive

rod scram times.

84-03 84-03 1/13-2/29/84 IV* 1 Operational pro-

cedural violations

84-02 84-02 1/16-20/84 IV 3 Failure to

adequately control

plant modification

activities.

84-03. 84-03 1/13-2/29/84 IV 5' Failure to

implement an

adequate fire

hydrant

maintenance

program

84-03 84-03 1/13-2/29/84 IV 1 Failure to report,

,

document and

properly disposi-

tion a

non-conforming

condition for the

torus vent header

84-07 84-07 3/1-4/20/84 IV 1 Failure to follow

SBGTS operating

procedure

84-07' 84-07 3/1-4/20/84 IV 7 Failure to

adequately control

a vital door area

84-08- 84-08 3/26-30/84 V 1 Failure to provide

adequate correc-

tive action

,

._. _ ._ --_- __ ________ _ ____ _ - _______- - __

.

T2-3

Table 2 (continued)

Inspection Inspection Severity Functional

Report No. Date Level Area Violation

Unit 2 Unit 3

84-09 84-09 3/26-29/84 IV 2 Failure to

,~

properly label

packages on radio-

active waste

84-09 84-09 3/26-29/8'4 IV 2 Failure to train

to NRC and DOT

guidelines

C4-09 84-09 3/26-29/84 V 2 Failure to verify

that shipping

manifests were

accurate

84-14 84-12 5/7-11/84 IV 1 Failure to provide

adequate cor-

rective actions

for audit and in-

spection findings

84-15 84-13 4/21-6/7/84 IV 2 Failure to post a

contaminated area

84-16 84-14 5/8/84 V 2 Failure to have

written approved

procedures for the

whole body

counting system

84-17 84-15 5/14-18/84 V 3 Failure to permit

evaluation of a

systems / components

performance

84-17 84-15 5/14-18/84 V 4 Failure to take

prompt corrective

action for sur-

veillance test

84-18 6/18-21/84 IV 2 Failure to train

HP technicians

,

. _ .

_ _ _ _ _ . _ _ ___________ _ _ -

T2-4

'

, Table 2 (continued)

Inspection Inspection Severity Functional

Report No. Date Level Area Violation

Unit 2 Unit 3

84-18 6/18-21/84 IV 2 Failure to pro-

vide specific

radiological

exposure controls

for RWPs

84-19 84-10 6/25-7/1/84 III** 7 Security plan

violations

84-20 84-16 6/8-7/15/84 IV 5 Failure to pro-

vide adequate

fire equipment

access

84-20 84-16 6/8-7/15/84 IV 1 Failure to

maintain adequate

document control-

84-22 7/16-20,23- V 1 Failure to main-

27/84 tain certification

requirements for

QC irspectors

84-24- 84-20 7/16-8/31/84 IV 1 Failure to perform

written safety

evaluation

84-25 84-21 7/20-23/84 V 2 Failure to follow

TLD procedures

84-31 84-25 9/1-10/10/84 IV 2 Failure to post a

-

  • radioactive con-

taminated area

84-33 84-27 10/16-18/84 IV 6 Failure to provide

accurate

initiating con-

ditions for

emergency action

levels of

Emergency Plan

, _ . _. _ . _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ - _ _ _ _ - _ _ . . - _ _ _ _ _ _ _ _ _ __ __ __-_-_.

_

T2-5

Table 2 (continued)

Inspection Inspection Severity Functional -

Report No. Date Level Area Violation

Unit 2 Unit 3

84-40 84-19 12/10-13/84 IV 5 Failure to main-

tain fire barrier

integrity

84-42 84-34 12/17-21/84 IV 2 Failure to provide

a QC program for

radwaste shipments

85-03 85-03 1/8-11/85 XXX 6 Two potential

violations

associated with

emergency plan -

training and

updating

emergency noti-

fication phone

lists.

85-11 2/13-15/85 XXXX 2 Potential

violations

associated with

radiation

protection and i

radiological

controls

  • EA 84-39 -
    • EA 84-94

XXXInspection Report not issued as of May 13, 1985

XXXXInspection Report issued, enforcement action pending as of May 13, 1985

w___

T3-1

TABLE 3

INSPECTION REPORT AiCTIVITIES (1/1/84 - 3/31/85)

PEACH BOTTOM ATOMIC POWER-STATION

Reoort Inspection Hours Areas Inspected

Unit 2 Unit 3

,

84-01- 84-01 118 Operational safety regarding l

individual rod scramming

activities

84-02 84-02 29 Plant Modification

Activities

84-03' 84-03 268 Operational Safety

84-04 84-04 38 Torus modification

requirements and IE

Bulletin 78-11

84-05 84-05 12 Review Eastern Testing

and Inspection, Inc.,

84-06 84-06 36 Security

84-07 84-07 172 Operational Safety

84-08 84-08 112 Previous inspection

findings, corrective and

preventive maintenance,

and document control

84-09 84-09 32 Transportation activities

'

84-11 84-11 33 Enforcement Conference

84-12 65 Review licensee's

preparations relating to

radiation protection for

planned modification to

recirculation and residual

heat removal (RHR) piping

84-13- 28 Recirculating and RHR pipe

replacement

,

- 84-14 84-12 75 QA/QC Program and the

piping replacement program

. - _- ._ -- -

T3-2

Table 3 (continued)

Report Inspection Hours Areas Inspected

Unit 2 Unit 3

84-15' 84-13 233 Operational Safety

84-16 84-14 8 Bioassay whole body

counting program

84-17 84-15 104 Corrective and preventive

maintenance programs

84-18 70 Radiation protection

program ,

84-19 84-10 70 Special Security

Inspection

,

84-20 84-16 147 Operational Safety

'

84-21 84-17 31 Recirculating and RHR

pipe replacement

84-22 593 Operations Assessment Team

Inspection (Outage

assessment)

84-23 84-18 31 Licensing issues on torus /

drywell vacuum breaker and

air sampling system; QA

program implementation

84-24 84-20 149 Operational Safety

.

84-25 84-11 112 Whole body counting

program

84-26 84-22 28 Closing electrical

inspection report

findings

84-27 84-23 Enforcement Conference

84-29 22 Radiation exposure to

three workers

_ - _ _ _ _ _ _ _ _ _ . _ _ . -- . . _ _ _

_ _ .

T3-3

Table 3 (continued)

Report Inspection Hours Areas Inspected

Unit 2 Unit 3

84-30. 84-24 26 Torus modification

requirements and IE Bulletin

78-11; and review of the

licensee's organization and

procedures for performance

and control of major

modifications

-84-31 '84-25 186 Operational Safety

l

84-32 84-26 101 Operational Safety

84-33 84-27 244 Emergency Preparedness

(Annual Exercise)

84-35 84-29 275 Operational Safety

84-38 84-31 36 Inspect licensee's

program for recirculating

and RHR pipe replacement

84-39 84-32 52 Operational Safety

84-40 84-19 34 Fire protection / prevention

program

84-41 84-33 48 Licensee's activities

related to NRC Bulletin

identified items and

surveillance of pipe

supports, restraints and

snubbers

84-42 84-34 40 Radioactive waste management

i- program

85-01 633 NRC Mobil NDE Van

85-02 85-02 33 Security and Safeguards

85-03 85-03 244 Emergency Planning Team

Inspection

m. -

T3-4

Table 3 (continued)

Report Inspection Hours Areas Inspected

^ Unit 2- Unit 3

85-04 85-04 29 Recirculation

safe end repair and

replacement

85-05 85-05 39 ISI/ PSI Activities

85-06 85-06 20 Nonradiological chemical

program

85-07 (3-07 40 Special Inspection

Operational Safety

85-08 85-08 406 Operational Safety

85-09' '85-09 78 Effluent control program

and radiochemical

measurements program using

the NRC:I Mobile

Radiological Measurements

Laboratory

85-10 20 Local Leak Rate Test (LLRT)

Program

85-11 85-11 29.5 Special inspection to review

the contamination of several

workers

85-12 85-12 After SALP period Operational Safety

'

85-13 1.5 Enforcement Conference

85-14 11 Assessments of external

and internal exposures

resulting from events

described in Inspection

50-277/85-11 and the

licensee's corrective

actions as described in

Report 50-277/85-13.

L .- - - .

..

T4-1

TABLE 4

INSPECTION HOURS SUMMARY

PEACH BOTTOM ATOMIC POWER-STATION

UNITS 2 and 3

Functional Area Hours  % of Time

1. . Plant Operations........................ 1850 34.0

2. Radiological Controls................... 489 9.0

3. Maintenance............................. 442 8.0

4. Surveillance............................ 170 3.0

5. Fire Protection.......................... 84 1.0

6. Emergency Preparedness.................. 538 10.0

7. Security and Safeguards................. 195 4.0

8. Refueling /0utage Activities............. 1654 31.0

9. Licensing Activities.................... *- ---

T0TAL....................................... 5422 100%

  • Hours expended in facility licensing activities are not included with direct

inspection effort statistics.

,

F

t. . _

T5-1

TABLE 5

U(!DLANNEDAUTOMATICSCRAMSANDFORCEDOUTAGES

PEACH BOTTOM ATOMIC POWER STATION

Unplanned Automatic Scrams

Unit Date Power Level (%) Cause

3 2/9/84 100 Power spike resulting from pressure

surge associated with malfunctioning

main turbine control valves

3 7/11/84 100 APRM high flux scram occurred

following lightning strike on 500 KV

bus tie line

3 8/21/84 100 Low reactor water level caused by

malfunction in feedwater control

circuit

3 11/14/84 20 APRM high flux scram as the B

recirculation pump was restarted

3 3/1/85 25 Low main condenser scram due to loss

of offgas system combined with high

condenser in leakage

Forced Outages

Unit Date Cause

3- 1/14/84 Loss of condensate pumps due to

room flooding

2 1/28/84 RCIC testable check valve

leak

2 2/18/84 MSIV and feedwater check valves

LLRT

2* 2/27/84 Control rod pattern adjustment

2* 3/2/84 Water box inspection and repair,

and control rod pattern

adjustment

3* 3/16/84 Water box inspection and repair,

and control rod pattern

adjustment

3* 3/20/84 Control rod pattern adjustment

'

'3* 3/23/84 Control rod pattern adjustment

-

T5-2

TABLE 5(continued)

Forced Outages (continued)

Unit- Date Cause

3* -4/20/84 Control rod pattern adjustment

and rondensate pump repair

2 4/28/84 Shutdown for sixth refueling

outage

3 6/2/84 RCIC valve and feedwater

heater repair; and weld

overlay of the jet pump

instrumentation nozzles

3* 9/29/84 Load reduction for control rod

adjustments, B and C circulation

pump work, B and C condensate

pump work

3* 10/25/84 Lead reduced to lower radiation

levels in the off gas

3 11/6/84 Repair valve packing leak in

drywell

3* 11/24/84 Load drop for condenser water

box work

3* 12/1/84 Load reduction for waterbox leak

repair

3* 12/10/84 Load drop to repair recombiner

condenser tubes

3* 12/15/84 Load drop for control rod

adjustment

3* '12/20/84 Load reduction to limit off gas

releases

3* 1/5/85 Load reduction to repair broken

test tap on the 3A condensate

pump

T5-3

TABLE 5(continued)

Forced Outages (continued)

Unit Date Cause

3* 1/15/85 Load drop due to the E4 diesel

and 39A RHR valve inoperability.

The valve was returned to service

prior to unit shutdown.

3 1/23/85 Generator taken off line to clean

up an oil leak which caused a

generator field ground.

3 2/1/85 Mini-outage for surveillance -

testing and miscellaneous

maintenance (main steam isolation

valves and leak testing).

3* 3/9/85 Control rod pattern adjustment

and condenser tube leak repair

  • Load drops / reductions only-

-

T6-1

TABLE 6

NRR SUPPORTING DATA AND SUMMARY

A. This following is summary of significant licensing actions and other

activities during the assessment period.

-1. NRR/ Licensee Meetings - 4

IGSCC (Pipe cracks) and pipe repair / replacement

Backup E0F

PECo-H. Thompson meeting

Purge / Vent TS

2. NRR Site or Component Officer Visits - 3

PM Annual Data Visit (1984 and 1985)

Audit of SPDS

Regulatory. Performance meeting

3. Schedules Extensions Granted - 2

Annual Emergency-Exercise

Equipment Qualification

4. Relief Granted - 1

ISI

5. Technical Exemptions Granted - 1

Fire Protection

.6. License Amendments Issues - 35

'7 . Emergency Technical Specification Changes Issued - none

!

8. Orders Issued - 1

Confirmatory Orders on NUREG-0737, Supplement 1 (both units)

9. 'NRR/ Licensee Management Conferences - none

.B. .The following details the NRR licensing actions completed during this

assessment period.

o Plant-specific actions (48 completed): Actions in this

category which were used.to provide input for this evaluation.

n -

I

T6-2

Table 6 (continued)

-

' Review of plant specific Appendix R technical exemptions

-

Coolant Leakage Technical Specifications (TSs)

-- Reactor water cleanup and scram discharge volume TSs

- TS on local leak rate testing

- Increased core flow TSs

-

Hydrogen chemistry test TSs

-

Requalification exam extension-

-

Unit 2 reload

o 20 multi plant actions (16 completed): Actions in this

' category which were used to provide input for this evaluation

are:

- Environmental Qualification

-

Generic Letter 83-36

- Purge / Vent Valve Operability

o 20 NUREG-0737 actions (10 completed): Actions in this

category.which were used to provide input for this' evaluation

are:

- Inadequate Core Cooling Guidelines (I.C.I.2.A)

-

SPDS (I.D.2)

- Post Accident Sampling (II.B.3)

-

Failures of Relief Valves (II.K.3.16)

!

.